ENS 45902
ENS Event | |
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15:44 May 5, 2010 | |
Title | Automatic Reactor Scram Due To Reactor Feed Pump Trip |
Event Description | On May 5, 2010, at 1144 hours0.0132 days <br />0.318 hours <br />0.00189 weeks <br />4.35292e-4 months <br /> Eastern Daylight Time (EDT), an automatic reactor scram occurred on Unit 1 following a trip of the 1B Reactor Feed Pump (RFP). Following the 1B RFP trip, the reactor recirculation pumps did not run back as expected. The resulting water level shrink caused level in the Reactor Pressure Vessel (RPV) to drop to Low Level 1, causing the activation of the Reactor Protection System (RPS) and the Primary Containment Isolation System (PCIS). All control rods properly inserted.
PCIS Group 2 (i.e., Drywell Equipment and Floor Drain, Residual Heat Removal (RHR) Discharge to Radwaste, and RHR Process Sample), Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems), and Group 8 (i.e., RHR Shutdown Cooling) isolation signals were received on Low Level 1. Actuations of the Primary Containment Isolation Valves (PCIVs) were completed and the affected equipment responded as designed. Due to the expected RPV level reduction following a reactor scram, water level in the RPV momentarily reached Low Level 2. This initiated the High Pressure Coolant Injection (HPCI) System, the Reactor Core Isolation Cooling (RCIC) System, and a partial Group 3 PCIS (i.e., RWCU) isolation. The HPCI and RCIC systems did not inject. The 1-G31-F001 isolated (i.e., inboard isolation) but 1-G31-F004 (i.e., outboard isolation) did not automatically isolate. Based on a preliminary assessment, this response appears to be in accordance with plant design. Further assessments of plant response are on-going to validate plant response. The licensee has notified the NRC Resident Inspector. The scram was uncomplicated. No SRVs lifted. Decay heat removal is via the 'A' feed water pump via the turbine bypass valves to the condenser. The electrical line-up of Unit 1 is normal. Brunswick Unit 2 was not affected. |
Where | |
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Brunswick North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000325/LER-2010-003 |
Time - Person (Reporting Time:+-0.55 h-0.0229 days <br />-0.00327 weeks <br />-7.5339e-4 months <br />) | |
Opened: | Dave Jester 15:11 May 5, 2010 |
NRC Officer: | Eric Simpson |
Last Updated: | May 5, 2010 |
45902 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Shutdown (0 %) |
Brunswick with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 569772024-02-19T04:25:00019 February 2024 04:25:00
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ECCS Discharge Reactor Scram Due to Trip from Neutron Monitoring System ENS 429862006-11-11T17:43:00011 November 2006 17:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scram Due to Conductivity Excursion ENS 429552006-11-01T23:37:0001 November 2006 23:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unit 2 Declared an Unusual Event Due to Loss of Offsite Power to the 4Kv Emergency Buses ENS 418372005-07-13T13:17:00013 July 2005 13:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip/Reactor Trip ENS 415822005-04-09T05:50:0009 April 2005 05:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scrammed from 61% Power Due to Low Reactor Water Level ENS 409542004-08-14T16:59:00014 August 2004 16:59:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Rps Actuation Due to Loss of Offsite Power ENS 402972003-11-04T22:32:0004 November 2003 22:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Brunswick Unit 2 Scram Due to Generator/Turbine Trip 2024-02-19T04:25:00 | |