ENS 53319
ENS Event | |
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12:36 Apr 7, 2018 | |
Title | Automatic Reactor Trip and Pcis Actuation During Stator Cooling System Testing |
Event Description | On April 7, 2018, at 0836 EDT, with Unit 1 in Mode 1 at approximately 100 percent power, the reactor automatically tripped during testing of the stator cooling system. The trip was uncomplicated with all systems responding normally. No safety-related equipment was inoperable at the time of the event. Due to the Reactor Protection System (RPS) actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B).
Operations responded using Emergency Operating Procedures and stabilized the plant in Mode 3. Reactor water level being maintained via normal feedwater system. Decay heat is being removed through the bypass valves. Reactor water level reached low level 1 (LL1) as a result of the reactor trip. The LL1 signal causes a Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves) and Group 8 (i.e., shutdown cooling isolation valves) isolations. The LL1 isolations occurred as designed; the Group 8 valves were closed at the time of the event. Due to the Primary Containment Isolation System (PCIS) actuation, this event is also being reported as an eight-hour, non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the PCIS. Unit 2 was not affected. There was no impact on the health and safety of the public or plant personnel. The safety significance of this event is minimal. The automatic reactor trip was not complicated and all safety-related systems operated as designed. Investigation of the cause of the Reactor Protection System actuation is in progress. The licensee notified the NRC Resident Inspector. |
Where | |
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Brunswick North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.43 h-0.0179 days <br />-0.00256 weeks <br />-5.89014e-4 months <br />) | |
Opened: | Michael Long 12:10 Apr 7, 2018 |
NRC Officer: | Donald Norwood |
Last Updated: | Apr 7, 2018 |
53319 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Shutdown (0 %) |
Brunswick with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 569772024-02-19T04:25:00019 February 2024 04:25:00
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ECCS Discharge Reactor Scram Due to Trip from Neutron Monitoring System ENS 429862006-11-11T17:43:00011 November 2006 17:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scram Due to Conductivity Excursion ENS 429552006-11-01T23:37:0001 November 2006 23:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unit 2 Declared an Unusual Event Due to Loss of Offsite Power to the 4Kv Emergency Buses ENS 418372005-07-13T13:17:00013 July 2005 13:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip/Reactor Trip ENS 415822005-04-09T05:50:0009 April 2005 05:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scrammed from 61% Power Due to Low Reactor Water Level ENS 409542004-08-14T16:59:00014 August 2004 16:59:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Rps Actuation Due to Loss of Offsite Power ENS 402972003-11-04T22:32:0004 November 2003 22:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Brunswick Unit 2 Scram Due to Generator/Turbine Trip 2024-02-19T04:25:00 | |