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 Issue dateTitleTopic
ML20073R43623 August 1974AO BFAO-50-260/746W:on 740813,HPCI Valve FCV 73-44 Failed to Open & RCIC Failed to Show Speed Indication When Turbine Manually Initiated During Surveillance Testing After Valve Failure.Valve Failure Cause Unknown
ML20084H39930 August 1974AO BFAO-50-260/749W:on 740820,during Routine Surveillance Testing,Valves FCV 64-28G & FCV 64-28L Position Indication Lights Observed Not to Operate as Required.Caused by Minor Corrosive Buildup on Operating Plunger on Green Light
ML20084H4086 September 1974AOs BFAO-50-260/747W & BFAO-50-260/7410W:on 740814 & 21, FCV 1-52 & Fvc 1-27 Outboard Containment Isolation Valves in Steamlines B & D,Respectively,Failed to Open When Manually Actuated.Caused by Foreign Particles
ML20084H41823 August 1974AO BFAO-50-259/7444W:on 740813,during Surveillance Testing, Recirculation Jet Pump Riser Differential Pressure Switch PDIS-68-17 Found to Operate Outside Tech Spec Setpoint Limit.Caused by Switch Contact Malfunction
ML20084H42214 August 1974Telecopy AO BFAO-50-259/7444T:on 740813,during Routine Surveillance Testing,Recirculation Jet Pump Riser Differential Pressure Switch PDIS-68-17 Found to Operate Outside Tech Spec Limits
ML20084H43313 August 1974Telecopy AO BFAO-50-260/746T:on 740813,two HPCI Valve Operators Failed During Routine Startup & RCIC Failed to Reach Rated Flow During Subsequent Required Surveillance Testing.Orderly Shutdown & Pressure Reduction Progressing
ML20084H43821 August 1974AO BFAO-50-260/745W:on 740811,HPCI Exhaust Line Rupture Disc Failed.No Cause or Other Info Stated
ML20084H44620 August 1974AO BFAO-50-260/744W:on 740810,HPCI Isolated Due to Excessive Steam Flow During Manual Start of Hpci.Caused by Spurious Spiking of Pdis Switches Monitoring HPCI Steamflow.Snubbers Added to Instrument Lines & 3 Delay Relays AddedSafe Shutdown
ML20084H45019 August 1974AO BFAO-50-260/743W:on 740809,RHR Pump Discharge Pressure Switch PS-74-19A Found Inoperable During Routine Surveillance Testing.Caused by Disorientation of Actuator Arm for Switch Contacts.Arm Became Wedged
ML20084H45316 August 1974AO BFAO-50-260/742W:on 740808,PdIS-71-1A Observed Indicating Downscale During RCIC Testing.Caused by Reversal of Sensing Lines on PdIS-71-1A.Sensing Lines Reversed on Local Instrument Panel
ML20084H4569 August 1974Telecopy AO BFAO-50-260/742T:on 740808,review of Startup Test Data Disclosed PDIS-71-1A RCIC High Steam Flow Isolation Switch Inoperable.Redundant PDIS71-1B Tested & Found Inoperable
ML20084H4709 August 1974AO BFAO-50-260/741W:on 740730,11 of 14 Seismic Restraints Supporting Yarway Water Columns on Reactor Pressure Vessel Found Inoperable.Caused by Failure to Lubricate Restraints During Factory Assembly.New Restraints Installed
ML20084H47223 August 1974AOs BFAO-50-260/747W & BFAO-50-260/741OW:on 740814 & 21, Valves FCV 1-52 & FCV 1-27 to Steamlines D & B,Respectively, Failed to Open.Other MSIVs Tested & Appear Fully Operational
ML20084H48226 July 1974AO BFAO-7443W:on 740717,MAPLHGR Calculated to Be Above Tech Spec Limits After Completion of Full Set of TIPs
ML20084H4961 July 1974AO BFAO-7442W:on 740621,reactor Scrammed by Low Condenser Vacuum Due to Steam Jet Air Ejector Malfunction.Hpci Sys Failed to Initiate Manually.Caused by Foreign Particles in Oil Sys Contributing to Pilot Valve Seating Failure
ML20084H49922 June 1974Telecopy AO BFAO-7442T:on 740621,addl Attempt to Start HPCI Manually Unsuccessful Following Reactor Trip.Hpci Started on Third Attempt
ML20084H50127 June 1974AO BFAO-7441W:on 740618,during Performance of Surveillance Instruction on Core Spray Sys Loop II Logic,Pumps 1B & 1D Failed to Start.Caused by Bent Contact Arm on Relay.Arm Repaired & Checked for Adequate Wipe
ML20084H50418 June 1974Telecopy AO BFAO-7441T:on 740618,core Spray Sys Logic Relay 14A-K23B Found to Be Inoperable.Cause Not Stated.Relay Repaired Immediately & Retested Satisfactorily
ML20084H50721 June 1974AO BFAO-7440W:on 740614 Radwaste Bldg Vent Monitoring Channel Was Out of Svc for More than 1 H W/O Temporary Monitor.Caused by Failure to Turn on High Voltage on Vent Monitoring Channel Constant Air Monitor After Maint
ML20084H51214 June 1974Telecopy AO BFAO-7440T:on 740614,radwaste Bldg Exhaust Continuous Air Monitor Out of Svc for 1.5 H.No Cause Stated. Bldg Surveys Indicate No Unusual Release
ML20084H51719 June 1974Telecopy AO BFAO-7439W:on 740609,several Manual Starts Attempted Before HPCI Turbine Started.Caused by Failure of Turbine Stop Valve to Open,Possibly Due to Low Operating Oil Pressure or Improperly Working Oil Relay Valve
ML20084H52111 June 1974AO BFAO-7439T:on 740609,difficulty Experienced in Manually Starting HPCI Started After Several Attempts.Hpci Was Not Called Upon for Automatic Start
ML20084H52714 June 1974AO BFAO-7438W:on 740606,main Steamline B Outboard Isolation Valve FCV 1-27 Closed Too Fast.Caused by Low Fluid Level in Dashpot Cylinder Due to Hydraulic Fluid Leaking Past Lower Seals on Valve Dashpot Cylinder
ML20084H5317 June 1974Telecopy AO BFAO-7438T:on 740606,during Startup Test,Main Steam Line B Outboard Oscillation Valve FCV-1-27 Closed Too Fast.No Cause Stated
ML20084H56812 June 1974AO BFAO-7437W:on 740602,switch 2 Failed to Operate at Tech Spec Setting of Greater than or Equal to 378 Inches Above Vessel Zero During Surveillance Testing.No Cause Stated. Switch Readjusted.Testing Frequency to Be Once Every 2 WksReactor Vessel Water Level
ML20084H5744 June 1974Telecopy AO BFAO-7437T:on 740602,reactor Water Level Switch LIS-3-58B Switch 2 Found to Operate Outside Tech Spec Setpoint During Surveillance Testing
ML20084H5773 June 1974Telecopy AO BFAO-7437T:on 740602,reactor Water Level Switch LIS-3-58B,switch 2,found to Operate Outside Tech Spec Setpoint of 378 Inches Above Vessel
ML20084H5837 June 1974AO BFAO-7436W:on 740528,spill of 12,000 Gallons of Potentially Contaminated Water Occurred to Unit 3 Condensate Backwash Receiver Tank Room.Caused by Failure of Procedures to Specify Closing 1-HCV-2-747 Valve After Maint
ML20084H59229 May 1974Telecopy AO BFAO-7436T:on 740528,80,000 Gallons of Condensate Water from Unit 1 Storage Tank Drained Into Pipe Tunnel & Subsequently Into Unit 3 Area.Water Pumped Back Into Unit 2 Sumps
ML20084H6195 June 1974AO BFAO-7435W:on 740526,HPCI Isolated on High Steam Flow & HPCI Inboard Containment Isolation Valve FCV 73-2 Could Not Be Reopened.Cause Unknown.Valve Operator & Motor Replaced & Valve Returned to Svc After Functional Testing
ML20084H62827 May 1974Telecopy AO BFAO-7435T:on 740526,HPCI Isolated on High Steam Flow & Subsequent Attempts to Open Inner HPCI Steam Line Containment Isolation Valve Unsuccessful
ML20084H66130 May 1974AO BFAO-7434W:on 740521,HPCI Pump Discharge Valve FCV 73-44 Discovered Inoperable During Investigation of Ground on 250-volt Dc Sys.Caused by Motor Failure.Motor Replaced,Valve Tested & Returned to Svc
ML20084H66622 May 1974Telecopy AO BFAO-7434T:on 740521,HPCI Injection Valve FCV-73-44 Discovered Inoperable Due to Burned Out Motor. Caused by 250-volt Dc Ground to Valve
ML20084H67430 May 1974AO BFAO-7433W:on 740521,FCO 64-44 Refueling Zone to Standby Gas Treatment Sys Crosstie Damper Failed to Open During Surveillance Test.Caused by Failure of Fsv 64-44 Pilot Solenoid Valve to Operate Due to Grease on Core Pole Face
ML20084H68422 May 1974Telecopy AO BFAO-7433T:on 740521,damper FCV-64-44 Failed to Open During Surveillance Test.Damper Is Refueling Zone Exhaust to Standby Gas Treatment Crosstie Damper
ML20084H68929 May 1974AO BFAO-7420W:on 740519,plant Exceeded ETS Limit of 5 F River Temp Increase.Caused by Natural Difference in Water Temp Between Upstream & Downstream Monitors at 5-foot Depth, Due to Conditions Other than Plant Operations
ML20084H71624 May 1974AO BFAO-7432W:between 740408 & 0514,Unit 2 Turbine Roof Exhaust Not Monitored for Gaseous Release Activity When Exhaust Fans Operated.Caused by Incorrect Assembly of Two Continuous Air Monitors So Sample Bypassed MonitorsTime of Discovery
ML20084H72015 May 1974Telecopy AO BFAO-7432T:turbine Bldg Exhaust Fans Operated Approx 16 Days W/O Continuous Air Monitoring.Caused by Vendor Assembly Error So Air Sample Bypassed All Radiation Detectors
ML20084H72824 May 1974AO BFAO-7431W:on 740514,15 Pipe Hangers on Torus Spray Header Found Failed,Allowing Header to Drop & Rest on Several Drywell Vents.Caused by Deficient Design of Hanger Assembly.Larger Hangers Installed
ML20084H74015 May 1974Telecopy AO BFAO-7431T:on 740514,torus Spray Header Type Hangers Discovered Disconnected During Torus Entry
ML20084H74623 May 1974AO BFAO-7430W:on 740513,reactor Bldg Closed Cooling Water Backup Cooling Water Supply Valve FCV 67-50 Failed to Open. Caused by Plugged Strainer in Water Supply Line.Strainer Changed & Mod Approved
ML20084H75114 May 1974Telecopy AO BFAO-7430T:on 740513,supply Valve FCV-67-50 to Reactor Bldg Closed Cooling Water Found Inoperable.Valve Operator Strainers Cleaned & Valve Tested Satisfactorily
ML20084H75723 May 1974AO BFAO-7429W:on 740513,RHR Isolation Shutdown Cooling Suction Isolation Valve FCV 74-47 & Shutdown Cooling Head Spray Isolation Valve FCV 74-77 Isolated RHR Shutdown Cooling Mode & Tripped Pumps.Caused by Disconnected Spring
ML20084H76214 May 1974Telecopy AO BFAO-7429T:on 740513,spring Found Disconnected on Armature of Isolation Relay 10AK-98B.No Cause Stated. Relay Repaired & Satisfactorily Tested
ML20084H76522 May 1974AO BFAO-7428W:on 740512,torus Spray Valve FCV 74-58 Tripped Out Electrically When Attempt Made to Operate Valve.Caused by Broken Yoke Due to Insufficient Amount of Weld or Overstress of Weld
ML20084H77113 May 1974Telecopy AO BFAO-7428W:on 740512,broken Yoke Found on FCV-74-58 Loop 1 Torus Spray Valve.Investigation Into Cause Continues
ML20084H78617 May 1974AO BFAO-7427W:on 740507,computer Identification Check Revealed Use of Hancock 1-inch 600-psig Forged Stainless Steel Globe Valves in Sys Whose Design Conditions Exceed Vendor pressure-temp Ratings for Valves
ML20084H7917 May 1974Telecopy AO BFAO-7427T:plant Designer Advised That Number of 1-inch Stainless Steel 600-psig Instrument Valves Wrongly Applied on Plants.Investigation Underway
ML20084H79615 May 1974AO BFAO-7426W:on 740505 & 06,Target Rock Main Steam Relief Valve PCV 1-19 Experienced Extended Blowdown.Caused by Leaking Pilot Seat & Burr on Second Stage Stem Insert Guide Sleeve Acting Together
ML20084H8057 May 1974Telecopy AO-BFAO-7426T:on 740505 & 06,safety Relief Valve Slow to Recede Following Reactor Trip & Isolation.Plant Shutdown in Progress.Investigation Continues