Similar Documents at Salem |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0261998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 1.With 990115 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr ML18106A9831998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With 981214 Ltr ML18106A9801998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With 981214 Ltr ML18106A9641998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with 981112 Ltr ML18106A9631998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with 981112 Ltr ML18106A9151998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With 981012 Ltr ML18106A9131998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With 981012 Ltr ML18106A8751998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With 980915 Ltr ML18106A8741998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Unit 1.With 980915 Ltr ML18106A8161998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 1. W/980817 Ltr ML18106A8151998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 2. W/980817 Ltr ML18106A7151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 2. W/980715 Ltr ML18106A7141998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr ML18106A6541998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 1. W/980615 Ltr ML18106A6531998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 2. W/980615 Ltr ML18106A6121998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 1.W/980515 Ltr ML18106A6111998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Unit 2. W/980515 Ltr ML18106A5561998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem,Unit 1. W/980415 Ltr ML18106A4591998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem Unit 2. W/980415 Ltr ML18106A3771998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 1.W/980316 Ltr ML18106A3761998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 2.W/980316 Ltr ML18106A3281998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 2. W/980217 Ltr ML18106A3271998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 1. W/980217 Ltr ML18106A2721997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem,Unit 2. W/980115 Ltr ML18106A2711997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem Generating Station,Unit 1.W/980115 Ltr ML18106A2081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 1. W/971212 Ltr ML18106A2071997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 2. W/971212 Ltr ML18102B6811997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/ 971117 Ltr ML18102B6801997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/ 971117 Ltr ML18102B6271997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Salem,Unit 2. W/971015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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- ' Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit January 13, 1995 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn.: Document Control Desk MONTHLY OPERATING REPORT SALEMNO. 2 DOCKET NO: 50-311 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of December are being sent to you. The following sections are included:
RH:vls Enclosures C Mr. Thomas T. Martin Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions 10CFR50.59 Evaluations Operating Summary Refueling Information John C. Summers General Manager -Salem Operations Regional Administrator USNRC, Region I 631 Park Avenue King of Prussia, PA 19046 8-1-7.R4 r -*
- 9*501-2303-oa 941231--------\ PDR ADOCK 05000311 R. _ . . PDR The power is in your hands.
- AVERAGE DAILY UNIT POWER LEVEL 1
- Docket No.: 50-311 Unit Name: Salem #2 Date: 1-10-95 Completed by: Mike Morroni Telephone:
339-5142 Month December 1994 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 6 O* 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0 31 0 16 0 P. 8.1-7 Rl
- Docket No: Date: Completed by: Mike Morroni Telephone:
Operating Status 1. unit Name *Salem No. 2 Notes 2. Reporting Period December 1994 3. Licensed Thermal Power (MWt) 3411 4. Nameplate Rating (Gross MWe) 1170 5*. Design Electrical Rating (Net MWe) 1115 6. Maximum Dependable Capacity(Gross MWe) 1149 7. Maximum Dependable Capacity (Net MWe) 1106 8. If Changes Occur in Capacity Ratings (items 3 through 7) Report, Give Reason N A. 9. Power Level to Which Restricted, if any (Net MWe) 10. Reasons for Restrictions, if any 11. Hours in Reporting Period 12. No. of Hrs. Rx. was Critical 13. Reactor Reserve Shutdown Hrs. 14. Hours Generator On-Line 15. Unit Reserve Shutdown Hours 16. Gross Thermal Energy Generated (MWH) Gross Elec. Energy Generated (MWH) 18. Net Elec. Energy Gen. (MWH) 19. Unit Service Factor 20. Unit Availability Factor 21. Unit Capacity Factor (using MDC Net) 22. Unit Capacity Factor (using DER Net) 23. Unit Forced Outage Rate NA This Month 744 0 0 0 0 0 0 -8818 0 0 0 0 0 Year to Date 8760 6335.7 0 6078. 4 0 18510844.8 5903490 5596267 69.4 69.4 57.8 57.3 10.1 50-311 1/10/95 339-5142 since Last N/A Cumulative 115873 75615.2 0 72967.9 0 180973784.2 76450008 72723544 63.0 63.0 56.7 56.3 21.8 24. Shutdowns scheduled over next 6 months (type, date and duration of each) We are presently in a maintenance and refueling outage. 25. If shutdown at end of Report Period, Estimated Date of Startup: January 13, 1995 8-l-7.R2 NO. DATE 1881 12-01-94 1 F: Forced S: Scheduled DURATION TYPE 1 (HOURS) REASON 2 s 744 c 2 Reason A-Equipment Failure (explain)
B-Maintenance or Test C-Refueling D-Requlatory Restriction UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH DECEMBER 1994 METHOD OF SHUTTING DOWN REACTOR 4 LICENSE EVENT REPORT # --------RC 3 Method: 1-Manual 2-Manual Scram SYSTEM CODE 4 E-Operator Training & License Examination 3-Automatic Scram 4-Continuation of Previous Outage 5-Load Reduction 9-0ther F-Administrative
- G-Operational Error (Explain)
H-Other (Explain)
COMPONENT CODE 5 DOCKET NO.:
UNIT NAME: Salem #2
- DATE: 1-10-95 COMPLETED BY: Mike Morroni TELEPHONE:
CAUSE AND CORRECTIVE ACTION TO PREVENT RECURRENCE FUEL XX NORMAL REFUELING 4 Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report CLER) File CNUREG-0161) 5 Exhibit 1 -Same Source *
- 10CFR50.59 EVALUATIONS MONTH: DECEMBER 1994 DOCKET NO: UNIT NAME: 50-311 SALEM2 01/10/95 DATE: COMPLETED BY: TELEPHONE:
R. HELLER 609-339-5162 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59.
The Station Operations Review Committee has reviewed and concurs with these evaluations.
- 1. Design Change Packages (DCP) 2EC-3342, Pkg. 2 Room Cooler Drain Piping Addition -This DCP provides condensate drain pipe for the Room Cooler (1 VHE35) located in the Auxiliary Building, elevation 84'. The Room cooler drip pan is presently plugged. This DCP proposes to remove the plug and install a 1 inch diameter drain pipe to the floor to the nearest floor drain. This piping does not perform any safety related function and does not affect any equipment that is important to safety. The proposed modification does not alter the design criteria, modes of operation, or function for which the contaminated drain system is currently analyzed.
There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 94-094) 2. DR Use-As-Is:
Safety Evaluations (S/E) S/E -2SJ69 Valve Yoke to Operator Shim Plate Weld, Unit 2 -The 2SJ69 valve yoke to operator adapter plate has a shim plate and weld design that is not per the vendor drawing. The welds and plate have been inspected under seating loads and no cracks or deformation were noted. Pursuant to the requirements of Generic Letter 89-10, a MOY capability evaluation of2SJ69 was performed (system calculation S-2-SJ-MDC-0908).
The results of this analysis indicate that the thrust output of the operator may be capable of failing the welds upon closing the valve. With the valve in the open position, the welded connection is capable of withstanding seismic loading.
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- IOCFR50.59 EVALUATIONS MONTH: DECEMBER 1994 DOCKET NO: UNIT NAME: 50-311 SALEM 2 01/10/95 R.HELLER 609-339-5162 S/E-2C DIG DATE: COMPLETED BY: TELEPHONE:
However, when closed, seismic loading would be superimposed upon the actuator thrust loading which could yield the weld. The 2SJ69 is considered operable for the following reasons: 1.) Inspection of the welded joint showed no visible signs of damage; 2.) Changes to the operating conditions evaluation for the GL 89-10 program have resulted in a decrease in the as-left maximum thrust setting from lbf. To lbf. This results in stress levels being proportionally lowered and decreases the likelihood of the weld failing; 3.) The 2SJ69 is seismically qualified in the open position.
The valve is open during power operations and is exempt from stroke testing at power. The only circumstance for which the valve is closed is the initiation of cold leg recirculation, which is a post LOCA event. The Salem accident analysis does not require the component to endure seismic loading in addition to a LOCA; and 4.) The safety function of2SJ69 is assured since the valve is open and would not be closed unless the plant is in a post LOCA condition.
If the actuator delivers enough thrust to fail the welds, it will already have closed the valve with enough force to wedge the valve closed. (SORC 94-094) 2C Diesel Generator Slow Voltage Buildup During Engine Start -2C Diesel Generator (D/G) failed to achieve rated speed and voltage prior to closing the DIG 4KV output breaker, and failed to achieve rated voltage within 10 seconds. When the breaker was closed, the 4KV Vital Bus, the 230/480 Volt Switchgear and the motor control centers were energized with less than 90% nominal bus voltage. However, all electrical equipment did start/function properly during the Mode-Op loaded sequence.
There are no credible failure modes because: 1.) The 4KV bus did not achieve rated voltage within 10 seconds (2: 4160 volts per UFSAR) but did achieve 4250 volts at T+ 13 seconds I I I * *
- 1 OCFR50.59 EVALUATIONS MONTH: DECEMBER 1994 DOCKET NO: UNIT NAME: 50-311 SALEM 2 01/10/95 R.HELLER 609-339-5162 (Cont'd) DATE: COMPLETED BY: TELEPHONE:
(2:3950 volts per Tech. Spec. 4.8.1.2.D.3.b and 4.8.1.2.d.6.b);
2.) No. 22 Charging Pump and all other auto connected shutdown and emergency loads did start successfully and operated for 2: 5 minutes during Mode-Op tests per Tech. Spec. Requirements above, and 3.) although 2C vital Bus loads were energized prior to T+ 13 seconds from the auto start signal, the loads did have sufficient voltage to perform their safety functions had they been energized at T + 13 seconds. Although the generator voltage buildup was degraded, the 2C DIG can perform its safety functions because: 1.) The voltage regulator returned generator voltage to 90% of nominal (2: 3744 volts) in .::S 2.4 seconds, per Reg. Guide 1. 9 requirements, when the largest load (Service Water Pump) was started. (SORC 94-095) 3. Technical Specification Interpretation (TSI) TSI Tech. Spec. Bases 3.4.10.3 (Unit 2)-POPS -Mass Addition of an ECCS Pump -The Bases of the Technical Specification is being changed to reflect a high head safety injection pump combined with a positive displacement charging pump. This change reflects actual mass addition.
transient assumptions based on actual plant operating procedures and administrative controls for preventing the injection of an intermediate head safety injection pump into a water solid Reactor Coolant System (RCS). The net effect of this change is minimal since the flow of the combined high head safety injection pump and the positive displacement charging pump is equivalent to an intermediate head safety injection pump. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 94-096) r * *
- 10CFR50.59 EVALUATIONS MONTH: DECEMBER 1994 DOCKET NO: UNIT NAME: 50-311 SALEM 2 01/10/95 DATE: COMPLETED BY: TELEPHONE:
R. HELLER 609-339-5162
- 4. Temporary Modifications (T-Mods) T-Mod 94-117 "Salem 2 Pressurizer Safety Valves/PORV Loop Seal" -This T-Mod will re-establish the loop seals for pressurizer safety valves (PR 3, 4 & 5) and possibly the Power Operated Relief Valves (PORV) (PR 1 & 2), in an attempt to stop steam leakage through the PR 3, 4 & 5 valves at normal operating pressure and temperature.
This T-Mod would permit current Salem Unit 2 operation (only in Mode III), with the (water) loop seals formed on both PORVs and all three pressurizer safety valves by temporarily modifying the plant design basis as described in the SAR. The pressurizer safety valves (PR 3, 4 & 5) and PORVs (PR 1 & 2) will be operable with the required lift setpoints along with the POR Vs during Mode III operation.
There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 94-098) ------, I I
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- SALEM GENERATING STATION MONTHLY OPERATING
SUMMARY
-UNIT 2 DECEMBER 1994 SALEM UNIT NO. 2 The Unit remained shutdown throughout the entire period as the 2R8 Refueling Outage activities continued.
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- REFUELING INFORMATION MONTH: DECEMBER 1994 MONTH: DECEMBER 1994
- DOCKET NO: UNIT NAME: DATE: COMPLETED BY: TELEPHONE:
50-311 SALEM2 01/10/95 R.HELLER 609-339-5162
- 1. Refueling information has changed from last month: YES X NO __ 2. Scheduled date for next refueling:
October 14. 1994 3. Scheduled date for restart following refueling:
January 21. 1995 4. a. Will Technical Specification changes or other license amendments be required?
YES NO_A_ NOT DETERMINED TO DATE --b. Has the reload fuel design been reviewed by the Station Operating Review Committee?
YES_X_NO If no, when is it scheduled?
- 5. Scheduled date(s) for submitting proposed licensing action: ___
____ _ 6. Important licensing considerations associated with refueling:
- 7. Number of Fuel Assemblies:
- a. Incore b. In Spent Fuel Storage 8. Present licensed spent fuel storage capacity:
Future spent fuel storage capacity:
- 9. Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
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