ENS 42986
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ENS Event | |
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17:43 Nov 11, 2006 | |
Title | Reactor Scram Due to Conductivity Excursion |
Event Description | At 1243 EST, during startup activities, a manual reactor scram was inserted as a result of high conductivity in the condenser. It is believed that the high conductivity was the result of a condenser tube leak. Upon receipt of the conductivity excursion alarm, abnormal operating procedures were consulted and the manual scram was inserted. Unit 2 was at approximately 1 percent of rated thermal power and reactor pressure was approximately 100 psi. At the time of the conductivity excursion, the condensate system was not in service and, as such, reactor water chemistry was not adversely affected. All safety systems operated per design. No emergency core cooling systems (ECCS) actuated.
Unit 2 will be taken to mode 4 and the necessary repairs will be completed. All control rods inserted as expected. The licensee believes there is no spread of high conductivity to adjacent systems (e.g. CRD and the CST). Confirmatory samples are in progress. Decay heat is being removed by RCIC in the pressure control mode with the intention of placing shutdown cooling in-service. The electrical system is in a normal shutdown lineup. The licensee notified the NRC Resident Inspector. |
Where | |
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Brunswick North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-1.2 h-0.05 days <br />-0.00714 weeks <br />-0.00164 months <br />) | |
Opened: | Mark Schall 16:31 Nov 11, 2006 |
NRC Officer: | Jason Kozal |
Last Updated: | Nov 11, 2006 |
42986 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Startup (1 %) |
After | Hot Shutdown (0 %) |
Brunswick with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 569772024-02-19T04:25:00019 February 2024 04:25:00
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