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Category:Letter
MONTHYEARML24289A1252024-10-22022 October 2024 – Authorized Alternative to Requirements of the ASME OM Code PLA-8145, Biennial 10 CFR 50.59 and 72.48 Summary Report and Changes to Regulatory Commitments - PLA-81452024-10-21021 October 2024 Biennial 10 CFR 50.59 and 72.48 Summary Report and Changes to Regulatory Commitments - PLA-8145 ML24291A1562024-10-16016 October 2024 Missed Annual Inventory Required by 40 CFR 266, Subpart in PLE 0026645 PLA-8148, Registration for the Use of Spent Fuel Storage Casks 311, 308, and 3102024-10-15015 October 2024 Registration for the Use of Spent Fuel Storage Casks 311, 308, and 310 PLA-8142, Registration for the Use of Spent Fuel Storage Casks 306, 309, and 307 - PLA-81422024-09-18018 September 2024 Registration for the Use of Spent Fuel Storage Casks 306, 309, and 307 - PLA-8142 PLA-8141, Response to Request for Additional Information Regarding Relief Request 1RR06, PLA-81412024-09-18018 September 2024 Response to Request for Additional Information Regarding Relief Request 1RR06, PLA-8141 ML24260A2312024-09-17017 September 2024 Senior Reactor and Reactor Operator Initial License Examinations 05000387/LER-2024-002, B Diesel Generator Inoperable Due to Failed Excitation System Linear Reactor2024-09-16016 September 2024 B Diesel Generator Inoperable Due to Failed Excitation System Linear Reactor ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 ML24233A2192024-09-0303 September 2024 – Authorized Alternative to Requirements of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code IR 05000387/20240052024-08-29029 August 2024 Updated Inspection Plan for Susquehanna Steam Electric Station, Units 1 and 2 (Report 05000387/2024005 and 05000388/2024005) 05000387/LER-2023-004-01, Manual Reactor Scram Due to Degraded Main Condenser Vacuum2024-08-26026 August 2024 Manual Reactor Scram Due to Degraded Main Condenser Vacuum 05000387/LER-2024-001-01, Main Steam Isolation Valve Leakage Due to Valve Body Seat Wear2024-08-21021 August 2024 Main Steam Isolation Valve Leakage Due to Valve Body Seat Wear IR 05000387/20240022024-08-12012 August 2024 Integrated Inspection Report 05000387/2024002 and 05000388/2024002 ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification PLA-8117, 23rd Refueling Outage Owners Activity Report (PLA-8117)2024-07-23023 July 2024 23rd Refueling Outage Owners Activity Report (PLA-8117) ML24197A0982024-07-15015 July 2024 Request for Information for a Biennial Problem Identification and Resolution Inspection; Inspection Report 05000387/2024010 and 05000388/2024010 ML24127A2262024-05-29029 May 2024 Issuance of Amendment Nos. 288 and 272 Adoption of TSTF-563 PLA-8126, Response to Request for Confirmation of Information Regarding Relief Request 1RR062024-05-29029 May 2024 Response to Request for Confirmation of Information Regarding Relief Request 1RR06 PLA-8122, Annual Radiological Environmental Operating Report (PLA-8122)2024-05-28028 May 2024 Annual Radiological Environmental Operating Report (PLA-8122) PLA-8115, Relief Request IRR06 One Time Extension to the Fourth 10-Year Inservice Testing Program Interval (PLA-8115)2024-05-23023 May 2024 Relief Request IRR06 One Time Extension to the Fourth 10-Year Inservice Testing Program Interval (PLA-8115) 05000387/LER-2024-001, Main Steam Isolation Valve Leakage2024-05-23023 May 2024 Main Steam Isolation Valve Leakage IR 05000387/20240012024-05-13013 May 2024 Integrated Inspection Report 05000387/2024001 and 05000388/2024001 IR 05000387/20244042024-05-0707 May 2024 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000387/2024404 and 05000388/2024404 PLA-8101, Re 2023 Annual Report of Radiation Exposure2024-04-22022 April 2024 Re 2023 Annual Report of Radiation Exposure ML24082A1372024-04-22022 April 2024 Issuance of Amendment Nos. 287 and 271 Adoption of TSTF-568, Revision 2 and Associated Technical Specification Changes PLA-8095, 2023 Annual Radiological Environmental Operating Report (PLA-8095)2024-04-22022 April 2024 2023 Annual Radiological Environmental Operating Report (PLA-8095) PLA-8094, Radioactive Effluent Release Report and Offsite Dose Calculation Manual PLA-80942024-04-22022 April 2024 Radioactive Effluent Release Report and Offsite Dose Calculation Manual PLA-8094 PLA-8102, Annual Environmental Operating Report (Nonradiological) PLA-81022024-04-11011 April 2024 Annual Environmental Operating Report (Nonradiological) PLA-8102 PLA-8113, Response to Request for Additional Information Regarding Relief Request 4RR-11 (PLA-8113)2024-04-11011 April 2024 Response to Request for Additional Information Regarding Relief Request 4RR-11 (PLA-8113) PLA-8112, Relief Request 4RR-11 Relief from End of Interval Boundary Leakage Test PLA-81122024-04-0909 April 2024 Relief Request 4RR-11 Relief from End of Interval Boundary Leakage Test PLA-8112 PLA-8110, Submittal of Unit 1 Cycle 24 Core Operating License Report (Pla 8110)2024-04-0404 April 2024 Submittal of Unit 1 Cycle 24 Core Operating License Report (Pla 8110) PLA-8100, Property Insurance Program (PLA-8100)2024-04-0101 April 2024 Property Insurance Program (PLA-8100) ML24092A4022024-04-0101 April 2024 Annual Financial Report (PLA-8098) PLA-8109, Supplement to Request for Exemption from Certain Requirements of 10 CR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance (PLA-8109)2024-03-21021 March 2024 Supplement to Request for Exemption from Certain Requirements of 10 CR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance (PLA-8109) ML24067A2512024-03-19019 March 2024 Authorized Alternative to Requirements of the ASME Code PLA-8107, Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance2024-03-19019 March 2024 Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance ML24044A2532024-03-14014 March 2024 Associated Independent Spent Fuel Storage Installation – Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0077 (Security Notifications, Reports, and Recordkeeping & Suspicious Activity Reporting)) IR 05000387/20240112024-02-29029 February 2024 Commercial Grade Dedication Inspection Report 05000387/2024011 and 05000388/2024011 IR 05000387/20230062024-02-28028 February 2024 Annual Assessment Letter for Susquehanna Steam Electric Station, Units 1 and 2 (Reports 05000387/2023006 and 05000388/2023006) ML24039A1882024-02-27027 February 2024 Issuance of Amendment Nos. 286 and 270 Changes to Technical Specifications for Control Rods ML24037A3072024-02-22022 February 2024 Summary of Regulatory Audit in Support of Relief Request 5RR-02 PLA-8099, Proof of Financial Protection and Guarantee of Payment of Deferred Premiums (PLA-8099)2024-02-13013 February 2024 Proof of Financial Protection and Guarantee of Payment of Deferred Premiums (PLA-8099) IR 05000387/20230042024-02-0707 February 2024 Integrated Inspection Report 05000387/2023004 and 05000388/2023004 05000387/LER-2023-004, Manual Reactor Scram Due to Degraded Main Condenser Vacuum2024-01-0909 January 2024 Manual Reactor Scram Due to Degraded Main Condenser Vacuum PLA-8096, Response to Request for Additional Information Regarding Proposed Relief Request for the Fifth 10-Year Inservice Test Program Interval2024-01-0404 January 2024 Response to Request for Additional Information Regarding Proposed Relief Request for the Fifth 10-Year Inservice Test Program Interval PLA-8077, Emergency Plan Revision 67 (PLA-8077)2023-12-27027 December 2023 Emergency Plan Revision 67 (PLA-8077) IR 05000387/20230102023-12-11011 December 2023 Fire Protection Team Inspection Report 05000387/2023010 and 05000388/2023010 PLA-8088, Request for Exemption from Enhanced Weapons, Firearms Background Checks and Security Event Notifications Implementation (PLA-8088)2023-12-0505 December 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks and Security Event Notifications Implementation (PLA-8088) 2024-09-06
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REGULATORY INFORMATION DISTRIBUTION SYSTEM (RID DISTRIBUTION FQR INCOMING MATERIAL 50-3 eS REC: GRIER B H ORG: CURTIS N W DOCDATE: 04j'17/78
'RC PA PNR 8. LIGHT DATE RCVD: 05J04f78 DOCTYPE: LETTER NOTARIZED: NO COPIES RECEIVED
SUBJECT:
LTR 1 ENCL 0 FURNISHING INFQ RE CONSTRUCTION DEFICIENCY REPT CONCERNING WESTINGHOUSE SUPPLIED MEDIUM VOLTAGES METAL CLAD SWITCHGEAR WHICH MAY NOT BE FULLY CAPABLE OF WITHSTANDING THE POSTULATED SEISMIC EVENT FOR SUB JECT FACILITY... ADVISING REQUIRED DEFINITIVE REPT WI PLANT NAME:SUSQUEHANNA UNIT REVIEWER INITIAL: X JM SUSQUEHANNA' UNIT 2 DISTRIBUTER INITIAL:~~
DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS ++++<%%%+<+<<<+<<+
CONSTRUCTION DEFICIENCY REPORT < 10CFR50. 55(E).
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r' \ LIP TWO NORTH NINTH STREET, ALLENTOWN, PA. 'I 8101 PHONE: (215) 821-5151 NORMAN W. CURTIS Vice President Engineering 8 Construction c<< C~
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@err M Mr. Boyce H. Grier Director, Region I ff$ X U.S. Nuclear Regulatory Comhtission CA 631 Park Avenue King of Prussia, Pennsylvania 19406 SUSQUEHANNA STEAM ELECTRIC STATION INTERIM REPORT OF REPORTABLE DEFICIENCY
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REGARDING POTENTIAL TRANSFORMERS ON 4.16KV SWITCHGEAR DOCKET NOS 50 387 g'0 388
~i g'/gg LICENSE NOSI CPPR-101, CPPR-102 ERs 100450/100508 FILE 840-4 PLA-246 Dear M . Griers This relates to a reportable deficiency, under the provision of 10CFR 50.55(e),
which was. identified to Mx' A Toth NRCg Region I by Mr. A. R. Sabol, PPGL during a'elephone conversation on 3/31/78. The deficiency involves Westing-house supplied medium voltage, metal clad switchgear which may not be fully capable of withstanding the postulated seismic event for the Susquehanna plant.
Z Specifically, Westinghouse C
has advised that, the potential transformer secondary disconnecting contact assemblies on equipment similar to that supplied for Susquehanna have failed to withstand recent seismic tests. Westinghouse further stated that, under seismic conditions, it is possible that the secondary contacts could be dislodged from their normal positions causing open circuiting or shorting of the secondary circuits.
It has been established that eight of the sixteen units, purchased for use in safety related applications, have been shipped to the SSES plant site. To preclude installation of this equipment, Bechtel has identified (3/16/78) these eight units in a QA Stop Work Report (No. 78-06) as being nonconforming. As a result, Bechtel QC has written a Nonconformance Report (NCR No. 2514) and each switchgear unit has had a "Hold Tag" attached.
Bechtel Engineering has reviewed the system design and they have concluded that the worst condition exists with the loss, on each switchgear bus, of the potential transformers on both incoming feeders coupled with the loss of one, or both, of the bus voltage monitoring transformers.
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Mr. Boyce pi. Grier 2 April 17'978 Under this condition, the incoming bus feeders from the safeguard transformers would be automatically disconnected and the diesel generator power source connected restoring power to the bus.
The feeder breakers supplying power to the shutdown loads are normally open.
A LOCA occurring during or after the postulated seismic event would initiate a closing signal to the motor feeder breakers of the shutdown loads, i.e. RHR and Core Spray Pumps.
These feeder breakers would close and immediately trip due to the false undervoltage indication as sensed by the undervoltage relay. The circuit breakers would be unable to close again because of 'the permanent undervoltage trip signal imposed on them.
The above analysis assumes that the failures concurrently occur on all'redundant switchgear buses.
Bechtel Engineering has further concluded that this loss of capability to supply power to shutdown equipment under a LOCA constitutes a safety hazard to the operation of the plant and represents a deficiency in final design.
As proposed remedial action, Westinghouse has advised that modification kits are available which, when installed, would eliminate the faulty secondary dis-connecting assemblies from the circuit. This is accomplished by hard wiring
'the secondary to the load circuits. Bechtel Engineering is considering the use of these modification kits pending assurance from Westinghouse that this modi-fication will meet all the requirements of the technical specification.
We anticipate submittal of the required definitive report of the deficiency by 7/31/78.
Very truly yours, N. W. Curtis Vice President-Engineering 6 Construction
$ 6iG/ARS: mcb cc: Ms. M. C. Bar to N4 Mr. H. F. Lilligh Bechtel SSES Mr. N. W. Curtis N4 Mr. E. M. Mead N5 Mr. R. L. Emery N4 Mr. M. R. Muir Bechtel SFHO Mr. J. W. Geiling N5 Mr. J. R. Schmiedel Bechtel SFHO Mr. J. D. Green SSES Mr. R. J. Shovlin N4 Mr. H. L. Harris SSES SpsE Correspondence File N3 Mr. Jo To Kauffman TW16 Susquehanna Letter File N3