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Category:Memoranda
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Al ML21130A0382021-05-21021 May 2021 Memo to File - Draft Request for Additional Information Relief Request CISI-03-01 Concerning Containment Unbonded Post-Tensioning System Inservice Inspection Requirements ML21067A0922021-04-20020 April 2021 Documentation of Decision by NRC Staff That EPRI Report 3002012988, Alternative Approaches for Addressing Seismic Risk in 10 CFR 50.69 Risk-Informed Categorization, Meets Criteria for a Federal Record ML20212L5772020-11-20020 November 2020 Memo to File: Environmental Assessment-Finding of No Significant Impact and NRC Financial Analysis for Constellation and Exelon Decommissioning Funding Plan Submitted in Accordance with 10 CFR 72.30(b) and (C) for Calvert Cliffs Nuclear Pow ML19298C9722019-10-31031 October 2019 50.69 Apla SE Input L-2018-LLA-0482 ML17142A2382017-05-25025 May 2017 OEDO-17-00280 - Briefing Package for Drop-In Visit on June 9, 2017, by Senior Management of Exelon Generation Company, LLC with Chairman Svinicki, Commissioner Baran, and Commissioner Burns ML16075A4562016-04-12012 April 2016 February 24, 2016, Summary of Meeting with Exelon Generation Company, LLC, to Discuss the Flaw Indication in the Calvert Cliffs Unit 1 Pressurizer Safety Valve Dissimilar Metal Weld ML16088A2052016-03-28028 March 2016 Enclosure 1 - (72.30 DFP Reviews to Be Completed 2015) - Memo T Bowers from s Ruffin, Technial Assistance Requests - Review 2015 Tri-Annual Decommissioning Funding Plans for Multiple Independent Spent Fuel Storage Installations ML16088A2042016-03-28028 March 2016 Memo T Bowers from s Ruffin, Technical Assistance Requests - Review 2015 Tri-Annual Decommissioning Funding Plans for Multiple Independent Spent Fuel Storage Installations W/ Encl 2 (Template) ML16075A3292016-03-16016 March 2016 OEDO-16-00165 - Briefing Package for Drop-In Visit on March 23, 2016, by Senior Management of Exelon Generation Company, LLC with the NRC Executive Director for Operations ML14363A0452014-12-29029 December 2014 Safety Evaluation Close-out Letter for Calvert Cliffs Nuclear Power Plant and Independent Spent Fuel Storage Installation with Enclosure ML14055A2132014-02-25025 February 2014 Summary of Telephone Conference Regarding the Verbal Authorization of Relief Request RR-ISI-04-08, Revision 1 ML14003A0242014-01-10010 January 2014 Summary of Telephone Conference Regarding the Verbal Authorization of Relief Request RR-ISI-04-09 ML13304B4032013-11-0101 November 2013 Notice of Forthcoming Meeting with Constellation Energy Nuclear Group, LLC, ML13267A2852013-09-25025 September 2013 Interim Staff Evaluation and Request for Additional Information - Calvert Cliffs Nuclear Plant, Unites 1 and 2 Regarding Overall Integrated Plan for Reliable Spent Fuel Pool Instrumentation (Order Number EA-12-051) ML13226A0902013-08-14014 August 2013 Notice of Forthcoming Meeting with Constellation Energy Nuclear Group, LLC ML13214A3532013-08-0606 August 2013 Notice of Forthcoming Pre-Application Meeting with Constellation Energy Nuclear Group, LLC (MF2516 and MF2517) ML13045A1822013-02-19019 February 2013 March 20, 2013, Notice of Forthcoming Teleconference with Calvert Cliffs and Nrc/Nrr Staff to Have Additional Discussions of Licensees'S Proposed Path for Resolution of Generic Letter 2004-02 ML13050A5112013-02-19019 February 2013 MC4672-3 Corrected Notice -Public Meeting on March 20, 2013 Re-GL2004-02 ML13196A2202012-06-0606 June 2012 Memo from B. 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Susco, NRR on Summary of Section 7 Consultation Activities Related to the National Marine Fisheries Service'S Final Rule to List the Atlantic Sturgeon ML12136A5672012-05-17017 May 2012 Summary of Meeting with Constellation Energy to Discuss the Constellation Apparent Violation of NRC Regulations at Title 10 of the Code of Federal Regulations Part 50.9 ML12107A5052012-04-16016 April 2012 Forthcoming Category 1 Public Meeting with Constellation Energy Nuclear Group, LLC to Discuss Preliminary Enforcement ML12073A2912012-03-13013 March 2012 Notice of Public Meeting with Constellation Energy Nuclear Group, LLC Regarding NRCs Assessment of Safety Performance at Calvert Cliffs Nuclear Power Plant ML1131102432011-10-24024 October 2011 October 14, 2011, Summary of License Amendment Request (LAR) No. 10 Pre-Application Meeting with Calvert Cliffs Nuclear Power Plant, LLC, (TAC No. L24576) ML1113206252011-05-17017 May 2011 Notice of Forthcoming Closed Meeting with Calvert Cliffs Nuclear Power Plant, LLC and Areva to Discuss Transition to Areva Fuel ML1011903842010-05-0606 May 2010 Notice of Forthcoming Conference Call with Calvert Cliffs to Discuss Supplemental Responses to Generic Ltr. 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized Water Reactors ML0909705822009-04-0707 April 2009 Phone Call Summary with Licensees and Alion Science and Technology on April 2, 2009 to Address NRC Staff Position on Chemical Effects Refinements ML0903701402009-02-0606 February 2009 Probabilistic Assessment of Flaw in Support of Calvert Cliffs Unit 2 Relief Request ISI-020 ML0833102772008-10-24024 October 2008 DHS, Calvert Cliffs Consultation Report ML0809200582008-04-18018 April 2008 Summary of Phone Call with Licensees Concerning Sump Strainer Head Loss Testing ML0807400842008-03-14014 March 2008 Draft Regulatory Guide for Comment ML0706400412007-03-0606 March 2007 Commitment Lists for Renewed Operating License (ROL) Plants with No Commitment Appendix Attached to Its ROL Sers/Nuregs for Use with IP-71003 ML0617805592006-07-10010 July 2006 Revised Closeout Letter for Bulletin 2003-01, Potential Impact of Debris Blockage on Emergency Sump Recirculation at Pressurized-Water Reactors. 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ML0524101502005-08-30030 August 2005 Summary of Telephone Conference on March 7, 2005, Regarding Steam Generator Tube Inspections, Calvert Cliffs Nuclear Power Plant, Unit No. 2 ML0503901492005-02-23023 February 2005 Response to Generic Letter 2004-01, Requirements for Steam Generator Tube Inspections ML0433501182004-12-0303 December 2004 Reactor Oversight Process Midcycle Self - Assessment Performance Metrics ML0336403322004-01-0606 January 2004 Correction of License Authority Files ML0332900462003-12-11011 December 2003 Review of Revision 32 to the Updated Final Safety Analysis Report (UFSAR) ML0327205272003-10-21021 October 2003 Plan and Schedule for Implementation of Staff Position on the Station Blackout (SBO) Issue ML0314906662003-06-0303 June 2003 Summary of Meeting Held on May 13, 2003, Between the U.S. Nuclear Regulatory Commission (NRC) Staff and Calvert Cliffs Nuclear Power Plant, Inc., the Elimination of Offsite Review Committees ML0310705002003-04-17017 April 2003 Basf, Radioactive Waste Manifests, Princeton and Ewing Sites, Dtd January 2001 to September 2002 ML0308404632003-04-0101 April 2003 Closure of TAC Nos. MB2437 and MB2438 ML0307205722003-03-26026 March 2003 Telephone Conversation with Representatives of Calvert Cliffs Nuclear Power Plant, Inc., Concerning the Licensee'S Ongoing Reactor Pressure Vessel Head Inspection Program ML0228801162002-10-15015 October 2002 Evaluation of the Risk Assessment Information Provided by Calvert Cliffs Nuclear Power Plant in Support of Its Request to Decrease the Surveillance Testing Interval for Verifying Boron Concentration in the Safety Injection Tanks from Once E ML0215803662002-06-0606 June 2002 Memo to R. Bellamy, RGN-I from: M. Tokar Subject: Region I Independent Spent Fuel Storage Installation Inspection Plans Attachment: Sfpo Comments to Region I Integrated Inspection Plans ML0210603052002-05-24024 May 2002 Reply to Licensee'S Response to Order for Interim Safeguards and Security Compensatory Measures ML0209101702002-04-0404 April 2002 Documentation of Conference Call to Calvert Cliffs Nuclear Power Plant, Unit No. 1 and 2 on March 26, 2002, Regarding Reactor Vessel Head Inspection Activities 2021-05-21
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August 30, 2005 MEMORANDUM TO: Richard J. Laufer, Chief, Section 1 Project Directorate I Division of Licensing Project Management FROM: Patrick D. Milano, Sr. Project Manager, Section 1 /RA/
Project Directorate I Division of Licensing Project Management
SUBJECT:
SUMMARY
OF TELEPHONE CONFERENCE ON MARCH 7, 2005, REGARDING STEAM GENERATOR TUBE INSPECTIONS, CALVERT CLIFFS NUCLEAR POWER PLANT, UNIT NO. 2 On March 7, 2005, the Nuclear Regulatory Commission (NRC) staff participated in a telephone conference call with representatives of Calvert Cliffs Nuclear Power Plant, Inc. (the licensee) regarding the inspection of the steam generator (SG) tubes at Calvert Cliffs Nuclear Power Plant, Unit No. 2 (Calvert Cliffs 2). In particular, the NRC staff was concerned about the finding of several loose part indications during the inspection. A summary of the information provided during the call is provided below.
Calvert Cliffs 2 has two SGs designed and fabricated by Babcock and Wilcox International.
The SGs were installed in 2003 and are fabricated with thermally-treated Alloy 690 tubes that have an outside diameter of 0.750-inch and a nominal wall thickness of 0.042-inch. The tubes are expanded for the full depth of the tubesheet at each end and are supported by a number of stainless steel lattice grids and fan bars. The tubes are arranged in a triangular pitch.
During the 2005 refueling outage ! the first following SG replacement at Calvert Cliffs 2, 100%
of the tubes in each of the two SGs were inspected for the full length with a eddy current testing (ECT) bobbin coil. In addition, a rotating probe was used to inspect any bobbin coil indications.
As a result of these inspections, several indications of wear at the fan bars were identified and several possible loose part indications were found.
In SG no. 22, a visual examination confirmed the presence of one possible loose part on the cold-leg side of the SG. The loose part was retrieved and identified as a 5.25-inch long, 0.045-inch diameter wire. The part is believed to have entered the SG through the secondary side of the plant. Further analysis of the part is planned. A visual inspection of neighboring tubes did not identify any additional loose parts. A rotating probe equipped with a +PointTM ECT coil was used to inspect 14 surrounding tubes from the top of the tubesheet to the first lattice grid tube support (approximately 35-inches in length). Three tubes were identified with wear.
The wear on these tubes was estimated to be 5% through-wall (1 tube) and 6% through-wall (2 tubes). No other possible loose part indications were found in this region. Two pictures of the loose part (Attachment 1 with the part in the SG, and Attachment 2 after the part was removed from the SG) were provided in support of the phone call. The tubes will be left in service.
R. Laufer In another location on the cold-leg side of SG no. 22, several (2 or 3) non-quantifiable indications were identified by the bobbin coil. These indications were in the same general vicinity. A rotating probe equipped with a +PointTM coil was used to inspect a number of tubes surrounding these indications and resulted in identifying 15 tubes with possible loose part indications. The extent of these rotating probe exams was from the top of the tubesheet to the first lattice grid tube support (approximately 35 inches in length). A one-tube buffer zone was established around the 15 possible loose part indications (i.e., the rotating probe examination was extended to neighboring tubes until at least 1 tube did not have an indication of a possible loose part). Of these 15 tubes with possible loose part indications, 4 tubes had wear indications. The wear in these tubes measured 3%, 4%, 6%, and 11% through-wall. The tubes were not next to each other and are not in the periphery of the tube bundle (i.e., the indications start to appear 6 tubes into the tube bundle). The location of the indications on the affected tubes varied from tube-to-tube. Some of the indications were located at 1 inch above the top of the tubesheet while other indications were located as high as 8 inches above the tubesheet.
The relative orientation of the indications (e.g., were they all on the same side of the tube or were they facing each other) was not determined. There was one additional wear indication in the vicinity of these 15 tubes; however, there was no evidence of the part still being present at this location. This tube had a wear scar measuring 9% through-wall.
Given the location of the tubes with indications, attempts to visually inspect the location of these indications were unsuccessful (see attached tubesheet map and the list of tubes with indications, Attachments 3 and 4, respectively). Since the presence of a part (or parts) could not be confirmed visually and the part (or parts) could not be removed, the licensee plans to plug and stabilize the 15 tubes and several tubes surrounding these 15 tubes including one tube downstream of these tubes. A total of 29 tubes are planned to be plugged and stabilized as a result of these indications.
To investigate the cause of these indications, previous ECT data (i.e., from the preservice inspection) were reviewed. The preservice inspection included rotating probe inspections near the top of the tubesheet. No indications of a possible loose part or wear were present. In addition to the historical review of the ECT data, a visual inspection of several secondary side internals was performed including various lattice grid locations. No degradation of the SG secondary side internals was identified.
There were no plans to sludge lance the SGs during this outage given the low levels of sludge.
There are no filters on the J-tubes that would limit the size of the parts entering the SG. There is no loose part monitor on the secondary side of the SG; however, there are primary side loose part monitors.
R. Laufer The plans for future inspections of the SG were not discussed; however, the NRC staff indicated that the licensees assessment of the operating time between inspections would be a challenge given the limited information on these indications.
Docket No. 50-318 Attachments: As stated
R. Laufer The plans for future inspections of the SG were not discussed; however, the NRC staff indicated that the licensees assessment of the operating time between inspections would be a challenge given the limited information on these indications.
Docket No. 50-318 Attachments: As stated DISTRIBUTION:
PUBLIC PDI-1 Reading File R. Laufer P. Milano K. Karwoski E. Murphy Y. Diaz P. Klein C. Lauron G. Makar L. Miller J. Terrel J. Trapp, R-I R. Lorson, R-I A. Passarelli, R-I Accession: ML052410150 OFFICE PDI-1/PM PDI-1/LA EMCB PDI-1/SC NAME PMilano SLittle KKarwoski RLaufer DATE 08/24/05 08/24/05 08/29/05 08/30/05 OFFICIAL RECORD COPY
Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2 cc:
President Patricia T. Birnie, Esquire Calvert County Board of Co-Director Commissioners Maryland Safe Energy Coalition 175 Main Street P.O. Box 33111 Prince Frederick, MD 20678 Baltimore, MD 21218 Carey Fleming, Esquire Mr. Loren F. Donatell Sr. Counsel - Nuclear Generation NRC Technical Training Center Constellation Generation Group, LLC 5700 Brainerd Road 750 East Pratt Street, 17th floor Chattanooga, TN 37411-4017 Baltimore, MD 21202 Lou Larragoite Calvert Cliffs Nuclear Power Plant 1650 Calvert Cliffs Parkway Lusby, MD 20657-4702 Resident Inspector U.S. Nuclear Regulatory Commission P.O. Box 287 St. Leonard, MD 20685 Mr. R. I. McLean, Administrator Radioecology Environ Impact Prog Department of Natural Resources Nuclear Evaluations 580 Taylor Avenue Tawes State Office Building Annapolis, MD 21401 Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Kristen A. Burger, Esquire Maryland People's Counsel 6 St. Paul Centre Suite 2102 Baltimore, MD 21202-1631