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| #REDIRECT [[05000266/LER-1980-015-01, /01T-1:on 801210,during Refueling Outage Surveillance Testing,Snubber 1-HS-14 on Power Operated Relief Valve Header Was Determined Inoperable.Caused by Low Level in Snubber Reservoir Due to O-ring Seal Leakage]]
| | {{Adams |
| | | number = ML19351F391 |
| | | issue date = 12/23/1980 |
| | | title = /01T-0:on 801210,during Refueling Outage Surveillance Testing of safety-related Shock Suppressors, Snubber 1-HS-14 Found to Be Inoperable.Caused by Low Level in Reservoir,Resulting from Piston Rod O-ring Seal Leakage |
| | | author name = Fay C |
| | | author affiliation = WISCONSIN ELECTRIC POWER CO. |
| | | addressee name = |
| | | addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| | | docket = 05000266 |
| | | license number = |
| | | contact person = |
| | | document report number = LER-80-015-01T, LER-80-15-1T, NUDOCS 8101120367 |
| | | package number = ML19351F371 |
| | | document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT |
| | | page count = 2 |
| | }} |
| | {{LER |
| | | Title = /01T-0:on 801210,during Refueling Outage Surveillance Testing of safety-related Shock Suppressors, Snubber 1-HS-14 Found to Be Inoperable.Caused by Low Level in Reservoir,Resulting from Piston Rod O-ring Seal Leakage |
| | | Plant = |
| | | Reporting criterion = |
| | | Power level = |
| | | Mode = |
| | | Docket = 05000266 |
| | | LER year = 1980 |
| | | LER number = 15 |
| | | LER revision = 1 |
| | | Event date = |
| | | Report date = |
| | | ENS = |
| | | abstract = |
| | }} |
| | |
| | =text= |
| | {{#Wiki_filter:* |
| | NEC FORM 366 U. S. NUCLE A3 CERULATOCY COMMISSION (747) |
| | LICENSEE EV~ ' REPORT CONTROL BLOCK: l l |
| | l l |
| | l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI k |
| | l W l I l P l B l H l 1 l@150 l 01 -l 0 l 0 l 0 l 0 l 0 l-1010 l@l 4 l 1 l1 l 1l 1 l@l l |
| | l@ |
| | F 8 9 LICENSEE CODE 14 LICENSE NuveER 2$ |
| | 26 LICENSE TYPE Jo |
| | $7 CAT $8 CCYT HI] |
| | 1 L l@l 0l 510 l 0 l 0 l 2 l 6 l 6 @l 1l 2 l 110 l 8 l 0 l@l 1l 2l 2 l3 l 810 l@ |
| | 5 uaC 7 |
| | 6 60 61 DOCK ET NUVS E R 68 69 EVENT DATE 74 75 REPORT O ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121lDurina refueline outace surveillance testino of safetv-related shock l |
| | tol2l lsuppressors of Unit 1, according to Technical Specification 15.4.13.2 I |
| | 10141 lon 12/10/80, snubber 1-HS-14 (utility identification), located on the I |
| | l o I s l lpower-operated relief valve header, was determined to be inoperable. |
| | I to161IThis event is reportable accordino to Technical Specification i |
| | 10171Il5.6.9.2.A.9 and similar to LER 78-015/OlT-0, 77-Oll/01T-0. |
| | I l o !s t I l |
| | $O0E C00E SysCODE COMPONENT CODE SusCODE SU E |
| | 10191 |
| | , S I H l @ [_E_j@ W @ I S l U l P I O I R l T lh ( D_J@ l_z_j @ |
| | 7 8 |
| | 9 10 11 12 13 18 19 20 SEQUENTie OCCURRENCE REPORT REVISION v |
| | L EVENTYEAR REPORT NO. |
| | CODE TYPE NO. |
| | O |
| | 'E n AO 18101 |
| | ( _j l0l115l M |
| | l011l lTl l,---J 101 Nu' g,, |
| | _ 21 22 23 24 26 27 28 29 JO 31 32 TAK N A T ON ON PLANT YET HOURS S e eT POR h 8. |
| | SUPPL MANUPACTURER IAl@lzl@ |
| | [ z_j@ |
| | 12l@ |
| | 10 1010 10 I [J_J@ |
| | l Yl@ |
| | lNl@ |
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| | 3J 34 Jb 36 31 40 el 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h litolIThe Grinnel I.D. No. 3146, Figure 200/llK, 2-1/2" x 5" (bore and stroke) l g isnubber was determined to be inoperable due to a low level in its reser-i Ivoir, resulting from piston rod 0-ring seal leakage. |
| | The snubber was l |
| | , 2 g l repaired on 12/10/80, and tested and returned to service on 12/11/80. |
| | I g lSimilar snubbers were checked in accordance with TS 15. 4.13. 2 on 12/11/80. l 7 |
| | 8 9 80 ST S |
| | % POWER OTHER STATUS S |
| | RY DISCOVERY DESCRIPTION l'IsI{,,H_j@ l010l0l@l NA l |
| | lBI@l Surveillance test l |
| | '8 88 CO0 TENT ACTIVITY RELE ASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OP RELEASE L'_LJ 1 z J @ l_z_l@l NA l |
| | l NA I |
| | 7 8 9 10 ft 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE |
| | |
| | ==DESCRIPTION== |
| | [TTT1 I o 101 Ol@l Z l@l l |
| | NA PERSONNE L INJURIES DESCRIPTION @ |
| | NUveER L'_LJ 1010101@l NA l |
| | 7 8 9 11 12 80 P,'E ESC !, TION ''''''" @ |
| | ' " ^" |
| | L' L9J Lz_J@l NA I |
| | l 7 |
| | 8 9 10 80 l,y_j,.o_j NSUE @S'SCaiPTiON @ |
| | 8101120 NRC uSe ONov l NA 3b1 l |
| | lllllllllllll$ |
| | iS 7 |
| | 8 9 10 68 69 80 414/277-2811 |
| | { |
| | C. W. Fay pgoug: |
| | NAME OF PREPARER |
| | |
| | e A |
| | ATTACHMENT TO LICENSEE EVENT REPORT NO. 80-015/01T-0 Wisconsin Electric Power Company Point Beach Nuclear Plant Unit 1 Docket No. 50-266 During refueling outage s rveillance testing of safety-related shock suppressors of Unit 1, in accordance with Technical Specification 15.4.13.2 on December 10, 1980, snubber 1-HS-14 (utility identification), located on the power-operated relief valve header, was found with a low fluid level in its reservoir. |
| | The Grinnel I.D. No. 3146, Figure 200/11k, 2-1/2" x 5" (bore and stroke) snubber was determined to be inoperable due to leakage past the piston rod 0-ring seals. |
| | Snubber 1-HS-14 was repaired on December 10, 1980 and retested satisfactorily on December 11, 1980. |
| | In accordance with Technical Specification 15.4.13.2, an additional 10% |
| | of all snubbers of the same type as 1-HS-14 (one snubber) were inspected. |
| | Snubber 1-HS-18 was inspected with satisfactory results on December 11, 1980. |
| | This event is reportable in accordance with Technical Specification 15.6.9.2.A.9 since remedial action was required to prevent operation in a less conservative manner than that assumed in the safety analysis report. |
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| | l l |
| | I l |
| | l |
| | }} |
| | |
| | {{LER-Nav}} |
LER-1980-015, /01T-0:on 801210,during Refueling Outage Surveillance Testing of safety-related Shock Suppressors, Snubber 1-HS-14 Found to Be Inoperable.Caused by Low Level in Reservoir,Resulting from Piston Rod O-ring Seal Leakage |
| Event date: |
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| Report date: |
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| 2661980015R01 - NRC Website |
|
text
NEC FORM 366 U. S. NUCLE A3 CERULATOCY COMMISSION (747)
LICENSEE EV~ ' REPORT CONTROL BLOCK: l l
l l
l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI k
l W l I l P l B l H l 1 l@150 l 01 -l 0 l 0 l 0 l 0 l 0 l-1010 l@l 4 l 1 l1 l 1l 1 l@l l
l@
F 8 9 LICENSEE CODE 14 LICENSE NuveER 2$
26 LICENSE TYPE Jo
$7 CAT $8 CCYT HI]
1 L l@l 0l 510 l 0 l 0 l 2 l 6 l 6 @l 1l 2 l 110 l 8 l 0 l@l 1l 2l 2 l3 l 810 l@
5 uaC 7
6 60 61 DOCK ET NUVS E R 68 69 EVENT DATE 74 75 REPORT O ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121lDurina refueline outace surveillance testino of safetv-related shock l
tol2l lsuppressors of Unit 1, according to Technical Specification 15.4.13.2 I
10141 lon 12/10/80, snubber 1-HS-14 (utility identification), located on the I
l o I s l lpower-operated relief valve header, was determined to be inoperable.
I to161IThis event is reportable accordino to Technical Specification i
10171Il5.6.9.2.A.9 and similar to LER 78-015/OlT-0, 77-Oll/01T-0.
I l o !s t I l
$O0E C00E SysCODE COMPONENT CODE SusCODE SU E
10191
, S I H l @ [_E_j@ W @ I S l U l P I O I R l T lh ( D_J@ l_z_j @
7 8
9 10 11 12 13 18 19 20 SEQUENTie OCCURRENCE REPORT REVISION v
L EVENTYEAR REPORT NO.
CODE TYPE NO.
O
'E n AO 18101
( _j l0l115l M
l011l lTl l,---J 101 Nu' g,,
_ 21 22 23 24 26 27 28 29 JO 31 32 TAK N A T ON ON PLANT YET HOURS S e eT POR h 8.
SUPPL MANUPACTURER IAl@lzl@
[ z_j@
12l@
10 1010 10 I [J_J@
l Yl@
lNl@
l G l 2 l 5 l 5 l@
3J 34 Jb 36 31 40 el 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h litolIThe Grinnel I.D. No. 3146, Figure 200/llK, 2-1/2" x 5" (bore and stroke) l g isnubber was determined to be inoperable due to a low level in its reser-i Ivoir, resulting from piston rod 0-ring seal leakage.
The snubber was l
, 2 g l repaired on 12/10/80, and tested and returned to service on 12/11/80.
I g lSimilar snubbers were checked in accordance with TS 15. 4.13. 2 on 12/11/80. l 7
8 9 80 ST S
% POWER OTHER STATUS S
RY DISCOVERY DESCRIPTION l'IsI{,,H_j@ l010l0l@l NA l
lBI@l Surveillance test l
'8 88 CO0 TENT ACTIVITY RELE ASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OP RELEASE L'_LJ 1 z J @ l_z_l@l NA l
l NA I
7 8 9 10 ft 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE
DESCRIPTION
[TTT1 I o 101 Ol@l Z l@l l
NA PERSONNE L INJURIES DESCRIPTION @
NUveER L'_LJ 1010101@l NA l
7 8 9 11 12 80 P,'E ESC !, TION '" @
' " ^"
L' L9J Lz_J@l NA I
l 7
8 9 10 80 l,y_j,.o_j NSUE @S'SCaiPTiON @
8101120 NRC uSe ONov l NA 3b1 l
lllllllllllll$
iS 7
8 9 10 68 69 80 414/277-2811
{
C. W. Fay pgoug:
NAME OF PREPARER
e A
ATTACHMENT TO LICENSEE EVENT REPORT NO. 80-015/01T-0 Wisconsin Electric Power Company Point Beach Nuclear Plant Unit 1 Docket No. 50-266 During refueling outage s rveillance testing of safety-related shock suppressors of Unit 1, in accordance with Technical Specification 15.4.13.2 on December 10, 1980, snubber 1-HS-14 (utility identification), located on the power-operated relief valve header, was found with a low fluid level in its reservoir.
The Grinnel I.D. No. 3146, Figure 200/11k, 2-1/2" x 5" (bore and stroke) snubber was determined to be inoperable due to leakage past the piston rod 0-ring seals.
Snubber 1-HS-14 was repaired on December 10, 1980 and retested satisfactorily on December 11, 1980.
In accordance with Technical Specification 15.4.13.2, an additional 10%
of all snubbers of the same type as 1-HS-14 (one snubber) were inspected.
Snubber 1-HS-18 was inspected with satisfactory results on December 11, 1980.
This event is reportable in accordance with Technical Specification 15.6.9.2.A.9 since remedial action was required to prevent operation in a less conservative manner than that assumed in the safety analysis report.
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| 05000266/LER-1980-001-01, /01T-0:on 800202,during Routine Calibr of Pressure Transmitters for Motor Driven Auxiliary Feed Pumps, Transmitter Isolation Block Valves Discovered Closed.Caused by Inadvertent Closing of Isolation Valves.Snubbers Added | /01T-0:on 800202,during Routine Calibr of Pressure Transmitters for Motor Driven Auxiliary Feed Pumps, Transmitter Isolation Block Valves Discovered Closed.Caused by Inadvertent Closing of Isolation Valves.Snubbers Added | | | 05000266/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000301/LER-1980-001-01, /01T-0:on 800221,during Full Power Operation, Momentary Loss of Red Instrument Bus Occurred,Resulting in Power Range Channel N41 Failing Low.Caused by Faulty Capacitor in 2DY01 Power Supply.Capacitor Replaced | /01T-0:on 800221,during Full Power Operation, Momentary Loss of Red Instrument Bus Occurred,Resulting in Power Range Channel N41 Failing Low.Caused by Faulty Capacitor in 2DY01 Power Supply.Capacitor Replaced | | | 05000301/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000301/LER-1980-002-01, /01T-0:on 800227,primary-to-secondary Leak Was Identified in Steam Generator a Resulting in Shutdown of Unit.Caused by Leaking Tube at Position R18C37.Six Defective Tubes Found in Steam Generator a | /01T-0:on 800227,primary-to-secondary Leak Was Identified in Steam Generator a Resulting in Shutdown of Unit.Caused by Leaking Tube at Position R18C37.Six Defective Tubes Found in Steam Generator a | | | 05000266/LER-1980-002, Updated LER 80-002/01T-01:on 800311,during 800 Psi Secondary to Primary Hydrostatic Leak Test,Tubes R23C44 & R8C37 & Plug End R23C50 Found Leaking.Eddy Current Insp Performed.Tube Holes & Leaking Explosive Plugs Were Plug Welde | Updated LER 80-002/01T-01:on 800311,during 800 Psi Secondary to Primary Hydrostatic Leak Test,Tubes R23C44 & R8C37 & Plug End R23C50 Found Leaking.Eddy Current Insp Performed.Tube Holes & Leaking Explosive Plugs Were Plug Welded | | | 05000266/LER-1980-002-01, /01T-0:on 800311,during shutdown,800 Psi secondary-to-primary Hydrostatic Leak Test of B Steam Generator Revealed Tube R23C44 Leaking,Tube R8C37 Wet & Plug End R23C50 Wet.Tube Holes Will Be Weld Plugged | /01T-0:on 800311,during shutdown,800 Psi secondary-to-primary Hydrostatic Leak Test of B Steam Generator Revealed Tube R23C44 Leaking,Tube R8C37 Wet & Plug End R23C50 Wet.Tube Holes Will Be Weld Plugged | | | 05000301/LER-1980-002, Updated LER 80-002/01T-1:on 800227,during Normal Operation, Indication of Increasing primary-to-secondary Leak in a Steam Generator Noted.Caused by Leaking Tube in a Steam Generator Position R18C37 | Updated LER 80-002/01T-1:on 800227,during Normal Operation, Indication of Increasing primary-to-secondary Leak in a Steam Generator Noted.Caused by Leaking Tube in a Steam Generator Position R18C37 | | | 05000266/LER-1980-003, Forwards LER 80-003/03T-0 | Forwards LER 80-003/03T-0 | | | 05000301/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000266/LER-1980-003-03, /03T-0:on 800318,during post-mod Testing of Containment Spray Sys,Relay 1CSB Would Not Latch.Caused by Latching Mechanism Misalignment.Latch Adjusted & Proper Operation Verified on 800318.Similar Relay Bench Tested | /03T-0:on 800318,during post-mod Testing of Containment Spray Sys,Relay 1CSB Would Not Latch.Caused by Latching Mechanism Misalignment.Latch Adjusted & Proper Operation Verified on 800318.Similar Relay Bench Tested | | | 05000301/LER-1980-003-01, /01T-0:on 800408,while Testing Pressurizer Logic Channels,Pressurizer Level Channel 427 Was Momentarily Failed Low by Instrumentation & Control Technicians.Caused by Personnel Error.Event Discussed W/Personnel | /01T-0:on 800408,while Testing Pressurizer Logic Channels,Pressurizer Level Channel 427 Was Momentarily Failed Low by Instrumentation & Control Technicians.Caused by Personnel Error.Event Discussed W/Personnel | | | 05000266/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000301/LER-1980-004-03, /03L-0:on 800417,during Seismic Analysis of as-built safety-related Sys Per IE Bulletin 79-14, Discovered Overstressed Condition in Component Cooling Sys Piping.Caused by Lack of Support Upstream of Juncture | /03L-0:on 800417,during Seismic Analysis of as-built safety-related Sys Per IE Bulletin 79-14, Discovered Overstressed Condition in Component Cooling Sys Piping.Caused by Lack of Support Upstream of Juncture | | | 05000301/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000266/LER-1980-004-03, /03L-0:on 800409,w/plant at Normal Steady State, Emergency Diesel Generator Failed to Start During Routine Surveillance Test.Second Attempt Unsuccessful.Caused by Broken Vane in Starting Air Motor.Air Motor Replaced | /03L-0:on 800409,w/plant at Normal Steady State, Emergency Diesel Generator Failed to Start During Routine Surveillance Test.Second Attempt Unsuccessful.Caused by Broken Vane in Starting Air Motor.Air Motor Replaced | | | 05000266/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000266/LER-1980-005-03, /03L-0:on 800417,during Normal Operation,Review of Security Logs Revealed That Designated Fire Brigade Was Below Min Supervision Requirements on Three Occasions.Caused by Operations Personnel Designation Error | /03L-0:on 800417,during Normal Operation,Review of Security Logs Revealed That Designated Fire Brigade Was Below Min Supervision Requirements on Three Occasions.Caused by Operations Personnel Designation Error | | | 05000301/LER-1980-005-03, /03L-0:on 800609,during Training Walkdown of Safeguards Electrical Supply Cabinets,Noted That Tie Breaker Between AO5 & AO6 Safeguards Buses Was Shut.Probably Caused by Improper Electrical Lineup After Loss of Ac Test | /03L-0:on 800609,during Training Walkdown of Safeguards Electrical Supply Cabinets,Noted That Tie Breaker Between AO5 & AO6 Safeguards Buses Was Shut.Probably Caused by Improper Electrical Lineup After Loss of Ac Test | | | 05000301/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000266/LER-1980-006-03, /03L-0:on 800417,during Analysis of as-built safety-related Piping Sys Per IE Bulletin 79-14,overstressed Condition Discovered in Cooling Sys Piping.Caused by Lack of Support Between Valves Upstream of Juncture | /03L-0:on 800417,during Analysis of as-built safety-related Piping Sys Per IE Bulletin 79-14,overstressed Condition Discovered in Cooling Sys Piping.Caused by Lack of Support Between Valves Upstream of Juncture | | | 05000301/LER-1980-006-01, /01T-0:on 800617,during Safeguards Logic Test W/ One Emergency Diesel Generator Out of Svc,Auto Containment Spray Pump Actuation Threatened During Loss of Ac & high- High Containment Pressure.Caused by Personnel Error | /01T-0:on 800617,during Safeguards Logic Test W/ One Emergency Diesel Generator Out of Svc,Auto Containment Spray Pump Actuation Threatened During Loss of Ac & high- High Containment Pressure.Caused by Personnel Error | | | 05000301/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000266/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000301/LER-1980-007-01, /01T-0:on 800619,at Full Power,Test IT-04 Was Performed W/Emergency Diesel Generator 3D Out of Svc. Emergency Safeguards Train Equipment Would Have Been Inoperable on Loss of Ac Power.Caused by Personnel Error | /01T-0:on 800619,at Full Power,Test IT-04 Was Performed W/Emergency Diesel Generator 3D Out of Svc. Emergency Safeguards Train Equipment Would Have Been Inoperable on Loss of Ac Power.Caused by Personnel Error | | | 05000266/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000266/LER-1980-007-01, /01T-0:on 800611,blue Instrument Bus 1Y02 Was de-energized,resulting in de-energization of 3 Containment Pressure Channels.Caused by Personnel Error.Power Restored & Instrumentation Returned to Normal | /01T-0:on 800611,blue Instrument Bus 1Y02 Was de-energized,resulting in de-energization of 3 Containment Pressure Channels.Caused by Personnel Error.Power Restored & Instrumentation Returned to Normal | | | 05000301/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000266/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000266/LER-1980-008-03, /03L-0:on 800606,during Normal Operation,Testing Revealed That Relay 1-247/AO2X in Train B Would Not Drop Out to Initiate Undervoltage Trip Function.Cause Not Determined. Relay Replaced & Tested Satisfactorily | /03L-0:on 800606,during Normal Operation,Testing Revealed That Relay 1-247/AO2X in Train B Would Not Drop Out to Initiate Undervoltage Trip Function.Cause Not Determined. Relay Replaced & Tested Satisfactorily | | | 05000301/LER-1980-008, Forwards LER 80-008/01T-0 | Forwards LER 80-008/01T-0 | | | 05000301/LER-1980-008-01, /01T-0:on 800912,following Trip from Full Power, Main Steam Stop Valve B Failed to Close Upon Receiving Close Signal.Caused by Deposit Buildup on Valve Shaft &/Or Hardening of Gland Packing | /01T-0:on 800912,following Trip from Full Power, Main Steam Stop Valve B Failed to Close Upon Receiving Close Signal.Caused by Deposit Buildup on Valve Shaft &/Or Hardening of Gland Packing | | | 05000301/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000301/LER-1980-009-03, /03L-0:on 801101,during Normal Operation, Performance of ICP 2.14 Found P8 Permissive Bistable from Channel N44 to Be Set at 50.5%.Caused by Instrument Drift. Bistable Adjusted & Tested Satisfactorily | /03L-0:on 801101,during Normal Operation, Performance of ICP 2.14 Found P8 Permissive Bistable from Channel N44 to Be Set at 50.5%.Caused by Instrument Drift. Bistable Adjusted & Tested Satisfactorily | | | 05000266/LER-1980-009, Forwards LER 80-009/01T-0 | Forwards LER 80-009/01T-0 | | | 05000266/LER-1980-009-01, /01T-0:on 800728 While in Cold Shutdown & During Hydrostatic Leak Test of Steam Generators,Two Dripping Explosive Plugs & Two Wet End Plugs Noted.Cause Not Stated. Dripping Plugs Weld Repaired | /01T-0:on 800728 While in Cold Shutdown & During Hydrostatic Leak Test of Steam Generators,Two Dripping Explosive Plugs & Two Wet End Plugs Noted.Cause Not Stated. Dripping Plugs Weld Repaired | | | 05000266/LER-1980-010-03, /03L-0:on 800827,during Normal Operation,After Redundant Containment Spray Pump Recirculation Phase Suction Valve Maint,Operability Test Was Not Performed.Caused by Personnel Failure to Fully Comprehend Maint Procedures | /03L-0:on 800827,during Normal Operation,After Redundant Containment Spray Pump Recirculation Phase Suction Valve Maint,Operability Test Was Not Performed.Caused by Personnel Failure to Fully Comprehend Maint Procedures | | | 05000266/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000301/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000301/LER-1980-010-03, /03L-0:on 801117,safety Injection Pump 2P15A Motor & Pump Shaft to Coupling Keys Found to Be Sheared.Cause Undetermined.Pump & Motor Checked for Damage,Keys Replaced & Pump Operability Verified | /03L-0:on 801117,safety Injection Pump 2P15A Motor & Pump Shaft to Coupling Keys Found to Be Sheared.Cause Undetermined.Pump & Motor Checked for Damage,Keys Replaced & Pump Operability Verified | | | 05000301/LER-1980-011-03, /03L-0:on 801118,axial Flux Difference Deviated from Target Band.Caused by Improper Interpretation of Tech Specs Resulting in Failure to Lower High Neutron Flux Setpoint.Instruction Clarified | /03L-0:on 801118,axial Flux Difference Deviated from Target Band.Caused by Improper Interpretation of Tech Specs Resulting in Failure to Lower High Neutron Flux Setpoint.Instruction Clarified | | | 05000301/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000266/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000266/LER-1980-011-03, /03L-0:on 800926,found That,Aug 1977-Sept 1980, Containment Spray Sys Spray Additive Valves Were Tested Per ASME Program Requirements Instead of Per Tech Specs.Caused by Administrative Error Re NRC | /03L-0:on 800926,found That,Aug 1977-Sept 1980, Containment Spray Sys Spray Additive Valves Were Tested Per ASME Program Requirements Instead of Per Tech Specs.Caused by Administrative Error Re NRC | | | 05000266/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000266/LER-1980-012-03, /03L-0:on 801005,logs Showed Decrease in Holdup Tank Pressure During 801002-05.Evaluation Showed Leak on Compression Fitting on Inlet to Valve IPCV-1022C.Caused by Improper Reinstallation of Valve After Cleaning | /03L-0:on 801005,logs Showed Decrease in Holdup Tank Pressure During 801002-05.Evaluation Showed Leak on Compression Fitting on Inlet to Valve IPCV-1022C.Caused by Improper Reinstallation of Valve After Cleaning | | | 05000301/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000301/LER-1980-012-03, /03L-0:on 801202,slippage Found in Shaft Driven Seal Water Pump Impeller Resulting in Overheating of Throttle Bushing.Caused by Reduced Seal Water Flow Due to Loosening of Pumping Ring.Shaft Sleeve & Bushing Replaced | /03L-0:on 801202,slippage Found in Shaft Driven Seal Water Pump Impeller Resulting in Overheating of Throttle Bushing.Caused by Reduced Seal Water Flow Due to Loosening of Pumping Ring.Shaft Sleeve & Bushing Replaced | | | 05000266/LER-1980-013, Forwards LER 80-013/01T-0 | Forwards LER 80-013/01T-0 | | | 05000266/LER-1980-013-01, /01T-0:on 801113,suction to 1P4B Boric Acid Transfer Pump Isolated,Rendering Pump Inoperable.Probably Caused by Personnel Error in Returning Valve Lineup to Normal Following Recirculation & Sampling | /01T-0:on 801113,suction to 1P4B Boric Acid Transfer Pump Isolated,Rendering Pump Inoperable.Probably Caused by Personnel Error in Returning Valve Lineup to Normal Following Recirculation & Sampling | |
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