01-07-2011 | At 1056 on November 10, 2010, Nine Mile Point Unit 1 scrammed from full power operation due to closure of outboard Main Steam Isolation Valves ( MSIVs) 01-03 and 01-04. Valves 01-03 and 01-04 closed following receipt of an invalid low-low reactor water level signal.
The scram was the result of a combination of two latent preexisting plant conditions and performance of a quarterly instrument channel surveillance test. The first preexisting condition was misaligned connector pins on Grayboot splice connectors for outboard MSIV Channel 11 solenoid operated valves. The cause of the misalignment was determined to be insufficient rigor in the behaviors and knowledge (training) used in identifying appropriate post maintenance testing (PMT) requirements. The second preexisting condition was a misaligned contact spring in isolation logic Channel 12 relay 12K74 (General Electric (GE) Model CR305).
The cause of this failure was excess material (plastic) left during fabrication of the relay's movable contact holder.
Immediate actions were to repair the Channel 11 Grayboot splice connectors and replace Channel 12 relay 12K74. Training will be provided to planning personnel to ensure an adequate understanding of complex/redundant circuits for the proper determination of PMT requirements. Procedure/manuals governing Grayboot connector maintenance activities will be revised to include additional post assembly inspections and testing. |
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I. DESCRIPTION OF EVENT
A. PRE-EVENT PLANT CONDITIONS:
Prior to the scram, Nine Mile Point Unit 1 (NMP1) was operating at 100 percent power.
B. EVENT:
At 1056 on November 10, 2010, NMP1 scrammed from full power operation due to closure of air-operated, outboard Main Steam Isolation Valves (MSIVs) 01-03 and 01-04. Valves 01-03 and 01-04 closed following receipt of an invalid low-low reactor water level signal during performance of the reactor low-low water level quarterly channel surveillance test.
Nine Mile Point Unit 1 outboard MSIVs 01-03 and 01-04 are air operated valves. Each MSIV is designed with two solenoid operated valves (SOVs) such that when one or both SOV(s) are energized, air is ported to the MSIV and the valve is held open. Each SOV receives an input from the reactor vessel isolation Channel 11 and Channel 12 one-out-of-two taken twice logic. If this logic is met, the SOVs will deenergize causing redirection of the air supply and the MSIVs to close (see attached Figure 1 for SOV and logic configuration). Reactor low-low level is an input signal to the reactor vessel isolation one-out-of-two taken twice logic.
On November 10, 2010, at approximately 1032, maintenance technicians were given permission to perform N1-ISP-036-004, Lo-Lo RPV Level Instrument Trip Channel Test/Calibration, Attachment 1, for isolation Channel 11. In performing Attachment 1, technicians inserted a reactor low-low level signal which deenergized the Channel 11 isolation relay logic. Normally, this would have resulted in generating only half Channel 11 and half Channel 12 isolation signals. However, two preexisting plant conditions resulted in an MSIV closure and the subsequent reactor scram on MSIV position. Specifically, the following conditions existed:
1) SOV-01-04D and SOV-01-03D, the Channel 11 MSIV SOVs, were each found to have misaligned connector pins in their respective Grayboot splice connectors. The connectors are located in the SOV's power circuit which meant that both Channel 11 MSIV SOVs were deenergized. In other words, one of the two SOVs associated with each outboard MSIV was deenergized prior to the surveillance test. Nine Mile Point Nuclear Station, LLC has determined that this condition existed since 2005 when the Grayboot connectors were installed as part of the MSIV SOV replacement effort.
2) Relay 12K74 (General Electric (GE) Model CR305) was found to have a misaligned contact spring and evidence of electrical arcing on the contact that provides input to the Channel 12 reactor vessel isolation logic. Nine Mile Point Nuclear Station, LLC believes that this contact failed open following performance of the previous relay surveillance performed on August 12, 2010.
As stated above, the misaligned connector pins meant that the Channel 11 side MSIV SOVs remained deenergized since the connectors were installed in 2005. The misaligned contact spring in relay 12K74 caused a half Channel 12 isolation signal. In this configuration, only Channel 11 of the one-out-of-two taken twice logic needed to be completed for an MSIV isolation to occur.
During performance of surveillance test N1-ISP-036-004, the induced Channel 11 low-low level completed the Channel 12 isolation signal and deenergized the Channel 12 MSIV SOVs.
Together with the two preexisting conditions, the performance of the surveillance test resulted in closure of the outboard MSIVs and the subsequent scram on MSIV position.
Following the scram, N1-SOP-1, Reactor Scram, and N1-E0P-2, RPV Control, were entered and executed. Reactor vessel pressure was controlled using Emergency Condenser 11 until use of the main heat sink (condenser) was reestablished. The High Pressure Coolant Injection (HPCI) System initiated, as designed, on a low reactor water level signal.
C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO
THE EVENT:
Relay 12K74 was found to have a misaligned contact spring and evidence of electrical arcing on the contact that provides input to the Channel 12 reactor vessel isolation logic.
SOV-01-04D and SOV-01-03D, the Channel 11 MSIV SOVs, were each found to have misaligned connector pins in their respective Grayboot splice connectors. However, the MSIVs remained operable in that the two preexisting conditions would not have prevented the MSIVs from closing.
D. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
4/25/2005 - The Grayboot splice connectors associated with Channel 11 MSIV solenoid operated valves SOV-01-04D and SOV-01-03D were installed in 2005. Nine Mile Point Nuclear Station, LLC has determined that the connecter pins in the Grayboot connectors have been misaligned since their installation.
8/12/2010 - Relay 12K74 was cycled for surveillance testing on August 12, 2010. The contact associated with the low-low reactor vessel isolation logic remained in an open state since performance of this test.
11/10/2010 - At 1056 on November 10, 2010, NMP1 scrammed from.full power operation due to closure of outboard MSIVs 01-03 and 01-04. Valves 01-03 and 01-04 closed following receipt of an invalid low-low reactor level signal.
E. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
No systems or secondary functions were affected by this condition. This event did not affect Nine Mile Point Unit 2.
F. METHOD OF DISCOVERY:
The reactor scram was self-revealing via multiple control room indications.
G. MAJOR OPERATOR ACTION:
Following the scram, Operations confirmed that all control rods had fully inserted. N1-SOP 1, Reactor Scram, and N1-EOP-2, RPV Control, were entered and executed. Plant operators took manual control of RPV level control and stabilized level between 53 and 95 inches. Reactor vessel pressure was controlled by manually initiating Emergency Condenser 11 until the main heat sink (condenser) was reestablished. Emergency Condenser 11 was then secured. The HPCI System initiated, as designed, on a low reactor vessel water level signal. The HPCI System was then secured following restoration of normal water level.
H. SAFETY SYSTEM RESPONSES:
Nine Mile Point Unit 1 outboard MSIVs 01-03 and 01-04 closed as expected with both Channel 11 and 12 SOVs deenergized due to a combination of preexisting plant conditions and performance of the low-low reactor water level surveillance test. All control rods fully inserted as designed on closure of the MSIVs. Partial closure of MSIVs in both main steam lines produces a scram so the reactor is not operated without its main heat sink. Reactor vessel pressure was controlled by manually initiating Emergency Condenser 11 until the main heat sink (condenser) was reestablished by reopening MSIVs 01-03 and 01-04. The HPCI System initiated, as designed, on a low reactor vessel water level signal. At NMP1, HPCI initiation on a reactor low level signal is an expected occurrence due to water level shrinkage following a scram.
II. CAUSE OF EVENT:
The November 10, 2010 scram was the result of the combination of two latent preexisting plant conditions and performance of a quarterly instrument channel surveillance test. The first preexisting condition was misaligned connector pins on the Grayboot splice connectors found in the power circuit of the outboard MSIV Channel 11 SOVs. The cause of the misalignment has been determined to be insufficient rigor in the behaviors and knowledge (training) used in determining the appropriate post maintenance testing (PMT) in 2005 for redundant/complex control circuits.
Following replacement of the SOVs (which included installation of the Grayboot connectors), the PMT identified and performed was cycling the outboard MSIVs per surveillance procedure.
However, since each MSIV is designed with two redundant SOVs, each capable of porting air to or away from the MSIV, the test performed was not adequate to identify the failed Grayboot connection or the deenergized SOV. A contributing cause was inadequate technical guidance in the maintenance procedure and vendor manual regarding inspection and testing of the Grayboot connectors.
The second preexisting condition was a misaligned contact spring in isolation logic Channel 12 relay 12K74 which was installed in April 2005. The cause of the misalignment has been determined to be excess material (plastic) left on the contact spring holding peg during fabrication of the relay's movable contact holder. The excess material allowed the position of the contact spring to change and uneven forces to be applied to the movable contact. Consequently, the contact associated with the low-low level isolation logic remained open since the relay was cycled during the previous surveillance test performed in August, 2010.
The misaligned connector pins and contact spring, together with insertion of a reactor vessel low low water level signal for surveillance testing, resulted in an MSIV closure and subsequent reactor scram on MSIV position.
Condition Report 2010-011008 applies to this LER.
III. ANALYSIS OF THE EVENT:
This event is reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph 10 CFR 50.73(a)(2)(iv)(B). On November 10, 2010, closure of outboard MSIVs 01-03 and 01-04 resulted in a reactor scram and initiation of HPCI.
The SOV Grayboot splice connectors were left in a misaligned position since 2005. However, this misalignment resulted in the subject SOVs being left in a deenergized state (i.e., the required state to port air away from the MSIVs) and therefore would not have prevented the MSIVs from closing.
Relay 12K74 failed in a position such that one path of the Channel 12 reactor vessel isolation logic was completed. Therefore, its failure would not have prevented the MSIVs from closing and performing their safety function.
The November 10, 2010 scram is bounded by the NMP1 Updated Final Safety Analysis Report (UFSAR) analyzed transient delineated in UFSAR Chapter XV, Section A.3.5, Main Steam Isolation Valve Closure, (With Scram). The analyzed event assumes the reactor is at rated power, an MSIV closure occurs and that a scram is initiated automatically by MSIV position. The UFSAR also states that the Electromatic Relief Valve (ERV) set pressures are low enough to prevent lifting of the Reactor Pressure Vessel (RPV) safety valves. No ERVs lifted during this event.
A walkdown of the Main Steam System was performed per procedure and identified no evidence of damage to snubbers or supporting structural members.
Based on the above, it is concluded that the safety significance of this event is low and the event did not pose a threat to the health and safety of the public or plant personnel.
This event does impact the NRC Regulatory Oversight Process (ROP) Index for Unplanned Scrams. Due to this scram, the Unplanned Scram Index value will be 0.8 compared to a Green-to- White threshold value of greater than 3.
IV. CORRECTIVE ACTIONS:
A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
Reactor vessel pressure was controlled using Emergency Condenser 11 until the main heat sink (condenser) was reestablished; the Emergency Condenser was then secured. The HPCI System initiated, as designed, on a low reactor vessel water level signal following the scram.
HPCI was secured following restoration of normal water level.
The Channel 11 Grayboot splice connector misaligned connector pins were repaired and an appropriate PMT performed to assure proper operation of the SOVs. Channel 12 relay 12K74 was replaced and tested to assure proper operation.
B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
Actions which were taken or are planned to be taken include the following:
Grayboot Splice Connector 1) Immediate actions were to repair the Channel 11 Grayboot splice connectors.
2) Training will be provided to planning personnel to ensure an adequate understanding of complex/redundant circuits for the proper determination of PMT requirements.
3) Procedure/manuals governing Grayboot connector maintenance activities will be revised to include additional post assembly inspections and testing. This will include a continuity check following each Grayboot installation.
General Electric (GE) Relay 12K74 1) Immediate action was to replace Channel 12 relay 12K74 and inspect two other CR305 relays.
2) Four additional CR305 relays from the same lot as the failed relay will be inspected. If additional deficiencies are found, additional corrective actions will be initiated.
V. ADDITIONAL INFORMATION:
A. FAILED COMPONENTS:
Relay 12K74 was found to have a misaligned contact spring and evidence of electrical arcing on the contact that provides input to the Channel 12 reactor vessel isolation logic.
SOV-01-04D and SOV-01-03D, the Channel 11 MSIV SOVs, were each found to have misaligned connector pins in their respective Grayboot splice connectors.
B. PREVIOUS LERs ON SIMILAR EVENTS:
None C. THE ENERGY INDUSTRY IDENTIFICATION SYSTEM (EllS) COMPONENT FUNCTION
IDENTIFIER AND SYSTEM NAME OF EACH COMPONENT OR SYSTEM REFERRED TO
IN THIS LER:
COMPONENT� IEEE 803 FUNCTION� IEEE 805 SYSTEM IDENTIFIER� IDENTIFICATION Plant Protection System� -� JC Reactor Vessel Isolation System� JM Emergency Condenser� COND� BL Main Steam Isolation Valve� ISV� SB Relay� RLY� JC Connector� CON� SB Solenoid Operated Valve� FSV� SB
None
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05000220/LER-2010-001 | Reactor Scram Due to Inadequate Post Maintenance Testing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000410/LER-2010-001 | Reactor Scram Due to Inadvertent Actuation of the Redundant Reactivity Control System During Maintenance | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000395/LER-2010-001 | Reactor Building Cooling Units Reduced Air Flow Rate Below Technical Specification Limits | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000382/LER-2010-001 | Spent Fuel Pool Cooling Single Failure | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000374/LER-2010-001 | High Pressure Core Spray System Declared Inoperable Due to Failed Room Ventilation Control Relay | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000373/LER-2010-001 | Unauthorized Individual Gained Access to the Protected Area. | | 05000370/LER-2010-001 | Loose connection in a panel board serving a Solid State Protection System Train concurrent with redundant train maintenance could have prevented fulfillment of a safety function. | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000261/LER-2010-001 | Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2010-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000255/LER-2010-001 | Potential Loss of Safety Function Due to a Service Water Pump Shaft Coupling Failure | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2010-001 | Engineered Safety Features Steam Line Pressure Dynamics Modules Discovered Outside of Technical Specification Values | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2010-001 | Unit 2 Turbine Trip during Reactor Shutdown Resulting in a Reactor Scram | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000305/LER-2010-001 | Safety Injection Pump Recirculation Line Isolation Results in Violation of Technical Specifications | | 05000298/LER-2010-001 | Cooper Nuclear Station 05000298 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000269/LER-2010-001 | Standby Shutdown Facility Letdown Line Orifice Strainer Blocked by Valve Gasket Material | 10 CFR 50.73(a)(2)(i)(b) | 05000282/LER-2010-001 | Unanalyzed Condition Due to Postulated High Energy Line Break On Cooling Water System | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000277/LER-2010-001 | Multiple Slow Control Rods Results in Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i) | 05000361/LER-2010-001 | Broken Manual Valve Prevents Timely Condensate Storage Tank Isolation | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000483/LER-2010-001 | Emergency Core Cooling System MODE 4 Operating Practices Prohibited by current Technical Specification 3.5.3 | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000498/LER-2010-001 | Unit Shutdown Required by Technical Specifications | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000316/LER-2010-001 | Valid Actuation of Auxiliary Feedwater System in Response to Valid Steam Generator Low-Low Levels | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000321/LER-2010-001 | Corrosion Induced Bonding Results in Safety Relief Valve Lift Setpoint Drift | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2010-001 | Millstone Power Station Unit 2 Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000413/LER-2010-001 | Technical Specification Violation Associated with Failure to Perform Offsite Circuit Verification | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2010-001 | Invalid Isolation Signal Results in Shutdown Cooling Interruption | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000424/LER-2010-001 | Breaker Failure Results in I B Train Containment Cooling System Being Declared Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000416/LER-2010-001 | Automatic Reactor Scram On Decreasing Reactor Water Level Due To Inadvertent Reactor Feed Pump Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000249/LER-2010-001 | OPRM Power Supply Failure during Maintenance Results in Unit 3 Automatic Reactor Scram | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000251/LER-2010-001 | Two Shutdown Bank Rods Were Dropped from Fully Withdrawn Position | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000261/LER-2010-002 | Plant Trip due to Electrical Fault | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000255/LER-2010-002 | Condition that Could Have Prevented the Fulfillment of a Safety Function | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000335/LER-2010-002 | Opened ECCS Boundary Door in Violation of Identified Compensatory Measures | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2010-002 | 270 Degree Circumferential Flaw Found on Residual Heat Removal System Drain Valve Socket Weld | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2010-002 | Containment Divider Barrier Seal Mounting Bolts Not Properly Installed | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2010-002 | Fuel Transfer Pump Failure Renders 3B Emergency Diesel Generator Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000269/LER-2010-002 | Manual Reactor Trip due to 1A1 and 1A2 Reactor Coolant PumDHigh Vibration Indication | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000315/LER-2010-002 | Manual Auxiliary Feedwater Actuation in Response to Main Feedpump Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000271/LER-2010-002 | Inoperability of Main Steam Safety Relief Valves due to Degraded Thread Seals | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000277/LER-2010-002 | Improperly Fastened Rod Hanger Results in Inoperable Subsystem of Emergency Service Water | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000413/LER-2010-002 | Discovery of Reactor Coolant System Pressure Boundary Leak at Thermowell 1NCTW5850 Seal Weld. | | 05000282/LER-2010-002 | Postulated Flooding of Unit 1 Fuel Oil Transfer Pump Motor Starters Could Have Resulted In Reduced Fuel Oil Inventory | | 05000414/LER-2010-002 | Duke Energy Corporation Catawba Nuclear Station 4800 Concord Road York, SC 29745 803-701-4251 803-701-3221 fax December 15, 2010 U.S. Nuclear Regulatory Commission
Attention: Document Control Desk
Washington, D.C. 20555
Subject:�Duke Energy Carolinas, LLC (Duke Energy)
Catawba Nuclear Station, Unit 2
Docket No. 50-414
Licensee Event Report 414/2010-002
Pursuant to 10 CFR 50.73(a)(1) and (d), attached is Licensee Event Report 414/2010-002, Revision 0 entitled, "Technical Specification Violation Involving Mode Change with Inoperable Auxiliary Feedwater System Train Due to Closed Pump Discharge Valves". This report is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B). There are no regulatory commitments contained in this letter or its attachment. This event is considered to be of no significance with respect to the health and safety of the public. If there are any questions on this report, please contact L.J. Rudy at (803) 701-3084. Sincerely, faius4- A James R. Morris LJR/s Attachment www.duke-energy.corn (14 Document Control Desk Page 2 December 15, 2010 xc (with attachment): L.A. Reyes Regional Administrator U.S. Nuclear Regulatory Commission - Region II Marquis One Tower 245 Peachtree Center Ave., NE Suite 1200 Atlanta, GA 30303-1257 J.H. Thompson (addressee only) NRC Project Manager U.S. Nuclear Regulatory Commission Mail Stop 8-G9A 11555 Rockville Pike Rockville, MD 20852-2738 G.A. Hutto, Ill NRC Senior Resident Inspector Catawba Nuclear Station INPO Records Center 700 Galleria Place Atlanta, GA 30339-5957 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-2010) Estimated burden per response to comply with this mandatory collection request: 80 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send commentsLICENSEE EVENT REPORT (LER) regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to infocollectssesource@nre.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used(See reverse for required number of to impose an information collection does not display a currently valid OMB control number, the NRCdigits/characters for each block) may not conduct or sponsor, and a person is not required to respond to, the info(mation collection. 1.. FACILITY NAME 2. DOCKET NUMBER I3. PAGE Catawba Nuclear Station, Unit 2 05000414 1 OF 7 4. TITLE Technical Specification Violation Involving Mode Change with Inoperable Auxiliary Feedwater System Train Due to Closed Pump Discharge ValvesD • | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2010-002 | Unit 2 Turbine Shutdown Due To the Loss of a Main Feed Water Pump That Resulted in a Reactor Scram | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000440/LER-2010-002 | Piping Leak Results in Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000382/LER-2010-002 | Main Feedwater Isolation Valve B exceeded allowed outage time due to tubing connection failure | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000370/LER-2010-002 | ref Energy® REGIS T. REPKO Vice President McGuire Nuclear Station Duke Energy MGO1VP / 12700 Hagers Ferry Rd. Huntersville, NC 28078 980-875-4111 980-875-4809 fax regis.repko(Codu ke-energy.corn 10 CFR 50.73 May 10, 2011 U.S. Nuclear Regulatory Commission ATTENTION: Document Control Desk Washington, D.C. 20555 Subject: D Duke Energy Carolinas, LLC McGuire Nuclear Station, Unit 2 Docket Nos. 50-370 Licensee Event Report (LER) 370/2010-02, Supplement 1 Problem Investigation Process (PIP) M-10-05982 Pursuant to 10 CFR 50.73 Sections (a) (1) and (d), attached is Supplement 1 to Licensee Event Report 370/2010-02, regarding past inoperability of the Unit 2 "A" Train Nuclear Service Water System and satisfies the commitment to supplement the LER following completion of the root cause analysis This supplement to LER 370/2010-02 supersedes the LER previously submitted December 20, 2010. Completion of the root cause analysis has not affected the original reporting criteria which was completed in accordance with 10 CFR 50.73 (a) (2) (i) (B), an Operation Prohibited by Technical Specifications, and 10 CFR 50.73 (a) (2) (v) (B), any Event or Condition That Could Have Prevented Fulfillment of the Safety Function needed to remove residual heat. Additionally, the supplement did not affect the significance of the event which was considered to be of no significance with respect to the health and safety of the public. There are no regulatory commitments contained in this report. If questions arise regarding this LER, contact Rick Abbott at 980-875-4685. Very truly yours, Zi1:77 Regis T. Repko Attachment www. duke-energy. corn U.S. Nuclear Regulatory Commission May 10, 2011 Page 2 cc:�V. M. McCree, Regional Administrator U.S. Nuclear Regulatory Commission, Region II
Marquis One Tower
245 Peachtree Center Ave., NC, Suite 1200
Atlanta, Georgia 30303-1257
Jon H. Thompson (Addressee Only)
Senior Project Manager (McGuire)
U.S. Nuclear Regulatory Commission
11555 Rockville Pike
Rockville, MD 20852-2738
J. B. Brady
Senior Resident Inspector
U.S. Nuclear Regulatory Commission
McGuire Nuclear Station
W. L. Cox Ill, Section Chief North Carolina Department of Environment and Natural Resources Division of Environmental Health Radiation Protection Section 1645 Mail Service Center Raleigh, NC 27699-1645 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB. NO 3150-0104 EXPIRES: 08/31/2013 (10-2010) Estimated burden per response to comply with this mandatory collection request: SO hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA/Privacy Section (T-5 F53), U.S. Nuclear Regulatory Commission. Washington, DC 20555-0001, or by Internet e-mail to info (See reverse for required number of collects resmirceOnrc.gov, and to the Desk Officer, Office of Information and Regulatory digits/characters for each block) Affairs, NEOB-10202, (3150-01041, Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. LICENSEE EVENT REPORT (LER) 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE McGuire Nuclear Station,2Unit 2 05000-212
0370 OF-7 4. TITLE Unit 2 Nuclear Service Water System "A" Train Past Inoperable due to
Failed Strainer Differential Pressure Instrument. | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2010-002 | | | 05000456/LER-2010-002 | Limiting Condition for Operation Action Not Completed Within the Required Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000249/LER-2010-003 | Steam Leak Results in HPCI Inoperability | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000251/LER-2010-003 | Damaged Speed Sensor Caused the 4A Emergency Diesel Generator to be Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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