ML20084H453

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AO BFAO-50-260/742W:on 740808,PdIS-71-1A Observed Indicating Downscale During RCIC Testing.Caused by Reversal of Sensing Lines on PdIS-71-1A.Sensing Lines Reversed on Local Instrument Panel
ML20084H453
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 08/16/1974
From: Eric Thomas
TENNESSEE VALLEY AUTHORITY
To: Oleary J
US ATOMIC ENERGY COMMISSION (AEC)
Shared Package
ML20084H454 List:
References
NUDOCS 8305040270
Download: ML20084H453 (2)


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e AUG20lN4- s Y!X MIDI Mr. John F. O' Leary, Director b g. "m ME8 d #4 Directorate of Licensing b '[ j Office of Regulation M s. m /

U.S. Atomic Energy Comission 4 Washington, DC 20545  %,Ng,V,.g

Dear Mr. O' Leary:

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TDi!ESSEE VALLEY AUTHORITY - BROWIS FERRY NUCLEAR PLANT UUIT 2 -

DOCKET NO. 50-260 - FACILITY OPERATIIU LICHTSE DPR ABNOTy).L OCCURREICE REIORT BFAO-50-260/742W The enclosed report is to provido details concerning reversal of RCIC stes= flow sensing lines and is submitted in accordance with Appendix A to Regulatory Guide 1.16, Revision 1, October 1973. This event occurred on Browns Ferry Nuclear Plant unit 2 on August 8, 1974 Very truly yours, 7mTESSEE VATJ37 AUTFORITV .

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'N.:ector of Power Production

  • Enclosure CC (Enclosure):

Mr. Homan C. Moseley, Director Region II Regulatory Operations Office, USAEC 230 Peachtree Street, I!W. , Suite 818 Atlanta, Georgia 30303 1

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ABNOR? E OCCURREHCE REPORT Report No.: BFAO-50-260/742W -

Report Date: August 16, 1974 Occurence Date: August 8, 1974 Facility: Browns Ferry Nuclear Plant unit 2 Identification of Occurrence Reversal of RCIC steamflow sensing lines. . ,

Conditions Prior to Occurrence .,

. Reactor was undergoing startup testing at approximately 1-percent power and 150 psig reactor pressure.

Description of Occurrence During RCIC testing at 150 psig, PdIG-71-1A vas observed indicating downscale.

Designation of Annarent cause of Occurrence An inspection of the instrument sensing lines on panel 25-7 revealed that the sensing lines were reversed on PdIS-71-1A.

Analysis of Occurrence Tno resum ant, swa. ten, EdI5-71-13, was LumiivnQ

  • eated cal fs;Jia te ci, crc.tc.

satisfactorily and would have performed its intended function. These switches are part of the isolation logic for the RCIC stecs supply system.

Co'rrective Action -

The sensing lines were reversed on the local instrument panel and during a subsequent RCIC test, EdIS-71-1A'was confirnci to indicate upscale as required.

All instrument lines to differential pressure instruments listed in the technical specifications will be checked for correct installation either by physical inspection or by observation of instrunent response during initial unit.

operation. We expect to have this completed by Friday, August 23, 1974.

l Failure Data Not applicable.

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