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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 4011728 August 2003 22:43:00Other Unspec Reqmnt24-Hour Condition of License Report Involving Potential Violation of Maximum Power LevelThis 24-hour report is being made as required by Byron Unit 1 License Condition 2.F and Byron Unit 2 License Condition 2.G as a potential violation of the maximum power level (3586.6 MWt) as stated in Unit 1 and Unit 2 License Condition 2.C(1). On August 28, 2003 at 17:43 CST Byron Station was notified by the ultrasonic flow measurement vendor via letter that there were discrepancies in the ultrasonic flow measurements used in the calorimetric calculation for reactor power. As part of an ongoing testing plan, ultrasonic flow measurements were being taken on the main feedwater system piping header on Byron Unit 1 and were compared to the results from the ultrasonic flow measurement devices on the four individual feedwater lines. Based on the results of the data analysis, and noted signal abnormalities, it was determined that Byron Unit 1 has potentially exceeded its licensed thermal power limit by approximately 1.5%. Based on the results of the testing on Unit 1, the ultrasonic flow measurements on Byron Unit 2 were also investigated. Similar signal abnormalities were identified on one of the four ultrasonic flow measurement devices installed on the individual feedwater lines on Unit 2. Subsequent evaluation indicates that Byron Unit 2 also has potentially exceeded its licensed thermal power limit by approximately 0.6%. The power level on both units was reduced to less than 100% power consistent with feedwater flow as measured directly by the venturis without using the correction factors from the ultrasonic flowmeters. Additional actions regarding investigation of the condition, determination of root cause and corrective action, and determination of the potential actual overpower will be included in the 30-day license event report. The licensee informed the NRC Resident Inspector.Feedwater
ENS 4129929 December 2004 20:00:00Information OnlyLoss of Communications to Site Due to Fiber Optic Line Cut

At approximately 1400 CST all commercial and FTS 2000 telephone communications to and from Byron Station was lost due to a fiber optic cable cut 20 miles North of the plant, near Rockford, Il. Licensee can contact the NRC Headquarters Operation Officer via a Control Room cell phone. NRC Headquarters Operation Officer is unable to call the site using the cell phone because incoming calls are routed through Rockford, Il. Licensee stated that the line problem is being worked on. NRC Resident Inspector has been notified of this event by the licensee.

  • * * Update 12/29/04 at 2139 EST by Koeplin to MacKinnon * * *

Commercial and FTS telephone service returned to service. Licensee will notified the NRC Resident Inspector. R3DO (C. Lipa) & NRR EO (Pat Hiland) notified.

ENS 4145028 February 2005 08:06:00Other Unspec ReqmntDiscovery of After-The-Fact Emergency Condition - Unusual EventThe following information was provided by the licensee via fax (licensee text in quotes): At 1535 (CST) hours on 2/28/05, Byron Station determined that an emergency classification for an Unusual Event was not declared previously at 0206 (CST) on 2/28/05. The missed Unusual Event classification was due to a RCS dose equivalent I-131 value for Byron Unit 1 exceeding the EAL threshold value of >1.0 microCuries/gm (Iodine) for EAL MU7. An RCS iodine sample was taken at 0106 hours on 2/28/05 during shutdown activities for the B1R13 refueling outage. The sample was analyzed and reported back to the Operations shift at 0206 hours with a value of 1.07 microCuries/gm(Iodine). This sample has been reconfirmed. At 0206 on 2/28/05, Byron Unit 1 was not in the mode of applicability for the RCS coolant activity Technical Specification 3.4.16. It was not recognized at that time that the EAL threshold value was exceeded until 1535 hours on 2/28/05. Note that a subsequent RCS sample taken at 0930 on 2/28/05 determined that the EAL threshold value is no longer exceeded and the current value remains less than the threshold. Byron Unit 1 has been operating the current cycle with an estimated 1-3 leaking fuel rods and special limitations were implemented by the site during shutdown. This notification is being made in accordance with the requirements of 10 CFR 50.72(a) for a missed declaration of an Unusual Event for RCS dose EQ I-131 exceeding the EAL threshold value of 1.0 microCuries/gm(Iodine) during shutdown activities for the Byron Unit 1 refueling outage. This issue has been placed in the Byron Corrective Action Program. The licensee will notify the NRC Resident Inspector, State and Local agencies.
ENS 4206319 October 2005 05:57:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Low 2 Steam Generator Water LevelUnit 2 reactor trip on low 2 S/G level. 2A CD/CB (condensate and condensate booster pump set is driven by a single motor) tripped while 2D CD/CB was out of service. The auto turbine runback was unsuccessful and turbine was runbacked manually. ESF actuations: AF (Auxiliary Feedwater) activation and FWI (Feedwater Isolation)." Only indication on the condensate and condensate booster pump trip was an over current flag. All rods fully inserted into the core. Both the motor driven and the diesel driven auxiliary feedwater pumps are operating. All Emergency Core Cooling systems and the Emergency Diesel Generators are fully operable if needed. The NRC Resident Inspector was paged by the licensee.Steam Generator
Feedwater
Emergency Diesel Generator
Auxiliary Feedwater
Emergency Core Cooling System
ENS 4221220 December 2005 23:12:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification - Press ReleaseThis notification is being made in accordance with 10CFR50.72(b)(2)(xi) due to a press release being issued. On 12/19/05 at 14:46 CST, a licensee employee was leaving the station and received a gunshot wound to the left leg/ankle while walking between the Byron Main Access Facility and the Byron Pre Access Facility. Onsite personnel provided first aid assistance, and an offsite ambulance responded to the scene. The injured individual was transported to St. Anthony's Hospital in Rockford, Illinois. The injured individual is in stable condition and is expected to make a full recovery. The Ogle County Sheriff's Office is conducting an investigation into the event. Byron Security Firing Range activities were in progress at the time of the event and were suspended immediately upon notification of the injury. A press release is being issued due to media attention related to this event. The NRC Resident Inspector has been notified, as well as NRC personnel from Region III and NRC Headquarters.
ENS 4237424 February 2006 14:54:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Due to Fire in the Protected Area Not Extinguished within 15 Minutes

At 0836 the control room received a Unit 1B CV/SI pump room fire alarm. An operator reported smoke in the 1B SI pump room at 0840. An unusual event was declared at 0854 due to HU6, fire in the protected area not extinguished within 15 minutes. Sounds of arcing can be heard but flames have not been located. It is suspected that an RWST heater has failed in a pipe tunnel above the 1B SI pump room. The breaker for the RWST heater has been deenergized. The RWST heater pump has been deenergized. Offsite fire department assistance has been requested. The licensee is ventilating the area in order to perform a more thorough inspection of the area and determine the cause of the fire. Both Units1 and 2 remain at 100% reactor power. The NRC Resident Inspector, State and local officials have been notified by the licensee. The NRC has entered the Monitoring Mode at 1036. The NRC Operations Center notified the following organizations: HHS/FDA (V. Howard-King), USDA (Brown), EPA/NRC (Rawls) and DOE (Silva).

  • * * UPDATE FROM MARCHIONDA TO KNOKE AT 12:49 EST ON 02/24/06 * * *

At 11:09 CST on 02/24/06, Byron terminated an Unusual Event that was declared at 08:54 CST today in accordance with HU6 due to a fire in the Protected Area not extinguished within 15 minutes. The RWST (Refueling Water Storage Tank) heater has been confirmed as the source of the smoke that caused the fire alarm. The heater has been deenergized and the area is being ventilated. The NRC exited the Monitoring Response Mode at 12:52 EST. The NRC Resident Inspector and State officials have been notified by the licensee. NRC made notifications to R3DO(Hills), IRD Managers (Leach, Blount, Wilson), NRR EO (Jung), NRR ET (Dyer), HQ PAO (Brenner), R4DO(Pick), DHS (Carledge), FEMA (Liggett), HHS/FDA( Miller), USDA (Byzustek), EPA/NRC (Rawls, Ribordy), and DOE (Silva).

ENS 4245731 March 2006 19:07:00Other Unspec ReqmntLow Tritium Concentration Levels Found Near Underground PipingFollowup information to the February 15, 2006, notification (ENS #42339 (at Braidwood)) involving the discovery of elevated levels of tritium in several vacuum breaker vaults located along the discharge piping to the Rock River. At that time we indicated we planned to install monitoring wells along this pipeline to determine if tritium has migrated from these vaults. Fifteen shallow test wells and eight deeper, more permanent wells were drilled on company property to obtain water samples. Of the 23 wells, two had measurable levels of tritium, however they were well below the Environmental Protection Agency's standard for drinking water (20,000 picocuries per liter). These elevated levels pose no health or safety hazard to the employees or public. Investigation into the source of the elevated tritium levels continues. A press release is planned for the afternoon of March 31, 2006 regarding the results obtained from these monitoring wells. Incident reported according to 10 CFR 50.72 (c)(2) and the licensee notified the NRC Resident Inspector.
ENS 4271218 July 2006 02:46:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessEmergency Evacuation Siren Failures Due to Thunderstorms

Greater than 25% of the emergency sirens have failed due to a severe thunderstorm in the area. The licensee stated that 30 sirens had failed and that restoration activities were currently in progress. The licensee will notify the NRC Resident Inspector.

  • * * UPDATE FROM J. KOEPLIN TO M. RIPLEY 0503 ET 07/18/06 * * *

As of 2317 CDT 07/18/06, the number of inoperable sirens fell below 25% of all sirens with 23 failed sirens not restored to service. Restoration activities remain in progress. The licensee will notify the NRC Resident Inspector. Notified R3 DO (Cameron)

ENS 436935 October 2007 14:30:0010 CFR 26.73, ApplicabilityPositive Fitness for Duty TestA non-licensed employee supervisor had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to Byron, Limerick, Oyster Creek, Peach Bottom, and Three Mile Island has been terminated. Contact the Headquarters Operations Officer for additional details. The licensee will notify the NRC Resident Inspector at the affected plants.
ENS 4373519 October 2007 23:30:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTech Spec Required Shutdown Due to Ultimate Heat Sink Inoperabilitylnitiated Unit 1 and Unit 2 plant shutdown due to inoperability of ultimate heat sink system. The inoperability is due to structural integrity failure of ASME Class 3 piping through wall leakage of the 0C Essential Service Water riser piping of the mechanical draft cooling tower. Licensee is in Technical Specification 3.7.9 which requires the units be in Mode 3 in 6 hours and Mode 5 in 36 hours. The licensee has notified the NRC Resident Inspector.Service water
ENS 4380727 November 2007 15:15:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationAlert Declared Due to Oxygen Deficient Atmosphere

An ALERT was declared at 0915 CST. A nitrogen freeze seal was being used on a 3 inch pipe in the 1B RHR and 1B Containment Spray pump room. A leak developed on the freeze seal jacket. This created an oxygen deficient atmosphere (less than 19.5 percent oxygen). The nitrogen supply was isolated. And the room was evacuated. The alert was declared in accordance with Emergency Action Level (EAL) "hazard alert #7 (HA7)." Additional ventilation was being placed in the area to restore normal oxygen levels. EAL table entry HA7 is for "Release of toxic or flammable gases within or restricting access to a vital area which jeopardizes operation of systems required to maintain safe operations or establish or maintain safe shutdown. No personnel injuries occurred. Oxygen levels were returned to acceptable levels at 0933 CST. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 1205 ON 11/27/2007 FROM PAUL CANTWELL TO MARK ABRAMOVITZ * * *

The ALERT was terminated at 1103 CST. Notified IRD (McDermott), R3DO (Lipa), DHS SWO (Mary Anne), FEMA (Dan Sullivan), DOE (Anthony Parsons), EPA (Ms Ross), USDA (Andrew Watts), and USDA (Rick Turner).

Containment Spray
ENS 4409425 March 2008 23:49:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationLoss of Offsite Power Due to Station Auxiliary Transformer Fault

At 1835 on March 25, 2008, Unit 2 experienced a Loss of Offsite Power. At 1849, an Unusual Event was declared. Station Auxiliary Transformer (SAT) 242-2, Phase C, experienced a Phase Overcurrent. This resulted in an isolation of the SAT, a loss of offsite power, and an automatic Fire Protection deluge of the SAT. No fire was confirmed. All equipment responded as required. The appropriate abnormal operating procedure was entered for event mitigation and is in progress. The Unit 2 Emergency Diesel Generators are supplying required safety-related power. Unit 2 remains at power. The plant is stable and all equipment is functioning as required. The licensee is assessing a cross-tie to Unit 1 which is unaffected by this event and in the refueling mode. The licensee notified the State and local authorities and the NRC Resident Inspector. Notified DHS (Greg Ray), FEMA (Erwin Casto), DOE (Sal Morrone), USDA (Timmons), HHS (Rick Turner), EPA/NRC (Petty Officer Thompson Report #866038).

  • * * UPDATE BY SCOTT PURIN TO NRC AT 2230 EDT ON 3/25/08 * * *

The emergency buses on Unit 2 have been re-energized by offsite power supply sources via Unit 1 SAT. The Unit 2 EDGs have been secured and placed back in standby. The licensee is developing a recovery plan to restore a Unit 2 SAT to supply offsite power to Unit 2 loads. This will require such things as analyzing chemistry samples of the affected SAT transformers and assessing the protective relaying. In addition, some switchyard realignment will be necessary. The licensee is currently in a 72 hour LCO under Tech Spec 3.8.1 for the current electrical alignment. The NRC Resident Inspector is onsite and the NRC Region continues to monitor the situation.

  • * * UPDATE FROM STEVE WIDOLFF TO HOWIE CROUCH AT 0022 EDT ON 3/28/08 * * *

At 2309 (hrs. CDT) on 3/27/08, Byron Unit 2 terminated an Unusual Event that was declared at 18:49 on 3/25/08, in accordance with EAL M.U.1 due to a loss of offsite power to transformers 242-1 and 242-2. Transformer 242-1has been energized from offsite power and is supplying Unit 2 ESF busses 241 and 242. The entry conditions for M.U.1 are no longer met. A press release will be issued. Transformer 242-2 is out of service and isolated for repairs. The licensee notified the NRC Resident Inspector. Notified R3DO (Hills), NRR EO (Ross-Lee), IRD (McDermott), DHS SWO (Doyle), FEMA (Liggett), DOE (Morrone), EPA (Allison), USDA (Timmon) and HHS (Dalziel).

Emergency Diesel Generator
ENS 443844 August 2008 23:45:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of 84 of 94 Emergency Sirens Due to Inclement Weather

At approximately 1830, a severe thunderstorm moved through Ogle County. At 1845, 84 of 94 emergency sirens for Byron Station became inoperable. There is currently no estimated time of repair due to the severe number of power outages. Sirens affected provide coverage for Ogle County (population ~52,000) and a small portion of Winnebago County (population ~296,000). These are utility owned sirens. These sirens are not shared with other sites. In the event of a need for the sirens, a contingency plan using a "route alert" by the state will be implemented. There are no off-site power or grid concerns. The NRC Resident Inspector was notified by the licensee. No other state or local government agencies have been notified by the licensee.

* * * UPDATE ON 8/5/08 AT 0321 FROM GODBY TO SNYDER * * *

Troubleshooting and restoration activities continue for the emergency sirens. Presently 73 of 94 sirens remain inoperable. Notified R3DO (Hills).

  • * * UPDATE AT 0645 ON 8/5/2008 FROM STEVE GODBY TO MARK ABRAMOVITZ * * *

At this time, 44 of the sirens are still inoperable. The licensee estimates that all sirens will be operable by 1800 CDT today. The licensee will notify the NRC Resident Inspector. Notified the R3DO (Hills).

  • * * UPDATE AT 0902 EDT ON 8/5/2008 FROM GREG BALESTRIERI TO MARK ABRAMOVITZ * * *

At 0755 CDT, 55 sirens were inoperable. The licensee will notify the NRC Resident Inspector. Notified the R3DO (Hills).

  • * * UPDATE AT 1258 EDT ON 8/5/2008 FROM GREG BALESTRIERI TO S. SANDIN * * *

At 1155 CDT, 48 sirens were inoperable. The licensee notified the NRC Resident Inspector. Notified the R3DO (Hills).

  • * * UPDATE AT 1713 EDT ON 8/5/2008 FROM GREG BALESTRIERI TO S. SANDIN * * *

At 1500 CDT, 46 sirens were inoperable. The licensee notified the NRC Resident Inspector. Notified the R3DO (Hills).

  • * * UPDATE AT 1933 EDT ON 8/5/2008 FROM JIM LYNDE TO S. SANDIN * * *

Six (6) more sirens have been returned to service. Forty (40) sirens remain inoperable. The licensee notified the NRC Resident Inspector. Notified the R3DO (Hills).

  • * * UPDATE AT 2255 EDT ON 8/5/2008 FROM JIM LYNDE TO J. KOZAL * * *

Seven (7) more sirens have been returned to service. Thirty-three (33) sirens remain inoperable. The licensee notified the NRC Resident Inspector. Notified the R3DO (Hills).

  • * * UPDATE AT 0757 EDT ON 8/6/2008 FROM MARTY WOLFE TO J. ROTTON * * *

As of 0600 CDT on 08/06/08, four (4) more sirens have been returned to service. Twenty-nine (29) sirens remain inoperable with estimate of greater than 24 hours before restoration. The licensee notified the NRC Resident Inspector. Notified the R3DO (Hills).

  • * * UPDATE AT 2345 ON 8/6/2008 FROM BRIAN HERRING TO MARK ABRAMOVITZ * * *

At 2200 CDT 8/6/2008, 17 sirens are still inoperable. The estimated time to repair the remaining sirens is approximately 24 hour. The licensee notified the NRC Resident Inspector. Notified the R3DO (Hills) via e-mail.

* * *  UPDATE AT 1542 ON 8/8/2008 FROM MIKE LINBEMANN TO JOHN KNOKE * * *

As of 1432 CDT on 08/08/08 all emergency sirens for Byron Station are operable. The licensee notified the NRC Resident Inspector. Notified the R3DO (Hills)

ENS 4444328 August 2008 11:15:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to Small Oil Spill Into Intake BayDuring a diver inspection of 0A SX (Essential Service Water) Makeup pump intake structure, hydraulic oil was spilled into the intake bay. The oil was Envirologic 146, a natural ester based hydraulic oil. It is believed a total of approximately 2 gallons of oil leaked from the pump into the intake bay. Approximately 6 inch - 12 inch oil sheen was seen on the Rock River. Oil booms used to capture spilled oil. Oil spill was contained at 0710 CDT. Licensee notified the National Response Center, Illinois Emergency Management Agency, and Ogle county Emergency Services Disaster Agency. The licensee notified the NRC Resident Inspector. National Response Center Report #: 882049
ENS 4490112 March 2009 09:20:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessProcess Computer and Erds Unavailable for Greater than 60 MinutesByron Unit 1 Process Computer was unavailable for use from 0420 to 0814 EDT on 3/12/09. This resulted in a loss of Unit 1's ability to send Emergency Response Data System (ERDS) to the NRC for greater than 60 minutes. The Unit 1 Process Computer and ERDS was restored at 0814 on 3/12/09. Byron's reportabllity procedure defines a loss of ERDS for greater than 60 minutes as being a major loss of emergency preparedness capability. NRC Resident Inspector was notified by licensee. Notified R3DO (Julio Lara)Emergency Response Data System
ENS 4502025 April 2009 15:48:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessErds Unavailability Due to Plant Process Computer FailureThe Unit One Plant Process Computer failed at 1048 CDT. The failure disabled plant data information inputs to the NRC Emergency Response Data System (ERDS). ERDS unavailability was validated by the NRC. ERDS was not restored within one hour, which necessitates this ENS notification per 50.72(b)(3)(xiii). The Plant Process Computer was restored at 1342, which restored ERDS. The NRC Resident Inspector has been notified.Emergency Response Data System
ENS 4505712 May 2009 07:44:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Emergency Assessment Capability

Communication problems between the plant process computer and radiation monitoring system occurred at 0244 CDT. The failure disabled 17% of the plant data information inputs to the NRC Emergency Response Data System (ERDS). ERDS was not restored within one hour, which necessitates this ENS notification per 50.72(b)(3)(xiii). The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM SHANE HARVEY TO JOHN KNOKE AT 1605 ON 05/12/09 * * *

Licensee stated that ERDS has been restored and Emergency Assessment capability is fully operable. The licensee notified the NRC Resident Inspector. Notified R3 (Michael Kunowski).

Emergency Response Data System
ENS 4531431 August 2009 14:45:0010 CFR 26.719, FFD Reporting requirementsFitness for Duty - Licensed Employee Confirmed Positive for AlcoholA licensed employee had a confirmed positive for alcohol during a fitness-for-duty test. The employee's access to the plant has been suspended. Contact the Headquarters Operations Officer for additional details. The licensee notified the NRC Resident Inspector.
ENS 4586719 April 2010 10:03:0010 CFR 50.72(b)(3)(iv)(A), System ActuationRps and Afw Actuation Signals While Shutdown in Mode 4Unit 2 was in Hot Shutdown (Mode 4) for a Refueling Outage. At 0503 (CDT) on April 19, 2010, a valid Lo-Lo Steam Generator level condition occurred during restoration of feedwater system testing. The feedwater test was a planned activity and included isolation of feedwater to the steam generators. During performance of the test, steam generator levels decreased and the Lo-Lo level setpoint was reached on the 2D steam generator. This generated a reactor trip signal and auxiliary feedwater system start signal. Since the Unit was in Hot Shutdown, the reactor trip breakers were already open, and the auxiliary feedwater system was already removed from service when the steam generator water level unintentionally reached the Lo-Lo level setpoint. Additionally, the open steam generator blowdown isolation valves closed as expected at the Lo-Lo steam generator level setpoint. Steam generator level was promptly restored above the Lo-Lo steam generator setpoint. There was no impact on the reactor cooldown that was concurrently in progress as part of the preparation for refueling. Initial screening of the condition determined as not reportable in accordance with 10 CFR 50.72(b)(3)(iv), however, based upon further review it has been determined the condition is reportable. At the time of the event, both trains of shutdown cooling were in service and there were no challenges to offsite power. The licensee was not required to enter any Technical Specification LCO action statements as a result of the event, and the licensee is still investigating the cause of the decrease in steam generator level below the Lo-Lo level setpoint. The licensee has informed the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
Shutdown Cooling
ENS 459711 June 2010 17:39:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Ventilation System Discovered to Be Non-FunctionalAt 1239 CDT on June 1, 2010, Byron Station Technical Support Center (TSC) ventilation (OW25C), filtration system was identified as nonfunctional. This failure affects the ability of the TSC ventilation to maintain adequate radiological habitability in the event of an emergency with an airborne radiological release. All other capabilities of the TSC are unaffected by this emergent condition. Currently, troubleshooting/investigation is being performed. This condition is considered a major loss of emergency assessment capability and is reportable under 10CFR50.72(b)(3)(xiii). The NRC Resident Inspector has been notified.
ENS 4599810 June 2010 13:30:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Ventilation Maintenance

On June 10, 2010, at 0830 hours CDT, Byron Station removed part of the Technical Support Center (TSC) ventilation (I.e., OVV25C) filtration system from service to facilitate necessary maintenance on the makeup fan. This work is expected to last approximately 10 hours. This maintenance affects the ability of the TSC ventilation to maintain adequate radiological habitability in the event of an emergency with an airborne radiological release. If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures. If the TSC becomes uninhabitable, then the Station Emergency Director will relocate the TSC staff to an alternate TSC location in accordance with applicable site procedures. This notification is being made in accordance with 10 CFR 50.72 (b)(3)(xiii) due to the potential loss of an emergency response facility because of the unavailability of the emergency filtration mode of the ventilation system. An update will be provided once the TSC ventilation has been restored to normal operation. The NRC Resident Inspector has been notified.

* * * UPDATE FROM MIKE LINDEMANN TO PETE SNYDER AT 1542 EDT ON 6/10/10 * * * 

Maintenance has been completed and the TSC ventilation system was returned to service as of 1430 CDT. The licensee notified the NRC Resident Inspector. Notified R3DO (Phillips).

ENS 4641612 November 2010 19:00:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionInaccurate Information Provided in License Amendment RequestAt 1300, on November 12, 2010, Exelon Generation Company LLC concluded that inaccurate information contained in the PRA technical bases for a 1987 License Amendment Request (LAR) for Byron and Braidwood Stations would have potentially impacted the acceptability of the LAR by the NRC. The LAR was to extend Allowed Outage Times (AOT) from 72 hours to 7 days for several systems, to include the Component Cooling (CC) and Residual Heat Removal (RH) Systems. The original design intent of the CC system was that each unit has two independent CC pumps and a fifth pump (U0) CC pump could be used as an operable spare for any of the unit specific pumps. This is how CC was modeled in the PRA technical justification for the 1987 LAR. However, a piping configuration design flaw was recently evaluated in that the U0 CC pump could not be considered an operable spare for either unit's B pumps was not modeled in the PRA. During the evaluation to assess the potential significance of this CC design flaw on the PRA justification for the 1987 LAR, another potentially significant discrepancy was discovered in that it appears the operational practice to always split CC trains after a design basis LOCA was not modeled correctly in the RH analysis. Administrative controls have been put in place to restrict the AOT for the CC pumps and RH trains to the pre-LAR timeframe of 72 hours pending the permanent corrective actions. In addition, administrative controls have been put in place to prohibit the U0 CC pump from being an operable spare for either unit's B trains. This event is being reported as an unanalyzed condition that significantly degrades plant safety under 10 CFR 50.72(b)(3)(ii). The NRC Resident Inspectors have been notifiedResidual Heat Removal
ENS 4661414 February 2011 15:20:0010 CFR 26.719, FFD Reporting requirementsFitness for Duty Report Involving a Non-Licensed SupervisorA non-licensed employee supervisor had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been suspended. Contact the Headquarters Operations Officer for additional details. The licensee informed the NRC Resident Inspector.
ENS 4668619 March 2011 13:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedUltrasonic Examination Results in Indications on Two Reactor Head Penetrations

On March 19, 2011, during the Byron Station Unit 1 refueling outage, it was determined that the results of planned ultrasonic (UT) examinations performed on two penetrations of the reactor vessel head would not meet the applicable acceptance criteria. Both require repair prior to returning the vessel head to service. These indications are not in the reactor coolant pressure boundary; however they are very near the toe of the J-groove weld. The examinations were being performed to meet the requirements of 10CFR50.55a(g)(6)(ii)(D) and ASME Code Case N-729-1, to ensure the structural integrity of the reactor vessel head pressure boundary. The UT examinations continue for the remaining head penetrations. All of the penetrations will be examined during the current refueling outage. Repairs are currently being planned and will be competed prior to startup. This is reportable pursuant to 10CFR50.72(b)(3)(ii)(A) since the as found indications did not meet the applicable acceptance criteria referenced in ASME Code Case N-729-1 to remain in-service without repair. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM BLAINE PETERS TO JOHN SHOEMAKER AT 0910 EDT ON 03/30/11 * * *

Ultrasonic examination (made on March 19, 2011) resulted in indications on two reactor head penetrations. As mentioned in Event Notification 46686, reactor vessel head penetrations (In-service inspection) ISI examinations were still in progress. On Wednesday, March 30, 2011, two additional Unit 1 reactor head penetrations were found to contain indications that will require repair prior to returning the reactor head to service. The indications on these two penetrations are within the reactor vessel head pressure boundary. The NRC Resident Inspector has been notified by the licensee. Notified the R3DO (Peterson).

ENS 4670830 March 2011 01:00:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Potential Voiding in Auxiliary Feedwater Alternate Suction LineThe design of the Auxiliary Feedwater (AF) system is for the AF pumps to normally take suction from the condensate storage tank. If the condensate storage tank is not available, the essential service water system provides the alternate supply. Due to the AF system suction piping and valve configuration, a voided section of pipe could exist in the portion that isolates the condensate storage tank supply from the essential service water supply. A preliminary vendor analysis has determined that the void fraction to reach the pump in a dynamic scenario exceeds the acceptance criteria for AF pump operability. Based on past operation in this configuration, the event is being reported as a unanalyzed condition that significantly degrades plant safety and a condition that could have prevented the fulfillment of a safety function (i.e., remove residual heat) under 10CFR50.72(b)(3)(ii) and 10CFR50.72(b)(3)(v). Further review of the void model and pump performance characteristics are planned. In 2011, prior to the completion of this analysis. The void was refilled and verified full for both trains at Byron U1 and U2. Unit 1 is defueled. This condition affects both 'A' and 'B' trains of auxiliary feedwater for both Unit 1 and Unit 2. The NRC Resident Inspector has been notified.Service water
Auxiliary Feedwater
ENS 4727719 September 2011 15:07:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessSpds and Erds Unavailable During Replacement of Plant Process Computer System

At 1007 CDT on September 19, 2011, the Unit 2 Plant Process Computer (PPC) was removed from service for a planned replacement in the current Unit 2 Refueling Outage. The Unit 2 PPC feeds the Safety Parameter Display System (SPDS) used in the Main Control Room (MCR) and the Technical Support Center (TSC). The Unit 2 PPC also feeds the Emergency Response Data System (ERDS). The Unit 1 and Unit 2 PPCs also feed the Plant Parameters Display System (PPDS) used in the MCR, TSC and Emergency Operations Facility (EOF). Meteorological data will remain available. The dose assessment program will remain functional as the Unit 1 PPC will be capable of providing the necessary data through PPDS to run the program. The dose assessment program is not affected by the Unit 2 PPC being out of service. As compensatory measures, a proceduralized backup method to fax or communicate via a phone circuit applicable data to the NRC, TSC, and EOF exists. There is no impact on the Emergency Notification System (ENS) or Health Physics Network (HPN) communication systems. The new Unit 2 PPC is scheduled to be functional on September 25, 2011. However, based on the Mode Unit 2 will be in, this will limit the number of points that would provide usable data. The Unit 2 PPC will be tested as Mode changes occur. The Unit 2 PPC is planned to be declared functional by Mode 2. A follow-up ENS call will be made once the Unit 2 PPC is declared functional. The loss of SPDS and ERDS is a 'major loss of assessment capability' and is reportable under 10CFR50.72(b)(3)(xiii). The NRC Senior Resident Inspector and the State of Illinois (through the Illinois Emergency Management Agency Resident Inspector) have been notified of this ENS call.

  • * * UPDATE ON 10/08/11 AT 2130 EDT FROM WELT TO HUFFMAN * * *

As of 1800 CDT on October 8, 2011, the Unit Two PPC is considered operational with respect to the Safety Parameter Display System (SPDS), Plant Parameter Display System (PPDS) and Emergency Response Data System (ERDS). Therefore, a major loss of assessment capability no longer exists on Unit 2. The Byron EP manager contacted the NRC ERDS Center yesterday on 10/7/11 to conduct an ERDS test for Unit 2 to ensure the data was being satisfactorily sent to the NRC. Unit-1 and Unit-2 ERDS data to NRC was tested satisfactory IAW EP-AA-124-F-01. The NRC Resident Inspector and the State of Illinois (through the Illinois Emergency Management Agency Resident Inspector) have been notified of this ENS update. R3DO (Phillips) notified.

Emergency Response Data System
Safety Parameter Display System
ENS 4762430 January 2012 16:01:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Unusual Event Due to Loss of Offsite Power Greater than 15 Minutes

At 1101 EST, Byron Unit-2 experienced a reactor trip due to RCP undervoltage. All rods fully inserted, MSIV's were manually closed and decay heat is being removed by Auxiliary Feedwater pumps running and steam leaving via atmospheric relief valves. The unit is currently in a natural circulation cooldown with the diesels supplying station emergency loads. Licensee will be cooling the plant down to Mode 5. At 1118 EST, Byron declared an Unusual Event due to a loss of offsite power on Unit 2 from a faulted Station Auxiliary Transformer (SAT). The faulted SAT caused both 6.9 kV and 4.1 kV bus voltage to drop. Smoke was observed coming from the SAT with no visible flames being apparent. This caused bus loads to trip without a complete loss of ESF busses 241 and 242. These buses were manually disconnected from the SAT, which transferred the load to the emergency diesel generators 2A and 2B. Both diesel generators started and loaded without incident. Offsite assistance was requested from the local fire department as a precaution. The licensee is also declaring notification for 10 CFR 50.72(b)(3)(v)(D) Unit 1 is not being affected by this event and remains at 100% power. The licensee has notified the NRC Resident Inspector.

  • * UPDATE FROM GREG BALESTRIERI TO JOHN KNOKE AT 2119 EST ON 01/31/12 * *

At 2000 CST on 1/31/12, Byron terminated their Unusual Event due to the Loss of Offsite Power to Unit 2. Switchyard repairs were completed and offsite power has been restored to essential busses 241 and 242 thru System Auxiliary Transformers 242-1 and 242-2. Unit 2 Emergency Diesel Generators have been shutdown. The licensee is citing classification 10 CFR 50.72(c)(1)(iii) The licensee has notified the NRC Resident Inspector. Notified R3DO (James Cameron), NRR EO (Louise Lund), IRD MOC (Scott Morris), DHS (Konopka) and FEMA (Hollis). Licensee may issue a press release.

Emergency Diesel Generator
Auxiliary Feedwater
ENS 476363 February 2012 06:00:00Other Unspec Reqmnt

VOLUNTARY REPORT - DESIGN VULNERABILITY IN 4.16kV BUS UNDER-VOLTAGE SCHEME

On January 30, 2012, a design vulnerability was discovered at Byron and Braidwood stations in the Engineered Safety Feature 4.16kV bus under-voltage protection scheme for Byron Station Units 1 and 2. Specifically a voltage unbalance created by an open circuit of either the A or C phase from the offsite grid to the System Auxiliary Transformers (SAT) is not designed to actuate the protective relays on the 4.16kV safety bus that provides isolation from the offsite grid and the automatic start and loading of the emergency onsite diesel generators.

Two under-voltage relays are provided on each 4.16kV safety bus, which are combined in a two out of two logic to generate a loss of power signal. The relays are sensing voltage between two phases (i.e., A&B and B&C). An open circuit condition on the C phase or the A phase would not satisfy the two out of two logic. This condition results in both 4.16kV safety buses remaining energized with a bus undervoltage situation and results in equipment protective devices actuating from over-current conditions.

This configuration is a non-conforming condition in that the design of the under-voltage relays and logic was intended to identify degraded grid conditions, not loss of a single phase. With an open circuit on the A or C phase from the grid to the SATs, during normal operations, operators have to diagnose the condition and manually isolate safety buses from offsite power which would automatically start and load the emergency diesel generators. During a design basis event concurrent with an open circuit on A or C phase from the grid to the SATs, analysis performed to date indicates that starting of the ECCS loads would have caused the bus voltage to decrease sufficiently to actuate the under-voltage protective relays and restore cooling with emergency onsite power without challenging fuel design limits.

The 4.16kV safety bus under-voltage protection scheme at Byron and Braidwood is believed to be a typical industry design. This design issue is being evaluated at the other Exelon stations. The results of this evaluation will be shared with the NRC. Therefore, this condition is being reported as a voluntary notification due to its potential generic industry applicability."

The licensee notified the NRC Resident Inspector.

Emergency Diesel Generator
ENS 476446 February 2012 23:19:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Rps Actuation Due to Turbine TripUnit 2 had been connected to the grid at 1431 CST today following a recent forced outage and was in the process of power ascension in accordance with plant procedures. At approximately 25% reactor power (approximately 240 MWe), the operators were transferring main feed flow to the steam generator lower nozzle through the feedwater isolation valves, (i.e. 2FW009A, B, C, D). 2FW009C was the first valve to be opened due to previously experienced problems with this valve being stuck in the seat. No issues were experienced during the opening of 2FW009C. Upon opening of 2FW009C, the 2C steam generator level began to rise as expected. The operators throttled back feedwater flow to control steam generator level. However, the 2C steam generator level increased to the High-High level setpoint of 80.8% (p-14). Since the reactor was below 30% (P-8), no automatic reactor trip signal was generated. However, the turbine automatically tripped, a feedwater isolation signal was initiated, and 2C Main Feedwater pump trip occurred as designed. With no main feedwater flow available, the operators manually tripped the reactor and entry into procedure 2BEP 0, Reactor Trip or Safety Injection Unit 2 was entered. The operators then manually started the 2A and 2B Auxiliary Feedwater pumps to supply water to the steam generators prior to reaching the Low-Low steam generator level setpoint of 36.3%. Transition from 2BEP 0 to 2BEP ES-0.1, Reactor Trip Response, was completed and the emergency procedures were exited. Unit 2 is being maintained in a stable condition in Mode 3. The NRC Resident Inspector has been informed.Steam Generator
Feedwater
Auxiliary Feedwater
ENS 4770828 February 2012 23:31:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unusual Event Due to Loss of Offsite Power

Byron Unit 1 declared an Unusual Event due to a loss of offsite power for greater than 15 minutes (EAL MU-1). The 1A and 1B emergency diesel generators auto-started and automatically restored power to ESF (Engineered Safety Feature) Busses 141 and 142. The 1A Auxiliary Feedwater pump auto-started due to an undervoltage signal to ESF bus 141. The 6.9 KV Busses (Non-ESF) and 4.16 KV Busses (Non-ESF) auto transferred to the Unit Auxiliary Transformers and Unit 1 remained online. The ESF reserve feed breakers are available and in the process of transferring ESF loads over to Unit 2 via the ESF cross-ties. This will allow shutdown of the 1A and 1B diesel-generators and allow alignment to standby status. Switchyard repairs are being initiated. The licensee notified the State of Illinois, Ogle County, Oregon and Byron municipalities and the NRC Resident Inspector. The licensee plans on issuing a news release. Unit 2 remained online and was unaffected throughout the event. Notified Nuclear SSA and NICC vie email.

  • * * UPDATE FROM CHRISTOPHER COTE TO CHARLES TEAL ON 2/29/12 AT 2222 EST * * *

Termination of Unusual Event. Repairs to switchyard components are complete. Offsite power has been restored to Unit One System Auxiliary Transformers. Unit One 4 KV ESF busses have been re-energized from Unit One System Auxiliary Transformers and are no longer cross tied to Unit Two System Auxiliary Transformers. This restores the normal electrical lineup to the ESF busses. The entry conditions for MU-1 are no longer met. The licensee has notified the NRC Resident Inspector, the State of Illinois, Ogle County, Oregon and Byron municipalities. Notified R3DO (Stone), NRR EO (Lee), IRD (Morris), and other FEDS (DHS SWO, DHS NICC, FEMA, and NuclearSSA via email).

Emergency Diesel Generator
Auxiliary Feedwater
ENS 477732 February 2012 02:00:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Report - Invalid System ActuationIn accordance with 10CFR50.73(a)(2)(iv)(A), this telephone notification reports an invalid actuation of the Unit 2 train B (2B) Emergency Diesel Generator (DG) on February 1, 2012, at 2100 hours. At the time of the event, Unit 2 was in Mode 5, Cold Shutdown. The 2B DG was being prepared for an operability surveillance following a planned work window. As part of this surveillance, a chart recorder is installed to monitor key DG parameters to include the DG start signal. When the second lead was connected across the starting relay contact test point, a DC ground alarm was received and the 2B DG started. The engine functioned successfully and as expected, the 2B DG did not automatically connect to its safety bus, since no bus under-voltage signal was present. The cause is attributed to a faulty chart recorder in that an inadvertent ground resulted in the actuation of the starting relay. This condition was entered into the corrective action program. The licensee notified the NRC Resident Inspector.Emergency Diesel Generator
ENS 482785 September 2012 17:25:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification of Sodium Hypochlorite SpillAt 1225 on 9/5/12, the Main Control Room received a report of a Sodium Hypochlorite spill estimated at 100 gallons at the Byron Circulating Water Pump House. The spill was caused by a leak from the hose of the Chemical Delivery truck. A spill of greater than 80 gallons of Sodium Hypochlorite is considered a reportable quantity. The spill was reported to the Illinois Emergency Management Agency (IEMA) in accordance with 29 IAC 430.30 and 35 IAC 750.304, and the National Response Center in accordance with 40 CFR 302.6. Notification to IEMA was performed at 1235 on 9/5/12, and notification to the National Response Center was performed at 1245 on 9/5/12. The notifications to other government agencies is reportable to the NRC in accordance with 10 CFR 50.72(b)(2)(xi). The licensee has notified the NRC Resident Inspector.
ENS 4829010 September 2012 14:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessPlant Process Computer Removed from Service for Maintenance

At 0900 CDT on September 10, 2012, the Unit 1 Plant Process Computer (PPC) was removed from service for a planned replacement in the current Unit 1 Refueling Outage. The Unit 1 PPC feeds the Safety Parameter Display System (SPDS) used in the Main Control Room (MCR) and the Technical Support Center (TSC). The Unit 1 PPC also feeds the Emergency Response Data System (ERDS). The Unit 1 and Unit 2 PPCs also feed the Plant Parameters Display System (PPDS) used in the MCR, TSC and Emergency Operations Facility (EOF). Meteorological data will remain available. The dose assessment program will remain functional as the Unit 2 PPC will be capable of providing the necessary data through PPDS to run the program. The dose assessment program is not affected by the Unit 1 PPC being out of service. As compensatory measures, a proceduralized backup method to fax or communicate via a phone circuit applicable data to the NRC, TSC, and EOF exists. There is no impact on the Emergency Notification System (ENS) or Health Physics Network (HPN) communication systems. The new Unit 1 PPC is scheduled to be functional on September 17, 2012. However, based on the Mode Unit 1 will be in, this will limit the number of points that would provide usable data. The Unit 1 PPC will be tested as Mode changes occur. The Unit 1 PPC is planned to be declared functional by Mode 2. A follow-up ENS call will be made once the Unit 1 PPC is declared functional. The loss of SPDS and ERDS is a 'major loss of assessment capability' and is reportable under 10CFR50.72(b)(3) (xiii). The NRC Senior Resident Inspector and the State of Illinois (through the Illinois Emergency Management Agency Resident Inspector) have been notified of this ENS call.

  • * * UPDATE FROM BRYAN GAPINSKI TO JOHN KNOKE AT 1510 EDT ON 10/03/12 * * *

As of 1245 CDT on October 3,2012, the Unit 1 PPC is considered operational with respect to the Safety Parameter Display System (SPDS), Plant Parameter Display System (PPDS), and Emergency Response Data System (ERDS). Therefore, a major loss of assessment capability no longer exists on Unit 1. The Byron EP manager contacted the NRC ERDS Center on 10/02/2012 to conduct an ERDS test for Unit 1 to ensure the data was being satisfactorily sent to the NRC. Unit 1 and Unit 2 ERDS data to NRC was tested satisfactory lAW EP-AA-124-F�01. The NRC Resident Inspector and the State of Illinois (through the Illinois Emergency Management Agency Resident Inspector) have been notified of this ENS update. Notified the R3DO (Dave Passehl)

ENS 4831115 September 2012 00:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedDegraded Condition Due to Indications on Reactor Vessel Head During Dye Penetrant TestOn September 14, 2012, during the Byron Station Unit 1 refueling outage, it was determined that the results of planned Liquid Penetrant (PT) examinations performed on two previous overlay repairs of the reactor vessel head do not meet applicable acceptance criteria. Both penetrations require repairs prior to returning the vessel head to service. These indications are not in the reactor coolant pressure boundary; however they are very near the previously repaired J-groove weld. The examinations were being performed to meet the requirements of 10 CFR 50.55a(g)(6)(ii)(D) and ASME Code Case N-729-1, to ensure the structural integrity of the reactor vessel head pressure boundary. No ultrasonic indications have been identified at this time. Repairs are currently being planned, which will include buff of the rejectable area and retest, and will be completed prior to returning the vessel head to service. If retest of the rejectable areas is unacceptable, then additional repairs will be required prior to returning the vessel head to service. This condition is reportable pursuant to 10 CFR 50.72(b)(3)(ii)(A) since the as found indications did not meet applicable acceptance criteria referenced in ASME Code Case N-729-1 to remain in-service without repair. Any further examination failures and repairs will be updated under this ENS Notification. The NRC Resident Inspector has been notified. The original indications that led to the two overlay repairs were discovered during ultrasonic testing and were reported to the NRC and assigned EN #46686.05000454/LER-2012-004
ENS 485111 October 2012 20:03:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of Invalid System ActuationIn accordance with 10CFR50.73(a)(2(iv)(A), this telephone notification reports an invalid actuation of the Unit 1 train A (1A) Emergency Diesel Generator (DG) on October 1, 2012, at 1403 hours. At the time of the event Unit 1 was in Mode 5, Cold Shutdown. The 1A DG was undergoing a surveillance procedure that verifies a safety injection override signal when a technician actuated the incorrect under voltage relay which resulted in the inadvertent start of the 1A DG. The engine functioned successfully and ran unloaded, as expected. The cause is attributed to the technicians failing to verify they were actuating the correct relay. This condition was entered into the corrective action program. The licensee notified the NRC Resident Inspector and the Illinois Department of Nuclear Safety.Emergency Diesel Generator
ENS 485727 December 2012 20:35:0010 CFR 26.719, FFD Reporting requirementsFitness for Duty - Employee Had a Confirmed Positive for AlcoholA non-licensed, non-supervisory employee had a confirmed positive for alcohol during a for-cause fitness-for-duty test. The employee's access to the plant has been suspended. The licensee notified the NRC Resident Inspector.
ENS 4883821 March 2013 00:51:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Loss of Generator Stator Cooling WaterAt 1951 CDT on March 20, 2013, Byron Unit 2 Reactor was manually tripped due to the loss of all Generator Stator Cooling Water. 2BEP-0, 'Reactor Trip or Safety Injection Unit 2' was entered and a transition was made to 2BEPES 0.1, 'Reactor Trip Response Unit 2.' The auxiliary feedwater pumps automatically actuated upon the expected low steam generator level. Upon the trip, it was noted that a Digital Rod Position Indication System Urgent Failure occurred with a General Warning on Control Rod position M12. Indication for the Train 'B' Reactor Trip breaker was lost. All Control Rods inserted upon Reactor trip and the Train 'B' Reactor trip breaker was locally verified open. The plant is in its normal shutdown electrical lineup. No safeties or reliefs lifted during the event. There was no impact on unit-1. The licensee notified the NRC Resident Inspector.Steam Generator
Auxiliary Feedwater
Stator Water
Control Rod
ENS 4913720 June 2013 11:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseSulfuric Acid Spill Requiring Offsite NotificationIn the owner controlled area, the plant has a tank of sulfuric acid (93% concentration, UN # 1830) for chemical control of the Circulating Water system used in the non-safety related electrical power production portion of the plant. At 0600 (CDT), a routine inspection of the tank found acid within the berm surrounding the tank. A leak was discovered in the berm and sulfuric acid leaked onto the surrounding area and nearby drainage ditch. The quantity of leaked acid has been estimated to be 120 gallons. The source of the leak has been determined to be a pipe on the tank and it has been isolated with a closed valve. The tank level has been stable for 4 hours. The leaked acid is contained within approximately 70 linear feet of the (limestone) ditch and has not left the site. On-site operations and chemistry personnel are neutralizing the acid with soda ash and a tanker truck was contracted to arrive on site this morning to empty the acid tank contents until a repair can be accomplished. The leak was discovered at 0600 and isolated about 0630 CDT. The licensee notified the NRC Resident Inspector.Circulating Water System
ENS 4913820 June 2013 16:18:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Ventilation Removed from Service for Maintenance

On June 20, 2013 at 1118 CDT, Byron Station removed part of the Technical Support Center (TSC) ventilation (i.e., 0VV23C) system from service to facilitate necessary maintenance on the supply fan. This work is expected to last approximately 2 hours. This maintenance affects the ability of the TSC ventilation to maintain adequate habitability during the duration of an emergency. If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures. If the TSC becomes uninhabitable, the Station Emergency Director will relocate the TSC staff to an alternate TSC location in accordance with applicable procedures. This notification is being made in accordance with 10CFR50.72(b)(3)(xiii) due to the potential loss of an emergency response facility because of the unavailability of the ventilation system. An update will be provided once the TSC ventilation has been restored to normal operation. The NRC Resident Inspector has been notified (by the Licensee).

  • * * UPDATE FROM NICK CRAWFORD TO JOHN SHOEMAKER ON 6/20/13 AT 1635 EDT * * *

Maintenance has been completed and the TSC ventilation system has be restored to service. The licensee will notify the NRC Resident Inspector. Notified R3DO (Daley).

ENS 4937521 September 2013 20:31:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Commercial and Ens Communications Due to an Area Phone OutageAt 1531 CDT, Byron Station was contacted via NARS (Nuclear Accident Reporting System) phone line by the Illinois Emergency Management Agency (IEMA) that an issue exists for the phone systems in the Byron area. Byron subsequently contacted lEMA via the NARS phone and was able to communicate with lEMA. At 1536 CDT, the ENS phone was verified to not be functioning and at 1541 CDT NRC Headquarters was contacted via Byron Main Control Room cell phone to report the failure of the ENS and commercial phones. The Byron Station Main Control Room cell phone is functioning normally. The loss of ENS and commercial phone capability is reportable under 10CFR50.72(b)(3)(xiii). The cause of the loss of phone capability is not known but is under investigation and an update will be provided upon restoration. ERDS has been verified as operable and the licensee is transmitting data. The licensee has notified the NRC Resident Inspector.
ENS 495993 December 2013 04:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center (Tsc) Non-Functional Due to Planned Maintenance

On December 2, 2013, activities are scheduled that will render the Technical Support Center (TSC) non-functional by removing the normal and emergency ventilation system from service. These activities are being performed in support of planned preventive maintenance. In preparation for these normal and emergency ventilation system outages, the TSC emergency responders were notified that if an emergency occurred during this outage the Emergency Coordinator and the TSC staff involved with classification, notification and PARS should report to the Work Execution Center. All other TSC personnel should report to the Operational Support Center. The duration of this TSC outage is expected to be less than 36 hours. The NRC Operations Center will be provided an update to this notification when the TSC normal and emergency ventilation is restored. This 8 hour notification in accordance with 10 CFR 50.72(b)(3)(xiii). The licensee notified the NRC Resident Inspector.

  • * * UPDATE ON 12/4/13 AT 0440 FROM BRIAN LEWIN TO DONG PARK * * *

The TSC is fully functional. The licensee will notify the NRC Resident Inspector. Notified R3DO (Riemer).

ENS 4991915 March 2014 16:02:0010 CFR 50.72(b)(3)(iv)(A), System ActuationMomentary Loss of Shutdown Cooling Due to a Loss of Offsite Power(Unit) 1 experienced a loss of offsite power (LOOP). (Unit) 1 station aux transformers (SATs) tripped. 1A and 1B emergency diesel generators (EDGs) started and properly restored power to ESF (engineered safety feature) bus 141 and 142. Safe shutdown loads (1A/B SX (essential service water) pumps and 1A/B CC (component cooling) pumps) properly started when signaled by the EDG sequencers. The 1A residual heat removal pump was manually restarted at 1105 (CDT) to restore shutdown cooling. There was no impact to RCS temperature. Additionally, a containment isolation signal was actuated when containment radiation monitors which are powered from the ESF buses briefly lost power until restored by the EDGs. All related equipment realigned as expected except for the 0A VC (control room) chiller that didn't start when required on the EDG sequencer. The cause of the LOOP and the 0A VC chiller issue is under investigation. Fuel moves were in progress and stopped safely. All fuel bundles are in a safe location. Unit 2 was not affected and remains in mode 1. The licensee has notified the NRC Resident Inspector.Emergency Diesel Generator
Shutdown Cooling
Residual Heat Removal
ENS 505178 October 2014 00:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedUltrasonic Testing Reveal Degraded Condition on One Control Rod Drive Mechanism PenetrationIn accordance with 10 CFR 50.72(b)(3)(ii)(A), this notification reports a degraded condition on Byron Station Unit 2 that occurred on October 7, 2014, when it was determined that the results of planned ultrasonic testing (UT) examinations performed on one CRDM penetration of the reactor vessel head would not meet the applicable acceptance criteria. Byron Station Unit 2 is presently in day eight of a refueling outage. The examinations were being performed to meet the requirements of 10 CFR 50.55a(g)(6)(ii)(D) and ASME Code Case N-729-1 to ensure the structural integrity of the reactor vessel head pressure boundary. The UT examinations continue for the remaining CRDM head penetrations. The repairs are currently being planned and will be completed prior to unit start-up. The NRC Resident Inspector has been notified of this condition.Control Rod
ENS 508593 March 2015 17:01:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Main Power Transformer Bushing ShortIn accordance with 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A), this notification reports an automatic reactor trip on Byron Unit 1. The trip occurred following a trip of the Byron Unit 1 East Main Power Transformer (MPT). Initial indications appear that the MPT trip was caused by a large (~ 5 foot) section of ice that fell from a bus bar over the 1E MPT. This ice shorted out a MPT bushing, resulting in the unit trip. Reactor operators performed a manual start of the Auxiliary Feedwater System in response to the unit trip. All other safety systems responded as expected. The plant trip occurred at 1101 CST on March 03, 2015. Unit 1 is presently in Mode 3 and stable. Unit 2, the opposite unit, is operating at 100% power and stable. This condition was entered into the Byron CAP Program. An investigation is in progress to determine the extent of required repairs, if any, required prior to unit restart. This event resulted in the actuation of the Reactor Protection System with a subsequent Reactor Trip and therefore, requires notification to the NRC within 4 hours of discovery in accordance with 10 CFR 50.72(b)(2)(iv)(B). This event resulted in the manual actuation of the Auxiliary Feedwater System and therefore, requires notification to the NRC within 8 hours of discovery in accordance with 10 CFR 50.72(b)(3)(iv)(A). This ENS call will be followed up with a Licensee Event Report (LER) within 60 days. All rods inserted during reactor trip, offsite power and emergency power sources are currently available and decay heat is being removed via the startup feedwater systems. No safety relief valves lifted as a result of the transient. The NRC Resident Inspector and the State of Illinois were notified.Feedwater
Reactor Protection System
Auxiliary Feedwater
Safety Relief Valve
ENS 5088112 March 2015 14:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of the Seismic Monitoring Computer

In accordance with 10 CFR 50.72(b)(3)(xiii), this notification reports a loss of Emergency Preparedness assessment capability with the unplanned inoperable condition for the Byron seismic monitor. Specifically, the seismic monitor was declared non-functional at 0345 CST on March 7, 2015 following an unplanned loss of the seismic monitoring central computer. This condition adversely impacted the capability to perform an ALERT EAL (HA4) assessment in accordance with the Radiological Emergency Plan Annex. The loss of assessment capability is reportable to the NRC within 8 hours of the discovery in accordance with 10 CFR 50.72(b)(3)(xiii) The seismic recorder was reset by Plant Engineering at 0440 CST on March 8 2015, which restored the seismic monitoring system to full capability. The unplanned non-functional condition of the seismic monitor was entered into the Byron CAP (Corrective Action) Program when the condition was discovered. Initially it was determined that the condition did not meet the requirements for an ENS notification as it was concluded that it did not substantially impair Byron station's emergency assessment capability in the event of an earthquake. Upon further review, at 0900 CDT on March 12, 2015, it was concluded that an ENS notification was warranted because the monitor was specifically Cited in the Emergency Action Level (EAL) HA4 threshold for identifying an ALERT due to an OBE (Reference procedure EP-AA-1002, Addendum 3, 'Emergency Action Levels for Byron Station'). A follow-up written notification is not required for this notification under 10 CFR 50.73. The NRC Resident Inspector has been notified." The State of Illinois Resident Inspector has been notified.

  • * * UPDATE AT 1144 EDT ON 3/19/15 FROM BRIAN CURRIER TO MARK ABRAMOVITZ * * *

Upon further review of this event for the time period of 3/07/12 through 3/17/15, Byron Station has identified six previous occurrences where the Seismic Monitor was declared non-functional, which impacted the capability to perform an ALERT EAL (HA4) assessment in accordance with the Radiological Emergency Plan Annex. These occurred on November 6, 2014; April17, 2013; January 2, 2013; October 10, 2012; July 18, 2012 and July 9, 2012. The NRC Resident Inspector has been notified. Notified the R3DO (Roach).

ENS 5098816 April 2015 10:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessScheduled Maintenance Affecting Technical Support Center Hvac

On April 16, 2015, Byron Station will remove part of the Technical Support Center (TSC) emergency ventilation system from service to facilitate necessary surveillance work on the fire protection system. This work is expected to last approximately 4 hours. This maintenance affects the ability of the TSC ventilation to maintain adequate habitability during the duration of an emergency. If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures. If the TSC becomes uninhabitable, the Station Emergency Director will relocate the TSC staff to an alternate TSC location in accordance with applicable procedures. This notification is being made in accordance with 10 CFR 50.72(b)(3)(xiii) due to the potential loss of an emergency response facility because of the unavailability of the ventilation system. An update will be provided once the TSC ventilation has been restored to normal operation. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM SHANE HARVEY TO JOHN SHOEMAKER AT 1646 EDT ON 4/16/15 * * *

Maintenance has been completed and the TSC emergency ventilation system was restored to service at 1300 CDT on 4/16/15. The NRC Resident Inspector will be notified. Notified the R3DO (McCraw).

ENS 511194 June 2015 13:39:0010 CFR 26.719, FFD Reporting requirementsFitness-For-Duty Report Involving a Non-Licensed Supervisory EmployeeA non-licensed supervisory employee had a confirmed positive for alcohol during a for-cause fitness-for-duty test. The employee's access to the plant has been suspended. The licensee notified the NRC Resident Inspector.
ENS 5133520 August 2015 22:55:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionCondition That Could Prevent Pressurizer Porv Block Valves from Operating

On 8/20/2015 at 1755 (CDT), a design flaw was discovered with the pressurizer power operated relief valve (PZR PORV) block valve control circuitry. Specifically, the circuit deficiency for which a design basis fire in the Main Control Room (MCR) or cable spreading room could prevent the PZR PORV block valves from being closed from the local control switch at their associated motor control center (MCC). Engineering has reviewed this issue and determined that a potential fire induced ground in the MCR or cable spreading room could clear the associated control power fuses which would prevent the block valves from operating at the local control switch. These valves are considered to form a High/Low pressure interface which requires postulating a proper polarity DC cable to cable fault. Engineering has reviewed the circuit design and cable routing associated with PORVs 1(2)RY455A and 1(2)RY456 and determined that their associated cables are routed with other DC circuit cables in the MCR control board and cable spreading room raceways, such that this postulated fault could potentially cause spurious opening of one of the PORVs even after the control power fuses have been removed as directed by the station abnormal operating procedures for control room inaccessibility. This identified block valve circuit deficiency prevents the credited safe shutdown action of locally closing the block valves to mitigate the spurious operation of a PORV. Hourly fire watches of the affected MCR and cable spreading room fire zones have been implemented. In addition, the MCR is continuously staffed and the affected cable spreading room fire zones are equipped with detection and automatic suppression. This event is being reported under 10CFR50.72(b)(3)(ii)(B) for 'Any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE AT 1816 EDT ON 9/2/2015 FROM BRIAN LEWIN TO MARK ABRAMOVITZ * * *

During the extent of condition review, an additional design deficiency was identified with respect to the PZR PORV and PZR PORV Block valves control circuitry. Specifically, the current mitigating strategy for removing PZR PORV control power fuses does not adequately prevent a PZR PORV from spuriously opening due to fire induced hot short. Furthermore, local actions to close the associated PZR PORV block valve at the motor control center (MCC) may not be effective because the MCC may not have electrical power during the design basis fire. Therefore, the credited safe shutdown action to remove the PZR PORV control power fuses does not prevent the PZR PORV from spuriously opening during design basis fires in some of the upper and lower cable spreading room fire zones. The affected Fire Zones are the same upper and lower spreading rooms previously identified and fire watches of the affected areas remain in place. The NRC Resident Inspector has been notified. Notified the R3DO (Skokowski).

05000454/LER-2015-004
ENS 5140117 September 2015 03:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Seismic Monitoring Instrumentation During Planned MaintenanceAt 2200 CDT on September 16, 2015, Byron Station's Seismic Instrumentation will be removed from service to support an electrical bus outage. During this time, the seismic instrumentation will not be able to generate Main Control Room annunciation or provide ground acceleration information necessary for Emergency Action Level (EAL) threshold determination until the seismic instrumentation is restored, which is scheduled for 1700 CDT on September 19, 2015. Since the duration of maintenance activity may last greater than 72 hours, with viable compensatory measures in place and communicated to applicable Emergency Response Decision Makers, this condition will result in a Loss of Emergency Assessment Capability while the Seismic Instrumentation is out of service and results in a reportable condition in accordance with 10 CFR 50.72(b)(xiii). The Licensee has notified the NRC Resident Inspector and informed the State of Illinois Resident Engineer .
ENS 5141019 September 2015 01:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedReactor Vessel Head Penetration Repair Did Not Meet Acceptance CriteriaOn 9/18/2015 at 20:00 (CDT), during the Byron Station Unit 1 refueling outage, it was determined that the results of a planned Liquid Penetrant (PT) examination performed on a previous overlay repair of the reactor vessel head did not meet applicable acceptance criteria. The penetration requires repairs prior to returning the vessel head to service. These indications are not in the reactor coolant pressure boundary; however they are very near the previously repaired J-groove weld. The examination was being performed to meet the requirements of 10 CFR 50.55a(g)(6)(ii)(D) and ASME Code Case N-729-1, to ensure the structural integrity of the reactor vessel head pressure boundary. No ultrasonic indications have been identified at this time. Repairs are currently being planned in accordance with the ASME Code of Record. The repairs will be completed prior to returning the vessel head to service. This event is being reported under 10 CFR 50.72(b)(3)(ii)(A) for 'Any event or condition that results in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded.' The licensee has notified the NRC Resident Inspector. Per regulatory commitment, Exelon Generation Company, LLC (EGC) is notifying NRC staff of the Division of Component Integrity or its successor, of changes in indication(s) or findings of new indication(s) in the penetration nozzle or J-groove weld beneath a seal weld repair, or new linear indications in the seal weld repair, prior to commencing repair activities. The original indications that led to the overlay repairs were discovered during ultrasonic testing and were reported to the NRC and assigned EN46686 and EN48311.05000454/LER-2015-005