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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES  
                            NUCLEAR REGULATORY COMMISSION
NUCLEAR REGULATORY COMMISSION  
                                              REGION III
REGION III  
                                2443 WARRENVILLE ROAD, SUITE 210
2443 WARRENVILLE ROAD, SUITE 210  
                                        LISLE, IL 60532-4352
LISLE, IL 60532-4352  
                                            August 7, 2012
Mr. Michael J. Pacilio
August 7, 2012  
Senior Vice President, Exelon Generation Company, LLC
President and Chief Nuclear Office (CNO), Exelon Nuclear
4300 Warrenville Road
Warrenville, IL 60555
Mr. Michael J. Pacilio  
SUBJECT:       BYRON STATION, UNITS 1 AND 2, NRC INTEGRATED INSPECTION
Senior Vice President, Exelon Generation Company, LLC  
                REPORT NOS 05000454/2012003; 05000455/2012003; 07200068/2012001
President and Chief Nuclear Office (CNO), Exelon Nuclear  
Dear Mr. Pacilio:
4300 Warrenville Road  
On June 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated
Warrenville, IL 60555  
inspection at your Byron Station, Units 1 and 2. The enclosed inspection report documents the
SUBJECT:  
inspection findings which were discussed at an exit meeting on July 2, 2012, with Mr. T. Tulon
BYRON STATION, UNITS 1 AND 2, NRC INTEGRATED INSPECTION  
and other members of your staff.
REPORT NOS 05000454/2012003; 05000455/2012003; 07200068/2012001  
The inspection examined activities conducted under your license as they relate to safety and
Dear Mr. Pacilio:  
compliance with the Commissions rules and regulations and with the conditions of your license.
On June 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated  
The inspectors reviewed selected procedures and records, observed activities, and interviewed
inspection at your Byron Station, Units 1 and 2. The enclosed inspection report documents the  
personnel.
inspection findings which were discussed at an exit meeting on July 2, 2012, with Mr. T. Tulon  
Two NRC-identified findings of very low safety significance (Green) were identified during
and other members of your staff.  
this inspection. These findings were determined to involve violations of NRC requirements.
The inspection examined activities conducted under your license as they relate to safety and  
The NRC is treating these violations as Non-Cited Violations (NCVs) consistent with
compliance with the Commissions rules and regulations and with the conditions of your license.
Section 2.3.2 of the NRC Enforcement Policy. Additionally, a license-identified violation is
The inspectors reviewed selected procedures and records, observed activities, and interviewed  
listed in Section 4OA7 of this report.
personnel.  
If you contest the subject or severity of an NCV, you should provide a response within 30 days
of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Two NRC-identified findings of very low safety significance (Green) were identified during  
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001,
this inspection. These findings were determined to involve violations of NRC requirements.
with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,
The NRC is treating these violations as Non-Cited Violations (NCVs) consistent with  
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,
Section 2.3.2 of the NRC Enforcement Policy. Additionally, a license-identified violation is  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
listed in Section 4OA7 of this report.  
Office at the Byron Station.
If you contest the subject or severity of an NCV, you should provide a response within 30 days  
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear  
response within 30 days of the date of this inspection report, with the basis for your
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001,  
disagreement, to the Regional Administrator, Region III, and the Resident Inspector Office
with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,  
at the Byron Station.
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector  
Office at the Byron Station.  
If you disagree with a cross-cutting aspect assignment in this report, you should provide a  
response within 30 days of the date of this inspection report, with the basis for your  
disagreement, to the Regional Administrator, Region III, and the Resident Inspector Office  
at the Byron Station.  


M. Pacilio                                   -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
M. Pacilio  
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is
accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public
Electronic Reading Room).
-2-  
                                            Sincerely,
                                            /RA/
                                            Eric R. Duncan, Chief
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its  
                                            Branch 3
enclosure, and your response (if any) will be available electronically for public inspection in the  
                                            Division of Reactor Projects
NRC Public Document Room or from the Publicly Available Records (PARS) component of  
Docket Nos. 50-454, 50-455, and 07200068
NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is  
License Nos. NPF-37 and NPF-66
accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public  
Enclosure:     Inspection Report No. 05000454/2012003; 05000455/2012003; and
Electronic Reading Room).  
              07200068/2012001
Sincerely,  
                w/Attachment: Supplemental Information
cc w/encl:     Distribution via ListServ
/RA/  
Eric R. Duncan, Chief  
Branch 3  
Division of Reactor Projects  
Docket Nos. 50-454, 50-455, and 07200068  
License Nos. NPF-37 and NPF-66  
Enclosure:  
Inspection Report No. 05000454/2012003; 05000455/2012003; and  
07200068/2012001  
  w/Attachment: Supplemental Information  
cc w/encl:  
Distribution via ListServ  


          U. S. NUCLEAR REGULATORY COMMISSION
Enclosure
                          REGION III
Docket Nos:         50-454; 50-455; 07200068
U. S. NUCLEAR REGULATORY COMMISSION  
License Nos:         NPF-37; NPF-66
REGION III  
Report Nos:         05000454/2012003; 05000455/2012003;
Docket Nos:  
                    07200068/2012001
50-454; 50-455; 07200068  
Licensee:           Exelon Generation Company, LLC
License Nos:  
Facility:           Byron Station, Units 1 and 2
NPF-37; NPF-66  
Location:           Byron, IL
Report Nos:  
Dates:               April 1, 2012, through June 30, 2012
05000454/2012003; 05000455/2012003;  
Inspectors:         B. Bartlett, Senior Resident Inspector
07200068/2012001  
                    J. Robbins, Resident Inspector
Licensee:  
                    R. Jickling, Emergency Preparedness Specialist
Exelon Generation Company, LLC  
                    J. Gilliam, Reactor Engineer
Facility:  
                    R. Langstaff, Reactor Engineer
Byron Station, Units 1 and 2  
                    K. Walton, Senior Operations Engineer
Location:  
                    M. Learn, Reactor Engineer
Byron, IL  
                    L. Rodriguez, Reactor Engineer
Dates:  
                    J. Tapp, Health Physicist
April 1, 2012, through June 30, 2012  
                    C. Crisden, Emergency Preparedness Inspector, Region I
Inspectors:  
                    C. Thompson, Resident Inspector, Illinois Emergency
B. Bartlett, Senior Resident Inspector  
                      Management Agency
Approved by:         E. Duncan, Chief
J. Robbins, Resident Inspector  
                    Branch 3
                    Division of Reactor Projects
R. Jickling, Emergency Preparedness Specialist  
                                                                    Enclosure
J. Gilliam, Reactor Engineer  
R. Langstaff, Reactor Engineer  
K. Walton, Senior Operations Engineer
M. Learn, Reactor Engineer  
L. Rodriguez, Reactor Engineer  
J. Tapp, Health Physicist  
C. Crisden, Emergency Preparedness Inspector, Region I  
C. Thompson, Resident Inspector, Illinois Emergency  
  Management Agency  
Approved by:  
E. Duncan, Chief  
Branch 3  
Division of Reactor Projects  


                                          TABLE OF CONTENTS
Enclosure
SUMMARY OF FINDINGS ......................................................................................................... 1
REPORT DETAILS..................................................................................................................... 3
TABLE OF CONTENTS  
Summary of Plant Status......................................................................................................... 3
SUMMARY OF FINDINGS ......................................................................................................... 1  
    1.   REACTOR SAFETY ..................................................................................................... 3
REPORT DETAILS ..................................................................................................................... 3  
      1R01     Adverse Weather Protection (71111.01) ............................................................ 3
Summary of Plant Status......................................................................................................... 3  
      1R04     Equipment Alignment (71111.04) ....................................................................... 4
1.  
      1R05     Fire Protection (71111.05) ................................................................................. 5
REACTOR SAFETY ..................................................................................................... 3  
      1R06     Flooding (71111.06) ........................................................................................... 7
1R01  
      1R11     Licensed Operator Requalification Program (71111.11)..................................... 7
Adverse Weather Protection (71111.01) ............................................................ 3  
      1R12     Maintenance Effectiveness (71111.12) .............................................................. 9
1R04  
      1R13     Maintenance Risk Assessments and Emergent Work Control (71111.13).......... 9
Equipment Alignment (71111.04) ....................................................................... 4  
      1R15     Operability Evaluations (71111.15) .................................................................. 10
1R05  
      1R19     Post Maintenance Testing (71111.19) ............................................................. 13
Fire Protection (71111.05) ................................................................................. 5  
      1R22     Surveillance Testing (71111.22)....................................................................... 14
1R06  
      1EP2     Alert and Notification System Evaluation (71114.02)........................................ 15
Flooding (71111.06) ........................................................................................... 7  
      1EP3     Emergency Response Organization Augmentation Testing (71114.03) ........... 15
1R11  
      1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies
Licensed Operator Requalification Program (71111.11) ..................................... 7  
              (71114.05) ......................................................................................................... 16
1R12  
      1EP6     Drill Evaluation (71114.06) ............................................................................... 16
Maintenance Effectiveness (71111.12) .............................................................. 9  
    2.   OTHER ACTIVITIES .................................................................................................. 17
1R13
      4OA1 Performance Indicator Verification (71151.EP01, EP02, EP03) ....................... 17
Maintenance Risk Assessments and Emergent Work Control (71111.13) .......... 9  
      4OA2 Identification and Resolution of Problems (71152) ........................................... 18
1R15  
      4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153) ............... 24
Operability Evaluations (71111.15) .................................................................. 10  
      4OA5 Other Activities................................................................................................. 24
1R19  
      4OA6 Management Meetings .................................................................................... 26
Post Maintenance Testing (71111.19) ............................................................. 13  
      4OA7 Licensee-Identified Violation ............................................................................ 26
1R22  
SUPPLEMENTAL INFORMATION ............................................................................................. 1
Surveillance Testing (71111.22)....................................................................... 14  
Key Points of Contact.............................................................................................................. 1
1EP2  
List of Items Opened, Closed, and Discussed ......................................................................... 2
Alert and Notification System Evaluation (71114.02) ........................................ 15  
List of Documents Reviewed ................................................................................................... 3
1EP3  
List of Acronymns Used .......................................................................................................... 9
Emergency Response Organization Augmentation Testing (71114.03) ........... 15  
                                                                                                                        Enclosure
1EP5  
Correction of Emergency Preparedness Weaknesses and Deficiencies  
(71114.05) ......................................................................................................... 16  
1EP6  
Drill Evaluation (71114.06) ............................................................................... 16  
2.  
OTHER ACTIVITIES .................................................................................................. 17  
4OA1  
Performance Indicator Verification (71151.EP01, EP02, EP03) ....................... 17  
4OA2  
Identification and Resolution of Problems (71152) ........................................... 18  
4OA3
Follow-up of Events and Notices of Enforcement Discretion (71153) ............... 24  
4OA5  
Other Activities ................................................................................................. 24  
4OA6
Management Meetings .................................................................................... 26  
4OA7  
Licensee-Identified Violation ............................................................................ 26  
SUPPLEMENTAL INFORMATION ............................................................................................. 1  
Key Points of Contact .............................................................................................................. 1  
List of Items Opened, Closed, and Discussed ......................................................................... 2  
List of Documents Reviewed ................................................................................................... 3  
List of Acronymns Used .......................................................................................................... 9  


                                      SUMMARY OF FINDINGS
1
Inspection Report (IR) 05000454/2012003, 05000455/2012003, 07200068/2012001;
Enclosure
04/01/2012 - 06/30/2012; Byron Station, Units 1 & 2; Operability Evaluations; Identification and
SUMMARY OF FINDINGS  
Resolution of Problems.
Inspection Report (IR) 05000454/2012003, 05000455/2012003, 07200068/2012001;  
This report covers a 3-month period of inspection by resident inspectors and announced
04/01/2012 - 06/30/2012; Byron Station, Units 1 & 2; Operability Evaluations; Identification and  
baseline inspections by regional inspectors. Two Green findings were identified by the
Resolution of Problems.  
inspectors. The findings were considered Non-Cited Violations (NCVs) of NRC regulations.
This report covers a 3-month period of inspection by resident inspectors and announced  
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using
baseline inspections by regional inspectors. Two Green findings were identified by the  
Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Assigned
inspectors. The findings were considered Non-Cited Violations (NCVs) of NRC regulations.
cross-cutting aspects were determined using IMC 0310, Components Within the Cross-Cutting
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using  
Areas. Findings for which the SDP does not apply may be Green or be assigned a severity
Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Assigned  
level after NRC management review. The NRCs program for overseeing the safe operation of
cross-cutting aspects were determined using IMC 0310, Components Within the Cross-Cutting  
commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,
Areas. Findings for which the SDP does not apply may be Green or be assigned a severity  
Revision 4, dated December 2006.
level after NRC management review. The NRCs program for overseeing the safe operation of  
A.     NRC-Identified and Self-Revealed Findings
commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,  
        Cornerstone: Initiating Events, Barrier Integrity
Revision 4, dated December 2006.  
        Green. A finding of very low safety significance and an associated NCV of
A.  
        10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,
NRC-Identified and Self-Revealed Findings  
        was identified by the inspectors when licensee personnel failed to identify boric acid
Cornerstone: Initiating Events, Barrier Integrity  
        accumulation that would have impeded flow from the containment leakage detection
Green. A finding of very low safety significance and an associated NCV of  
        trough to the containment sump. The licensee entered this issue into the Corrective
10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,  
        Action Program (CAP) as Issue Report (IR) 1339957. Corrective actions included
was identified by the inspectors when licensee personnel failed to identify boric acid  
        removing the boric acid accumulation from the leakage detection trough and passing
accumulation that would have impeded flow from the containment leakage detection  
        water through the drain to verify associated piping was free of obstruction.
trough to the containment sump. The licensee entered this issue into the Corrective  
        The finding was determined to be more than minor because the finding was similar to
Action Program (CAP) as Issue Report (IR) 1339957. Corrective actions included  
        IMC 0612, Appendix E, Example 4(a). Example 4 focuses on procedural errors. The
removing the boric acid accumulation from the leakage detection trough and passing  
        not minor if section in Example 4(a) discussed that if a later evaluation determines that
water through the drain to verify associated piping was free of obstruction.  
        the safety-related equipment was adversely impacted, it was more than minor. The flow
The finding was determined to be more than minor because the finding was similar to  
        obstruction in the leakage detection trough would have delayed the flow of water to the
IMC 0612, Appendix E, Example 4(a). Example 4 focuses on procedural errors. The  
        sump thereby delaying any subsequent alarm. Therefore, this performance deficiency
not minor if section in Example 4(a) discussed that if a later evaluation determines that  
        adversely impacted the Equipment Performance aspect of the Initiating Events
the safety-related equipment was adversely impacted, it was more than minor. The flow  
        Cornerstone. The inspectors determined the finding could be evaluated using the SDP
obstruction in the leakage detection trough would have delayed the flow of water to the  
        in accordance with IMC 0609, Significance Determination Process, Attachment
sump thereby delaying any subsequent alarm. Therefore, this performance deficiency  
        0609.04, Phase 1 - Initial Screening and Characterization of Findings, Table 4a,
adversely impacted the Equipment Performance aspect of the Initiating Events  
        Characterization Worksheet for Initiating Events Cornerstone. The inspectors
Cornerstone. The inspectors determined the finding could be evaluated using the SDP  
        answered No to Question 1: Assuming worst case degradation, would the finding result
in accordance with IMC 0609, Significance Determination Process, Attachment  
        in exceeding the Technical Specification (TS) limit for any RCS [Reactor Coolant
0609.04, Phase 1 - Initial Screening and Characterization of Findings, Table 4a,  
        System] leakage or could the finding have likely affected other mitigation systems
Characterization Worksheet for Initiating Events Cornerstone. The inspectors  
        resulting in a total loss of their safety function? Therefore, this finding was determined
answered No to Question 1: Assuming worst case degradation, would the finding result  
        to be of very low safety significance (Green). This finding had a cross-cutting aspect in
in exceeding the Technical Specification (TS) limit for any RCS [Reactor Coolant  
        the Corrective Action Program component of the Problem Identification and Resolution
System] leakage or could the finding have likely affected other mitigation systems  
        cross-cutting area because licensee personnel failed to ensure that an issue potentially
resulting in a total loss of their safety function? Therefore, this finding was determined  
        impacting nuclear safety was promptly identified and fully evaluated, and that actions
to be of very low safety significance (Green). This finding had a cross-cutting aspect in  
        were taken to address safety issues in a timely manner, commensurate with their
the Corrective Action Program component of the Problem Identification and Resolution  
        significance [P.1(d)]. (Section 1R15)
cross-cutting area because licensee personnel failed to ensure that an issue potentially  
                                                  1                                  Enclosure
impacting nuclear safety was promptly identified and fully evaluated, and that actions  
were taken to address safety issues in a timely manner, commensurate with their  
significance [P.1(d)]. (Section 1R15)  


  Green. A self-revealed finding with two examples of very low safety significance and an
2
  associated NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
Enclosure
  and Drawings, was identified when licensee personnel failed to properly torque a RCS
Green. A self-revealed finding with two examples of very low safety significance and an  
  pressure boundary valve closed and failed to properly re-install a Reactor Containment
associated NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,  
  Fan Cooler (RCFC) interior access panel during the previous Unit 1 refueling outage.
and Drawings, was identified when licensee personnel failed to properly torque a RCS  
  The licensee replaced the valve and reinstalled the RCFC internal access panel upon
pressure boundary valve closed and failed to properly re-install a Reactor Containment  
  identification and entered the item into the CAP as IR 1339375 and IR 1347450,
Fan Cooler (RCFC) interior access panel during the previous Unit 1 refueling outage.
  respectively. Additional corrective actions included modifying the installation procedure
The licensee replaced the valve and reinstalled the RCFC internal access panel upon  
  to add clarity in the selection of the proper torque value and to add detail and tracking
identification and entered the item into the CAP as IR 1339375 and IR 1347450,  
  aids for the RCFC interior access panels.
respectively. Additional corrective actions included modifying the installation procedure  
  In accordance with IMC 0612, Appendix B, Issue Screening, the first example was
to add clarity in the selection of the proper torque value and to add detail and tracking  
  determined to be more than minor because it was associated with the Procedure Quality
aids for the RCFC interior access panels.  
  attribute of the Initiating Events Cornerstone and adversely affected the cornerstone
In accordance with IMC 0612, Appendix B, Issue Screening, the first example was  
  objective of limiting the likelihood of those events that upset plant stability and challenge
determined to be more than minor because it was associated with the Procedure Quality  
  critical safety functions during shutdown as well as power operations. Specifically, this
attribute of the Initiating Events Cornerstone and adversely affected the cornerstone  
  issue increased the risk of a small break loss of coolant accident. The inspectors
objective of limiting the likelihood of those events that upset plant stability and challenge  
  performed a Phase 1 SDP screening using IMC 0609, Attachment 4, Table 4a,
critical safety functions during shutdown as well as power operations. Specifically, this  
  Characterization Worksheet for Initiating Events Cornerstone. The inspectors
issue increased the risk of a small break loss of coolant accident. The inspectors  
  determined that the finding would not result in exceeding the TS limit for any RCS
performed a Phase 1 SDP screening using IMC 0609, Attachment 4, Table 4a,  
  leakage or could have likely affected other mitigation systems resulting in a total loss of
Characterization Worksheet for Initiating Events Cornerstone. The inspectors  
  their safety function.
determined that the finding would not result in exceeding the TS limit for any RCS  
  The second example was determined to be more than minor because it was associated
leakage or could have likely affected other mitigation systems resulting in a total loss of  
  with the Configuration Control attribute of the Barrier Integrity Cornerstone and adversely
their safety function.  
  affected the cornerstone objective of providing reasonable assurance that physical
The second example was determined to be more than minor because it was associated  
  design barriers, including the containment, protect the public from radionuclide releases
with the Configuration Control attribute of the Barrier Integrity Cornerstone and adversely  
  caused by accidents and events. Specifically, this issue decreased the availability and
affected the cornerstone objective of providing reasonable assurance that physical  
  reliability of the RCFCs for use during a design basis accident. The inspectors
design barriers, including the containment, protect the public from radionuclide releases  
  determined that the issue was of very low safety significance (Green) because the
caused by accidents and events. Specifically, this issue decreased the availability and  
  finding did not represent a degradation of the radiological barrier function, did not
reliability of the RCFCs for use during a design basis accident. The inspectors  
  represent a degradation of the barrier function of the control room, did not represent an
determined that the issue was of very low safety significance (Green) because the  
  actual open pathway in the physical integrity of reactor containment, and did not involve
finding did not represent a degradation of the radiological barrier function, did not  
  an actual reduction in function of hydrogen igniters in the reactor containment.
represent a degradation of the barrier function of the control room, did not represent an  
  Both examples had a cross-cutting aspect in the Work Practices component of the
actual open pathway in the physical integrity of reactor containment, and did not involve  
  Human Performance cross-cutting area [H.4(a)] because licensee personnel failed to
an actual reduction in function of hydrogen igniters in the reactor containment.  
  properly utilize human error prevention techniques. These two examples of the finding
Both examples had a cross-cutting aspect in the Work Practices component of the  
  with a cross-cutting aspect were considered as a single NCV. (Section 4OA2)
Human Performance cross-cutting area [H.4(a)] because licensee personnel failed to  
B. Licensee-Identified Violations
properly utilize human error prevention techniques. These two examples of the finding  
  A violation of very low safety significance that was identified by the licensee has been
with a cross-cutting aspect were considered as a single NCV. (Section 4OA2)  
  reviewed by inspectors. Corrective actions planned or taken by the licensee have been
B.  
  entered into the licensees corrective action program. The violation and corrective action
Licensee-Identified Violations  
  tracking number are listed in Section 4OA7 of this report.
A violation of very low safety significance that was identified by the licensee has been  
                                            2                                  Enclosure
reviewed by inspectors. Corrective actions planned or taken by the licensee have been  
entered into the licensees corrective action program. The violation and corrective action  
tracking number are listed in Section 4OA7 of this report.  


                                        REPORT DETAILS
3
Summary of Plant Status
Enclosure
Unit 1 operated at or near full power throughout most of the inspection period. The performance
REPORT DETAILS  
of the Unit 1 nonsafety-related Natural Draft Cooling Tower that had been degrading over
Summary of Plant Status  
several years worsened during the inspection period. The decrease in cooling tower efficiency
Unit 1 operated at or near full power throughout most of the inspection period. The performance  
resulted in elevated circulating water temperatures. This in turn resulted in less efficient cooling
of the Unit 1 nonsafety-related Natural Draft Cooling Tower that had been degrading over  
of the main condenser and increasing condenser vacuum backpressure. During the morning
several years worsened during the inspection period. The decrease in cooling tower efficiency  
and early afternoon hours, as outside air temperatures warmed, the licensee routinely reduced
resulted in elevated circulating water temperatures. This in turn resulted in less efficient cooling  
reactor power levels in order to maintain condenser vacuum margins. As outside temperatures
of the main condenser and increasing condenser vacuum backpressure. During the morning  
cooled during the evening and nighttime hours, the licensee routinely increased reactor power.
and early afternoon hours, as outside air temperatures warmed, the licensee routinely reduced  
On some days, the licensee reduced and subsequently increased unit power many times. For
reactor power levels in order to maintain condenser vacuum margins. As outside temperatures  
example, during one 72-hour period, the licensee reduced and increased power 54 times. At
cooled during the evening and nighttime hours, the licensee routinely increased reactor power.
the end of the inspection period the licensee revised their power change strategies to perform
On some days, the licensee reduced and subsequently increased unit power many times. For  
fewer, but larger, changes. As a result, power level changes were altered less frequently.
example, during one 72-hour period, the licensee reduced and increased power 54 times. At  
Unit 2 operated at or near full power throughout most of the inspection period. The performance
the end of the inspection period the licensee revised their power change strategies to perform  
of the Unit 2 Natural Draft Cooling Tower was similar to Unit 1 with a consequent similar impact
fewer, but larger, changes. As a result, power level changes were altered less frequently.  
upon plant power level changes.
Unit 2 operated at or near full power throughout most of the inspection period. The performance  
1.     REACTOR SAFETY
of the Unit 2 Natural Draft Cooling Tower was similar to Unit 1 with a consequent similar impact  
        Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity and
upon plant power level changes.  
        Emergency Preparedness
1.  
1R01 Adverse Weather Protection (71111.01)
REACTOR SAFETY  
  .1   Readiness For Impending Hot Summer Weather Conditions
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity and  
    a. Inspection Scope
Emergency Preparedness  
        The inspectors evaluated the licensees preparations for hot summer weather conditions,
1R01 Adverse Weather Protection (71111.01)  
        focusing on the electrical distribution system and the plant chilled water system.
.1  
        During the weeks of May 21, 2012, and May 28, 2012, the inspectors performed a
Readiness For Impending Hot Summer Weather Conditions  
        detailed review of severe weather and plant de-winterization procedures and performed
a.  
        general area plant walkdowns. The inspectors focused on plant-specific design features
Inspection Scope  
        and implementation of procedures for responding to or mitigating the effects of hot
The inspectors evaluated the licensees preparations for hot summer weather conditions,  
        summer weather conditions on the operation of the plant. The inspectors reviewed
focusing on the electrical distribution system and the plant chilled water system.
        system health reports and system engineering summer readiness review documents for
During the weeks of May 21, 2012, and May 28, 2012, the inspectors performed a  
        the above systems.
detailed review of severe weather and plant de-winterization procedures and performed  
        Additionally, the inspectors verified that adverse weather related issues were entered
general area plant walkdowns. The inspectors focused on plant-specific design features  
        into the licensees corrective action program with the appropriate characterization and
and implementation of procedures for responding to or mitigating the effects of hot  
        significance. Selected action requests were reviewed to verify that corrective actions
summer weather conditions on the operation of the plant. The inspectors reviewed  
        were appropriate and implemented as scheduled.
system health reports and system engineering summer readiness review documents for  
        This inspection constituted one seasonal extreme weather readiness inspection sample
the above systems.  
        as defined in Inspection Procedure (IP) 71111.01-05.
Additionally, the inspectors verified that adverse weather related issues were entered  
                                                3                                Enclosure
into the licensees corrective action program with the appropriate characterization and  
significance. Selected action requests were reviewed to verify that corrective actions  
were appropriate and implemented as scheduled.  
This inspection constituted one seasonal extreme weather readiness inspection sample  
as defined in Inspection Procedure (IP) 71111.01-05.  


  b. Findings
4
      No findings were identified.
Enclosure
.2   Readiness For Impending Adverse Weather - High Winds
b.  
  a. Inspection Scope
Findings  
      Since thunderstorms with potential tornados and high winds were forecast in the vicinity
No findings were identified.  
      of the facility for the week of June 18, 2012, while emergent work was being performed
.2  
      on the Unit 2 Train B Station Air Compressor, the inspectors reviewed the licensees
Readiness For Impending Adverse Weather - High Winds  
      overall preparations/protection for the expected conditions. The inspectors toured the
a.  
      plant grounds in the vicinity of the main power transformers, unit auxiliary transformer,
Inspection Scope  
      station auxiliary transformers, and containment access facility to look for loose debris,
Since thunderstorms with potential tornados and high winds were forecast in the vicinity  
      which if present could become missiles during a tornado or with high winds. During the
of the facility for the week of June 18, 2012, while emergent work was being performed  
      inspections, the inspectors focused on plant-specific design features and the licensees
on the Unit 2 Train B Station Air Compressor, the inspectors reviewed the licensees  
      procedure used to respond to tornado and high wind conditions. Documents reviewed
overall preparations/protection for the expected conditions. The inspectors toured the  
      are listed in the Attachment.
plant grounds in the vicinity of the main power transformers, unit auxiliary transformer,  
      This inspection constituted one readiness for impending adverse weather condition
station auxiliary transformers, and containment access facility to look for loose debris,  
      inspection sample as defined in IP 71111.01-05.
which if present could become missiles during a tornado or with high winds. During the  
  b. Findings
inspections, the inspectors focused on plant-specific design features and the licensees  
      No findings were identified.
procedure used to respond to tornado and high wind conditions. Documents reviewed  
1R04 Equipment Alignment (71111.04)
are listed in the Attachment.
.1   Quarterly Partial System Walkdowns
This inspection constituted one readiness for impending adverse weather condition  
  a. Inspection Scope
inspection sample as defined in IP 71111.01-05.  
      The inspectors performed partial system walkdowns of the following risk-significant
b.  
      systems:
Findings  
      *       Unit 1 Train A Containment Spray (CS) while Unit 1 Train B CS was Out of
No findings were identified.  
              Service for Maintenance; and
1R04 Equipment Alignment (71111.04)  
      *       Unit 2 Train A CS while Unit 2 Train B CS was Out of Service for Maintenance.
.1  
      The inspectors selected these systems based on their risk significance relative to the
Quarterly Partial System Walkdowns  
      Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted
a.  
      to identify any discrepancies that could impact the function of the system and therefore
Inspection Scope  
      potentially increase risk. The inspectors reviewed applicable operating procedures,
The inspectors performed partial system walkdowns of the following risk-significant  
      system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical
systems:  
      Specification (TS) requirements, outstanding work orders (WOs), condition reports, and
*  
      the impact of ongoing work activities on redundant trains of equipment in order to identify
Unit 1 Train A Containment Spray (CS) while Unit 1 Train B CS was Out of  
      conditions that could have rendered the systems incapable of performing their intended
Service for Maintenance; and  
      functions. The inspectors also walked down accessible portions of the systems to verify
*  
      system components and support equipment were aligned correctly and operable. The
Unit 2 Train A CS while Unit 2 Train B CS was Out of Service for Maintenance.  
      inspectors examined the material condition of the components and observed operating
The inspectors selected these systems based on their risk significance relative to the  
      parameters of equipment to verify that there were no obvious deficiencies. The
Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted  
                                            4                                  Enclosure
to identify any discrepancies that could impact the function of the system and therefore  
potentially increase risk. The inspectors reviewed applicable operating procedures,  
system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical  
Specification (TS) requirements, outstanding work orders (WOs), condition reports, and  
the impact of ongoing work activities on redundant trains of equipment in order to identify  
conditions that could have rendered the systems incapable of performing their intended  
functions. The inspectors also walked down accessible portions of the systems to verify  
system components and support equipment were aligned correctly and operable. The  
inspectors examined the material condition of the components and observed operating  
parameters of equipment to verify that there were no obvious deficiencies. The  


      inspectors also verified that the licensee had properly identified and resolved equipment
5
      alignment problems that could cause initiating events or impact the capability of
Enclosure
      mitigating systems or barriers and entered them into the Corrective Action Program
inspectors also verified that the licensee had properly identified and resolved equipment  
      (CAP) with the appropriate significance characterization. Documents reviewed are listed
alignment problems that could cause initiating events or impact the capability of  
      in the Attachment.
mitigating systems or barriers and entered them into the Corrective Action Program  
      These activities constituted two partial system walkdown samples as defined in
(CAP) with the appropriate significance characterization. Documents reviewed are listed  
      IP 71111.04-05.
in the Attachment.  
  b. Findings
These activities constituted two partial system walkdown samples as defined in  
      No findings were identified.
IP 71111.04-05.  
.2   Semi-Annual Complete System Walkdown
b.  
  a. Inspection Scope
Findings  
      During the week of June 25, 2012, the inspectors performed a complete system
No findings were identified.  
      alignment inspection of the Unit 2 Auxiliary Feedwater system to verify the functional
.2  
      capability of the system. This system was selected because it was considered both
Semi-Annual Complete System Walkdown  
      safety significant and risk significant in the licensees probabilistic risk assessment. In
a.  
      addition, a recent modification had been performed which affected certain important air
Inspection Scope  
      operated valves in the system. The inspectors walked down the system to review
During the week of June 25, 2012, the inspectors performed a complete system  
      mechanical and electrical equipment lineups; electrical power availability; system
alignment inspection of the Unit 2 Auxiliary Feedwater system to verify the functional  
      pressure and temperature indications, as appropriate; component labeling; component
capability of the system. This system was selected because it was considered both  
      lubrication; component and equipment cooling; hangers and supports; operability of
safety significant and risk significant in the licensees probabilistic risk assessment. In  
      support systems; and to ensure that ancillary equipment or debris did not interfere with
addition, a recent modification had been performed which affected certain important air  
      equipment operation. A review of a sample of past and outstanding WOs was
operated valves in the system. The inspectors walked down the system to review  
      performed to determine whether any deficiencies significantly affected the system
mechanical and electrical equipment lineups; electrical power availability; system  
      function. In addition, the inspectors reviewed the CAP database to ensure that system
pressure and temperature indications, as appropriate; component labeling; component  
      equipment alignment problems were being identified and appropriately resolved.
lubrication; component and equipment cooling; hangers and supports; operability of  
      Documents reviewed are listed in the Attachment.
support systems; and to ensure that ancillary equipment or debris did not interfere with  
      These activities constituted one complete system walkdown sample as defined in
equipment operation. A review of a sample of past and outstanding WOs was  
      IP 71111.04-05.
performed to determine whether any deficiencies significantly affected the system  
  b. Findings
function. In addition, the inspectors reviewed the CAP database to ensure that system  
      No findings were identified.
equipment alignment problems were being identified and appropriately resolved.
1R05 Fire Protection (71111.05)
Documents reviewed are listed in the Attachment.  
.1   Routine Resident Inspector Tours (71111.05Q)
These activities constituted one complete system walkdown sample as defined in  
  a. Inspection Scope
IP 71111.04-05.  
      The inspectors conducted fire protection walkdowns which were focused on availability,
b.  
      accessibility, and the condition of firefighting equipment in the following risk-significant
Findings  
      plant areas:
No findings were identified.  
                                              5                                    Enclosure
1R05 Fire Protection (71111.05)  
.1  
Routine Resident Inspector Tours (71111.05Q)  
a.  
Inspection Scope  
The inspectors conducted fire protection walkdowns which were focused on availability,  
accessibility, and the condition of firefighting equipment in the following risk-significant  
plant areas:  


    *       Unit 1 Train A Residual Heat Removal (RH) Pump Room - Fire Zone 11.2A-1;
6
    *       Unit 1 Train B RH Pump Room - Fire Zone 11.2D-1;
Enclosure
    *       Unit 1 Train A CS Pump Room - Fire Zone 11.2B-1;
*  
    *       Unit 1 Train B CS Pump Room - Fire Zone 11.2C-2; and
Unit 1 Train A Residual Heat Removal (RH) Pump Room - Fire Zone 11.2A-1;  
    *       Unit 2 Division 22 Miscellaneous Electrical Equipment Room and Battery Room -
*  
            Fire Zone 5.4-2.
Unit 1 Train B RH Pump Room - Fire Zone 11.2D-1;  
    The inspectors reviewed areas to assess if the licensee had implemented a fire
*  
    protection program that adequately controlled combustibles and ignition sources within
Unit 1 Train A CS Pump Room - Fire Zone 11.2B-1;  
    the plant, effectively maintained fire detection and suppression capability, maintained
*  
    passive fire protection features in good material condition, and implemented adequate
Unit 1 Train B CS Pump Room - Fire Zone 11.2C-2; and  
    compensatory measures for out-of-service, degraded or inoperable fire protection
*  
    equipment, systems, or features in accordance with the licensees fire plan. The
Unit 2 Division 22 Miscellaneous Electrical Equipment Room and Battery Room -  
    inspectors selected fire areas based on their overall contribution to internal fire risk as
Fire Zone 5.4-2.  
    documented in the plants Individual Plant Examination of External Events with later
The inspectors reviewed areas to assess if the licensee had implemented a fire  
    additional insights, their potential to impact equipment which could initiate or mitigate a
protection program that adequately controlled combustibles and ignition sources within  
    plant transient, or their impact on the plants ability to respond to a security event. Using
the plant, effectively maintained fire detection and suppression capability, maintained  
    the documents listed in the Attachment to this report, the inspectors verified that fire
passive fire protection features in good material condition, and implemented adequate  
    hoses and extinguishers were in their designated locations and available for immediate
compensatory measures for out-of-service, degraded or inoperable fire protection  
    use; that fire detectors and sprinklers were unobstructed; that transient material loading
equipment, systems, or features in accordance with the licensees fire plan. The  
    was within the analyzed limits; and fire doors, dampers, and penetration seals appeared
inspectors selected fire areas based on their overall contribution to internal fire risk as  
    to be in satisfactory condition. The inspectors also verified that minor issues identified
documented in the plants Individual Plant Examination of External Events with later  
    during the inspection were entered into the licensees CAP.
additional insights, their potential to impact equipment which could initiate or mitigate a  
    These activities constituted five quarterly fire protection inspection samples as defined in
plant transient, or their impact on the plants ability to respond to a security event. Using  
    IP 71111.05-05.
the documents listed in the Attachment to this report, the inspectors verified that fire  
  b. Findings
hoses and extinguishers were in their designated locations and available for immediate  
    No findings were identified
use; that fire detectors and sprinklers were unobstructed; that transient material loading  
.2   Fire Protection - Drill Observation (71111.05A)
was within the analyzed limits; and fire doors, dampers, and penetration seals appeared  
  a. Inspection Scope
to be in satisfactory condition. The inspectors also verified that minor issues identified  
    During an announced drill on May 16, 2012, associated with a simulated fire in the
during the inspection were entered into the licensees CAP.  
    outside barrel storage area, the inspectors assessed the timeliness of the fire brigade in
These activities constituted five quarterly fire protection inspection samples as defined in  
    arriving at the scene, the fire fighting equipment brought to the scene, the donning of fire
IP 71111.05-05.  
    protective clothing, the effectiveness of communications, and the exercise of command
b.  
    and control by the fire brigade leader. The inspectors also assessed the acceptance
Findings  
    criteria for the drill objectives; the rigor and thoroughness of the post-drill critique; and
No findings were identified  
    verified that fire protection drill issues were being entered into the licensee's CAP with
.2  
    the appropriate characterization and significance. Documents reviewed are listed in the
Fire Protection - Drill Observation (71111.05A)  
    Attachment.
a.  
    This inspection constituted one annual fire protection drill inspection sample as defined
Inspection Scope  
    in IP 71111.05AQ.
During an announced drill on May 16, 2012, associated with a simulated fire in the  
  b. Findings
outside barrel storage area, the inspectors assessed the timeliness of the fire brigade in  
    No findings were identified.
arriving at the scene, the fire fighting equipment brought to the scene, the donning of fire  
                                                6                                Enclosure
protective clothing, the effectiveness of communications, and the exercise of command  
and control by the fire brigade leader. The inspectors also assessed the acceptance  
criteria for the drill objectives; the rigor and thoroughness of the post-drill critique; and  
verified that fire protection drill issues were being entered into the licensee's CAP with  
the appropriate characterization and significance. Documents reviewed are listed in the  
Attachment.  
This inspection constituted one annual fire protection drill inspection sample as defined  
in IP 71111.05AQ.  
b.  
Findings  
No findings were identified.  


1R06 Flooding (71111.06)
7
.1   Internal Flooding
Enclosure
  a. Inspection Scope
1R06 Flooding (71111.06)  
      The inspectors reviewed selected risk important plant design features and licensee
.1  
      procedures intended to protect the plant and its safety-related equipment from internal
Internal Flooding  
      flooding events. The inspectors reviewed flood analyses and design documents,
a.  
      including the UFSAR, engineering calculations, and abnormal operating procedures to
Inspection Scope  
      identify licensee commitments. The specific documents reviewed are listed in the
The inspectors reviewed selected risk important plant design features and licensee  
      Attachment to this report. In addition, the inspectors reviewed licensee drawings to
procedures intended to protect the plant and its safety-related equipment from internal  
      identify areas and equipment that may be affected by internal flooding caused by the
flooding events. The inspectors reviewed flood analyses and design documents,  
      failure or misalignment of nearby sources of water, such as the fire suppression or the
including the UFSAR, engineering calculations, and abnormal operating procedures to  
      circulating water systems. The inspectors also reviewed the licensees corrective action
identify licensee commitments. The specific documents reviewed are listed in the  
      documents with respect to past flood-related items identified in the CAP to verify the
Attachment to this report. In addition, the inspectors reviewed licensee drawings to  
      adequacy of the corrective actions. The inspectors performed a walkdown of the
identify areas and equipment that may be affected by internal flooding caused by the  
      following plant area to assess the adequacy of watertight doors and verify drains and
failure or misalignment of nearby sources of water, such as the fire suppression or the  
      sumps were clear of debris and were operable, and that the licensee complied with its
circulating water systems. The inspectors also reviewed the licensees corrective action  
      commitments:
documents with respect to past flood-related items identified in the CAP to verify the  
      *     Floor Drains Located in Auxiliary Building 364 Elevation, General Area
adequacy of the corrective actions. The inspectors performed a walkdown of the  
      This inspection constituted one internal flooding sample as defined in IP 71111.06-05.
following plant area to assess the adequacy of watertight doors and verify drains and  
  b. Findings
sumps were clear of debris and were operable, and that the licensee complied with its  
      No findings were identified.
commitments:  
1R11 Licensed Operator Requalification Program (71111.11)
*  
.1   Resident Inspector Quarterly Review (71111.11Q)
Floor Drains Located in Auxiliary Building 364 Elevation, General Area  
  a. Inspection Scope
This inspection constituted one internal flooding sample as defined in IP 71111.06-05.  
      On May 8, 2012, the inspectors observed a crew of licensed operators in the plants
b.  
      simulator during licensed operator requalification examinations to verify that operator
Findings  
      performance was adequate, evaluators were identifying and documenting crew
No findings were identified.
      performance problems, and training was being conducted in accordance with licensee
1R11 Licensed Operator Requalification Program (71111.11)  
      procedures. The inspectors evaluated the following areas:
.1  
      *     licensed operator performance;
Resident Inspector Quarterly Review (71111.11Q)  
      *     crews clarity and formality of communications;
a.  
      *     ability to take timely actions in the conservative direction;
Inspection Scope  
      *     prioritization, interpretation, and verification of annunciator alarms;
On May 8, 2012, the inspectors observed a crew of licensed operators in the plants  
      *     correct use and implementation of abnormal and emergency procedures;
simulator during licensed operator requalification examinations to verify that operator  
      *     control board manipulations;
performance was adequate, evaluators were identifying and documenting crew  
      *     oversight and direction from supervisors; and
performance problems, and training was being conducted in accordance with licensee  
      *     ability to identify and implement appropriate TS actions and Emergency Plan
procedures. The inspectors evaluated the following areas:  
            actions and notifications.
*  
                                              7                                  Enclosure
licensed operator performance;  
*  
crews clarity and formality of communications;  
*  
ability to take timely actions in the conservative direction;  
*  
prioritization, interpretation, and verification of annunciator alarms;  
*  
correct use and implementation of abnormal and emergency procedures;  
*  
control board manipulations;  
*  
oversight and direction from supervisors; and  
*  
ability to identify and implement appropriate TS actions and Emergency Plan  
actions and notifications.  


    The crews performance in these areas was compared to pre-established operator action
8
    expectations and successful critical task completion requirements. Documents reviewed
Enclosure
    are listed in the Attachment.
The crews performance in these areas was compared to pre-established operator action  
    In addition, the inspectors observed licensed operator performance in the actual plant
expectations and successful critical task completion requirements. Documents reviewed  
    and the main control room during this calendar quarter.
are listed in the Attachment.  
    This inspection constituted one quarterly licensed operator requalification program
In addition, the inspectors observed licensed operator performance in the actual plant  
    sample as defined in IP 71111.11-05.
and the main control room during this calendar quarter.  
  b. Findings
This inspection constituted one quarterly licensed operator requalification program  
    No findings were identified.
sample as defined in IP 71111.11-05.  
.2   Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q)
b.  
    On June 28, 2012, the inspectors observed control room operators immediately following
Findings  
    the loss of the Unit 1 Train B Main Feedwater Pump, while the operators were also
No findings were identified.  
    addressing elevated outside air temperatures, which caused main generator hydrogen
.2  
    cooling concerns, instrument air dryer failures, spurious fire alarms, main generator
Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q)  
    reactive load adjustments, and a reported failure of the Unit 2 E Natural Draft Cooling
On June 28, 2012, the inspectors observed control room operators immediately following  
    Tower riser. This was an activity that required heightened awareness or was related to
the loss of the Unit 1 Train B Main Feedwater Pump, while the operators were also  
    increased risk. The inspectors evaluated the following areas:
addressing elevated outside air temperatures, which caused main generator hydrogen  
    *       licensed operator performance;
cooling concerns, instrument air dryer failures, spurious fire alarms, main generator  
    *       crews clarity and formality of communications;
reactive load adjustments, and a reported failure of the Unit 2 E Natural Draft Cooling  
    *       ability to take timely actions in the conservative direction;
Tower riser. This was an activity that required heightened awareness or was related to  
    *       prioritization, interpretation, and verification of annunciator alarms;
increased risk. The inspectors evaluated the following areas:  
    *       correct use and implementation of procedures;
*  
    *       control board manipulations;
licensed operator performance;  
    *       oversight and direction from supervisors; and
*  
    *       ability to identify and implement appropriate TS actions and Emergency Plan
crews clarity and formality of communications;  
            actions and notifications.
*  
    The performance in these areas was compared to pre-established operator action
ability to take timely actions in the conservative direction;  
    expectations, procedural compliance, and task completion requirements. Documents
*  
    reviewed are listed in the Attachment.
prioritization, interpretation, and verification of annunciator alarms;  
    This inspection constituted one quarterly licensed operator heightened activity/risk
*  
    sample as defined in IP 71111.11-05.
correct use and implementation of procedures;  
  b. Findings
*  
    No findings were identified.
control board manipulations;  
.3   Conformance With Examination Security Requirements (71111.11B)
*  
  a. Inspection Scope
oversight and direction from supervisors; and  
    The inspectors reviewed the facility licensees physical security controls (e.g., access
*  
    restrictions and simulator input/output (I/O) controls, simulator software) and integrity
ability to identify and implement appropriate TS actions and Emergency Plan  
                                              8                                  Enclosure
actions and notifications.  
The performance in these areas was compared to pre-established operator action  
expectations, procedural compliance, and task completion requirements. Documents  
reviewed are listed in the Attachment.  
This inspection constituted one quarterly licensed operator heightened activity/risk  
sample as defined in IP 71111.11-05.  
b.  
Findings  
No findings were identified.  
.3  
Conformance With Examination Security Requirements (71111.11B)  
a.  
Inspection Scope  
The inspectors reviewed the facility licensees physical security controls (e.g., access  
restrictions and simulator input/output (I/O) controls, simulator software) and integrity  


      measures (e.g., security agreements, simulator software access) throughout the
9
      inspection period.
Enclosure
  b. Findings
measures (e.g., security agreements, simulator software access) throughout the  
      One licensee-identified finding with an Non-Cited Violation (NCV) is documented in
inspection period.  
      Section 4OA7 of this report. No other findings were identified.
b.  
1R12 Maintenance Effectiveness (71111.12)
Findings  
.1   Routine Quarterly Evaluations (71111.12Q)
One licensee-identified finding with an Non-Cited Violation (NCV) is documented in  
  a. Inspection Scope
Section 4OA7 of this report. No other findings were identified.
      The inspectors evaluated degraded performance issues involving the following
1R12 Maintenance Effectiveness (71111.12)  
      risk-significant systems:
.1  
      *       Unit 1 and Unit 2 Natural Draft Cooling Tower Fill Degradation; and
Routine Quarterly Evaluations (71111.12Q)  
      *       Non-Essential Service Water Increased Silt and Fill Issues.
a.  
      The inspectors assessed performance issues with respect to the reliability, availability,
Inspection Scope  
      and condition monitoring of the system. In addition, the inspectors verified maintenance
The inspectors evaluated degraded performance issues involving the following  
      effectiveness issues were entered into the CAP with the appropriate significance
risk-significant systems:  
      characterization. Documents reviewed are listed in the Attachment.
*  
      This inspection constituted two quarterly maintenance effectiveness samples as defined
Unit 1 and Unit 2 Natural Draft Cooling Tower Fill Degradation; and  
      in IP 71111.12-05.
*  
  b. Findings
Non-Essential Service Water Increased Silt and Fill Issues.  
      No findings were identified
The inspectors assessed performance issues with respect to the reliability, availability,  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
and condition monitoring of the system. In addition, the inspectors verified maintenance  
.1   Maintenance Risk Assessments and Emergent Work Control
effectiveness issues were entered into the CAP with the appropriate significance  
  a. Inspection Scope
characterization. Documents reviewed are listed in the Attachment.  
      The inspectors reviewed the licensee's evaluation and management of plant risk for the
This inspection constituted two quarterly maintenance effectiveness samples as defined  
      maintenance and emergent work activities affecting risk-significant and safety-related
in IP 71111.12-05.  
      equipment listed below to verify that the appropriate risk assessments were performed
b.  
      prior to removing equipment for work:
Findings  
      *       Work Week Schedule for the Week of May 21, 2012;
No findings were identified  
      *       Unit 2 Train B CS Inoperable while Unit 2 Loop C Steam Generator Power
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
              Operated Relief Valve was Inoperable;
.1  
      *       Activities During the Modification of Unit Common Component Cooling Heat
Maintenance Risk Assessments and Emergent Work Control  
              Exchanger Discharge Valve 0SX007; and
a.  
      *       Unit 2 Change in Risk Status Due to Emergent Failure of Unit 2 Train B Station Air
Inspection Scope  
              Compressor during Planned Outage of Unit 1 Train A Station Air Compressor.
The inspectors reviewed the licensee's evaluation and management of plant risk for the  
                                              9                                Enclosure
maintenance and emergent work activities affecting risk-significant and safety-related  
equipment listed below to verify that the appropriate risk assessments were performed  
prior to removing equipment for work:  
*  
Work Week Schedule for the Week of May 21, 2012;  
*  
Unit 2 Train B CS Inoperable while Unit 2 Loop C Steam Generator Power  
Operated Relief Valve was Inoperable;  
*  
Activities During the Modification of Unit Common Component Cooling Heat  
Exchanger Discharge Valve 0SX007; and  
*  
Unit 2 Change in Risk Status Due to Emergent Failure of Unit 2 Train B Station Air  
Compressor during Planned Outage of Unit 1 Train A Station Air Compressor.  


      These activities were selected based on their potential risk significance relative to the
10
      Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
Enclosure
      risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
These activities were selected based on their potential risk significance relative to the  
      and complete. When emergent work was performed, the inspectors verified that the
Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that  
      plant risk was promptly reassessed and managed. The inspectors reviewed the scope
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate  
      of maintenance work, discussed the results of the assessment with the licensee's
and complete. When emergent work was performed, the inspectors verified that the  
      probabilistic risk analyst or shift technical advisor, and verified plant conditions were
plant risk was promptly reassessed and managed. The inspectors reviewed the scope  
      consistent with the risk assessment. The inspectors also reviewed TS requirements and
of maintenance work, discussed the results of the assessment with the licensee's  
      walked down portions of redundant safety systems, when applicable, to verify risk
probabilistic risk analyst or shift technical advisor, and verified plant conditions were  
      analysis assumptions were valid and applicable requirements were met.
consistent with the risk assessment. The inspectors also reviewed TS requirements and  
      These maintenance risk assessments and emergent work control activities constituted
walked down portions of redundant safety systems, when applicable, to verify risk  
      four samples as defined in IP 71111.13-05.
analysis assumptions were valid and applicable requirements were met.  
  b. Findings
These maintenance risk assessments and emergent work control activities constituted  
      No findings were identified.
four samples as defined in IP 71111.13-05.  
1R15 Operability Evaluations (71111.15)
b.  
.1   Operability Evaluations
Findings  
  a. Inspection Scope
No findings were identified.  
      The inspectors reviewed the following issues:
1R15 Operability Evaluations (71111.15)  
      *     Steam Generator Margin to Overfill Issues;
.1  
      *     Unit 1 Train A Reactor Containment Fan Cooler Missing Internal Access Hatch;
Operability Evaluations  
      *     Operability Evaluation 12-001, Potential Design Vulnerability in Switchyard Single
a.  
            Open Phase Detection;
Inspection Scope  
      *     Operability Evaluation 09-001, Diesel Oil Storage Tank Vent Lines Crimp Versus
The inspectors reviewed the following issues:  
            Break;
*  
      *     Operability Evaluation 12-005, High Energy Line Break (HELB) Load Not
Steam Generator Margin to Overfill Issues;  
            considered in Structural Calculation;
*  
      *     Operability Evaluation 11-005, Turbine Building HELB Input Errors; and
Unit 1 Train A Reactor Containment Fan Cooler Missing Internal Access Hatch;  
      *     Unit 1 Containment Leakage Detection System Due to Boric Acid Accumulation in
*  
            System Drain. (Sample previously credited in Inspection Report
Operability Evaluation 12-001, Potential Design Vulnerability in Switchyard Single  
            050000454/2012002; 05000455/2012002)
Open Phase Detection;  
            The inspectors selected these potential operability issues based on the risk
*  
            significance of the associated components and systems. The inspectors
Operability Evaluation 09-001, Diesel Oil Storage Tank Vent Lines Crimp Versus  
            evaluated the technical adequacy of the evaluations to ensure that TS operability
Break;  
            was properly justified and the subject component or system remained available
*  
            such that no unrecognized increase in risk occurred. The inspectors compared
Operability Evaluation 12-005, High Energy Line Break (HELB) Load Not  
            the operability and design criteria in the appropriate sections of the TS and
considered in Structural Calculation;  
            UFSAR to the licensees evaluations to determine whether the components or
*  
            systems were operable. Where compensatory measures were required to
Operability Evaluation 11-005, Turbine Building HELB Input Errors; and  
            maintain operability, the inspectors determined whether the measures in place
*  
            would function as intended and were properly controlled. The inspectors
Unit 1 Containment Leakage Detection System Due to Boric Acid Accumulation in  
            determined, where appropriate, compliance with bounding limitations associated
System Drain. (Sample previously credited in Inspection Report  
            with the evaluations. Additionally, the inspectors reviewed a sample of corrective
050000454/2012002; 05000455/2012002)  
                                              10                                  Enclosure
The inspectors selected these potential operability issues based on the risk  
significance of the associated components and systems. The inspectors  
evaluated the technical adequacy of the evaluations to ensure that TS operability  
was properly justified and the subject component or system remained available  
such that no unrecognized increase in risk occurred. The inspectors compared  
the operability and design criteria in the appropriate sections of the TS and  
UFSAR to the licensees evaluations to determine whether the components or  
systems were operable. Where compensatory measures were required to  
maintain operability, the inspectors determined whether the measures in place  
would function as intended and were properly controlled. The inspectors  
determined, where appropriate, compliance with bounding limitations associated  
with the evaluations. Additionally, the inspectors reviewed a sample of corrective  


            action documents to verify that the licensee was identifying and correcting any
11
            deficiencies associated with operability evaluations. Documents reviewed are
Enclosure
            listed in the Attachment.
action documents to verify that the licensee was identifying and correcting any  
    This operability inspection constituted six samples as defined in IP 71111.15-05.
deficiencies associated with operability evaluations. Documents reviewed are  
b. Findings
listed in the Attachment.  
(1) (Closed) Unresolved Item 05000454/2012002-03, Boric Acid Accumulation Identified in
This operability inspection constituted six samples as defined in IP 71111.15-05.  
    Leakage Detection Trough
b.  
    Introduction: A finding of very low safety significance (Green) and an associated NCV of
Findings  
    10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,
(1) (Closed) Unresolved Item 05000454/2012002-03, Boric Acid Accumulation Identified in  
    was identified by the inspectors when licensee personnel failed to identify boric acid
Leakage Detection Trough  
    accumulation that would have impeded flow from the containment leakage detection
Introduction: A finding of very low safety significance (Green) and an associated NCV of  
    trough to the containment sump.
10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,  
    Description: During a Unit 1 maintenance outage, the inspectors identified a boric acid
was identified by the inspectors when licensee personnel failed to identify boric acid  
    leak on sample valve 1PS9365B on the 426 elevation of containment. The 426
accumulation that would have impeded flow from the containment leakage detection  
    elevation of containment had a grated floor; therefore, the inspectors proceeded to the
trough to the containment sump.
    lower levels of containment to determine if any other equipment had been impacted by
Description: During a Unit 1 maintenance outage, the inspectors identified a boric acid  
    the leak. On the 377 elevation, the inspectors identified a large area of boric acid
leak on sample valve 1PS9365B on the 426 elevation of containment. The 426  
    accumulation. Radiation Protection (RP) personnel were in containment to
elevation of containment had a grated floor; therefore, the inspectors proceeded to the  
    decontaminate an area associated with a previously identified leak on 1RC8042B when
lower levels of containment to determine if any other equipment had been impacted by  
    this additional leak was identified. The inspectors made an RP supervisor that was in
the leak. On the 377 elevation, the inspectors identified a large area of boric acid  
    the area aware of this additional source of leakage. Additionally, photographs were
accumulation. Radiation Protection (RP) personnel were in containment to  
    taken and provided to the Outage Control Center. The licensee entered this issue into
decontaminate an area associated with a previously identified leak on 1RC8042B when  
    their CAP as IR 1339957, 1PS9365 Has Leak From Either Packing or Bonnet.
this additional leak was identified. The inspectors made an RP supervisor that was in  
    In preparation for a planned change from Mode 5 to Mode 4, the licensee routinely
the area aware of this additional source of leakage. Additionally, photographs were  
    performed an assessment of containment in accordance with the Containment Loose
taken and provided to the Outage Control Center. The licensee entered this issue into  
    Debris Inspection procedure, 1BOSR Z.5.b.1-1. The purpose of this inspection was to
their CAP as IR 1339957, 1PS9365 Has Leak From Either Packing or Bonnet.  
    ensure that the material condition of containment was sufficient to support at power
In preparation for a planned change from Mode 5 to Mode 4, the licensee routinely  
    operations. The inspectors performed an independent assessment following the
performed an assessment of containment in accordance with the Containment Loose  
    licensees assessment. The inspectors identified that boric acid associated with the leak
Debris Inspection procedure, 1BOSR Z.5.b.1-1. The purpose of this inspection was to  
    identified in IR 1339957 on the 377 elevation was still present. Specifically, boric acid
ensure that the material condition of containment was sufficient to support at power  
    had accumulated in a trough along the wall of the inner containment structure. The
operations. The inspectors performed an independent assessment following the  
    accumulated boric acid completely covered the drain in the trough. The purpose of this
licensees assessment. The inspectors identified that boric acid associated with the leak  
    trough was to collect any potential leakage and direct that leakage to a sump. The flow
identified in IR 1339957 on the 377 elevation was still present. Specifically, boric acid  
    of water into, as well as the level of this sump was monitored to facilitate the prompt
had accumulated in a trough along the wall of the inner containment structure. The  
    identification of leaks that may occur in containment. The reactor coolant system (RCS)
accumulated boric acid completely covered the drain in the trough. The purpose of this  
    leakage detection instrumentation was required to be operable in Modes 1-4 and Unit 1
trough was to collect any potential leakage and direct that leakage to a sump. The flow  
    was in Mode 4 at the time of this discovery. This issue was entered into the licensees
of water into, as well as the level of this sump was monitored to facilitate the prompt  
    CAP as IR 1341380. Corrective actions included removing the boric acid accumulation
identification of leaks that may occur in containment. The reactor coolant system (RCS)  
    from the leakage detection trough and passing water through the drain to verify
leakage detection instrumentation was required to be operable in Modes 1-4 and Unit 1  
    associated piping was free of obstruction.
was in Mode 4 at the time of this discovery. This issue was entered into the licensees  
    Unresolved Item (URI) 05000454/2012002-03 was opened pending the licensees
CAP as IR 1341380. Corrective actions included removing the boric acid accumulation  
    completion of their assessment of the issue and the inspectors review of that
from the leakage detection trough and passing water through the drain to verify  
    assessment in NRC Inspection Report 05000454/2012002; 05000455/2012002. A
associated piping was free of obstruction.  
                                            11                                Enclosure
Unresolved Item (URI) 05000454/2012002-03 was opened pending the licensees  
completion of their assessment of the issue and the inspectors review of that  
assessment in NRC Inspection Report 05000454/2012002; 05000455/2012002. A  


subsequent evaluation by the licensee determined that the obstruction did not
12
completely block the flow of water to the drain.
Enclosure
The significance of RCS leakage varies widely depending on its source, rate, and
subsequent evaluation by the licensee determined that the obstruction did not  
duration. Therefore, detecting RCS leakage into containment is necessary. The ability
completely block the flow of water to the drain.  
to separate identified leakage from unidentified leakage provides quantitative information
The significance of RCS leakage varies widely depending on its source, rate, and  
to the operators. This information supports the risk assessment process and facilitates
duration. Therefore, detecting RCS leakage into containment is necessary. The ability  
timely initiation of corrective actions.
to separate identified leakage from unidentified leakage provides quantitative information  
Analysis: The inspectors determined that the failure to identify a flow obstruction in the
to the operators. This information supports the risk assessment process and facilitates  
leakage detection trough was contrary to the requirements of 1BOSR Z.5.b.1-1, Unit
timely initiation of corrective actions.  
One Containment Loose Debris Inspection, and was a performance deficiency.
Analysis: The inspectors determined that the failure to identify a flow obstruction in the  
The finding was determined to be more than minor because the finding was similar to
leakage detection trough was contrary to the requirements of 1BOSR Z.5.b.1-1, Unit  
IMC 0612, Appendix E, Example 4(a). Example 4 focused on procedural errors. The
One Containment Loose Debris Inspection, and was a performance deficiency.  
not minor if section in Example 4(a) discussed that if a later evaluation determines that
The finding was determined to be more than minor because the finding was similar to  
the safety-related equipment was adversely impacted, it was more than minor. The flow
IMC 0612, Appendix E, Example 4(a). Example 4 focused on procedural errors. The  
obstruction in the leakage detection trough would have delayed the flow of water to the
not minor if section in Example 4(a) discussed that if a later evaluation determines that  
sump thereby delaying any subsequent alarm. Therefore, this performance deficiency
the safety-related equipment was adversely impacted, it was more than minor. The flow  
adversely impacted the Equipment Performance attribute of the Initiating Events
obstruction in the leakage detection trough would have delayed the flow of water to the  
Cornerstone.
sump thereby delaying any subsequent alarm. Therefore, this performance deficiency  
The inspectors determined the finding could be evaluated using the SDP in accordance
adversely impacted the Equipment Performance attribute of the Initiating Events  
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Cornerstone.    
Initial Screening and Characterization of Findings, Table 4a for the Initiating Events
The inspectors determined the finding could be evaluated using the SDP in accordance  
Cornerstone. The inspectors selected this cornerstone due to the affected equipment
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -  
being used to inform operations staff of changing conditions in containment. Reactor
Initial Screening and Characterization of Findings, Table 4a for the Initiating Events  
coolant system leakage was one of many analyzed initiating events. The inspectors
Cornerstone. The inspectors selected this cornerstone due to the affected equipment  
answered No to Question 1: Assuming worst case degradation, would the finding result
being used to inform operations staff of changing conditions in containment. Reactor  
in exceeding the Tech Spec [Technical Specification] limit for any RCS leakage or could
coolant system leakage was one of many analyzed initiating events. The inspectors  
the finding have likely affected other mitigation systems resulting in a total loss of their
answered No to Question 1: Assuming worst case degradation, would the finding result  
safety function? Therefore, this finding was determined to be of very low safety
in exceeding the Tech Spec [Technical Specification] limit for any RCS leakage or could  
significance (Green).
the finding have likely affected other mitigation systems resulting in a total loss of their  
This finding had a cross-cutting aspect in the CAP component of the Problem
safety function? Therefore, this finding was determined to be of very low safety  
Identification and Resolution cross-cutting area because licensee personnel did not
significance (Green).  
ensure that an issue potentially impacting nuclear safety was promptly identified, fully
This finding had a cross-cutting aspect in the CAP component of the Problem  
evaluated, and that actions were taken to address safety issues in a timely manner,
Identification and Resolution cross-cutting area because licensee personnel did not  
commensurate with their significance. Specifically, the accumulated boric acid
ensure that an issue potentially impacting nuclear safety was promptly identified, fully  
obstructed flow through the leakage detection trough. The cause of this accumulation,
evaluated, and that actions were taken to address safety issues in a timely manner,  
leakage from sample valve 1PS9365B, was previously identified and entered into the
commensurate with their significance. Specifically, the accumulated boric acid  
CAP. [P.1(d)]
obstructed flow through the leakage detection trough. The cause of this accumulation,  
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and
leakage from sample valve 1PS9365B, was previously identified and entered into the  
Drawings, requires, in part, that activities affecting quality shall be prescribed by
CAP. [P.1(d)]  
documented instructions, procedures, or drawings, of a type appropriate to the
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and  
circumstances and shall be accomplished in accordance with these instructions,
Drawings, requires, in part, that activities affecting quality shall be prescribed by  
procedures, or drawings. Surveillance procedure 1BOSR Z.5.b.1-1, Unit 1 Containment
documented instructions, procedures, or drawings, of a type appropriate to the  
Loose Debris Inspection, Revision 15, was written in accordance with 10 CFR Part 50,
circumstances and shall be accomplished in accordance with these instructions,  
accomplished an activity affecting quality, and required that the drain trough and floor
procedures, or drawings. Surveillance procedure 1BOSR Z.5.b.1-1, Unit 1 Containment  
drains be free of debris and that flow not be impeded. Step 4(a) of 1BOSR Z.5.b.1-1
Loose Debris Inspection, Revision 15, was written in accordance with 10 CFR Part 50,  
                                        12                                  Enclosure
accomplished an activity affecting quality, and required that the drain trough and floor  
drains be free of debris and that flow not be impeded. Step 4(a) of 1BOSR Z.5.b.1-1  


      required licensee personnel to verify that drain trough and floor drains located on the
13
      377 elevation to be free of flow obstructions.
Enclosure
      Contrary to the above, on March 14, 2012, the licensee failed to accomplish the Unit
required licensee personnel to verify that drain trough and floor drains located on the  
      One Containment Loose Debris Inspection, an activity affecting quality, in accordance
377 elevation to be free of flow obstructions.
      with the applicable instructions, procedures, or drawings. Specifically, the licensee failed
Contrary to the above, on March 14, 2012, the licensee failed to accomplish the Unit  
      to adequately implement procedure 1BOSR Z.5.b.1-1 to verify that drain trough and floor
One Containment Loose Debris Inspection, an activity affecting quality, in accordance  
      drains located on the 377 elevation of the containment were free of flow obstructions, in
with the applicable instructions, procedures, or drawings. Specifically, the licensee failed  
      that the inspectors identified boric acid accumulation that would have impeded flow from
to adequately implement procedure 1BOSR Z.5.b.1-1 to verify that drain trough and floor  
      the leakage detection trough to the sump. Because this violation was of very low safety
drains located on the 377 elevation of the containment were free of flow obstructions, in  
      significance and this issue was entered into the licensees CAP as IR 1339957, this
that the inspectors identified boric acid accumulation that would have impeded flow from  
      violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC
the leakage detection trough to the sump. Because this violation was of very low safety  
      Enforcement Policy. (NCV 05000454/2012003-01, Leakage Detection Trough with
significance and this issue was entered into the licensees CAP as IR 1339957, this  
      Large Accumulation of Boric Acid Identified)
violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC  
      URI 05000454/2012002-03 is closed.
Enforcement Policy. (NCV 05000454/2012003-01, Leakage Detection Trough with  
1R19 Post Maintenance Testing (71111.19)
Large Accumulation of Boric Acid Identified)  
.1   Post Maintenance Testing
URI 05000454/2012002-03 is closed.  
  a. Inspection Scope
1R19 Post Maintenance Testing (71111.19)  
      The inspectors reviewed the following post maintenance testing activities to verify that
.1  
      procedures and test activities were adequate to ensure system operability and functional
Post Maintenance Testing  
      capability:
a.  
      *       Unit 2 Essential Service Water Valve 2SX010 following Modification;
Inspection Scope  
      *       Unit 1 C Loop Steam Generator Power Operated Relief Valve following Hand
The inspectors reviewed the following post maintenance testing activities to verify that  
              Pump Replacement;
procedures and test activities were adequate to ensure system operability and functional  
      *       Unit 2 Train B Auxiliary Feedwater Pump following Scheduled Maintenance; and
capability:  
      *       Unit Common Component Cooling Heat Exchanger Discharge Valve 0SX007
*  
              following Electrical Modification.
Unit 2 Essential Service Water Valve 2SX010 following Modification;  
      These activities were selected based upon the structure, system, and components
*  
      (SSCs) ability to impact risk. The inspectors evaluated these activities for the following
Unit 1 C Loop Steam Generator Power Operated Relief Valve following Hand  
      (as applicable): the effect of testing on the plant had been adequately addressed; testing
Pump Replacement;  
      was adequate for the maintenance performed; acceptance criteria were clear and
*  
      demonstrated operational readiness; test instrumentation was appropriate; tests were
Unit 2 Train B Auxiliary Feedwater Pump following Scheduled Maintenance; and  
      performed as written in accordance with properly reviewed and approved procedures;
*  
      equipment was returned to its operational status following testing (temporary
Unit Common Component Cooling Heat Exchanger Discharge Valve 0SX007  
      modifications or jumpers required for test performance were properly removed after test
following Electrical Modification.  
      completion); and test documentation was properly evaluated. The inspectors evaluated
These activities were selected based upon the structure, system, and components  
      the activities against TSs, the UFSAR, 10 CFR Part 50 requirements, licensee
(SSCs) ability to impact risk. The inspectors evaluated these activities for the following  
      procedures, and various NRC generic communications to ensure that the test results
(as applicable): the effect of testing on the plant had been adequately addressed; testing  
      adequately ensured that the equipment met the licensing basis and design
was adequate for the maintenance performed; acceptance criteria were clear and  
      requirements. In addition, the inspectors reviewed corrective action documents
demonstrated operational readiness; test instrumentation was appropriate; tests were  
      associated with post maintenance tests to determine whether the licensee was
performed as written in accordance with properly reviewed and approved procedures;  
      identifying problems and entering them in the CAP and that the problems were being
equipment was returned to its operational status following testing (temporary  
      corrected commensurate with their importance to safety. Documents reviewed are listed
modifications or jumpers required for test performance were properly removed after test  
      in the Attachment.
completion); and test documentation was properly evaluated. The inspectors evaluated  
                                              13                                Enclosure
the activities against TSs, the UFSAR, 10 CFR Part 50 requirements, licensee  
procedures, and various NRC generic communications to ensure that the test results  
adequately ensured that the equipment met the licensing basis and design  
requirements. In addition, the inspectors reviewed corrective action documents  
associated with post maintenance tests to determine whether the licensee was  
identifying problems and entering them in the CAP and that the problems were being  
corrected commensurate with their importance to safety. Documents reviewed are listed  
in the Attachment.  


        This inspection constituted four post maintenance testing samples as defined in
14
        IP 71111.19-05.
Enclosure
    b. Findings
This inspection constituted four post maintenance testing samples as defined in  
        No findings were identified.
IP 71111.19-05.  
1R22 Surveillance Testing (71111.22)
b. Findings  
.1     Surveillance Testing
No findings were identified.  
  a.   Inspection Scope
1R22 Surveillance Testing (71111.22)  
        The inspectors reviewed the test results for the following activities to determine whether
.1  
        risk significant systems and equipment were capable of performing their intended safety
Surveillance Testing  
        function and to verify testing was conducted in accordance with applicable procedural
a.  
        and TS requirements:
Inspection Scope  
        *       Unit 1 Train A Diesel Generator Routine Monthly Surveillance;
The inspectors reviewed the test results for the following activities to determine whether  
        *       Unit 1 Train B Auxiliary Feedwater Pump Monthly Surveillance; and
risk significant systems and equipment were capable of performing their intended safety  
        *       Unit 1 Train B CS Valve Stroke Test 1BOSR 0.5-2.CS.1-2.
function and to verify testing was conducted in accordance with applicable procedural  
        The inspectors observed in-plant activities and reviewed procedures and associated
and TS requirements:  
        records to determine the following:
*  
        *       did preconditioning occur;
Unit 1 Train A Diesel Generator Routine Monthly Surveillance;  
        *       were the effects of the testing adequately addressed by control room personnel or
*  
                engineers prior to the commencement of the testing;
Unit 1 Train B Auxiliary Feedwater Pump Monthly Surveillance; and  
        *       were acceptance criteria clearly stated, demonstrated operational readiness, and
*  
                consistent with the system design basis;
Unit 1 Train B CS Valve Stroke Test 1BOSR 0.5-2.CS.1-2.  
        *       plant equipment calibration was correct, accurate, and properly documented;
The inspectors observed in-plant activities and reviewed procedures and associated  
        *       as left setpoints were within required ranges; and the calibration frequency were
records to determine the following:  
                in accordance with TSs, the UFSAR, procedures, and applicable commitments;
*  
        *       measuring and test equipment calibration was current;
did preconditioning occur;
        *       test equipment was used within the required range and accuracy; applicable
*  
                prerequisites described in the test procedures were satisfied;
were the effects of the testing adequately addressed by control room personnel or  
        *       test frequencies met TS requirements to demonstrate operability and reliability;
engineers prior to the commencement of the testing;  
                tests were performed in accordance with the test procedures and other applicable
*  
                procedures; jumpers and lifted leads were controlled and restored where used;
were acceptance criteria clearly stated, demonstrated operational readiness, and  
        *       test data and results were accurate, complete, within limits, and valid;
consistent with the system design basis;  
        *       test equipment was removed after testing;
*  
        *       where applicable for inservice testing (IST) activities, testing was performed in
plant equipment calibration was correct, accurate, and properly documented;  
                accordance with the applicable version of Section XI of the American Society of
*  
                Mechnical Engineers (ASME) Code, and reference values were consistent with
as left setpoints were within required ranges; and the calibration frequency were  
                the system design basis;
in accordance with TSs, the UFSAR, procedures, and applicable commitments;  
        *       where applicable, test results not meeting acceptance criteria were addressed
*  
                with an adequate operability evaluation or the system or component was declared
measuring and test equipment calibration was current;  
                inoperable;
*  
        *       where applicable for safety-related instrument control surveillance tests, reference
test equipment was used within the required range and accuracy; applicable  
                setting data were accurately incorporated in the test procedure;
prerequisites described in the test procedures were satisfied;  
                                                14                                  Enclosure
*  
test frequencies met TS requirements to demonstrate operability and reliability;  
tests were performed in accordance with the test procedures and other applicable  
procedures; jumpers and lifted leads were controlled and restored where used;  
*  
test data and results were accurate, complete, within limits, and valid;  
*  
test equipment was removed after testing;  
*  
where applicable for inservice testing (IST) activities, testing was performed in  
accordance with the applicable version of Section XI of the American Society of  
Mechnical Engineers (ASME) Code, and reference values were consistent with  
the system design basis;  
*  
where applicable, test results not meeting acceptance criteria were addressed  
with an adequate operability evaluation or the system or component was declared  
inoperable;  
*  
where applicable for safety-related instrument control surveillance tests, reference  
setting data were accurately incorporated in the test procedure;  


      *     where applicable, actual conditions encountering high resistance electrical
15
            contacts were such that the intended safety function could still be accomplished;
Enclosure
      *     prior procedure changes had not provided an opportunity to identify problems
*  
            encountered during the performance of the surveillance or calibration test;
where applicable, actual conditions encountering high resistance electrical  
      *     equipment was returned to a position or status required to support the
contacts were such that the intended safety function could still be accomplished;  
            performance of its safety functions; and
*  
      *     all problems identified during the testing were appropriately documented and
prior procedure changes had not provided an opportunity to identify problems  
            dispositioned in the CAP.
encountered during the performance of the surveillance or calibration test;  
      Documents reviewed are listed in the Attachment.
*  
      This inspection constituted two routine surveillance testing samples and one IST sample
equipment was returned to a position or status required to support the  
      as defined in IP 71111.22, Sections -02 and -05.
performance of its safety functions; and  
  b. Findings
*  
      No findings were identified.
all problems identified during the testing were appropriately documented and  
      Cornerstone: Emergency Preparedness
dispositioned in the CAP.  
1EP2 Alert and Notification System Evaluation (71114.02)
Documents reviewed are listed in the Attachment.  
.1   Alert and Notification System Evaluation
This inspection constituted two routine surveillance testing samples and one IST sample  
  a. Inspection Scope
as defined in IP 71111.22, Sections -02 and -05.  
      The inspectors reviewed documents and conducted discussions with Emergency
b.  
      Preparedness (EP) staff and management regarding the operation, maintenance, and
Findings  
      periodic testing of the Alert and Notification System (ANS) in the Byron Station's plume
No findings were identified.  
      pathway Emergency Planning Zone. The inspectors reviewed monthly trend reports and
Cornerstone: Emergency Preparedness  
      the daily and monthly operability records from August 2010 through May 2012.
1EP2 Alert and Notification System Evaluation (71114.02)  
      Information gathered during document reviews and interviews was used to determine
.1  
      whether the ANS equipment was maintained and tested in accordance with Emergency
Alert and Notification System Evaluation  
      Plan commitments and procedures. Documents reviewed are listed in the Attachment to
a.  
      this report.
Inspection Scope  
      This ANS inspection constituted one sample as defined in IP 71114.02-05.
The inspectors reviewed documents and conducted discussions with Emergency  
  b. Findings
Preparedness (EP) staff and management regarding the operation, maintenance, and  
      No findings were identified.
periodic testing of the Alert and Notification System (ANS) in the Byron Station's plume  
1EP3 Emergency Response Organization Augmentation Testing (71114.03)
pathway Emergency Planning Zone. The inspectors reviewed monthly trend reports and  
.1   Emergency Response Organization Augmentation Testing
the daily and monthly operability records from August 2010 through May 2012.
  a. Inspection Scope
Information gathered during document reviews and interviews was used to determine  
      The inspectors reviewed and discussed with plant EP management and staff the
whether the ANS equipment was maintained and tested in accordance with Emergency  
      emergency plan commitments and procedures that addressed the primary and alternate
Plan commitments and procedures. Documents reviewed are listed in the Attachment to  
      methods of initiating an Emergency Response Organization (ERO) activation to augment
this report.  
                                              15                                Enclosure
This ANS inspection constituted one sample as defined in IP 71114.02-05.  
b.  
Findings  
No findings were identified.  
1EP3 Emergency Response Organization Augmentation Testing (71114.03)  
.1  
Emergency Response Organization Augmentation Testing  
a.  
Inspection Scope  
The inspectors reviewed and discussed with plant EP management and staff the  
emergency plan commitments and procedures that addressed the primary and alternate  
methods of initiating an Emergency Response Organization (ERO) activation to augment  


      the on shift ERO as well as the provisions for maintaining the stations ERO qualification
16
      and team lists. The inspectors reviewed reports and a sample of corrective action
Enclosure
      program records of unannounced off-hour augmentation tests and pager tests, which
the on shift ERO as well as the provisions for maintaining the stations ERO qualification  
      were conducted between August 2010 and May 2012, to determine the adequacy of the
and team lists. The inspectors reviewed reports and a sample of corrective action  
      drill critiques and associated corrective actions. The inspectors also reviewed a sample
program records of unannounced off-hour augmentation tests and pager tests, which  
      of the EP training records of approximately 18 ERO personnel who were assigned to key
were conducted between August 2010 and May 2012, to determine the adequacy of the  
      and support positions, to determine the status of their training as it related to their
drill critiques and associated corrective actions. The inspectors also reviewed a sample  
      assigned ERO positions. Documents reviewed are listed in the Attachment.
of the EP training records of approximately 18 ERO personnel who were assigned to key  
      This ERO augmentation testing inspection constituted one sample as defined in
and support positions, to determine the status of their training as it related to their  
      IP 71114.03-05.
assigned ERO positions. Documents reviewed are listed in the Attachment.  
  b. Findings
This ERO augmentation testing inspection constituted one sample as defined in  
      No findings were identified.
IP 71114.03-05.  
1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)
b.  
.1   Correction of Emergency Preparedness Weaknesses and Deficiencies
Findings  
  a. Inspection Scope
No findings were identified.  
      The inspectors reviewed a sample of Nuclear Oversight (NOS) staffs 2011 and 2012
1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)  
      audits of the Byron Station's EP program to determine that the independent
.1  
      assessments met the requirements of 10 CFR 50.54(t). The inspectors also reviewed
Correction of Emergency Preparedness Weaknesses and Deficiencies  
      samples of corrective action program records associated with the 2011 biennial
a.  
      exercise, as well as various EP drills conducted in 2011 and 2012, in order to determine
Inspection Scope  
      whether the licensee fulfilled drill commitments and to evaluate the licensees efforts to
The inspectors reviewed a sample of Nuclear Oversight (NOS) staffs 2011 and 2012  
      identify and resolve identified issues. The inspectors reviewed a sample of EP items
audits of the Byron Station's EP program to determine that the independent  
      and corrective actions related to the facilitys EP program and activities to determine
assessments met the requirements of 10 CFR 50.54(t). The inspectors also reviewed  
      whether corrective actions were completed in accordance with the sites corrective
samples of corrective action program records associated with the 2011 biennial  
      action program. Documents reviewed are listed in the Attachment.
exercise, as well as various EP drills conducted in 2011 and 2012, in order to determine  
      This correction of EP weaknesses and deficiencies inspection constituted one sample as
whether the licensee fulfilled drill commitments and to evaluate the licensees efforts to  
      defined in IP 71114.05-05.
identify and resolve identified issues. The inspectors reviewed a sample of EP items  
  b. Findings
and corrective actions related to the facilitys EP program and activities to determine  
      No findings were identified.
whether corrective actions were completed in accordance with the sites corrective  
1EP6 Drill Evaluation (71114.06)
action program. Documents reviewed are listed in the Attachment.  
.1   Emergency Preparedness Drill Observation
This correction of EP weaknesses and deficiencies inspection constituted one sample as  
  a. Inspection Scope
defined in IP 71114.05-05.  
      The inspectors evaluated the conduct of a routine licensee emergency drill on
b.  
      June 28, 2012, to identify any weaknesses and deficiencies in classification, notification,
Findings  
      and protective action recommendation development activities. The inspectors observed
No findings were identified.  
      emergency response operations in the simulator to determine whether the event
1EP6 Drill Evaluation (71114.06)  
      classification, notifications, and protective action recommendations were performed in
.1  
                                              16                                  Enclosure
Emergency Preparedness Drill Observation  
a.  
Inspection Scope  
The inspectors evaluated the conduct of a routine licensee emergency drill on  
June 28, 2012, to identify any weaknesses and deficiencies in classification, notification,  
and protective action recommendation development activities. The inspectors observed  
emergency response operations in the simulator to determine whether the event  
classification, notifications, and protective action recommendations were performed in  


      accordance with procedures. The inspectors also attended the licensee drill critique to
17
      compare any inspector-observed weakness with those identified by the licensee staff in
Enclosure
      order to evaluate the critique and to verify whether the licensee staff was properly
accordance with procedures. The inspectors also attended the licensee drill critique to  
      identifying weaknesses and entering them into the corrective action program. As part of
compare any inspector-observed weakness with those identified by the licensee staff in  
      the inspection, the inspectors reviewed the drill package and other documents listed in
order to evaluate the critique and to verify whether the licensee staff was properly  
      the Attachment to this report.
identifying weaknesses and entering them into the corrective action program. As part of  
      This emergency preparedness drill inspection constituted one sample as defined in
the inspection, the inspectors reviewed the drill package and other documents listed in  
      IP 71114.06-05.
the Attachment to this report.  
  b. Findings
This emergency preparedness drill inspection constituted one sample as defined in  
      No findings were identified.
IP 71114.06-05.  
2.   OTHER ACTIVITIES
b.  
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and
Findings  
      Emergency Preparedness
No findings were identified.  
4OA1 Performance Indicator Verification (71151)
2.  
.1   Drill/Exercise Performance
OTHER ACTIVITIES  
  a. Inspection Scope
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and  
      The inspectors sampled licensee submittals for the Drill and Exercise Performance
Emergency Preparedness  
      (DEP) Performance Indicator (PI) for the period from the third quarter 2011 through
4OA1 Performance Indicator Verification (71151)  
      first quarter 2012. To determine the accuracy of the PI data reported during those
.1  
      periods, PI definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02,
Drill/Exercise Performance  
      Regulatory Assessment Performance Indicator Guideline, Revision 6, were used. The
a.  
      inspectors reviewed the licensees records associated with the PI to verify that the
Inspection Scope  
      licensee accurately reported the DEP indicator in accordance with relevant procedures
The inspectors sampled licensee submittals for the Drill and Exercise Performance  
      and the NEI guidance. Specifically, the inspectors reviewed licensee records and
(DEP) Performance Indicator (PI) for the period from the third quarter 2011 through  
      processes including procedural guidance on assessing opportunities for the PI;
first quarter 2012. To determine the accuracy of the PI data reported during those  
      assessments of PI opportunities during pre-designated control room simulator training
periods, PI definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02,  
      sessions, performance during the 2011 biennial exercise, and performance during other
Regulatory Assessment Performance Indicator Guideline, Revision 6, were used. The  
      drills. Specific documents reviewed are listed in the Attachment.
inspectors reviewed the licensees records associated with the PI to verify that the  
      This inspection constitutes one DEP sample as defined in IP 71151-05.
licensee accurately reported the DEP indicator in accordance with relevant procedures  
  b. Findings
and the NEI guidance. Specifically, the inspectors reviewed licensee records and  
      No findings were identified.
processes including procedural guidance on assessing opportunities for the PI;  
.2   Emergency Response Organization Drill Participation
assessments of PI opportunities during pre-designated control room simulator training  
  a. Inspection Scope
sessions, performance during the 2011 biennial exercise, and performance during other  
      The inspectors sampled licensee submittals for the ERO Drill Participation PI for the
drills. Specific documents reviewed are listed in the Attachment.  
      period from the third quarter 2011 through first quarter 2012. To determine the accuracy
This inspection constitutes one DEP sample as defined in IP 71151-05.  
      of the PI data reported during those periods, PI definitions and guidance contained in the
b.  
                                            17                                Enclosure
Findings  
No findings were identified.  
.2  
Emergency Response Organization Drill Participation  
a.  
Inspection Scope  
The inspectors sampled licensee submittals for the ERO Drill Participation PI for the  
period from the third quarter 2011 through first quarter 2012. To determine the accuracy  
of the PI data reported during those periods, PI definitions and guidance contained in the  


      NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, were
18
      used. The inspectors reviewed the licensees records associated with the PI to verify
Enclosure
      that the licensee accurately reported the indicator in accordance with relevant
NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, were  
      procedures and the NEI guidance. Specifically, the inspectors reviewed licensee
used. The inspectors reviewed the licensees records associated with the PI to verify  
      records and processes including procedural guidance on assessing opportunities for the
that the licensee accurately reported the indicator in accordance with relevant  
      PI; performance during the 2011 biennial exercise and other drills; and revisions of the
procedures and the NEI guidance. Specifically, the inspectors reviewed licensee  
      roster of personnel assigned to key emergency response organization positions.
records and processes including procedural guidance on assessing opportunities for the  
      Specific documents reviewed are listed in the Attachment.
PI; performance during the 2011 biennial exercise and other drills; and revisions of the  
      This inspection constitutes one ERO drill participation sample as defined in IP 71151-05.
roster of personnel assigned to key emergency response organization positions.
  b. Findings
Specific documents reviewed are listed in the Attachment.  
      No findings were identified.
This inspection constitutes one ERO drill participation sample as defined in IP 71151-05.  
.3   Alert and Notification System
b.  
  a. Inspection Scope
Findings  
      The inspectors sampled licensee submittals for the ANS PI for the period from the third
No findings were identified.  
      quarter 2011 through first quarter 2012. To determine the accuracy of the PI data
.3  
      reported during those periods, PI definitions and guidance contained in the NEI 99-02,
Alert and Notification System  
      Regulatory Assessment Performance Indicator Guideline, Revision 6, were used. The
a.  
      inspectors reviewed the licensees records associated with the PI to verify that the
Inspection Scope  
      licensee accurately reported the indicator in accordance with relevant procedures and
The inspectors sampled licensee submittals for the ANS PI for the period from the third  
      the NEI guidance. Specifically, the inspectors reviewed licensee records and processes
quarter 2011 through first quarter 2012. To determine the accuracy of the PI data  
      including procedural guidance on assessing opportunities for the PI and results of
reported during those periods, PI definitions and guidance contained in the NEI 99-02,  
      periodic ANS operability tests. Specific documents reviewed are listed in the
Regulatory Assessment Performance Indicator Guideline, Revision 6, were used. The  
      Attachment.
inspectors reviewed the licensees records associated with the PI to verify that the  
      This inspection constitutes one ANS sample as defined in IP 71151-05.
licensee accurately reported the indicator in accordance with relevant procedures and  
  b. Findings
the NEI guidance. Specifically, the inspectors reviewed licensee records and processes  
      No findings were identified.
including procedural guidance on assessing opportunities for the PI and results of  
4OA2 Identification and Resolution of Problems (71152)
periodic ANS operability tests. Specific documents reviewed are listed in the  
.1   Routine Review of Items Entered into the Corrective Action Program
Attachment.  
  a. Inspection Scope
This inspection constitutes one ANS sample as defined in IP 71151-05.  
      As part of the various baseline inspection procedures discussed in previous sections of
b.  
      this report, the inspectors routinely reviewed issues during baseline inspection activities
Findings  
      and plant status reviews to verify that they were being entered into the licensees CAP at
No findings were identified.  
      an appropriate threshold, that adequate attention was being given to timely corrective
4OA2 Identification and Resolution of Problems (71152)  
      actions, and that adverse trends were identified and addressed. Attributes reviewed
.1  
      included the complete and accurate identification of the problem; that timeliness was
Routine Review of Items Entered into the Corrective Action Program  
      commensurate with the safety significance; that evaluation and disposition of
a.  
      performance issues, generic implications, common causes, contributing factors, root
Inspection Scope  
      causes, extent-of-condition reviews, and previous occurrence reviews were proper and
As part of the various baseline inspection procedures discussed in previous sections of  
                                              18                                Enclosure
this report, the inspectors routinely reviewed issues during baseline inspection activities  
and plant status reviews to verify that they were being entered into the licensees CAP at  
an appropriate threshold, that adequate attention was being given to timely corrective  
actions, and that adverse trends were identified and addressed. Attributes reviewed  
included the complete and accurate identification of the problem; that timeliness was  
commensurate with the safety significance; that evaluation and disposition of  
performance issues, generic implications, common causes, contributing factors, root  
causes, extent-of-condition reviews, and previous occurrence reviews were proper and  


    adequate; and that the classification, prioritization, focus, and timeliness of corrective
19
    actions were commensurate with safety and sufficient to prevent recurrence of the issue.
Enclosure
    Minor issues entered into the licensees CAP as a result of the inspectors observations
adequate; and that the classification, prioritization, focus, and timeliness of corrective  
    are included in the attached List of Documents Reviewed.
actions were commensurate with safety and sufficient to prevent recurrence of the issue.
    These routine reviews for the identification and resolution of problems did not constitute
Minor issues entered into the licensees CAP as a result of the inspectors observations  
    any additional inspection samples. Instead, by procedure they were considered an
are included in the attached List of Documents Reviewed.  
    integral part of the inspections performed during the quarter and documented in
These routine reviews for the identification and resolution of problems did not constitute  
    Section 1 of this report.
any additional inspection samples. Instead, by procedure they were considered an  
  b. Findings
integral part of the inspections performed during the quarter and documented in  
    No findings were identified.
Section 1 of this report.  
.2   Daily Corrective Action Program Reviews
b.  
  a. Inspection Scope
Findings  
    In order to assist with the identification of repetitive equipment failures and specific
No findings were identified.  
    human performance issues for follow-up, the inspectors performed a daily screening
.2  
    of items entered into the licensees CAP. This review was accomplished through
Daily Corrective Action Program Reviews  
    inspection of the stations daily condition report packages.
a.  
    These daily reviews were performed by procedure as part of the inspectors daily plant
Inspection Scope  
    status monitoring activities and, as such, did not constitute any separate inspection
In order to assist with the identification of repetitive equipment failures and specific  
    samples.
human performance issues for follow-up, the inspectors performed a daily screening  
  b. Findings
of items entered into the licensees CAP. This review was accomplished through  
    No findings were identified.
inspection of the stations daily condition report packages.  
.3   Semi-Annual Trend Review
These daily reviews were performed by procedure as part of the inspectors daily plant  
  a. Inspection Scope
status monitoring activities and, as such, did not constitute any separate inspection  
    The inspectors performed a review of the licensees CAP and associated documents to
samples.  
    identify trends that could indicate the existence of a more significant safety issue.
b.  
    The inspectors review was focused on repetitive equipment issues, but also considered
Findings  
    the results of daily inspector CAP item screening discussed in Section 4OA2.2 above,
No findings were identified.  
    licensee trending efforts, and licensee human performance results. The inspectors
.3  
    review nominally considered the six month period of July 01 through March 31, 2012,
Semi-Annual Trend Review  
    although some examples expanded beyond those dates where the scope of the trend
a.  
    warranted.
Inspection Scope  
    As part of this inspection, the inspectors also reviewed issues that could be documented
The inspectors performed a review of the licensees CAP and associated documents to  
    outside the normal CAP such as in major equipment problem lists, repetitive and/or
identify trends that could indicate the existence of a more significant safety issue.
    rework maintenance lists, departmental problem/challenges lists, system health reports,
The inspectors review was focused on repetitive equipment issues, but also considered  
    quality assurance audit/surveillance reports, self assessment reports, and Maintenance
the results of daily inspector CAP item screening discussed in Section 4OA2.2 above,  
    Rule assessments. The inspectors compared and contrasted their results with the
licensee trending efforts, and licensee human performance results. The inspectors  
    results contained in the licensees CAP trending reports.
review nominally considered the six month period of July 01 through March 31, 2012,  
                                              19                                  Enclosure
although some examples expanded beyond those dates where the scope of the trend  
warranted.  
As part of this inspection, the inspectors also reviewed issues that could be documented  
outside the normal CAP such as in major equipment problem lists, repetitive and/or  
rework maintenance lists, departmental problem/challenges lists, system health reports,  
quality assurance audit/surveillance reports, self assessment reports, and Maintenance  
Rule assessments. The inspectors compared and contrasted their results with the  
results contained in the licensees CAP trending reports.  


b. Findings
20
    One finding with two examples was identified. The examples are discussed below. Both
Enclosure
    examples had the same cause and the same cross-cutting aspect.
b.  
(1) (Closed) Unresolved Item 05000454/2012002-02: Potential Under-Torque of Valve
Findings  
    1RC8042B
One finding with two examples was identified. The examples are discussed below. Both  
    Introduction: The first of the two examples of a self-revealed finding of very low safety
examples had the same cause and the same cross-cutting aspect.  
    significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B,
(1) (Closed) Unresolved Item 05000454/2012002-02: Potential Under-Torque of Valve  
    Criterion V, Instructions, Procedures, and Drawings, was identified when licensee
1RC8042B
    personnel failed to properly torque an RCS pressure boundary valve closed. The valve
Introduction: The first of the two examples of a self-revealed finding of very low safety  
    closure bolts subsequently relaxed and internal bypass around a diaphragm occurred
significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B,  
    resulting in a small RCS leak into containment.
Criterion V, Instructions, Procedures, and Drawings, was identified when licensee  
    Description: On March 11, 2012, the licensee reduced power on Unit 1 to perform
personnel failed to properly torque an RCS pressure boundary valve closed. The valve  
    robotic inspections inside of containment. Based on the results of the inspections, the
closure bolts subsequently relaxed and internal bypass around a diaphragm occurred  
    licensee shut down Unit 1 and replaced valve 1RC8042B. URI 05000454/2012002-02
resulting in a small RCS leak into containment.  
    was open in NRC Inspection Report 05000454/2012002; 05000455/2012002 pending
Description: On March 11, 2012, the licensee reduced power on Unit 1 to perform  
    the licensees completion of the rework evaluation and the inspectors review and follow
robotic inspections inside of containment. Based on the results of the inspections, the  
    up of the evaluation. Subsequently, licensee personnel performed a root cause
licensee shut down Unit 1 and replaced valve 1RC8042B. URI 05000454/2012002-02  
    evaluation and determined that procedure BMP 3100-13, Kerotest Globe Valve Repair,
was open in NRC Inspection Report 05000454/2012002; 05000455/2012002 pending  
    failed to provide sufficient detail to ensure the proper torque value was selected.
the licensees completion of the rework evaluation and the inspectors review and follow  
    For valve 1RC8042B, BMP 3100-13 required that the maintenance worker select the
up of the evaluation. Subsequently, licensee personnel performed a root cause  
    required torque from a table which contained both stainless steel and carbon steel
evaluation and determined that procedure BMP 3100-13, Kerotest Globe Valve Repair,  
    values. During refueling outage B1R17, the maintenance crews repaired valve
failed to provide sufficient detail to ensure the proper torque value was selected.  
    1RC8042B along with 1RC8042D. As the valves contained stainless steel and carbon
For valve 1RC8042B, BMP 3100-13 required that the maintenance worker select the  
    steel sub-components, the maintenance crews requested their supervisors to provide
required torque from a table which contained both stainless steel and carbon steel  
    guidance as to which torque value to use. The supervisor for the crew repairing valve
values. During refueling outage B1R17, the maintenance crews repaired valve  
    1RC8042D selected the correct (higher) torque valve. The supervisor for the crew
1RC8042B along with 1RC8042D. As the valves contained stainless steel and carbon  
    repairing valve 1RC8042B selected the incorrect (lower) torque value.
steel sub-components, the maintenance crews requested their supervisors to provide  
    Several months following restart after the refueling outage, valve 1RC8042B began
guidance as to which torque value to use. The supervisor for the crew repairing valve  
    leaking into containment as the inadequate retention forces allowed reactor coolant to
1RC8042D selected the correct (higher) torque valve. The supervisor for the crew  
    flow around an internal diaphragm. This leakage resulted in erosion and corrosion of the
repairing valve 1RC8042B selected the incorrect (lower) torque value.  
    carbon steel yoke threads and eventually resulted in external valve leakage.
Several months following restart after the refueling outage, valve 1RC8042B began  
    The reactor coolant leakage was small and did not raise the daily unidentified leak rate
leaking into containment as the inadequate retention forces allowed reactor coolant to  
    calculations sufficiently to clearly indicate a problem. However, the leak slowly
flow around an internal diaphragm. This leakage resulted in erosion and corrosion of the  
    increased containment airborne tritium levels. The increase in containment tritium levels
carbon steel yoke threads and eventually resulted in external valve leakage.  
    along with an occasional elevated RCS leak rate value eventually caused the licensee to
The reactor coolant leakage was small and did not raise the daily unidentified leak rate  
    conclude that a small leak existed that needed to be evaluated. Subsequent to the
calculations sufficiently to clearly indicate a problem. However, the leak slowly  
    identification of the leak the licensee performed an assessment to determine if they
increased containment airborne tritium levels. The increase in containment tritium levels  
    could have identified the leak sooner. The licensee determined the available information
along with an occasional elevated RCS leak rate value eventually caused the licensee to  
    was discounted and not well understood, which led to an unnecessary delay in
conclude that a small leak existed that needed to be evaluated. Subsequent to the  
    performing a down power to search for the leak. The inspectors agreed with the
identification of the leak the licensee performed an assessment to determine if they  
    licensees determination.
could have identified the leak sooner. The licensee determined the available information  
                                            20                              Enclosure
was discounted and not well understood, which led to an unnecessary delay in  
performing a down power to search for the leak. The inspectors agreed with the  
licensees determination.  


The inspectors reviewed the licensees root cause analysis of this self-revealed RCS
21
leak documented in IR 1339375. The inspectors performed their own assessment and
Enclosure
agreed with the licensees root cause determination of  an inadequate maintenance
The inspectors reviewed the licensees root cause analysis of this self-revealed RCS  
procedure instruction for Kerotest globe valve repairThe maintenance procedure was
leak documented in IR 1339375. The inspectors performed their own assessment and  
not written explicitly to apply the torque value based on valve body material. Corrective
agreed with the licensees root cause determination of  an inadequate maintenance  
action included replacing the leaking valve upon identification. Additional corrective
procedure instruction for Kerotest globe valve repairThe maintenance procedure was  
actions included modifying the installation procedure to add clarity in the selection of the
not written explicitly to apply the torque value based on valve body material. Corrective  
proper torque value.
action included replacing the leaking valve upon identification. Additional corrective  
Analysis: The inspectors determined that the failure to have adequate work instructions
actions included modifying the installation procedure to add clarity in the selection of the  
for a Kerotest Globe valve repair was a performance deficiency. The finding was
proper torque value.  
determined to be more than minor in accordance with IMC 0612, Appendix B, Issue
Analysis: The inspectors determined that the failure to have adequate work instructions  
Screening, because it was associated with the Procedure Quality attribute of the
for a Kerotest Globe valve repair was a performance deficiency. The finding was  
Initiating Events Cornerstone and adversely affected the cornerstone objective of limiting
determined to be more than minor in accordance with IMC 0612, Appendix B, Issue  
the likelihood of those events that upset plant stability and challenge critical safety
Screening, because it was associated with the Procedure Quality attribute of the  
functions during shutdown as well as power operations. Specifically, this issue increased
Initiating Events Cornerstone and adversely affected the cornerstone objective of limiting  
the risk of a small break loss of coolant accident.
the likelihood of those events that upset plant stability and challenge critical safety  
The inspectors performed a Phase 1 SDP screening using IMC 0609, Attachment 4,
functions during shutdown as well as power operations. Specifically, this issue increased  
Table 4a, Characterization Worksheet for Initiating Events Cornerstone. The
the risk of a small break loss of coolant accident.  
inspectors answered No to the question Assuming worst case degradation, would the
The inspectors performed a Phase 1 SDP screening using IMC 0609, Attachment 4,  
finding result in exceeding the Tech Spec [Technical Specification] limit for any RCS
Table 4a, Characterization Worksheet for Initiating Events Cornerstone. The  
leakage or could the finding have likely affected other mitigation systems resulting in a
inspectors answered No to the question Assuming worst case degradation, would the  
total loss of their safety function. Therefore, example one of this finding was
finding result in exceeding the Tech Spec [Technical Specification] limit for any RCS  
determined to be of very low safety significance (Green).
leakage or could the finding have likely affected other mitigation systems resulting in a  
This example had a cross-cutting aspect in the Work Practices component of the Human
total loss of their safety function. Therefore, example one of this finding was  
Performance cross-cutting area because licensee personnel failed to utilize human error
determined to be of very low safety significance (Green).  
prevention techniques, such as using the correct procedural torqueing requirement
This example had a cross-cutting aspect in the Work Practices component of the Human  
[H.4(a)].
Performance cross-cutting area because licensee personnel failed to utilize human error  
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
prevention techniques, such as using the correct procedural torqueing requirement  
and Drawings, requires, in part, that activities affecting quality shall be prescribed by
[H.4(a)].  
documented instructions, procedures or drawings of a type appropriate to the
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,  
circumstances and shall include appropriate quantitative or qualitative acceptance
and Drawings, requires, in part, that activities affecting quality shall be prescribed by  
criteria for determining that important activities have been satisfactorily accomplished.
documented instructions, procedures or drawings of a type appropriate to the  
Licensee procedure BMP 3100-13, Revision 10, Kerotest Globe Valve Repair, was
circumstances and shall include appropriate quantitative or qualitative acceptance  
written in accordance with 10 CFR Part 50, Appendix B and prescribed an activity
criteria for determining that important activities have been satisfactorily accomplished.  
affecting quality. Step F.1 of procedure BMP 3100-13 required that the maintenance
Licensee procedure BMP 3100-13, Revision 10, Kerotest Globe Valve Repair, was  
workers select which torque value to use to reassemble the valve body.
written in accordance with 10 CFR Part 50, Appendix B and prescribed an activity  
Contrary to the above, as of March 14, 2012, the licensee failed to have an adequate
affecting quality. Step F.1 of procedure BMP 3100-13 required that the maintenance  
procedure for the Kerotest globe valve repair, an activity affecting quality, which included
workers select which torque value to use to reassemble the valve body.  
appropriate quantitative or qualitative acceptance criteria for determining that important
Contrary to the above, as of March 14, 2012, the licensee failed to have an adequate  
activities have been satisfactorily accomplished. Specifically, procedure BMP 3100-13
procedure for the Kerotest globe valve repair, an activity affecting quality, which included  
did not contain the appropriate instructions for determining the torque value to use to
appropriate quantitative or qualitative acceptance criteria for determining that important  
reassemble the valve body such that the valve leaked following restart. Because this
activities have been satisfactorily accomplished. Specifically, procedure BMP 3100-13  
violation was of very low safety significance and because this issue was entered into the
did not contain the appropriate instructions for determining the torque value to use to  
                                        21                                  Enclosure
reassemble the valve body such that the valve leaked following restart. Because this  
violation was of very low safety significance and because this issue was entered into the


    licensees CAP as IR 133975, this violation is being treated as a NCV, consistent with
22
    Section 2.3.2 of the NRC Enforcement Policy. The is the first example of the NCV.
Enclosure
    (NCV 05000454/2012003-02; Failure to Have Instructions Appropriate to the
licensees CAP as IR 133975, this violation is being treated as a NCV, consistent with  
    Circumstances)
Section 2.3.2 of the NRC Enforcement Policy. The is the first example of the NCV.
    URI 05000454/2010002-02 is closed.
(NCV 05000454/2012003-02; Failure to Have Instructions Appropriate to the  
(2) One Train of Containment Cooling System Inoperable Longer Than Allowed by
Circumstances)  
    Technical Specifications Due to Inadequate Work Instructions
URI 05000454/2010002-02 is closed.  
    Introduction: The second of the two examples of a self-revealed finding of very low
(2) One Train of Containment Cooling System Inoperable Longer Than Allowed by  
    safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B,
Technical Specifications Due to Inadequate Work Instructions
    Criterion V, Instructions, Procedures, and Drawings, was identified when licensee
Introduction: The second of the two examples of a self-revealed finding of very low  
    personnel failed to properly re-install a Reactor Containment Fan Cooler (RCFC) interior
safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B,  
    access panel during the previous refueling outage.
Criterion V, Instructions, Procedures, and Drawings, was identified when licensee  
    Description: On March 29, 2012, the licensee was performing an inspection inside the
personnel failed to properly re-install a Reactor Containment Fan Cooler (RCFC) interior  
    Unit 1 Train A RCFC when personnel identified an access hatch that was not properly
access panel during the previous refueling outage.
    installed. The hatch was four feet by six feet and allowed air to bypass the safety-
Description: On March 29, 2012, the licensee was performing an inspection inside the  
    related cooling coils.
Unit 1 Train A RCFC when personnel identified an access hatch that was not properly  
    The licensee determined that the cause of the hatch not being properly installed during
installed. The hatch was four feet by six feet and allowed air to bypass the safety-
    the previous refueling outage was an inadequate level of detail provided in the work
related cooling coils.  
    package. The work package only contained a general work instruction to remove interior
The licensee determined that the cause of the hatch not being properly installed during  
    panels as necessary. In addition, the RCFC interior hatches did not contain any unique
the previous refueling outage was an inadequate level of detail provided in the work  
    identifiers. Safety-related drawings which were referenced in the work package and
package. The work package only contained a general work instruction to remove interior  
    might have assisted the workers did not contain any unique identifiers for the interior
panels as necessary. In addition, the RCFC interior hatches did not contain any unique  
    hatches.
identifiers. Safety-related drawings which were referenced in the work package and  
    There are four RCFCs in each of the two containments at Byron. Two RCFCs are in
might have assisted the workers did not contain any unique identifiers for the interior  
    each of the two safety-related trains of containment cooling. The failure to properly
hatches.  
    reinstall the access hatch affected the ability of the Unit 1 Train A RCFC to remove heat
There are four RCFCs in each of the two containments at Byron. Two RCFCs are in  
    from containment when using only the safety-related Essential Service Water (SX)
each of the two safety-related trains of containment cooling. The failure to properly  
    system. However, the A RCFC as well as the other RCFC in the train would still have
reinstall the access hatch affected the ability of the Unit 1 Train A RCFC to remove heat  
    removed a significant amount of heat following an accident.
from containment when using only the safety-related Essential Service Water (SX)  
    The licensees WO during the refueling outage referenced two safety-related drawings to
system. However, the A RCFC as well as the other RCFC in the train would still have  
    assist maintenance workers in the identification of the access hatches inside of the
removed a significant amount of heat following an accident.  
    RCFCs. The licensees cause determination team concluded that the drawings failed to
The licensees WO during the refueling outage referenced two safety-related drawings to  
    adequately identify the internal access hatches. This weakness combined with the lack
assist maintenance workers in the identification of the access hatches inside of the  
    of detailed work instructions in the WO caused the failure of the workers to ensure that
RCFCs. The licensees cause determination team concluded that the drawings failed to  
    all internal access hatches had been reinstalled following the required maintenance.
adequately identify the internal access hatches. This weakness combined with the lack  
    The inspectors reviewed the licensees cause determination, interviewed personnel, and
of detailed work instructions in the WO caused the failure of the workers to ensure that  
    assessed other license documents and agreed with the conclusion. The licensee
all internal access hatches had been reinstalled following the required maintenance.
    entered this issue into the CAP as IR 1347450 and planned to modify the RCFC
The inspectors reviewed the licensees cause determination, interviewed personnel, and  
    maintenance procedures to add detail and tracking aids for the removal of interior
assessed other license documents and agreed with the conclusion. The licensee  
    access panels prior to the next use of the procedures.
entered this issue into the CAP as IR 1347450 and planned to modify the RCFC  
                                            22                                Enclosure
maintenance procedures to add detail and tracking aids for the removal of interior  
access panels prior to the next use of the procedures.  


In addition, the licensee reinstalled the missing internal access hatch and inspected the
23
other RCFCs. No other access hatches were found to be uninstalled.
Enclosure
Analysis: The inspectors determined that the failure to have adequate work instructions
In addition, the licensee reinstalled the missing internal access hatch and inspected the  
for the removal and reinstallation of the interior access hatches for the RCFCs was a
other RCFCs. No other access hatches were found to be uninstalled.  
performance deficiency that required an evaluation using the SDP. The inspectors
Analysis: The inspectors determined that the failure to have adequate work instructions  
concluded that this second example of a finding was more than minor in accordance with
for the removal and reinstallation of the interior access hatches for the RCFCs was a  
Appendix B, Issue Screening, of IMC 0612, Power Reactor Inspection Reports,
performance deficiency that required an evaluation using the SDP. The inspectors  
because the finding was associated with the Configuration Control attribute of the Barrier
concluded that this second example of a finding was more than minor in accordance with  
Integrity Cornerstone and adversely affected the cornerstone objective of providing
Appendix B, Issue Screening, of IMC 0612, Power Reactor Inspection Reports,  
reasonable assurance that physical design barriers, including the containment, protect
because the finding was associated with the Configuration Control attribute of the Barrier  
the public from radionuclide releases caused by accidents and events. Specifically, this
Integrity Cornerstone and adversely affected the cornerstone objective of providing  
issue decreased the availability and reliability of the RCFCs for use during a design
reasonable assurance that physical design barriers, including the containment, protect  
basis accident.
the public from radionuclide releases caused by accidents and events. Specifically, this  
The inspectors completed a significance determination of this issue using IMC 0609,
issue decreased the availability and reliability of the RCFCs for use during a design  
Appendix A, Significance Determination of Reactor Inspection Findings for At Power
basis accident.  
Situations, Phase 1 Screening. The inspectors determined that because the finding did
The inspectors completed a significance determination of this issue using IMC 0609,  
not represent a degradation of the radiological barrier function, did not represent a
Appendix A, Significance Determination of Reactor Inspection Findings for At Power  
degradation of the barrier function of the control room, did not represent an actual open
Situations, Phase 1 Screening. The inspectors determined that because the finding did  
pathway in the physical integrity of reactor containment, and did not involve an actual
not represent a degradation of the radiological barrier function, did not represent a  
reduction in the function of hydrogen igniters in the reactor containment, the issue was of
degradation of the barrier function of the control room, did not represent an actual open  
very low safety significance (Green). In addition, the inspectors contacted the Region III
pathway in the physical integrity of reactor containment, and did not involve an actual  
Senior Risk Analysts (SRAs) and requested that a Phase 2 determination be performed.
reduction in the function of hydrogen igniters in the reactor containment, the issue was of  
The SRA also determined that the issue was of very low safety significance (Green).
very low safety significance (Green). In addition, the inspectors contacted the Region III  
This finding had a cross-cutting aspect in the Work Practices component of the Human
Senior Risk Analysts (SRAs) and requested that a Phase 2 determination be performed.
Performance cross-cutting area because licensee personnel failed to utilize human error
The SRA also determined that the issue was of very low safety significance (Green).  
prevention techniques, such as documenting which internal hatches had been removed
This finding had a cross-cutting aspect in the Work Practices component of the Human  
for maintenance so as to ensure that all hatches were reinstalled at the conclusion of the
Performance cross-cutting area because licensee personnel failed to utilize human error  
refueling outage [H.4(a)].
prevention techniques, such as documenting which internal hatches had been removed  
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
for maintenance so as to ensure that all hatches were reinstalled at the conclusion of the  
and Drawings, required, in part, that activities affecting quality shall be prescribed by
refueling outage [H.4(a)].  
documented instructions, procedures or drawings of a type appropriate to the
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,  
circumstances and shall include appropriate quantitative or qualitative acceptance
and Drawings, required, in part, that activities affecting quality shall be prescribed by  
criteria for determining that important activities have been satisfactorily accomplished.
documented instructions, procedures or drawings of a type appropriate to the  
Licensee work instructions and safety-related drawings M-1254, Revision F, RCFC
circumstances and shall include appropriate quantitative or qualitative acceptance  
Partial Plan, and M-1250 Revision V, RCFC Partial Plan, were developed in
criteria for determining that important activities have been satisfactorily accomplished.
accordance with 10 CFR Part 50, Appendix B, to accomplish an activity affecting quality.
Licensee work instructions and safety-related drawings M-1254, Revision F, RCFC  
Contrary to the above, as of March 29, 2012, the licensees work instructions for the
Partial Plan, and M-1250 Revision V, RCFC Partial Plan, were developed in  
repair of RCFCs, an activity affecting quality, failed to have instructions and drawings of
accordance with 10 CFR Part 50, Appendix B, to accomplish an activity affecting quality.  
a type appropriate to the circumstances. Specifically, drawings M-1254, Revision F; and
Contrary to the above, as of March 29, 2012, the licensees work instructions for the  
M-1250, Revision V, failed to adequately identify the internal hatches necessary to
repair of RCFCs, an activity affecting quality, failed to have instructions and drawings of  
accomplish repair activities. Because this violation was of very low safety significance
a type appropriate to the circumstances. Specifically, drawings M-1254, Revision F; and  
and because this issue was entered into the licensees CAP as IR 1347450, this second
M-1250, Revision V, failed to adequately identify the internal hatches necessary to  
example of a violation is being treated as a NCV, consistent with Section 2.3.2 of the
accomplish repair activities. Because this violation was of very low safety significance  
NRC Enforcement Policy. This is the second example of the NCV.
and because this issue was entered into the licensees CAP as IR 1347450, this second  
(NCV 05000454/2012002-02; Failure to Have Instructions Appropriate to the
example of a violation is being treated as a NCV, consistent with Section 2.3.2 of the  
Circumstances)
NRC Enforcement Policy. This is the second example of the NCV.
                                        23                                  Enclosure
(NCV 05000454/2012002-02; Failure to Have Instructions Appropriate to the  
Circumstances)  


4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)
24
.1   (Closed) Licensee Event Report 05000454/2012002-00: One Train of Containment
Enclosure
      Cooling System Inoperable Longer Than Allowed by Technical Specifications Due to
4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)  
      Inadequate Work Instructions
.1  
      The licensee submitted this Licensee Event Report (LER) on May 29, 2012, as an event
(Closed) Licensee Event Report 05000454/2012002-00: One Train of Containment  
      that could have prevented the fulfillment of a safety system. The inspectors performed
Cooling System Inoperable Longer Than Allowed by Technical Specifications Due to  
      follow up on the LER and documented the results of the followup in Paragraph 4OA2 as
Inadequate Work Instructions  
      the second example of a self-revealed example of an NCV.
The licensee submitted this Licensee Event Report (LER) on May 29, 2012, as an event  
      This LER is closed to NCV 05000454/2012003-02 above.
that could have prevented the fulfillment of a safety system. The inspectors performed  
4OA5 Other Activities
follow up on the LER and documented the results of the followup in Paragraph 4OA2 as  
  .1 Pre-operational Testing of an Independent Spent Fuel Storage Facility Installation at
the second example of a self-revealed example of an NCV.  
      Operating Plants (60854.1)
This LER is closed to NCV 05000454/2012003-02 above.  
  a. Inspection Scope
4OA5 Other Activities  
      Dry Run Activities
.1  
      The licensee performed pre-operational dry run activities to fulfill the requirements of the
Pre-operational Testing of an Independent Spent Fuel Storage Facility Installation at  
      Certificate of Compliance (CoC). Specifically, the licensee performed forced helium
Operating Plants (60854.1)  
      dehydration and supplemental cooling system pre-operational testing and training
a.  
      exercises prior to the second Independent Spent Fuel Storage Facility Installation
Inspection Scope  
      (ISFSI) campaign. These operations had not been performed prior to the first loading
Dry Run Activities  
      campaign as the first campaigns spent nuclear fuel characteristics did not necessitate
The licensee performed pre-operational dry run activities to fulfill the requirements of the  
      use of the equipment. The inspectors were on site to observe dry run activities on
Certificate of Compliance (CoC). Specifically, the licensee performed forced helium  
      February 24, 2012, and March 16, 2012.
dehydration and supplemental cooling system pre-operational testing and training  
      The inspectors reviewed loading procedures to ensure that they contained commitments
exercises prior to the second Independent Spent Fuel Storage Facility Installation  
      and requirements specified in the license, the TS, the Final Safety Analysis Report
(ISFSI) campaign. These operations had not been performed prior to the first loading  
      (FSAR), and Title 10 of the Code of Federal Regulations (CFR) Part 72.
campaign as the first campaigns spent nuclear fuel characteristics did not necessitate  
  b. Findings
use of the equipment. The inspectors were on site to observe dry run activities on  
      No violations of NRC requirements were identified.
February 24, 2012, and March 16, 2012.  
  .2 Review of 10 CFR 72.212(b) Evaluations at Operating Plants (60856.1)
The inspectors reviewed loading procedures to ensure that they contained commitments  
  a. Inspection Scope
and requirements specified in the license, the TS, the Final Safety Analysis Report  
      Review of Site Characteristics Against Safety Analysis Report and Safety Evaluation
(FSAR), and Title 10 of the Code of Federal Regulations (CFR) Part 72.  
      Report
b.  
      The inspectors evaluated the licensees compliance with the requirements of
Findings  
      10 CFR 72.212 and 10 CFR 72.48. The inspection consisted of interviews with
No violations of NRC requirements were identified.  
      cognizant personnel and review of documentation.
.2  
      During the licensees initial loading campaign Holtec HI-STORM 100 CoC 1014,
Review of 10 CFR 72.212(b) Evaluations at Operating Plants (60856.1)  
      Amendment 3, was used under the general license process; however, for the licensees
a.  
                                            24                                  Enclosure
Inspection Scope  
Review of Site Characteristics Against Safety Analysis Report and Safety Evaluation  
Report  
The inspectors evaluated the licensees compliance with the requirements of  
10 CFR 72.212 and 10 CFR 72.48. The inspection consisted of interviews with  
cognizant personnel and review of documentation.  
During the licensees initial loading campaign Holtec HI-STORM 100 CoC 1014,  
Amendment 3, was used under the general license process; however, for the licensees  


    second campaign HI-STORM 100 CoC 1014, Amendment 7 was used. A written
25
    evaluation was required per 10 CFR 72.212(b)(5), prior to use, to establish that the
Enclosure
    conditions of the CoC have been met. Byron Nuclear Power Station, Units 1 and 2,
second campaign HI-STORM 100 CoC 1014, Amendment 7 was used. A written  
    10 CFR 72.212 Evaluation Report, Revision 3, dated February 2012, documented the
evaluation was required per 10 CFR 72.212(b)(5), prior to use, to establish that the  
    evaluations performed by the licensee.
conditions of the CoC have been met. Byron Nuclear Power Station, Units 1 and 2,  
    The inspectors reviewed and assessed the licensees 10 CFR 72.212 Evaluation Report.
10 CFR 72.212 Evaluation Report, Revision 3, dated February 2012, documented the  
    The inspectors determined whether applicable reactor site parameters, such as fire and
evaluations performed by the licensee.  
    explosions, tornadoes, wind-generated missile impacts, seismic qualifications, lightning,
The inspectors reviewed and assessed the licensees 10 CFR 72.212 Evaluation Report.
    flooding and temperature, had been evaluated for acceptability with bounding values
The inspectors determined whether applicable reactor site parameters, such as fire and  
    specified in the Holtec HI-STORM 100 FSAR and associated analyses.
explosions, tornadoes, wind-generated missile impacts, seismic qualifications, lightning,  
  b. Findings
flooding and temperature, had been evaluated for acceptability with bounding values  
    No violations of NRC requirements were identified.
specified in the Holtec HI-STORM 100 FSAR and associated analyses.  
.2   Operation of an Independent Spent Fuel Storage Facility Installation at Operating Plants
b.  
    (60855.1)
Findings  
  a. Inspection Scope
No violations of NRC requirements were identified.  
    The inspectors observed and evaluated the licensees loading of the second canister
.2  
    during the licensees second ISFSI loading campaign to verify compliance with the CoC,
Operation of an Independent Spent Fuel Storage Facility Installation at Operating Plants  
    TS, regulations, and associated procedures.
(60855.1)  
    The inspectors observed the heavy load movement of the transfer cask (HI-TRAC) from
a.  
    the spent fuel pool to the dry decontamination pit inside the Fuel Handling Building. The
Inspection Scope  
    inspectors also observed multi-purpose canister (MPC) processing operations, including
The inspectors observed and evaluated the licensees loading of the second canister  
    decontamination and surveying, MPC welding, non-destructive weld examinations, MPC
during the licensees second ISFSI loading campaign to verify compliance with the CoC,  
    draining, forced helium dehydration, helium backfilling, and the use of the supplemental
TS, regulations, and associated procedures.
    cooling system.
The inspectors observed the heavy load movement of the transfer cask (HI-TRAC) from  
    During performance of these activities, the inspectors evaluated the licensee staffs
the spent fuel pool to the dry decontamination pit inside the Fuel Handling Building. The  
    familiarity with procedures, supervisory oversight, and communication and coordination
inspectors also observed multi-purpose canister (MPC) processing operations, including
    between the groups involved. The inspectors reviewed loading and monitoring
decontamination and surveying, MPC welding, non-destructive weld examinations, MPC  
    procedures and evaluated the licensees adherence to these procedures.
draining, forced helium dehydration, helium backfilling, and the use of the supplemental  
    The inspectors performed tours of the ISFSI pad to assess the material condition of the
cooling system.  
    pad and the loaded storage casks (HI-STORM). The inspectors reviewed
During performance of these activities, the inspectors evaluated the licensee staffs  
    documentation of the licensees ISFSI radiation monitoring program. Additionally, the
familiarity with procedures, supervisory oversight, and communication and coordination  
    inspectors performed independent radiation surveys around the ISFSI pad and loaded
between the groups involved. The inspectors reviewed loading and monitoring  
    HI-STORM casks. The inspectors reviewed the contamination and radiation levels from
procedures and evaluated the licensees adherence to these procedures.  
    a previously loaded MPC during the campaign to determine whether they were below
The inspectors performed tours of the ISFSI pad to assess the material condition of the  
    the regulatory limits. The inspectors also reviewed the As-Low-As-Is-Reasonably-
pad and the loaded storage casks (HI-STORM). The inspectors reviewed  
    Achievable (ALARA) Work-In-Progress Review for the loading of the previous cask to
documentation of the licensees ISFSI radiation monitoring program. Additionally, the  
    determine the adequacy of the licensees radiological controls and to ensure that
inspectors performed independent radiation surveys around the ISFSI pad and loaded  
    radiation worker doses were ALARA and that project dose goals could be achieved.
HI-STORM casks. The inspectors reviewed the contamination and radiation levels from  
    The inspectors attended licensee briefings to assess the licensees ability to identify
a previously loaded MPC during the campaign to determine whether they were below  
    critical steps of the evolution, potential failure scenarios, and tools to prevent errors.
the regulatory limits. The inspectors also reviewed the As-Low-As-Is-Reasonably-
                                            25                                  Enclosure
Achievable (ALARA) Work-In-Progress Review for the loading of the previous cask to  
determine the adequacy of the licensees radiological controls and to ensure that  
radiation worker doses were ALARA and that project dose goals could be achieved.  
The inspectors attended licensee briefings to assess the licensees ability to identify  
critical steps of the evolution, potential failure scenarios, and tools to prevent errors.  


      The inspectors reviewed the licensees program associated with fuel characterization
26
      and selection for storage. The inspectors reviewed cask fuel selection packages to
Enclosure
      verify that the licensee was loading fuel in accordance with the CoC TS. The licensee
The inspectors reviewed the licensees program associated with fuel characterization  
      did not plan to load any damaged fuel assemblies during this campaign.
and selection for storage. The inspectors reviewed cask fuel selection packages to  
      The inspectors reviewed issue reports and the associated follow-up actions that were
verify that the licensee was loading fuel in accordance with the CoC TS. The licensee  
      generated since the licensees last loading campaign. The inspectors reviewed the
did not plan to load any damaged fuel assemblies during this campaign.  
      licensees 10 CFR 72.48 screenings.
The inspectors reviewed issue reports and the associated follow-up actions that were  
  b. Findings
generated since the licensees last loading campaign. The inspectors reviewed the  
      No findings were identified.
licensees 10 CFR 72.48 screenings.  
4OA6 Management Meetings
b.  
.1   Exit Meeting Summary
Findings  
      On July 2, 2012, the inspectors presented the inspection results to Mr. T. Tulon, and
No findings were identified.  
      other members of the licensee staff.
4OA6 Management Meetings  
      The licensee acknowledged the issues presented. The inspectors confirmed that none
.1  
      of the potential report input discussed was considered proprietary.
Exit Meeting Summary  
.2   Interim Exit Meetings
On July 2, 2012, the inspectors presented the inspection results to Mr. T. Tulon, and  
      On April 13, 2012, the inspectors presented the inspection results of the ISFSI
other members of the licensee staff.  
      inspection to members of the licensee management and staff. Licensee personnel
The licensee acknowledged the issues presented. The inspectors confirmed that none  
      acknowledged the issues presented. The inspectors confirmed that none of the potential
of the potential report input discussed was considered proprietary.  
      report input discussed was considered proprietary. Proprietary material received during
.2  
      the inspection was returned to the licensee.
Interim Exit Meetings  
      On June 27, 2012, the inspectors presented inspection results of the licensed operator
On April 13, 2012, the inspectors presented the inspection results of the ISFSI  
      examination security issue to Mr. S. Gackstetter and other members of the licensee
inspection to members of the licensee management and staff. Licensee personnel  
      staff. No proprietary information was identified during the interim exit.
acknowledged the issues presented. The inspectors confirmed that none of the potential  
      On June 30, 2012, the inspectors presented the inspection results of the Emergency
report input discussed was considered proprietary. Proprietary material received during  
      Preparedness Program inspection to members of licensee management and staff. No
the inspection was returned to the licensee.  
      proprietary information was identified during the interim exit.
On June 27, 2012, the inspectors presented inspection results of the licensed operator  
4OA7 Licensee-Identified Violation
examination security issue to Mr. S. Gackstetter and other members of the licensee  
      The following violation of very low significance (Green) or Severity Level IV was
staff. No proprietary information was identified during the interim exit.  
      identified by the licensee and is a violation of NRC requirements which meet the criteria
On June 30, 2012, the inspectors presented the inspection results of the Emergency  
      of Section VI of the NRC Enforcement Policy for being dispositioned as an NCV:
Preparedness Program inspection to members of licensee management and staff. No  
              Title 10 CFR 55.49, Integrity of Examinations and Tests, requires, in part,
proprietary information was identified during the interim exit.  
              that the licensee shall not engage in activities that compromises the integrity
4OA7 Licensee-Identified Violation  
              of any application, test, or examination required by 10 CFR Part 55. Contrary
The following violation of very low significance (Green) or Severity Level IV was  
              to the above, on March 30, 2012, at the Clinton Power Station, the licensee
identified by the licensee and is a violation of NRC requirements which meet the criteria  
              identified activities that compromised the integrity of the examinations required
of Section VI of the NRC Enforcement Policy for being dispositioned as an NCV:  
              by 10 CFR Part 55. Specifically, the licensee identified that the control room
              simulators plant process computer model was saving sequence of events files
Title 10 CFR 55.49, Integrity of Examinations and Tests, requires, in part,  
                                              26                                Enclosure
that the licensee shall not engage in activities that compromises the integrity  
of any application, test, or examination required by 10 CFR Part 55. Contrary  
to the above, on March 30, 2012, at the Clinton Power Station, the licensee  
identified activities that compromised the integrity of the examinations required  
by 10 CFR Part 55. Specifically, the licensee identified that the control room  
simulators plant process computer model was saving sequence of events files  


          on a routine basis, which contained examination materials related to
27
          examinations required by 10 CFR Part 55. A licensee investigation determined
Enclosure
          that the same condition existed at other Midwest Exelon sites, including the
on a routine basis, which contained examination materials related to  
          Byron Station. The licensee determined that some of the files contained
examinations required by 10 CFR Part 55. A licensee investigation determined  
          examination materials related to examinations required by 10 CFR Part 55.
that the same condition existed at other Midwest Exelon sites, including the  
          The integrity of a test or examination is considered compromised if any activity,
Byron Station. The licensee determined that some of the files contained  
          regardless of intent, affected, or, but for detection, would have affected the
examination materials related to examinations required by 10 CFR Part 55.
          equitable and consistent administration of the test or examination.
The integrity of a test or examination is considered compromised if any activity,  
          Although the examination materials were available for scrutiny by unauthorized
regardless of intent, affected, or, but for detection, would have affected the  
          personnel, (compromised), the licensee was able to demonstrate that the files
equitable and consistent administration of the test or examination.  
          were not readily viewable, required interpretation and additional administrative
          controls were in place that would likely inhibit access to, and reconstruction of
Although the examination materials were available for scrutiny by unauthorized  
          simulator events. No individuals had an unfair advantage in taking any
personnel, (compromised), the licensee was able to demonstrate that the files  
          NRC-related examinations. Therefore, this finding was of very low safety
were not readily viewable, required interpretation and additional administrative  
          significance (Green). This issue was documented in the facilitys corrective
controls were in place that would likely inhibit access to, and reconstruction of  
          action program as IR 1350674. Corrective actions for this issue included revising
simulator events. No individuals had an unfair advantage in taking any  
          the simulators software to delete data from the sequence of events files being
NRC-related examinations. Therefore, this finding was of very low safety  
          generated by the simulator upon reset of the simulator.
significance (Green). This issue was documented in the facilitys corrective  
ATTACHMENT: SUPPLEMENTAL INFORMATION
action program as IR 1350674. Corrective actions for this issue included revising  
                                          27                                Enclosure
the simulators software to delete data from the sequence of events files being  
generated by the simulator upon reset of the simulator.  
 
ATTACHMENT: SUPPLEMENTAL INFORMATION  


                              SUPPLEMENTAL INFORMATION
1
                                  KEY POINTS OF CONTACT
Attachment
Licensee
B. Youman, Plant Manager
SUPPLEMENTAL INFORMATION  
D. Gudger, Regulatory Assurance Manager
KEY POINTS OF CONTACT  
J. Langan, Regulatory Assurance Licensing Engineer
B. Spahr, Maintenance Director
Licensee  
D. Drawbaugh, Emergency Preparedness Manager
B. Youman, Plant Manager  
B. Kartheiser, Emergency Preparedness Coordinator
D. Gudger, Regulatory Assurance Manager  
S. Kerr, Work Management Manager
J. Langan, Regulatory Assurance Licensing Engineer  
D. Spitizer, Regulatory Assurance
B. Spahr, Maintenance Director  
T. Eliakis, ISFSI Project Manager
D. Drawbaugh, Emergency Preparedness Manager  
T. Hulbert, Regulatory Assurance Assistant
B. Kartheiser, Emergency Preparedness Coordinator  
S. Briggs, Operations Director
S. Kerr, Work Management Manager  
Nuclear Regulatory Commission
D. Spitizer, Regulatory Assurance  
E. Duncan, Chief, Branch 3, Division of Reactor Projects
T. Eliakis, ISFSI Project Manager  
                                          1            Attachment
T. Hulbert, Regulatory Assurance Assistant  
S. Briggs, Operations Director  
Nuclear Regulatory Commission  
E. Duncan, Chief, Branch 3, Division of Reactor Projects  


                LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
2
Opened
Attachment
05000454/2012003-01   NCV   Leakage Detection Trough with Large Accumulation of Boric
                            Acid Identified (Section 1R15)
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
05000454/2012003-02   NCV   Failure to Have Instructions Appropriate to the
Opened  
                            Circumstances (Section 4OA2)
05000454/2012003-01  
Closed
NCV  
05000454/2012002-02   URI   Potential Under-Torque of Valve 1RC8042B (Section 4OA2)
Leakage Detection Trough with Large Accumulation of Boric  
05000454/2012002-03   URI   Boric Acid Accumulation Identified in Leakage Detection
Acid Identified (Section 1R15)  
                            Trough (Section 1R15)
05000454/2012003-02  
05000454/2012003-01   NCV   Leakage Detection Trough with Large Accumulation of Boric
NCV  
                            Acid Identified (Section 1R15)
Failure to Have Instructions Appropriate to the  
05000454/2012003-02   NCV   Failure to Have Instructions Appropriate to the
Circumstances (Section 4OA2)  
                            Circumstances (Section 4OA2)
05000454/2012-002-00 LER   One Train of Containment Cooling System Inoperable Longer
Closed  
                            Than Allowed by Technical Specifications Due to Inadequate
05000454/2012002-02  
                            Work Instructions
URI  
Discussed
Potential Under-Torque of Valve 1RC8042B (Section 4OA2)  
None
05000454/2012002-03  
                                      2                                Attachment
URI  
Boric Acid Accumulation Identified in Leakage Detection  
Trough (Section 1R15)  
05000454/2012003-01  
NCV  
Leakage Detection Trough with Large Accumulation of Boric  
Acid Identified (Section 1R15)  
05000454/2012003-02  
NCV  
Failure to Have Instructions Appropriate to the  
Circumstances (Section 4OA2)  
05000454/2012-002-00  
LER  
One Train of Containment Cooling System Inoperable Longer  
Than Allowed by Technical Specifications Due to Inadequate  
Work Instructions  
Discussed  
None  


                                  LIST OF DOCUMENTS REVIEWED
3
The following is a list of documents reviewed during the inspection. Inclusion on this list does
Attachment
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that
selected sections of portions of the documents were evaluated as part of the overall inspection
LIST OF DOCUMENTS REVIEWED  
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
The following is a list of documents reviewed during the inspection. Inclusion on this list does  
any part of it, unless this is stated in the body of the inspection report.
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that  
Section 1R01: Adverse Weather Protection (Quarterly)
selected sections of portions of the documents were evaluated as part of the overall inspection  
- IR 1360541; Not Enough Charcoal Filters on Hand for Summer Readiness, April 30, 2012
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
- IR 1360553; Byron Summer Readiness Maintenance Review Results, April 30, 2012
any part of it, unless this is stated in the body of the inspection report.  
- IR 1361366; Summer Readiness Contingency Work Packages Not Ready, April 26, 2012
Section 1R01: Adverse Weather Protection (Quarterly)  
- IR 1365484; 2012 Transformer Replacement Summer Readiness Exceptions, May 11, 2012
- IR 1360541; Not Enough Charcoal Filters on Hand for Summer Readiness, April 30, 2012  
- WC-AA-107; Summer Seasonal Readiness, June 1 through August 31, 2012
- IR 1360553; Byron Summer Readiness Maintenance Review Results, April 30, 2012  
- Plant System Readiness Review; System AP, Revision 9
- IR 1361366; Summer Readiness Contingency Work Packages Not Ready, April 26, 2012  
- IR 1360510; Summer Readiness Contingency WO Review Gaps, April 28, 2012
- IR 1365484; 2012 Transformer Replacement Summer Readiness Exceptions, May 11, 2012  
- System Engineer System Summary Sheet/Recommendation Form
- WC-AA-107; Summer Seasonal Readiness, June 1 through August 31, 2012  
- Certification of 2012 Summer Readiness, May 15, 2012
- Plant System Readiness Review; System AP, Revision 9  
- OP-AA-108-107-1001; Station Response to Grid Capacity Conditions, Revision 4
- IR 1360510; Summer Readiness Contingency WO Review Gaps, April 28, 2012  
- OP-AA-108-107-1002; Interface Procedure Between ComEd/PRCO and Exelon Generation
- System Engineer System Summary Sheet/Recommendation Form  
  (Nuclear/Power) for Transmission Operations, Revision 6
- Certification of 2012 Summer Readiness, May 15, 2012  
- WC-AA-107; Seasonal Readiness, Revision 9
- OP-AA-108-107-1001; Station Response to Grid Capacity Conditions, Revision 4  
Section 1R05: Fire Protection (Quarterly)
- OP-AA-108-107-1002; Interface Procedure Between ComEd/PRCO and Exelon Generation  
- FZ 5.4-2; Auxiliary Building 451-0 Elevation, Division 22 Miscellaneous Electrical Equipment
(Nuclear/Power) for Transmission Operations, Revision 6  
  and Battery Room, Rev.0
- WC-AA-107; Seasonal Readiness, Revision 9  
- A-269; Drawing, Auxiliary Building Main Floor Area 4, Rev. AP
Section 1R05: Fire Protection (Quarterly)  
- S-1328; Drawing, Auxiliary Building Roof Framing Plan Area 4, Rev. AJ
- FZ 5.4-2; Auxiliary Building 451-0 Elevation, Division 22 Miscellaneous Electrical Equipment  
Corrective Action Documents As a Result of NRC Inspection
and Battery Room, Rev.0  
- IR 1367933; NRC Observed Fire Drill, May 17, 2012
- A-269; Drawing, Auxiliary Building Main Floor Area 4, Rev. AP  
Section 1R06: Flooding
- S-1328; Drawing, Auxiliary Building Roof Framing Plan Area 4, Rev. AJ
- 0BOSR WF-SA1; Auxiliary Building Floor Drain Semi-Annual Surveillance, Rev. 6
- A-223; Auxiliary Building Upper Basement, Floor Plan EL. 364-0 Area 6, Rev. BM
Corrective Action Documents As a Result of NRC Inspection  
Corrective Action Documents As a Result of NRC Inspection
- IR 1362200; 0BOSR WF-SA1 Acceptance Criteria Needs Engineering Calc., May 3, 2012
- IR 1367933; NRC Observed Fire Drill, May 17, 2012  
Section 1R12: Maintenance Effectiveness (Quarterly)
Section 1R06: Flooding  
- IR 1349587; Investigate Unit 1 & 2 CW Flume Temperature Differences, April 3, 2012
- 0BOSR WF-SA1; Auxiliary Building Floor Drain Semi-Annual Surveillance, Rev. 6  
- IR 1352076; 2E NDCT Riser Pipe Rupture, April 10, 2012
- A-223; Auxiliary Building Upper Basement, Floor Plan EL. 364-0 Area 6, Rev. BM  
- IR 1353164; Leak at U1 NDCT 1B Riser at Clamp, April 12, 2012
- IR 1357297; U2 NDCT Cold Basin Water Lapping Out West Door Area, April 23, 2012
Corrective Action Documents As a Result of NRC Inspection  
- IR 1358209; U2 NDCT Cold Basin Water Wave Lapping Out West Door Area, April 25, 2012
                                                3                              Attachment
- IR 1362200; 0BOSR WF-SA1 Acceptance Criteria Needs Engineering Calc., May 3, 2012  
Section 1R12: Maintenance Effectiveness (Quarterly)  
- IR 1349587; Investigate Unit 1 & 2 CW Flume Temperature Differences, April 3, 2012  
- IR 1352076; 2E NDCT Riser Pipe Rupture, April 10, 2012  
- IR 1353164; Leak at U1 NDCT 1B Riser at Clamp, April 12, 2012  
- IR 1357297; U2 NDCT Cold Basin Water Lapping Out West Door Area, April 23, 2012  
- IR 1358209; U2 NDCT Cold Basin Water Wave Lapping Out West Door Area, April 25, 2012  


- IR 1361821; Rapid Rise in U1 NDCT Debris Fence Delta Level, May 3, 2012
4
- IR 1363647; U1 NDCT 1B Riser Leak, May 7, 2012
Attachment
- IR 1363702; Recommend Temporary Set Point Change, May 7, 2012
- IR 1364085; What is the Plan for CW Blowdown, May 8, 2012
- IR 1361821; Rapid Rise in U1 NDCT Debris Fence Delta Level, May 3, 2012  
- IR 1364405; Safety Concerns with the Operation of CW PP Intakes, May 9, 2012
- IR 1363647; U1 NDCT 1B Riser Leak, May 7, 2012  
- IR 1366347; U1 NDCT Debris Fence Level at 1.5 Feet, May 14, 2012
- IR 1363702; Recommend Temporary Set Point Change, May 7, 2012  
- IR 1366348; U2 NDCT Debris Fence Level at 1.5 Feet, May 14, 2012
- IR 1364085; What is the Plan for CW Blowdown, May 8, 2012  
- IR 1366507; Adverse Trend Identified with Performance of the NDCT, May 15, 2012
- IR 1364405; Safety Concerns with the Operation of CW PP Intakes, May 9, 2012  
- IR 1367711; Vendor Damaged 0C CW M/U Seal Injection Pipe Coupling, May 17, 2012
- IR 1366347; U1 NDCT Debris Fence Level at 1.5 Feet, May 14, 2012  
- IR 1369171; Improper Grouting of 0C CW M/U Base Plate to Foundation, May 21, 2012
- IR 1366348; U2 NDCT Debris Fence Level at 1.5 Feet, May 14, 2012  
- IR 1371687; Fill Damage to 2F NDCT Riser Pipe, May 29, 2012
- IR 1366507; Adverse Trend Identified with Performance of the NDCT, May 15, 2012  
- IR 1373743; Excessive CW Material in U1 Debris Fence, June 2, 2012
- IR 1367711; Vendor Damaged 0C CW M/U Seal Injection Pipe Coupling, May 17, 2012  
- IR 1373797; 1B CW Riser Piping Significantly Degraded, June 3, 2012
- IR 1369171; Improper Grouting of 0C CW M/U Base Plate to Foundation, May 21, 2012  
- IR 1374981; U2 CW Water Outfall Screen High Delta Level, June 6, 2012
- IR 1371687; Fill Damage to 2F NDCT Riser Pipe, May 29, 2012  
- IR 1374981; U1 CW Water Outfall Screen High Delta Level, June 6, 2012
- IR 1373743; Excessive CW Material in U1 Debris Fence, June 2, 2012  
- IR 1379221; U2 NDCT Outfall Screen High Delta Level June 18, 2012
- IR 1373797; 1B CW Riser Piping Significantly Degraded, June 3, 2012  
- IR 1380630; 1F NDCT Riser Leak, June 21, 2012
- IR 1374981; U2 CW Water Outfall Screen High Delta Level, June 6, 2012  
- IR 1381098; U2 CW Box DP Pegged High, Tube Sheet Fouling, June 22, 2012
- IR 1374981; U1 CW Water Outfall Screen High Delta Level, June 6, 2012  
- IR 1381376; Falling Concrete on North Side of U2 NDCT, June 24
- IR 1379221; U2 NDCT Outfall Screen High Delta Level June 18, 2012  
- IR 1383022; U2 NDCT 2E Riser Leaking, June 28, 2012
- IR 1380630; 1F NDCT Riser Leak, June 21, 2012  
- IR 1383848; 2E Riser Leakage has Worsened, June 30, 2012
- IR 1381098; U2 CW Box DP Pegged High, Tube Sheet Fouling, June 22, 2012  
Section 1R13: Maintenance Risk Assessments & Emergent Work control
- IR 1381376; Falling Concrete on North Side of U2 NDCT, June 24  
- IR 1358649; DSA - Work Not Performed Due to OLR Not Evaluated, April 26, 2012
- IR 1383022; U2 NDCT 2E Riser Leaking, June 28, 2012  
- IR 1378982; 2B SAC Tripped on Low Bearing Oil Pressure, Revision 21
- IR 1383848; 2E Riser Leakage has Worsened, June 30, 2012  
- Online Risk Evaluation; Week of June 11, 2012, Revisions 0 through 6
Section 1R13: Maintenance Risk Assessments & Emergent Work control  
- Online Risk Evaluation; Week of June 18, 2012, Revisions 0 through 9
- IR 1358649; DSA - Work Not Performed Due to OLR Not Evaluated, April 26, 2012  
Section 1R15: Operability Evaluations (Quarterly)
- IR 1378982; 2B SAC Tripped on Low Bearing Oil Pressure, Revision 21  
- BY-MISC-017; Risk Profile Improvements for Single Phase Conditions, Revision 0
- Online Risk Evaluation; Week of June 11, 2012, Revisions 0 through 6  
- EC 374391 010; OP Eval 09-001, DOST-DG Vent Lines Crimp Vs Break, May 21, 2012
- Online Risk Evaluation; Week of June 18, 2012, Revisions 0 through 9  
- EC 383599 003; BYR OP Eval 11-005, Turbine Building HELB Input Errors, October 05, 2011
Section 1R15: Operability Evaluations (Quarterly)  
- EC 387590 002; Potential Design Vulnerability in Switchyard Single Open Phase Detection,
- BY-MISC-017; Risk Profile Improvements for Single Phase Conditions, Revision 0  
  May 18, 2012
- EC 374391 010; OP Eval 09-001, DOST-DG Vent Lines Crimp Vs Break, May 21, 2012  
- EC 389402 000; OP Eval 12-005, HELB Load Not Considered in Structural Calculation,
- EC 383599 003; BYR OP Eval 11-005, Turbine Building HELB Input Errors, October 05, 2011  
  June 05, 2012
- EC 387590 002; Potential Design Vulnerability in Switchyard Single Open Phase Detection,  
- 1BOSR Z.5.b.1-1; Unit One Containment Loose Debris Inspection, Rev. 15
May 18, 2012  
- OP-AA-108-108-1001; Drywell / Containment Closeout, Rev. 1
- EC 389402 000; OP Eval 12-005, HELB Load Not Considered in Structural Calculation,  
- A-336; Drawing, Containment Building Basement Floor Plan Area 4, Rev. Q
June 05, 2012  
- A-335; Drawing, Containment Building Basement Floor Plan Area 3, Rev. T
- 1BOSR Z.5.b.1-1; Unit One Containment Loose Debris Inspection, Rev. 15  
- A-334; Drawing, Containment Building Basement Floor Plan Area 2, Rev. U
- OP-AA-108-108-1001; Drywell / Containment Closeout, Rev. 1  
- A-333; Drawing, Containment Building Basement Floor Plan Area 1, Rev. W
- A-336; Drawing, Containment Building Basement Floor Plan Area 4, Rev. Q  
- IR 1378106; Potential Impact from Reduced SG PORV Relief Capacity, June 14, 2012
- A-335; Drawing, Containment Building Basement Floor Plan Area 3, Rev. T  
- IR 1359137; Probable Reduced SG PORV Capacity for Original Valves, April 26, 2012
- A-334; Drawing, Containment Building Basement Floor Plan Area 2, Rev. U  
- EC 367065; Op Eval 07-007, Main Steam PORV Steam Relief Capacity, Rev. 4
- A-333; Drawing, Containment Building Basement Floor Plan Area 1, Rev. W  
                                            4                              Attachment
- IR 1378106; Potential Impact from Reduced SG PORV Relief Capacity, June 14, 2012  
- IR 1359137; Probable Reduced SG PORV Capacity for Original Valves, April 26, 2012  
- EC 367065; Op Eval 07-007, Main Steam PORV Steam Relief Capacity, Rev. 4  


Corrective Action Documents As a Result of NRC Inspection
5
- IR 1339957; 1PS9365B Has Leak From Either Packing Leak or Bonnet, March 12, 2012
Attachment
- IR 1341380; NRC Identified Boric Acid Covering Floor, March 15, 2012
- IR 1382405; NRC (B1M03) Unit 1 IMB Drain Covered with Boric Acid, June 27, 2012
Corrective Action Documents As a Result of NRC Inspection  
Section 1R19: Post Maintenance Testing (Quarterly)
- IR 1370582; PMT Run Required for B AF PP TS-1 Opening for Battery Test, May 25, 2012
- IR 1339957; 1PS9365B Has Leak From Either Packing Leak or Bonnet, March 12, 2012  
- IR 1370734; Evaluate Test Frequency for 2AF01EA-B, May 25, 2012
- IR 1341380; NRC Identified Boric Acid Covering Floor, March 15, 2012  
- 2BOSR 0.5-2.SX.3-3; Unit 2 Position Indication Test of 2SX004, 2SX010, 2SX011, 2SX033,
- IR 1382405; NRC (B1M03) Unit 1 IMB Drain Covered with Boric Acid, June 27, 2012  
  2SX034, and 2SX136
Section 1R19: Post Maintenance Testing (Quarterly)  
- WO 1423904; OPS PMT: Stroke 2SX010 Using BOP SX-T3, May 23, 2012
- IR 1370582; PMT Run Required for B AF PP TS-1 Opening for Battery Test, May 25, 2012  
- 1BOSR 6.3.5-19; Unit 1 Main Steam System Containment Isolation Valve Stroke Test, Rev. 4
- IR 1370734; Evaluate Test Frequency for 2AF01EA-B, May 25, 2012  
- 1BOSR MS-R1; Unit 1 Manual Stroke of the S/G PORVs 18 Month Surveillance, Rev. 5
- 2BOSR 0.5-2.SX.3-3; Unit 2 Position Indication Test of 2SX004, 2SX010, 2SX011, 2SX033,  
- 2BOSR 0.5-3.AF.1-2; Unit 2 ASME Surveillance Requirements for the B Train Auxiliary
2SX034, and 2SX136  
  Feedwater SX Supply Valves, Rev. 10
- WO 1423904; OPS PMT: Stroke 2SX010 Using BOP SX-T3, May 23, 2012  
- 0BOSR 0.5-3.SX.1-3; Unit 0 Test of the Unit 0 Component Cooling Water Heat Exchangers
- 1BOSR 6.3.5-19; Unit 1 Main Steam System Containment Isolation Valve Stroke Test, Rev. 4  
  Essential Service Water Throttle and Outlet Isolation Valves, Rev. 3
- 1BOSR MS-R1; Unit 1 Manual Stroke of the S/G PORVs 18 Month Surveillance, Rev. 5  
Section 1R22: Surveillance Testing (Quarterly)
- 2BOSR 0.5-3.AF.1-2; Unit 2 ASME Surveillance Requirements for the B Train Auxiliary  
- 1359972; 1B AF STT and PIT Procedures Dont Work Together, April 28, 2012
Feedwater SX Supply Valves, Rev. 10  
- 1325427; Unit 1 & 2 AF013s Stem Lube Conflicts with C&T Level 4, February 10, 2012
- 0BOSR 0.5-3.SX.1-3; Unit 0 Test of the Unit 0 Component Cooling Water Heat Exchangers  
- 1197504; 1AF013D Local Indication Shows 10% Open with Valve Closed, April 4, 2011
Essential Service Water Throttle and Outlet Isolation Valves, Rev. 3  
- 1197493; 1AF013A Local Indication Shows 70% Open with Valve Closed, April 4, 2012
Section 1R22: Surveillance Testing (Quarterly)  
- 1BOSR 0.5-2.AF.1-2; Unit 1 1AF013 E/F/G/H Stroke Test, Rev. 5
- 1359972; 1B AF STT and PIT Procedures Dont Work Together, April 28, 2012  
- 1BOSR 7.5.4-2; Unit 1 Diesel Driven Auxiliary Feedwater Pump Monthly Surveillance, Rev. 14
- 1325427; Unit 1 & 2 AF013s Stem Lube Conflicts with C&T Level 4, February 10, 2012  
- 1BOSR 5.5.8.AF.5-2b; Unit 1 Group B Inservice Testing Requirements for Diesel Driven
- 1197504; 1AF013D Local Indication Shows 10% Open with Valve Closed, April 4, 2011  
  Auxiliary Feedwater Pump 1AF01PB, Rev. 1
- 1197493; 1AF013A Local Indication Shows 70% Open with Valve Closed, April 4, 2012  
- 1BOSR 8.1.2-1; Unit 1 1A Diesel Generator Operability Surveillance, Rev. 20
- 1BOSR 0.5-2.AF.1-2; Unit 1 1AF013 E/F/G/H Stroke Test, Rev. 5  
- IR 1312027; 1A DG Lower JW Cooler Leaking from End Cover Bolting, January 11, 2012
- 1BOSR 7.5.4-2; Unit 1 Diesel Driven Auxiliary Feedwater Pump Monthly Surveillance, Rev. 14  
- IR 1301853; 1A DG R-9 Fuel Injector Tell Tale Drain Leaking, December 31, 2011
- 1BOSR 5.5.8.AF.5-2b; Unit 1 Group B Inservice Testing Requirements for Diesel Driven  
- IR 1300657; 1A DG JW Heater Not Controlling Temperature in Automatic, December 10, 2011
Auxiliary Feedwater Pump 1AF01PB, Rev. 1  
- IR 1227745; 1A DG Possible Water in Crank Case, June 12, 2011
- 1BOSR 8.1.2-1; Unit 1 1A Diesel Generator Operability Surveillance, Rev. 20  
- IR 1212228; 1A DG Generic Letter 89-13 Inspection Relief Requested, May 5, 2011
- IR 1312027; 1A DG Lower JW Cooler Leaking from End Cover Bolting, January 11, 2012  
- IR 1028474; 1A DG JW Leak at R-9 Supply Flange - 30 Drops Per Minute, February 10, 2010
- IR 1301853; 1A DG R-9 Fuel Injector Tell Tale Drain Leaking, December 31, 2011  
1EP2 Alert and Notification (ANS) Evaluation
- IR 1300657; 1A DG JW Heater Not Controlling Temperature in Automatic, December 10, 2011  
- Offsite Emergency Plan Alert and Notification System Addendum for Byron Station;
- IR 1227745; 1A DG Possible Water in Crank Case, June 12, 2011  
  November 2009
- IR 1212228; 1A DG Generic Letter 89-13 Inspection Relief Requested, May 5, 2011  
- EP-AA-1000; Exelon Nuclear Standardized Radiological Emergency Plan Section E;
- IR 1028474; 1A DG JW Leak at R-9 Supply Flange - 30 Drops Per Minute, February 10, 2010  
  Revision 21
1EP2 Alert and Notification (ANS) Evaluation  
- EP-AA-1002; Exelon Nuclear Radiological Emergency Plan Annex for Byron Station,
- Offsite Emergency Plan Alert and Notification System Addendum for Byron Station;  
  Section 4; Revision 29
November 2009  
- Byron Station Warning System Annual Maintenance & Operational Reports; June 15, 2011
- EP-AA-1000; Exelon Nuclear Standardized Radiological Emergency Plan Section E;  
- Byron Station Monthly Siren Availability Reports; August 2010 - June 2012
Revision 21  
- Exelon Semi-Annual Siren Reports; July 2010 and December 31, 2011
- EP-AA-1002; Exelon Nuclear Radiological Emergency Plan Annex for Byron Station,  
- IR 1254150; Semi-Annual Review of 1st Half of 2011 Siren Data; August 22, 2011
Section 4; Revision 29  
- IR 1245065; Single Siren Failures; July 28, 2011
- Byron Station Warning System Annual Maintenance & Operational Reports; June 15, 2011  
                                            5                              Attachment
- Byron Station Monthly Siren Availability Reports; August 2010 - June 2012  
- Exelon Semi-Annual Siren Reports; July 2010 and December 31, 2011  
- IR 1254150; Semi-Annual Review of 1st Half of 2011 Siren Data; August 22, 2011  
- IR 1245065; Single Siren Failures; July 28, 2011  


1EP3 Emergency Response Organization Augmentation Testing
6
- EP-AA-1000; Exelon Nuclear Standardized Radiological Emergency Plan, Sections B and N;
Attachment
  Revision 21
- EP-AA-1002; Exelon Nuclear Radiological Emergency Plan Annex for Byron Station,
1EP3 Emergency Response Organization Augmentation Testing  
  Section 2; Revision 29
- EP-AA-1000; Exelon Nuclear Standardized Radiological Emergency Plan, Sections B and N;  
- EP-AA-112-100-F-06; Midwest ERO Notification or Augmentation; Revision O
Revision 21  
- TQ-AA-113; ERO Training and Qualification; Revision 19
- EP-AA-1002; Exelon Nuclear Radiological Emergency Plan Annex for Byron Station,  
- Quarterly Unannounced Off-Hours Call-In Augmentation Drill Results; May 2010 - May 2012
Section 2; Revision 29  
- Emergency Response Organization Call-Out Roster; May 18, 2012
- EP-AA-112-100-F-06; Midwest ERO Notification or Augmentation; Revision O  
- IR 1367175; May 2021 Unannounced Off-Hours Call-In Augmentation Drill 2 Duty ERO Did
- TQ-AA-113; ERO Training and Qualification; Revision 19  
  Not Respond; May 16, 2012
- Quarterly Unannounced Off-Hours Call-In Augmentation Drill Results; May 2010 - May 2012  
1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies
- Emergency Response Organization Call-Out Roster; May 18, 2012  
- EP-AA-120; Section 4.4, Review of Actual Events; Revision 14
- IR 1367175; May 2021 Unannounced Off-Hours Call-In Augmentation Drill 2 Duty ERO Did  
- EP-AA-120-1001; 10 CFR 50.54(q) Change Evaluation; Revision 7
Not Respond; May 16, 2012  
- EP-AA-121; Emergency Response Facilities and Equipment Readiness; Revision 11
1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies  
- EP-AA-121-F-02; Byron Station Equipment Matrix; Revision 1
- EP-AA-120; Section 4.4, Review of Actual Events; Revision 14  
- BRP 5800-3; Area Radiation Monitoring System Alert/High Alarm Setpoints; Revision 25
- EP-AA-120-1001; 10 CFR 50.54(q) Change Evaluation; Revision 7  
- BRP 5820-12; Response to Area and Process Radiation Monitor LCOARS or Out-of-Service
- EP-AA-121; Emergency Response Facilities and Equipment Readiness; Revision 11  
  Conditions; Revision 29
- EP-AA-121-F-02; Byron Station Equipment Matrix; Revision 1  
- BRP 5820-14; Process Radiation Monitoring System Alert/High Alarm Setpoints; Revision 44
- BRP 5800-3; Area Radiation Monitoring System Alert/High Alarm Setpoints; Revision 25  
- LS-AA-126-1005; Check-In-Self-Assessment Emergency Preparedness Report; April 25, 2012
- BRP 5820-12; Response to Area and Process Radiation Monitor LCOARS or Out-of-Service  
- NOSA-BYR-12-03; Emergency Preparedness Audit Report; April 27, 2012
Conditions; Revision 29  
- NOSA-BYR-11-03; Emergency Preparedness Audit Report; April 15, 2011
- BRP 5820-14; Process Radiation Monitoring System Alert/High Alarm Setpoints; Revision 44  
- 0BOSR CQ-1; Test of the Employee Alarm System; Revision 6
- LS-AA-126-1005; Check-In-Self-Assessment Emergency Preparedness Report; April 25, 2012  
- WC-AA-106; Work Screening and Processing; Revision 19
- NOSA-BYR-12-03; Emergency Preparedness Audit Report; April 27, 2012  
- Monday Muster Meeting EP Weekly Newsletter; June 25, 2012
- NOSA-BYR-11-03; Emergency Preparedness Audit Report; April 15, 2011  
- Byron Station January 30, 2012, Unusual Event Report; February 27, 2012
- 0BOSR CQ-1; Test of the Employee Alarm System; Revision 6  
- Byron Station February 28, 2012, Unusual Event Report; March 26, 2012
- WC-AA-106; Work Screening and Processing; Revision 19  
- List of Inaudible Public Address System Locations and Status; May 29, 2012
- Monday Muster Meeting EP Weekly Newsletter; June 25, 2012  
- Biennial Letters of Agreement; October 11, 2011
- Byron Station January 30, 2012, Unusual Event Report; February 27, 2012  
- Evacuation Time Estimates for the Byron Station; December 2003
- Byron Station February 28, 2012, Unusual Event Report; March 26, 2012  
- UFSAR, Table 11.5-1; Airborne Process and Effluent Monitors; Revision 7
- List of Inaudible Public Address System Locations and Status; May 29, 2012  
- IR 1358442; NOS ID-Errors In Mailing List For EP Information Brochure; April 25, 2012
- Biennial Letters of Agreement; October 11, 2011  
- IR 1353670; TSC HVAC Equipment Vulnerability; April 13, 2012
- Evacuation Time Estimates for the Byron Station; December 2003  
- IR 1320571; Byron Fire Department Response to Unusual Event; January 31, 2012
- UFSAR, Table 11.5-1; Airborne Process and Effluent Monitors; Revision 7  
- IR 1319175; Additional Areas Are Deficient on the Quarterly Public Address Test;
- IR 1358442; NOS ID-Errors In Mailing List For EP Information Brochure; April 25, 2012  
  January 27, 2012
- IR 1353670; TSC HVAC Equipment Vulnerability; April 13, 2012  
- IR 1300315-10; NOS Objective Evidence Report; EP Offsite Agency Interface
- IR 1320571; Byron Fire Department Response to Unusual Event; January 31, 2012  
- IR 1269312; MET Tower Wind Direction Erratic; September 28, 2011
- IR 1319175; Additional Areas Are Deficient on the Quarterly Public Address Test;  
- IR 1267919; Request For Additional Clarification For EAL HU6; September 25, 2011
January 27, 2012  
- IR 1247327; Exercise-OSC Failed Demonstration Criteria; August 3, 2011
- IR 1300315-10; NOS Objective Evidence Report; EP Offsite Agency Interface  
- IR 1237774; Pre-Exercise TSC Failed Demonstration Criteria; July 8, 2011
- IR 1269312; MET Tower Wind Direction Erratic; September 28, 2011  
- IR 1130872-10; NOS Objective Evidence Report; EP Offsite Agency Interface
- IR 1267919; Request For Additional Clarification For EAL HU6; September 25, 2011  
4OA1 Performance Indicator Verification
- IR 1247327; Exercise-OSC Failed Demonstration Criteria; August 3, 2011  
- LS-AA-2110; Monthly Data Elements for NRC ERO Drill Participation;
- IR 1237774; Pre-Exercise TSC Failed Demonstration Criteria; July 8, 2011  
  September 2011 - March 2012
- IR 1130872-10; NOS Objective Evidence Report; EP Offsite Agency Interface  
                                            6                                Attachment
4OA1 Performance Indicator Verification  
- LS-AA-2110; Monthly Data Elements for NRC ERO Drill Participation;  
September 2011 - March 2012  


- LS-AA-2120; Monthly Data Elements for NRC Drill/Exercise Performance;
7
  July 2011 - March 2012
Attachment
- LS-AA-2130; Monthly Data Elements for NRC Alert and Notification System Reliability;
  July 2011 - March 2012
- LS-AA-2120; Monthly Data Elements for NRC Drill/Exercise Performance;  
- Byron ANS Test Reports; July 2011 - March 2012
July 2011 - March 2012  
- IR 1304945; Training-DEP Failures for LORT Annual Exam Cycle; December 20, 2011
- LS-AA-2130; Monthly Data Elements for NRC Alert and Notification System Reliability;  
Section 4OA2: Identification and Resolution of Problems (71152)
July 2011 - March 2012  
- IR 1071667; Non-Conservative Degraded Voltage Time Delay With a Due Date of
- Byron ANS Test Reports; July 2011 - March 2012  
  September 13, 2013, May 20, 2010
- IR 1304945; Training-DEP Failures for LORT Annual Exam Cycle; December 20, 2011  
- IR 1237140; Non-Conservative Input to HELB Analysis, July 6, 2011
Section 4OA2: Identification and Resolution of Problems (71152)  
- IR 1275710; Braidwood NCV - Non-Conservative EQ Classification in HELB,
- IR 1071667; Non-Conservative Degraded Voltage Time Delay With a Due Date of  
  October 12, 2011
September 13, 2013, May 20, 2010  
- IR 1288474; Potential Green NCV - Classification of EQ Zones from HELB,
- IR 1237140; Non-Conservative Input to HELB Analysis, July 6, 2011  
  November 8, 2011
- IR 1275710; Braidwood NCV - Non-Conservative EQ Classification in HELB,  
- IR 1354220; Need to Replace Primary Rosettes on S.O#01Y017B4-7, April 16, 2012
October 12, 2011  
- IR 1350467; Mass and Energy Analysis Could Impact UHS Temp and Inventory Limits,
- IR 1288474; Potential Green NCV - Classification of EQ Zones from HELB,  
  April 8, 2012
November 8, 2011  
- IR 1359137; Probable Reduced SG PORV Capacity for Original Valves, April 26, 2012
- IR 1354220; Need to Replace Primary Rosettes on S.O#01Y017B4-7, April 16, 2012  
- IR 1359198; DG Full Load Reject Testing, April 26, 2012
- IR 1350467; Mass and Energy Analysis Could Impact UHS Temp and Inventory Limits,  
- IR 1359686; Chillers in TSC Computer Room Not Providing Adequate Cooling, April 27, 2012
April 8, 2012  
- IR 1360458; Recommended Work Not Performed Prior to RTS, April 30, 2012
- IR 1359137; Probable Reduced SG PORV Capacity for Original Valves, April 26, 2012  
- IR 1361284; 1CS001B STT Acceptance Criteria Data Sheet Not Revised, May 02, 2012
- IR 1359198; DG Full Load Reject Testing, April 26, 2012  
- IR 1361939; Chart Recorder Not Logged into Temporary Change Tracking Log, May 03, 2012
- IR 1359686; Chillers in TSC Computer Room Not Providing Adequate Cooling, April 27, 2012  
- IR 1362451; 2TO081 Found Closed, Valve Should Have Been Opened, May 04, 2012
- IR 1360458; Recommended Work Not Performed Prior to RTS, April 30, 2012  
Section 40A5: Other Activities
- IR 1361284; 1CS001B STT Acceptance Criteria Data Sheet Not Revised, May 02, 2012  
- ALARA Work-In-Progress Review; 2012 Dry Cask Storage Campaign; March 29, 2012
- IR 1361939; Chart Recorder Not Logged into Temporary Change Tracking Log, May 03, 2012  
- BFP FH-20; Operation of Fuel Handling Building Crane; Revision 26
- IR 1362451; 2TO081 Found Closed, Valve Should Have Been Opened, May 04, 2012  
- BFP FH-35; Contingency Fuel Handling Building Crane Operations; Revision 0
Section 40A5: Other Activities  
- BFP FH-64; Transporter Operations; Revision 7
- ALARA Work-In-Progress Review; 2012 Dry Cask Storage Campaign; March 29, 2012  
- BFP FH-65; Spent Fuel Cask Site Transportation; Revision 10
- BFP FH-20; Operation of Fuel Handling Building Crane; Revision 26  
- BFP FH-68; HI-TRAC Preparation; Revision 3
- BFP FH-35; Contingency Fuel Handling Building Crane Operations; Revision 0  
- BFP FH-69; HI-TRAC Movement within the Fuel Building; Revision 10
- BFP FH-64; Transporter Operations; Revision 7  
- BFP FH-70; HI-TRAC Loading Operations; Revision 9
- BFP FH-65; Spent Fuel Cask Site Transportation; Revision 10  
- BFP FH-71; MPC Processing; Revision 12, 13, 14 and 15
- BFP FH-68; HI-TRAC Preparation; Revision 3  
- BFP FH-72; HI-STORM Processing; Revision 2
- BFP FH-69; HI-TRAC Movement within the Fuel Building; Revision 10  
- BFP FH-79; MPC Alternate Cooling; Revision 4
- BFP FH-70; HI-TRAC Loading Operations; Revision 9  
- BFP FH-83; Spent Fuel Cask Contingency Actions; Revision; Revision 3
- BFP FH-71; MPC Processing; Revision 12, 13, 14 and 15  
- BHP 4200-101; General Inspection of Fuel Handling Building Overhead Crane 0HC03G;
- BFP FH-72; HI-STORM Processing; Revision 2  
  Revision 0
- BFP FH-79; MPC Alternate Cooling; Revision 4  
- NF-AP-622; Fuel Selection and Documentation for Dry Cask Storage; Revision 4
- BFP FH-83; Spent Fuel Cask Contingency Actions; Revision; Revision 3  
- OP-AA-201-004; Fire Prevention for Hot Work; Revision 9
- BHP 4200-101; General Inspection of Fuel Handling Building Overhead Crane 0HC03G;  
- PI-CNSTR-T-OP-220; Closure Welding of Holtec Multi-Purpose Canisters at Exelon Facilities;
Revision 0  
  Revision 2
- NF-AP-622; Fuel Selection and Documentation for Dry Cask Storage; Revision 4  
- RP-BY-304-1001; HI-TRAC Radiation Survey; Revision 2
- OP-AA-201-004; Fire Prevention for Hot Work; Revision 9  
- RP-BY-304-1002; HI-STORM Radiation Survey; Revision 3
- PI-CNSTR-T-OP-220; Closure Welding of Holtec Multi-Purpose Canisters at Exelon Facilities;  
- 0BDCSR 3.1.1.1; Multi-Purpose Canister (MPC) Integrity Verification; Revision 1
Revision 2  
- 0BDCSR 3.1.3.1; Multi-Purpose Canister (MPC) Cavity Pressure Verification; Revision 1
- RP-BY-304-1001; HI-TRAC Radiation Survey; Revision 2  
                                          7                                Attachment
- RP-BY-304-1002; HI-STORM Radiation Survey; Revision 3  
- 0BDCSR 3.1.1.1; Multi-Purpose Canister (MPC) Integrity Verification; Revision 1  
- 0BDCSR 3.1.3.1; Multi-Purpose Canister (MPC) Cavity Pressure Verification; Revision 1  


- 0BDCSR 3.1.4.1; Supplemental Cooling System (SCS) Operability Verification; Revision 3
8
- 0BDCSR 3.2.2.1; MPC Surface Contamination Verification; Revision 1
Attachment
- 0BDCSR 3.3.1.1; Wet Cask Pit/MPC Boron Concentration Verification; Revision 1
- Byron Dry Cask Storage Training Matrix, Revision 1
- 0BDCSR 3.1.4.1; Supplemental Cooling System (SCS) Operability Verification; Revision 3  
- Byron ISFSI Lessons Learned Readiness Brief; February 10, 2012
- 0BDCSR 3.2.2.1; MPC Surface Contamination Verification; Revision 1  
- Byron Nuclear Power Station, Units 1 and 2; 10 CFR 72.212 Evaluation Report; Revision 3
- 0BDCSR 3.3.1.1; Wet Cask Pit/MPC Boron Concentration Verification; Revision 1  
- BYR11-197; Fuel Selection Package BYR-0016 for MPC0187; Revision 0
- Byron Dry Cask Storage Training Matrix, Revision 1  
- BYR11-198; Fuel Selection Package BYR-0017 for MPC0186; Revision 0
- Byron ISFSI Lessons Learned Readiness Brief; February 10, 2012  
- BYR11-199; Fuel Selection Package BYR-0018 for MPC0183; Revision 0
- Byron Nuclear Power Station, Units 1 and 2; 10 CFR 72.212 Evaluation Report; Revision 3  
- Forced Helium Dehydration System [Training], Revision 00
- BYR11-197; Fuel Selection Package BYR-0016 for MPC0187; Revision 0  
- Fuel Move Sheet Package 2012 Dry Cask - MPC0187; February 27, 2012
- BYR11-198; Fuel Selection Package BYR-0017 for MPC0186; Revision 0  
- Holtec Letter to Byron; FHD Dew Point Operability; March 22, 2012
- BYR11-199; Fuel Selection Package BYR-0018 for MPC0183; Revision 0  
- Holtec Report No. HI-2084113; Dose versus Distance from a HI-STORM 100S Version B
- Forced Helium Dehydration System [Training], Revision 00  
  Containing the MPC-32 for Byron/Braidwood; Revision 7
- Fuel Move Sheet Package 2012 Dry Cask - MPC0187; February 27, 2012  
- One Month Readiness Review, Byron Nuclear Station Dry Cask Storage 2012 Campaign;
- Holtec Letter to Byron; FHD Dew Point Operability; March 22, 2012  
  February 6, 2012
- Holtec Report No. HI-2084113; Dose versus Distance from a HI-STORM 100S Version B  
- IR 01319213; Unclear Scope of Site Reactor Engineering Review for Fuel Selection
Containing the MPC-32 for Byron/Braidwood; Revision 7  
  Packages; January 28, 2012
- One Month Readiness Review, Byron Nuclear Station Dry Cask Storage 2012 Campaign;  
- IR 01319283; Dry Cask Storage Project Review for Process Alignment; January 28, 2012
February 6, 2012  
- IR 01324010; HI-TRAC Trunnions Bound in HI-TRAC; February 7, 2012
- IR 01319213; Unclear Scope of Site Reactor Engineering Review for Fuel Selection  
- IR 01334080; Fuel Handling Building Crane 0HC03G Scoreboard Weight Readout;
Packages; January 28, 2012  
  February 29, 2012
- IR 01319283; Dry Cask Storage Project Review for Process Alignment; January 28, 2012  
- IR 01337745; Dry Cask Storage - Review of Holtec Information Bulletin 54 FHD Wiring;
- IR 01324010; HI-TRAC Trunnions Bound in HI-TRAC; February 7, 2012  
  March 7, 2012
- IR 01334080; Fuel Handling Building Crane 0HC03G Scoreboard Weight Readout;  
- IR 01339936; DCS - MPC Number 187 Discovered to be Oblong; March 12, 2012
February 29, 2012  
- IR 01342065; NRC Dry Cask Storage Results; March 16, 2012
- IR 01337745; Dry Cask Storage - Review of Holtec Information Bulletin 54 FHD Wiring;  
- IR 01344618; Helium Supply Flow to FHD Skid Blocked; March 23, 2012
March 7, 2012  
- IR 01345214; DCS Surveillance Change Needed for 0BDCSR 3.1.4.1; March 24, 2012
- IR 01339936; DCS - MPC Number 187 Discovered to be Oblong; March 12, 2012  
- IR 01349932; NRC IDD - DCS - Critique of Welding Operations; April 4, 2012
- IR 01342065; NRC Dry Cask Storage Results; March 16, 2012  
- IR 01350170; Dry Cask Process Recommendation - MPC Blowdown Phase; April 4, 2012
- IR 01344618; Helium Supply Flow to FHD Skid Blocked; March 23, 2012
- IR 01350552; Procedure Documentation Incomplete; April 5, 2012
- IR 01345214; DCS Surveillance Change Needed for 0BDCSR 3.1.4.1; March 24, 2012  
- IR 01350663; Procedure Revision Required - 0BDCSR 3.1.1.1; April 5, 2012
- IR 01349932; NRC IDD - DCS - Critique of Welding Operations; April 4, 2012  
- IR 01350712; Vendor Welding Procedure Revision Requested; April 5, 2012
- IR 01350170; Dry Cask Process Recommendation - MPC Blowdown Phase; April 4, 2012  
- IR 01350933; NRC Identified Bags of DAW Not Stored in Covered Carts; April 6, 2012
- IR 01350552; Procedure Documentation Incomplete; April 5, 2012  
- WO 01322216; Fuel Handling Building Overhead Bridge Crane Electrical Inspection;
- IR 01350663; Procedure Revision Required - 0BDCSR 3.1.1.1; April 5, 2012  
  June 30, 2011
- IR 01350712; Vendor Welding Procedure Revision Requested; April 5, 2012  
- WO 01323391, Fuel Handling Building Crane Mechanical Inspection; June 8, 2011
- IR 01350933; NRC Identified Bags of DAW Not Stored in Covered Carts; April 6, 2012  
- WO 01437840; MPC Lift Cleat Inspection; February 8, 2012
- WO 01322216; Fuel Handling Building Overhead Bridge Crane Electrical Inspection;  
- WO 01438159; Lift Yoke Inspection; February 6, 2012
June 30, 2011  
- WO 01500091; Mechanical [Fuel Handling Building] Crane Inspection; January 18, 2012
- WO 01323391, Fuel Handling Building Crane Mechanical Inspection; June 8, 2011  
- 72.48-032; Wet Cask Pit/MPC Boron Concentration Verification; September 14, 2011
- WO 01437840; MPC Lift Cleat Inspection; February 8, 2012  
- 72.48-033; MPC Surface Contamination Verification; September 14, 2011
- WO 01438159; Lift Yoke Inspection; February 6, 2012  
- 72.48-038; Mating Device Modification; December 15, 2011
- WO 01500091; Mechanical [Fuel Handling Building] Crane Inspection; January 18, 2012  
- 72.48-039; OU-AA-630; December 30, 2011
- 72.48-032; Wet Cask Pit/MPC Boron Concentration Verification; September 14, 2011  
- 72.48-045; 72.212 Evaluation Changes for FSAR Revision 9 and CoC Amendment 7
- 72.48-033; MPC Surface Contamination Verification; September 14, 2011  
                                          8                              Attachment
- 72.48-038; Mating Device Modification; December 15, 2011  
- 72.48-039; OU-AA-630; December 30, 2011  
- 72.48-045; 72.212 Evaluation Changes for FSAR Revision 9 and CoC Amendment 7  


                            LIST OF ACRONYMNS USED
9
ADAMS   Agencywide Document Access and Management System
Attachment
ALARA   As-Low-As-Is-Reasonably-Achievable
ANS     Alert and Notification System
LIST OF ACRONYMNS USED  
ASME     American Society of Mechanical Engineers
CAP     Corrective Action Program
ADAMS  
CFR     Code of Federal Regulations
Agencywide Document Access and Management System  
CoC     Certificate of Compliance
ALARA  
CS       Containment Spray
As-Low-As-Is-Reasonably-Achievable  
DEP     Drill and Exercise Performance
ANS  
EP       Emergency Preparedness
Alert and Notification System  
ERO     Emergency Response Organization
ASME  
FSAR     Final Safety Analysis Report
American Society of Mechanical Engineers  
HELB     High Energy Line Break
CAP  
HI-STORM Storage Cask
Corrective Action Program  
HI-TRAC Transfer Cask
CFR  
IMC     Inspection Manual Chapter
Code of Federal Regulations  
I/O     Input/Output
CoC  
IP       Inspection Procedure
Certificate of Compliance  
IR       Inspection Report
CS  
IR       Issue Report
Containment Spray  
ISFSI   Independent Spent Fuel Storage Installation
DEP  
IST     Inservice Testing
Drill and Exercise Performance  
LER     Licensee Event Report
EP  
MCID     Materials Control, ISFSI, and Decommissioning
Emergency Preparedness  
MPC     Multi-Purpose Canister
ERO  
NCV     Non-Cited Violation
Emergency Response Organization  
NEi     Nuclear Energy Institute
FSAR  
NRC     U.S. Nuclear Regulatory Commission
Final Safety Analysis Report  
PARS     Publicly Available Records System
HELB  
PI       Performance Indicator
High Energy Line Break  
RCFC     Reactor Containment Fan Cooler
HI-STORM  
RCS     Reactor Coolant System
Storage Cask  
RH       Residual Heat Removal
HI-TRAC  
RP       Radiation Protection
Transfer Cask  
SDP     Significance Determination Process
IMC  
SER     Safety Evaluation Report
Inspection Manual Chapter  
SSC     Structure, System, and Component
I/O  
SX       Essential Service Water
Input/Output  
TS       Technical Specification
IP  
UFSAR   Updated Final Safety Analysis Report
Inspection Procedure  
WO       Work Order
IR  
                                      9                  Attachment
Inspection Report  
IR  
Issue Report  
ISFSI  
Independent Spent Fuel Storage Installation  
IST  
Inservice Testing  
LER  
Licensee Event Report  
MCID  
Materials Control, ISFSI, and Decommissioning  
MPC  
Multi-Purpose Canister  
NCV  
Non-Cited Violation  
NEi  
Nuclear Energy Institute  
NRC  
U.S. Nuclear Regulatory Commission  
PARS  
Publicly Available Records System  
PI  
Performance Indicator  
RCFC  
Reactor Containment Fan Cooler  
RCS  
Reactor Coolant System  
RH  
Residual Heat Removal  
RP  
Radiation Protection  
SDP  
Significance Determination Process  
SER  
Safety Evaluation Report  
SSC  
Structure, System, and Component  
SX  
Essential Service Water  
TS  
Technical Specification  
UFSAR  
Updated Final Safety Analysis Report  
WO  
Work Order  


M. Pacilio                                                                 -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
M. Pacilio  
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                                                          Sincerely,
-2-  
                                                                          /RA/
                                                                          Eric R. Duncan, Chief
                                                                          Branch 3
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its  
                                                                          Division of Reactor Projects
enclosure, and your response (if any) will be available electronically for public inspection in the  
Docket Nos. 50-454; 50-455; and 07200068
NRC Public Document Room or from the Publicly Available Records (PARS) component of  
License Nos. NPF-37 and NPF-66
NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at  
Enclosure:               Inspection Report No. 05000454/2012003 and 05000455/2012003;
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
                          07200068/2012001
Sincerely,  
                            w/Attachment: Supplemental Information
cc w/encl:               Distribution via ListServ
DISTRIBUTION:
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DOCUMENT NAME: G:\DRPIII\BYRO\Byron 2012 003.docx
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To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE             RIII                                 RIII
/RA/  
  NAME               Duncan                               Ng
  DATE               08/07/12                             08/03/12
                                                          OFFICIAL RECORD COPY
Eric R. Duncan, Chief  
Branch 3  
Division of Reactor Projects  
Docket Nos. 50-454; 50-455; and 07200068  
License Nos. NPF-37 and NPF-66  
Enclosure:  
Inspection Report No. 05000454/2012003 and 05000455/2012003;  
07200068/2012001  
  w/Attachment: Supplemental Information  
cc w/encl:  
Distribution via ListServ  
DISTRIBUTION:  
See next page  
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Non-Publicly Available  
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Non-Sensitive  
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy  
OFFICE  
RIII  
RIII  
   
NAME  
Duncan  
Ng  
   
DATE  
08/07/12  
08/03/12  
OFFICIAL RECORD COPY  


Letter to M. Pacilio from E. Duncan dated August 7, 2012.
SUBJECT:       BYRON STATION, UNITS 1 AND 2, NRC INTEGRATED INSPECTION
Letter to M. Pacilio from E. Duncan dated August 7, 2012.  
              REPORT 05000454/2012003; 05000455/2012003; 07200068/2012001
DISTRIBUTION:
Shawn Williams
SUBJECT:  
RidsNrrDorlLpl3-2 Resource
BYRON STATION, UNITS 1 AND 2, NRC INTEGRATED INSPECTION  
RidsNrrPMByron Resource
REPORT 05000454/2012003; 05000455/2012003; 07200068/2012001  
RidsNrrDirsIrib Resource
Chuck Casto
DISTRIBUTION:  
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Shawn Williams
Steven Orth
RidsNrrDorlLpl3-2 Resource  
Jared Heck
RidsNrrPMByron Resource  
Allan Barker
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Carole Ariano
Chuck Casto  
Linda Linn
Cynthia Pederson  
DRPIII
Steven Orth  
DRSIII
Jared Heck  
Patricia Buckley
Allan Barker  
Tammy Tomczak
Carole Ariano  
Linda Linn  
DRPIII  
DRSIII  
Patricia Buckley  
Tammy Tomczak  
ROPreports.Resource@nrc.gov
ROPreports.Resource@nrc.gov
}}
}}

Latest revision as of 23:07, 11 January 2025

IR 05000454-12-003, 05000455-12-003, 07200068/2012001; 04/01/2012 - 06/30/2012; Byron Station, Units 1 & 2; Operability Evaluations; Identification and Resolution of Problems
ML12221A069
Person / Time
Site: Byron  
Issue date: 08/07/2012
From: Eric Duncan
Region 3 Branch 3
To: Pacilio M
Exelon Generation Co, Exelon Nuclear
References
IR-12-003
Download: ML12221A069 (42)


See also: IR 05000454/2012003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

August 7, 2012

Mr. Michael J. Pacilio

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Office (CNO), Exelon Nuclear

4300 Warrenville Road

Warrenville, IL 60555

SUBJECT:

BYRON STATION, UNITS 1 AND 2, NRC INTEGRATED INSPECTION

REPORT NOS 05000454/2012003; 05000455/2012003; 07200068/2012001

Dear Mr. Pacilio:

On June 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Byron Station, Units 1 and 2. The enclosed inspection report documents the

inspection findings which were discussed at an exit meeting on July 2, 2012, with Mr. T. Tulon

and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Two NRC-identified findings of very low safety significance (Green) were identified during

this inspection. These findings were determined to involve violations of NRC requirements.

The NRC is treating these violations as Non-Cited Violations (NCVs) consistent with

Section 2.3.2 of the NRC Enforcement Policy. Additionally, a license-identified violation is

listed in Section 4OA7 of this report.

If you contest the subject or severity of an NCV, you should provide a response within 30 days

of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001,

with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Byron Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region III, and the Resident Inspector Office

at the Byron Station.

M. Pacilio

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

Eric R. Duncan, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 50-454, 50-455, and 07200068

License Nos. NPF-37 and NPF-66

Enclosure:

Inspection Report No. 05000454/2012003; 05000455/2012003; and

07200068/2012001

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-454; 50-455; 07200068

License Nos:

NPF-37; NPF-66

Report Nos:

05000454/2012003; 05000455/2012003;

07200068/2012001

Licensee:

Exelon Generation Company, LLC

Facility:

Byron Station, Units 1 and 2

Location:

Byron, IL

Dates:

April 1, 2012, through June 30, 2012

Inspectors:

B. Bartlett, Senior Resident Inspector

J. Robbins, Resident Inspector

R. Jickling, Emergency Preparedness Specialist

J. Gilliam, Reactor Engineer

R. Langstaff, Reactor Engineer

K. Walton, Senior Operations Engineer

M. Learn, Reactor Engineer

L. Rodriguez, Reactor Engineer

J. Tapp, Health Physicist

C. Crisden, Emergency Preparedness Inspector, Region I

C. Thompson, Resident Inspector, Illinois Emergency

Management Agency

Approved by:

E. Duncan, Chief

Branch 3

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ......................................................................................................... 1

REPORT DETAILS ..................................................................................................................... 3

Summary of Plant Status......................................................................................................... 3

1.

REACTOR SAFETY ..................................................................................................... 3

1R01

Adverse Weather Protection (71111.01) ............................................................ 3

1R04

Equipment Alignment (71111.04) ....................................................................... 4

1R05

Fire Protection (71111.05) ................................................................................. 5

1R06

Flooding (71111.06) ........................................................................................... 7

1R11

Licensed Operator Requalification Program (71111.11) ..................................... 7

1R12

Maintenance Effectiveness (71111.12) .............................................................. 9

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13) .......... 9

1R15

Operability Evaluations (71111.15) .................................................................. 10

1R19

Post Maintenance Testing (71111.19) ............................................................. 13

1R22

Surveillance Testing (71111.22)....................................................................... 14

1EP2

Alert and Notification System Evaluation (71114.02) ........................................ 15

1EP3

Emergency Response Organization Augmentation Testing (71114.03) ........... 15

1EP5

Correction of Emergency Preparedness Weaknesses and Deficiencies

(71114.05) ......................................................................................................... 16

1EP6

Drill Evaluation (71114.06) ............................................................................... 16

2.

OTHER ACTIVITIES .................................................................................................. 17

4OA1

Performance Indicator Verification (71151.EP01, EP02, EP03) ....................... 17

4OA2

Identification and Resolution of Problems (71152) ........................................... 18

4OA3

Follow-up of Events and Notices of Enforcement Discretion (71153) ............... 24

4OA5

Other Activities ................................................................................................. 24

4OA6

Management Meetings .................................................................................... 26

4OA7

Licensee-Identified Violation ............................................................................ 26

SUPPLEMENTAL INFORMATION ............................................................................................. 1

Key Points of Contact .............................................................................................................. 1

List of Items Opened, Closed, and Discussed ......................................................................... 2

List of Documents Reviewed ................................................................................................... 3

List of Acronymns Used .......................................................................................................... 9

1

Enclosure

SUMMARY OF FINDINGS

Inspection Report (IR) 05000454/2012003, 05000455/2012003, 07200068/2012001;

04/01/2012 - 06/30/2012; Byron Station, Units 1 & 2; Operability Evaluations; Identification and

Resolution of Problems.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two Green findings were identified by the

inspectors. The findings were considered Non-Cited Violations (NCVs) of NRC regulations.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Assigned

cross-cutting aspects were determined using IMC 0310, Components Within the Cross-Cutting

Areas. Findings for which the SDP does not apply may be Green or be assigned a severity

level after NRC management review. The NRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4, dated December 2006.

A.

NRC-Identified and Self-Revealed Findings

Cornerstone: Initiating Events, Barrier Integrity

Green. A finding of very low safety significance and an associated NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

was identified by the inspectors when licensee personnel failed to identify boric acid

accumulation that would have impeded flow from the containment leakage detection

trough to the containment sump. The licensee entered this issue into the Corrective

Action Program (CAP) as Issue Report (IR) 1339957. Corrective actions included

removing the boric acid accumulation from the leakage detection trough and passing

water through the drain to verify associated piping was free of obstruction.

The finding was determined to be more than minor because the finding was similar to

IMC 0612, Appendix E, Example 4(a). Example 4 focuses on procedural errors. The

not minor if section in Example 4(a) discussed that if a later evaluation determines that

the safety-related equipment was adversely impacted, it was more than minor. The flow

obstruction in the leakage detection trough would have delayed the flow of water to the

sump thereby delaying any subsequent alarm. Therefore, this performance deficiency

adversely impacted the Equipment Performance aspect of the Initiating Events

Cornerstone. The inspectors determined the finding could be evaluated using the SDP

in accordance with IMC 0609, Significance Determination Process, Attachment

0609.04, Phase 1 - Initial Screening and Characterization of Findings, Table 4a,

Characterization Worksheet for Initiating Events Cornerstone. The inspectors

answered No to Question 1: Assuming worst case degradation, would the finding result

in exceeding the Technical Specification (TS) limit for any RCS [Reactor Coolant

System] leakage or could the finding have likely affected other mitigation systems

resulting in a total loss of their safety function? Therefore, this finding was determined

to be of very low safety significance (Green). This finding had a cross-cutting aspect in

the Corrective Action Program component of the Problem Identification and Resolution

cross-cutting area because licensee personnel failed to ensure that an issue potentially

impacting nuclear safety was promptly identified and fully evaluated, and that actions

were taken to address safety issues in a timely manner, commensurate with their

significance P.1(d). (Section 1R15)

2

Enclosure

Green. A self-revealed finding with two examples of very low safety significance and an

associated NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, was identified when licensee personnel failed to properly torque a RCS

pressure boundary valve closed and failed to properly re-install a Reactor Containment

Fan Cooler (RCFC) interior access panel during the previous Unit 1 refueling outage.

The licensee replaced the valve and reinstalled the RCFC internal access panel upon

identification and entered the item into the CAP as IR 1339375 and IR 1347450,

respectively. Additional corrective actions included modifying the installation procedure

to add clarity in the selection of the proper torque value and to add detail and tracking

aids for the RCFC interior access panels.

In accordance with IMC 0612, Appendix B, Issue Screening, the first example was

determined to be more than minor because it was associated with the Procedure Quality

attribute of the Initiating Events Cornerstone and adversely affected the cornerstone

objective of limiting the likelihood of those events that upset plant stability and challenge

critical safety functions during shutdown as well as power operations. Specifically, this

issue increased the risk of a small break loss of coolant accident. The inspectors

performed a Phase 1 SDP screening using IMC 0609, Attachment 4, Table 4a,

Characterization Worksheet for Initiating Events Cornerstone. The inspectors

determined that the finding would not result in exceeding the TS limit for any RCS

leakage or could have likely affected other mitigation systems resulting in a total loss of

their safety function.

The second example was determined to be more than minor because it was associated

with the Configuration Control attribute of the Barrier Integrity Cornerstone and adversely

affected the cornerstone objective of providing reasonable assurance that physical

design barriers, including the containment, protect the public from radionuclide releases

caused by accidents and events. Specifically, this issue decreased the availability and

reliability of the RCFCs for use during a design basis accident. The inspectors

determined that the issue was of very low safety significance (Green) because the

finding did not represent a degradation of the radiological barrier function, did not

represent a degradation of the barrier function of the control room, did not represent an

actual open pathway in the physical integrity of reactor containment, and did not involve

an actual reduction in function of hydrogen igniters in the reactor containment.

Both examples had a cross-cutting aspect in the Work Practices component of the

Human Performance cross-cutting area H.4(a) because licensee personnel failed to

properly utilize human error prevention techniques. These two examples of the finding

with a cross-cutting aspect were considered as a single NCV. (Section 4OA2)

B.

Licensee-Identified Violations

A violation of very low safety significance that was identified by the licensee has been

reviewed by inspectors. Corrective actions planned or taken by the licensee have been

entered into the licensees corrective action program. The violation and corrective action

tracking number are listed in Section 4OA7 of this report.

3

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at or near full power throughout most of the inspection period. The performance

of the Unit 1 nonsafety-related Natural Draft Cooling Tower that had been degrading over

several years worsened during the inspection period. The decrease in cooling tower efficiency

resulted in elevated circulating water temperatures. This in turn resulted in less efficient cooling

of the main condenser and increasing condenser vacuum backpressure. During the morning

and early afternoon hours, as outside air temperatures warmed, the licensee routinely reduced

reactor power levels in order to maintain condenser vacuum margins. As outside temperatures

cooled during the evening and nighttime hours, the licensee routinely increased reactor power.

On some days, the licensee reduced and subsequently increased unit power many times. For

example, during one 72-hour period, the licensee reduced and increased power 54 times. At

the end of the inspection period the licensee revised their power change strategies to perform

fewer, but larger, changes. As a result, power level changes were altered less frequently.

Unit 2 operated at or near full power throughout most of the inspection period. The performance

of the Unit 2 Natural Draft Cooling Tower was similar to Unit 1 with a consequent similar impact

upon plant power level changes.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1

Readiness For Impending Hot Summer Weather Conditions

a.

Inspection Scope

The inspectors evaluated the licensees preparations for hot summer weather conditions,

focusing on the electrical distribution system and the plant chilled water system.

During the weeks of May 21, 2012, and May 28, 2012, the inspectors performed a

detailed review of severe weather and plant de-winterization procedures and performed

general area plant walkdowns. The inspectors focused on plant-specific design features

and implementation of procedures for responding to or mitigating the effects of hot

summer weather conditions on the operation of the plant. The inspectors reviewed

system health reports and system engineering summer readiness review documents for

the above systems.

Additionally, the inspectors verified that adverse weather related issues were entered

into the licensees corrective action program with the appropriate characterization and

significance. Selected action requests were reviewed to verify that corrective actions

were appropriate and implemented as scheduled.

This inspection constituted one seasonal extreme weather readiness inspection sample

as defined in Inspection Procedure (IP) 71111.01-05.

4

Enclosure

b.

Findings

No findings were identified.

.2

Readiness For Impending Adverse Weather - High Winds

a.

Inspection Scope

Since thunderstorms with potential tornados and high winds were forecast in the vicinity

of the facility for the week of June 18, 2012, while emergent work was being performed

on the Unit 2 Train B Station Air Compressor, the inspectors reviewed the licensees

overall preparations/protection for the expected conditions. The inspectors toured the

plant grounds in the vicinity of the main power transformers, unit auxiliary transformer,

station auxiliary transformers, and containment access facility to look for loose debris,

which if present could become missiles during a tornado or with high winds. During the

inspections, the inspectors focused on plant-specific design features and the licensees

procedure used to respond to tornado and high wind conditions. Documents reviewed

are listed in the Attachment.

This inspection constituted one readiness for impending adverse weather condition

inspection sample as defined in IP 71111.01-05.

b.

Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

.1

Quarterly Partial System Walkdowns

a.

Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

Unit 1 Train A Containment Spray (CS) while Unit 1 Train B CS was Out of

Service for Maintenance; and

Unit 2 Train A CS while Unit 2 Train B CS was Out of Service for Maintenance.

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system and therefore

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical

Specification (TS) requirements, outstanding work orders (WOs), condition reports, and

the impact of ongoing work activities on redundant trains of equipment in order to identify

conditions that could have rendered the systems incapable of performing their intended

functions. The inspectors also walked down accessible portions of the systems to verify

system components and support equipment were aligned correctly and operable. The

inspectors examined the material condition of the components and observed operating

parameters of equipment to verify that there were no obvious deficiencies. The

5

Enclosure

inspectors also verified that the licensee had properly identified and resolved equipment

alignment problems that could cause initiating events or impact the capability of

mitigating systems or barriers and entered them into the Corrective Action Program

(CAP) with the appropriate significance characterization. Documents reviewed are listed

in the Attachment.

These activities constituted two partial system walkdown samples as defined in

IP 71111.04-05.

b.

Findings

No findings were identified.

.2

Semi-Annual Complete System Walkdown

a.

Inspection Scope

During the week of June 25, 2012, the inspectors performed a complete system

alignment inspection of the Unit 2 Auxiliary Feedwater system to verify the functional

capability of the system. This system was selected because it was considered both

safety significant and risk significant in the licensees probabilistic risk assessment. In

addition, a recent modification had been performed which affected certain important air

operated valves in the system. The inspectors walked down the system to review

mechanical and electrical equipment lineups; electrical power availability; system

pressure and temperature indications, as appropriate; component labeling; component

lubrication; component and equipment cooling; hangers and supports; operability of

support systems; and to ensure that ancillary equipment or debris did not interfere with

equipment operation. A review of a sample of past and outstanding WOs was

performed to determine whether any deficiencies significantly affected the system

function. In addition, the inspectors reviewed the CAP database to ensure that system

equipment alignment problems were being identified and appropriately resolved.

Documents reviewed are listed in the Attachment.

These activities constituted one complete system walkdown sample as defined in

IP 71111.04-05.

b.

Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1

Routine Resident Inspector Tours (71111.05Q)

a.

Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

6

Enclosure

Unit 1 Train A Residual Heat Removal (RH) Pump Room - Fire Zone 11.2A-1;

Unit 1 Train B RH Pump Room - Fire Zone 11.2D-1;

Unit 1 Train A CS Pump Room - Fire Zone 11.2B-1;

Unit 1 Train B CS Pump Room - Fire Zone 11.2C-2; and

Unit 2 Division 22 Miscellaneous Electrical Equipment Room and Battery Room -

Fire Zone 5.4-2.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded or inoperable fire protection

equipment, systems, or features in accordance with the licensees fire plan. The

inspectors selected fire areas based on their overall contribution to internal fire risk as

documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the Attachment to this report, the inspectors verified that fire

hoses and extinguishers were in their designated locations and available for immediate

use; that fire detectors and sprinklers were unobstructed; that transient material loading

was within the analyzed limits; and fire doors, dampers, and penetration seals appeared

to be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees CAP.

These activities constituted five quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b.

Findings

No findings were identified

.2

Fire Protection - Drill Observation (71111.05A)

a.

Inspection Scope

During an announced drill on May 16, 2012, associated with a simulated fire in the

outside barrel storage area, the inspectors assessed the timeliness of the fire brigade in

arriving at the scene, the fire fighting equipment brought to the scene, the donning of fire

protective clothing, the effectiveness of communications, and the exercise of command

and control by the fire brigade leader. The inspectors also assessed the acceptance

criteria for the drill objectives; the rigor and thoroughness of the post-drill critique; and

verified that fire protection drill issues were being entered into the licensee's CAP with

the appropriate characterization and significance. Documents reviewed are listed in the

Attachment.

This inspection constituted one annual fire protection drill inspection sample as defined

in IP 71111.05AQ.

b.

Findings

No findings were identified.

7

Enclosure

1R06 Flooding (71111.06)

.1

Internal Flooding

a.

Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the UFSAR, engineering calculations, and abnormal operating procedures to

identify licensee commitments. The specific documents reviewed are listed in the

Attachment to this report. In addition, the inspectors reviewed licensee drawings to

identify areas and equipment that may be affected by internal flooding caused by the

failure or misalignment of nearby sources of water, such as the fire suppression or the

circulating water systems. The inspectors also reviewed the licensees corrective action

documents with respect to past flood-related items identified in the CAP to verify the

adequacy of the corrective actions. The inspectors performed a walkdown of the

following plant area to assess the adequacy of watertight doors and verify drains and

sumps were clear of debris and were operable, and that the licensee complied with its

commitments:

Floor Drains Located in Auxiliary Building 364 Elevation, General Area

This inspection constituted one internal flooding sample as defined in IP 71111.06-05.

b.

Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1

Resident Inspector Quarterly Review (71111.11Q)

a.

Inspection Scope

On May 8, 2012, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems, and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

licensed operator performance;

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

8

Enclosure

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment.

In addition, the inspectors observed licensed operator performance in the actual plant

and the main control room during this calendar quarter.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in IP 71111.11-05.

b.

Findings

No findings were identified.

.2

Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q)

On June 28, 2012, the inspectors observed control room operators immediately following

the loss of the Unit 1 Train B Main Feedwater Pump, while the operators were also

addressing elevated outside air temperatures, which caused main generator hydrogen

cooling concerns, instrument air dryer failures, spurious fire alarms, main generator

reactive load adjustments, and a reported failure of the Unit 2 E Natural Draft Cooling

Tower riser. This was an activity that required heightened awareness or was related to

increased risk. The inspectors evaluated the following areas:

licensed operator performance;

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The performance in these areas was compared to pre-established operator action

expectations, procedural compliance, and task completion requirements. Documents

reviewed are listed in the Attachment.

This inspection constituted one quarterly licensed operator heightened activity/risk

sample as defined in IP 71111.11-05.

b.

Findings

No findings were identified.

.3

Conformance With Examination Security Requirements (71111.11B)

a.

Inspection Scope

The inspectors reviewed the facility licensees physical security controls (e.g., access

restrictions and simulator input/output (I/O) controls, simulator software) and integrity

9

Enclosure

measures (e.g., security agreements, simulator software access) throughout the

inspection period.

b.

Findings

One licensee-identified finding with an Non-Cited Violation (NCV) is documented in

Section 4OA7 of this report. No other findings were identified.

1R12 Maintenance Effectiveness (71111.12)

.1

Routine Quarterly Evaluations (71111.12Q)

a.

Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

Unit 1 and Unit 2 Natural Draft Cooling Tower Fill Degradation; and

Non-Essential Service Water Increased Silt and Fill Issues.

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment.

This inspection constituted two quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b.

Findings

No findings were identified

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1

Maintenance Risk Assessments and Emergent Work Control

a.

Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

Work Week Schedule for the Week of May 21, 2012;

Unit 2 Train B CS Inoperable while Unit 2 Loop C Steam Generator Power

Operated Relief Valve was Inoperable;

Activities During the Modification of Unit Common Component Cooling Heat

Exchanger Discharge Valve 0SX007; and

Unit 2 Change in Risk Status Due to Emergent Failure of Unit 2 Train B Station Air

Compressor during Planned Outage of Unit 1 Train A Station Air Compressor.

10

Enclosure

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These maintenance risk assessments and emergent work control activities constituted

four samples as defined in IP 71111.13-05.

b.

Findings

No findings were identified.

1R15 Operability Evaluations (71111.15)

.1

Operability Evaluations

a.

Inspection Scope

The inspectors reviewed the following issues:

Steam Generator Margin to Overfill Issues;

Unit 1 Train A Reactor Containment Fan Cooler Missing Internal Access Hatch;

Operability Evaluation 12-001, Potential Design Vulnerability in Switchyard Single

Open Phase Detection;

Operability Evaluation 09-001, Diesel Oil Storage Tank Vent Lines Crimp Versus

Break;

Operability Evaluation 12-005, High Energy Line Break (HELB) Load Not

considered in Structural Calculation;

Operability Evaluation 11-005, Turbine Building HELB Input Errors; and

Unit 1 Containment Leakage Detection System Due to Boric Acid Accumulation in

System Drain. (Sample previously credited in Inspection Report

050000454/2012002; 05000455/2012002)

The inspectors selected these potential operability issues based on the risk

significance of the associated components and systems. The inspectors

evaluated the technical adequacy of the evaluations to ensure that TS operability

was properly justified and the subject component or system remained available

such that no unrecognized increase in risk occurred. The inspectors compared

the operability and design criteria in the appropriate sections of the TS and

UFSAR to the licensees evaluations to determine whether the components or

systems were operable. Where compensatory measures were required to

maintain operability, the inspectors determined whether the measures in place

would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated

with the evaluations. Additionally, the inspectors reviewed a sample of corrective

11

Enclosure

action documents to verify that the licensee was identifying and correcting any

deficiencies associated with operability evaluations. Documents reviewed are

listed in the Attachment.

This operability inspection constituted six samples as defined in IP 71111.15-05.

b.

Findings

(1) (Closed) Unresolved Item 05000454/2012002-03, Boric Acid Accumulation Identified in

Leakage Detection Trough

Introduction: A finding of very low safety significance (Green) and an associated NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

was identified by the inspectors when licensee personnel failed to identify boric acid

accumulation that would have impeded flow from the containment leakage detection

trough to the containment sump.

Description: During a Unit 1 maintenance outage, the inspectors identified a boric acid

leak on sample valve 1PS9365B on the 426 elevation of containment. The 426

elevation of containment had a grated floor; therefore, the inspectors proceeded to the

lower levels of containment to determine if any other equipment had been impacted by

the leak. On the 377 elevation, the inspectors identified a large area of boric acid

accumulation. Radiation Protection (RP) personnel were in containment to

decontaminate an area associated with a previously identified leak on 1RC8042B when

this additional leak was identified. The inspectors made an RP supervisor that was in

the area aware of this additional source of leakage. Additionally, photographs were

taken and provided to the Outage Control Center. The licensee entered this issue into

their CAP as IR 1339957, 1PS9365 Has Leak From Either Packing or Bonnet.

In preparation for a planned change from Mode 5 to Mode 4, the licensee routinely

performed an assessment of containment in accordance with the Containment Loose

Debris Inspection procedure, 1BOSR Z.5.b.1-1. The purpose of this inspection was to

ensure that the material condition of containment was sufficient to support at power

operations. The inspectors performed an independent assessment following the

licensees assessment. The inspectors identified that boric acid associated with the leak

identified in IR 1339957 on the 377 elevation was still present. Specifically, boric acid

had accumulated in a trough along the wall of the inner containment structure. The

accumulated boric acid completely covered the drain in the trough. The purpose of this

trough was to collect any potential leakage and direct that leakage to a sump. The flow

of water into, as well as the level of this sump was monitored to facilitate the prompt

identification of leaks that may occur in containment. The reactor coolant system (RCS)

leakage detection instrumentation was required to be operable in Modes 1-4 and Unit 1

was in Mode 4 at the time of this discovery. This issue was entered into the licensees

CAP as IR 1341380. Corrective actions included removing the boric acid accumulation

from the leakage detection trough and passing water through the drain to verify

associated piping was free of obstruction.

Unresolved Item (URI)05000454/2012002-03 was opened pending the licensees

completion of their assessment of the issue and the inspectors review of that

assessment in NRC Inspection Report 05000454/2012002; 05000455/2012002. A

12

Enclosure

subsequent evaluation by the licensee determined that the obstruction did not

completely block the flow of water to the drain.

The significance of RCS leakage varies widely depending on its source, rate, and

duration. Therefore, detecting RCS leakage into containment is necessary. The ability

to separate identified leakage from unidentified leakage provides quantitative information

to the operators. This information supports the risk assessment process and facilitates

timely initiation of corrective actions.

Analysis: The inspectors determined that the failure to identify a flow obstruction in the

leakage detection trough was contrary to the requirements of 1BOSR Z.5.b.1-1, Unit

One Containment Loose Debris Inspection, and was a performance deficiency.

The finding was determined to be more than minor because the finding was similar to

IMC 0612, Appendix E, Example 4(a). Example 4 focused on procedural errors. The

not minor if section in Example 4(a) discussed that if a later evaluation determines that

the safety-related equipment was adversely impacted, it was more than minor. The flow

obstruction in the leakage detection trough would have delayed the flow of water to the

sump thereby delaying any subsequent alarm. Therefore, this performance deficiency

adversely impacted the Equipment Performance attribute of the Initiating Events

Cornerstone.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, Table 4a for the Initiating Events

Cornerstone. The inspectors selected this cornerstone due to the affected equipment

being used to inform operations staff of changing conditions in containment. Reactor

coolant system leakage was one of many analyzed initiating events. The inspectors

answered No to Question 1: Assuming worst case degradation, would the finding result

in exceeding the Tech Spec [Technical Specification] limit for any RCS leakage or could

the finding have likely affected other mitigation systems resulting in a total loss of their

safety function? Therefore, this finding was determined to be of very low safety

significance (Green).

This finding had a cross-cutting aspect in the CAP component of the Problem

Identification and Resolution cross-cutting area because licensee personnel did not

ensure that an issue potentially impacting nuclear safety was promptly identified, fully

evaluated, and that actions were taken to address safety issues in a timely manner,

commensurate with their significance. Specifically, the accumulated boric acid

obstructed flow through the leakage detection trough. The cause of this accumulation,

leakage from sample valve 1PS9365B, was previously identified and entered into the

CAP. P.1(d)

Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings. Surveillance procedure 1BOSR Z.5.b.1-1, Unit 1 Containment

Loose Debris Inspection, Revision 15, was written in accordance with 10 CFR Part 50,

accomplished an activity affecting quality, and required that the drain trough and floor

drains be free of debris and that flow not be impeded. Step 4(a) of 1BOSR Z.5.b.1-1

13

Enclosure

required licensee personnel to verify that drain trough and floor drains located on the

377 elevation to be free of flow obstructions.

Contrary to the above, on March 14, 2012, the licensee failed to accomplish the Unit

One Containment Loose Debris Inspection, an activity affecting quality, in accordance

with the applicable instructions, procedures, or drawings. Specifically, the licensee failed

to adequately implement procedure 1BOSR Z.5.b.1-1 to verify that drain trough and floor

drains located on the 377 elevation of the containment were free of flow obstructions, in

that the inspectors identified boric acid accumulation that would have impeded flow from

the leakage detection trough to the sump. Because this violation was of very low safety

significance and this issue was entered into the licensees CAP as IR 1339957, this

violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC

Enforcement Policy. (NCV 05000454/2012003-01, Leakage Detection Trough with

Large Accumulation of Boric Acid Identified)

URI 05000454/2012002-03 is closed.

1R19 Post Maintenance Testing (71111.19)

.1

Post Maintenance Testing

a.

Inspection Scope

The inspectors reviewed the following post maintenance testing activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

Unit 2 Essential Service Water Valve 2SX010 following Modification;

Unit 1 C Loop Steam Generator Power Operated Relief Valve following Hand

Pump Replacement;

Unit 2 Train B Auxiliary Feedwater Pump following Scheduled Maintenance; and

Unit Common Component Cooling Heat Exchanger Discharge Valve 0SX007

following Electrical Modification.

These activities were selected based upon the structure, system, and components

(SSCs) ability to impact risk. The inspectors evaluated these activities for the following

(as applicable): the effect of testing on the plant had been adequately addressed; testing

was adequate for the maintenance performed; acceptance criteria were clear and

demonstrated operational readiness; test instrumentation was appropriate; tests were

performed as written in accordance with properly reviewed and approved procedures;

equipment was returned to its operational status following testing (temporary

modifications or jumpers required for test performance were properly removed after test

completion); and test documentation was properly evaluated. The inspectors evaluated

the activities against TSs, the UFSAR, 10 CFR Part 50 requirements, licensee

procedures, and various NRC generic communications to ensure that the test results

adequately ensured that the equipment met the licensing basis and design

requirements. In addition, the inspectors reviewed corrective action documents

associated with post maintenance tests to determine whether the licensee was

identifying problems and entering them in the CAP and that the problems were being

corrected commensurate with their importance to safety. Documents reviewed are listed

in the Attachment.

14

Enclosure

This inspection constituted four post maintenance testing samples as defined in

IP 71111.19-05.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

.1

Surveillance Testing

a.

Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

Unit 1 Train A Diesel Generator Routine Monthly Surveillance;

Unit 1 Train B Auxiliary Feedwater Pump Monthly Surveillance; and

Unit 1 Train B CS Valve Stroke Test 1BOSR 0.5-2.CS.1-2.

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

did preconditioning occur;

were the effects of the testing adequately addressed by control room personnel or

engineers prior to the commencement of the testing;

were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented;

as left setpoints were within required ranges; and the calibration frequency were

in accordance with TSs, the UFSAR, procedures, and applicable commitments;

measuring and test equipment calibration was current;

test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other applicable

procedures; jumpers and lifted leads were controlled and restored where used;

test data and results were accurate, complete, within limits, and valid;

test equipment was removed after testing;

where applicable for inservice testing (IST) activities, testing was performed in

accordance with the applicable version of Section XI of the American Society of

Mechnical Engineers (ASME) Code, and reference values were consistent with

the system design basis;

where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was declared

inoperable;

where applicable for safety-related instrument control surveillance tests, reference

setting data were accurately incorporated in the test procedure;

15

Enclosure

where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

equipment was returned to a position or status required to support the

performance of its safety functions; and

all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment.

This inspection constituted two routine surveillance testing samples and one IST sample

as defined in IP 71111.22, Sections -02 and -05.

b.

Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System Evaluation (71114.02)

.1

Alert and Notification System Evaluation

a.

Inspection Scope

The inspectors reviewed documents and conducted discussions with Emergency

Preparedness (EP) staff and management regarding the operation, maintenance, and

periodic testing of the Alert and Notification System (ANS) in the Byron Station's plume

pathway Emergency Planning Zone. The inspectors reviewed monthly trend reports and

the daily and monthly operability records from August 2010 through May 2012.

Information gathered during document reviews and interviews was used to determine

whether the ANS equipment was maintained and tested in accordance with Emergency

Plan commitments and procedures. Documents reviewed are listed in the Attachment to

this report.

This ANS inspection constituted one sample as defined in IP 71114.02-05.

b.

Findings

No findings were identified.

1EP3 Emergency Response Organization Augmentation Testing (71114.03)

.1

Emergency Response Organization Augmentation Testing

a.

Inspection Scope

The inspectors reviewed and discussed with plant EP management and staff the

emergency plan commitments and procedures that addressed the primary and alternate

methods of initiating an Emergency Response Organization (ERO) activation to augment

16

Enclosure

the on shift ERO as well as the provisions for maintaining the stations ERO qualification

and team lists. The inspectors reviewed reports and a sample of corrective action

program records of unannounced off-hour augmentation tests and pager tests, which

were conducted between August 2010 and May 2012, to determine the adequacy of the

drill critiques and associated corrective actions. The inspectors also reviewed a sample

of the EP training records of approximately 18 ERO personnel who were assigned to key

and support positions, to determine the status of their training as it related to their

assigned ERO positions. Documents reviewed are listed in the Attachment.

This ERO augmentation testing inspection constituted one sample as defined in

IP 71114.03-05.

b.

Findings

No findings were identified.

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)

.1

Correction of Emergency Preparedness Weaknesses and Deficiencies

a.

Inspection Scope

The inspectors reviewed a sample of Nuclear Oversight (NOS) staffs 2011 and 2012

audits of the Byron Station's EP program to determine that the independent

assessments met the requirements of 10 CFR 50.54(t). The inspectors also reviewed

samples of corrective action program records associated with the 2011 biennial

exercise, as well as various EP drills conducted in 2011 and 2012, in order to determine

whether the licensee fulfilled drill commitments and to evaluate the licensees efforts to

identify and resolve identified issues. The inspectors reviewed a sample of EP items

and corrective actions related to the facilitys EP program and activities to determine

whether corrective actions were completed in accordance with the sites corrective

action program. Documents reviewed are listed in the Attachment.

This correction of EP weaknesses and deficiencies inspection constituted one sample as

defined in IP 71114.05-05.

b.

Findings

No findings were identified.

1EP6 Drill Evaluation (71114.06)

.1

Emergency Preparedness Drill Observation

a.

Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on

June 28, 2012, to identify any weaknesses and deficiencies in classification, notification,

and protective action recommendation development activities. The inspectors observed

emergency response operations in the simulator to determine whether the event

classification, notifications, and protective action recommendations were performed in

17

Enclosure

accordance with procedures. The inspectors also attended the licensee drill critique to

compare any inspector-observed weakness with those identified by the licensee staff in

order to evaluate the critique and to verify whether the licensee staff was properly

identifying weaknesses and entering them into the corrective action program. As part of

the inspection, the inspectors reviewed the drill package and other documents listed in

the Attachment to this report.

This emergency preparedness drill inspection constituted one sample as defined in

IP 71114.06-05.

b.

Findings

No findings were identified.

2.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

4OA1 Performance Indicator Verification (71151)

.1

Drill/Exercise Performance

a.

Inspection Scope

The inspectors sampled licensee submittals for the Drill and Exercise Performance

(DEP) Performance Indicator (PI) for the period from the third quarter 2011 through

first quarter 2012. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 6, were used. The

inspectors reviewed the licensees records associated with the PI to verify that the

licensee accurately reported the DEP indicator in accordance with relevant procedures

and the NEI guidance. Specifically, the inspectors reviewed licensee records and

processes including procedural guidance on assessing opportunities for the PI;

assessments of PI opportunities during pre-designated control room simulator training

sessions, performance during the 2011 biennial exercise, and performance during other

drills. Specific documents reviewed are listed in the Attachment.

This inspection constitutes one DEP sample as defined in IP 71151-05.

b.

Findings

No findings were identified.

.2

Emergency Response Organization Drill Participation

a.

Inspection Scope

The inspectors sampled licensee submittals for the ERO Drill Participation PI for the

period from the third quarter 2011 through first quarter 2012. To determine the accuracy

of the PI data reported during those periods, PI definitions and guidance contained in the

18

Enclosure

NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, were

used. The inspectors reviewed the licensees records associated with the PI to verify

that the licensee accurately reported the indicator in accordance with relevant

procedures and the NEI guidance. Specifically, the inspectors reviewed licensee

records and processes including procedural guidance on assessing opportunities for the

PI; performance during the 2011 biennial exercise and other drills; and revisions of the

roster of personnel assigned to key emergency response organization positions.

Specific documents reviewed are listed in the Attachment.

This inspection constitutes one ERO drill participation sample as defined in IP 71151-05.

b.

Findings

No findings were identified.

.3

Alert and Notification System

a.

Inspection Scope

The inspectors sampled licensee submittals for the ANS PI for the period from the third

quarter 2011 through first quarter 2012. To determine the accuracy of the PI data

reported during those periods, PI definitions and guidance contained in the NEI 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 6, were used. The

inspectors reviewed the licensees records associated with the PI to verify that the

licensee accurately reported the indicator in accordance with relevant procedures and

the NEI guidance. Specifically, the inspectors reviewed licensee records and processes

including procedural guidance on assessing opportunities for the PI and results of

periodic ANS operability tests. Specific documents reviewed are listed in the

Attachment.

This inspection constitutes one ANS sample as defined in IP 71151-05.

b.

Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

.1

Routine Review of Items Entered into the Corrective Action Program

a.

Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent-of-condition reviews, and previous occurrence reviews were proper and

19

Enclosure

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the attached List of Documents Reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b.

Findings

No findings were identified.

.2

Daily Corrective Action Program Reviews

a.

Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening

of items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b.

Findings

No findings were identified.

.3

Semi-Annual Trend Review

a.

Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue.

The inspectors review was focused on repetitive equipment issues, but also considered

the results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. The inspectors

review nominally considered the six month period of July 01 through March 31, 2012,

although some examples expanded beyond those dates where the scope of the trend

warranted.

As part of this inspection, the inspectors also reviewed issues that could be documented

outside the normal CAP such as in major equipment problem lists, repetitive and/or

rework maintenance lists, departmental problem/challenges lists, system health reports,

quality assurance audit/surveillance reports, self assessment reports, and Maintenance

Rule assessments. The inspectors compared and contrasted their results with the

results contained in the licensees CAP trending reports.

20

Enclosure

b.

Findings

One finding with two examples was identified. The examples are discussed below. Both

examples had the same cause and the same cross-cutting aspect.

(1) (Closed) Unresolved Item 05000454/2012002-02: Potential Under-Torque of Valve

1RC8042B

Introduction: The first of the two examples of a self-revealed finding of very low safety

significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, was identified when licensee

personnel failed to properly torque an RCS pressure boundary valve closed. The valve

closure bolts subsequently relaxed and internal bypass around a diaphragm occurred

resulting in a small RCS leak into containment.

Description: On March 11, 2012, the licensee reduced power on Unit 1 to perform

robotic inspections inside of containment. Based on the results of the inspections, the

licensee shut down Unit 1 and replaced valve 1RC8042B. URI 05000454/2012002-02

was open in NRC Inspection Report 05000454/2012002; 05000455/2012002 pending

the licensees completion of the rework evaluation and the inspectors review and follow

up of the evaluation. Subsequently, licensee personnel performed a root cause

evaluation and determined that procedure BMP 3100-13, Kerotest Globe Valve Repair,

failed to provide sufficient detail to ensure the proper torque value was selected.

For valve 1RC8042B, BMP 3100-13 required that the maintenance worker select the

required torque from a table which contained both stainless steel and carbon steel

values. During refueling outage B1R17, the maintenance crews repaired valve

1RC8042B along with 1RC8042D. As the valves contained stainless steel and carbon

steel sub-components, the maintenance crews requested their supervisors to provide

guidance as to which torque value to use. The supervisor for the crew repairing valve

1RC8042D selected the correct (higher) torque valve. The supervisor for the crew

repairing valve 1RC8042B selected the incorrect (lower) torque value.

Several months following restart after the refueling outage, valve 1RC8042B began

leaking into containment as the inadequate retention forces allowed reactor coolant to

flow around an internal diaphragm. This leakage resulted in erosion and corrosion of the

carbon steel yoke threads and eventually resulted in external valve leakage.

The reactor coolant leakage was small and did not raise the daily unidentified leak rate

calculations sufficiently to clearly indicate a problem. However, the leak slowly

increased containment airborne tritium levels. The increase in containment tritium levels

along with an occasional elevated RCS leak rate value eventually caused the licensee to

conclude that a small leak existed that needed to be evaluated. Subsequent to the

identification of the leak the licensee performed an assessment to determine if they

could have identified the leak sooner. The licensee determined the available information

was discounted and not well understood, which led to an unnecessary delay in

performing a down power to search for the leak. The inspectors agreed with the

licensees determination.

21

Enclosure

The inspectors reviewed the licensees root cause analysis of this self-revealed RCS

leak documented in IR 1339375. The inspectors performed their own assessment and

agreed with the licensees root cause determination of an inadequate maintenance

procedure instruction for Kerotest globe valve repairThe maintenance procedure was

not written explicitly to apply the torque value based on valve body material. Corrective

action included replacing the leaking valve upon identification. Additional corrective

actions included modifying the installation procedure to add clarity in the selection of the

proper torque value.

Analysis: The inspectors determined that the failure to have adequate work instructions

for a Kerotest Globe valve repair was a performance deficiency. The finding was

determined to be more than minor in accordance with IMC 0612, Appendix B, Issue

Screening, because it was associated with the Procedure Quality attribute of the

Initiating Events Cornerstone and adversely affected the cornerstone objective of limiting

the likelihood of those events that upset plant stability and challenge critical safety

functions during shutdown as well as power operations. Specifically, this issue increased

the risk of a small break loss of coolant accident.

The inspectors performed a Phase 1 SDP screening using IMC 0609, Attachment 4,

Table 4a, Characterization Worksheet for Initiating Events Cornerstone. The

inspectors answered No to the question Assuming worst case degradation, would the

finding result in exceeding the Tech Spec [Technical Specification] limit for any RCS

leakage or could the finding have likely affected other mitigation systems resulting in a

total loss of their safety function. Therefore, example one of this finding was

determined to be of very low safety significance (Green).

This example had a cross-cutting aspect in the Work Practices component of the Human

Performance cross-cutting area because licensee personnel failed to utilize human error

prevention techniques, such as using the correct procedural torqueing requirement

H.4(a).

Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures or drawings of a type appropriate to the

circumstances and shall include appropriate quantitative or qualitative acceptance

criteria for determining that important activities have been satisfactorily accomplished.

Licensee procedure BMP 3100-13, Revision 10, Kerotest Globe Valve Repair, was

written in accordance with 10 CFR Part 50, Appendix B and prescribed an activity

affecting quality. Step F.1 of procedure BMP 3100-13 required that the maintenance

workers select which torque value to use to reassemble the valve body.

Contrary to the above, as of March 14, 2012, the licensee failed to have an adequate

procedure for the Kerotest globe valve repair, an activity affecting quality, which included

appropriate quantitative or qualitative acceptance criteria for determining that important

activities have been satisfactorily accomplished. Specifically, procedure BMP 3100-13

did not contain the appropriate instructions for determining the torque value to use to

reassemble the valve body such that the valve leaked following restart. Because this

violation was of very low safety significance and because this issue was entered into the

22

Enclosure

licensees CAP as IR 133975, this violation is being treated as a NCV, consistent with

Section 2.3.2 of the NRC Enforcement Policy. The is the first example of the NCV.

(NCV 05000454/2012003-02; Failure to Have Instructions Appropriate to the

Circumstances)

URI 05000454/2010002-02 is closed.

(2) One Train of Containment Cooling System Inoperable Longer Than Allowed by

Technical Specifications Due to Inadequate Work Instructions

Introduction: The second of the two examples of a self-revealed finding of very low

safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, was identified when licensee

personnel failed to properly re-install a Reactor Containment Fan Cooler (RCFC) interior

access panel during the previous refueling outage.

Description: On March 29, 2012, the licensee was performing an inspection inside the

Unit 1 Train A RCFC when personnel identified an access hatch that was not properly

installed. The hatch was four feet by six feet and allowed air to bypass the safety-

related cooling coils.

The licensee determined that the cause of the hatch not being properly installed during

the previous refueling outage was an inadequate level of detail provided in the work

package. The work package only contained a general work instruction to remove interior

panels as necessary. In addition, the RCFC interior hatches did not contain any unique

identifiers. Safety-related drawings which were referenced in the work package and

might have assisted the workers did not contain any unique identifiers for the interior

hatches.

There are four RCFCs in each of the two containments at Byron. Two RCFCs are in

each of the two safety-related trains of containment cooling. The failure to properly

reinstall the access hatch affected the ability of the Unit 1 Train A RCFC to remove heat

from containment when using only the safety-related Essential Service Water (SX)

system. However, the A RCFC as well as the other RCFC in the train would still have

removed a significant amount of heat following an accident.

The licensees WO during the refueling outage referenced two safety-related drawings to

assist maintenance workers in the identification of the access hatches inside of the

RCFCs. The licensees cause determination team concluded that the drawings failed to

adequately identify the internal access hatches. This weakness combined with the lack

of detailed work instructions in the WO caused the failure of the workers to ensure that

all internal access hatches had been reinstalled following the required maintenance.

The inspectors reviewed the licensees cause determination, interviewed personnel, and

assessed other license documents and agreed with the conclusion. The licensee

entered this issue into the CAP as IR 1347450 and planned to modify the RCFC

maintenance procedures to add detail and tracking aids for the removal of interior

access panels prior to the next use of the procedures.

23

Enclosure

In addition, the licensee reinstalled the missing internal access hatch and inspected the

other RCFCs. No other access hatches were found to be uninstalled.

Analysis: The inspectors determined that the failure to have adequate work instructions

for the removal and reinstallation of the interior access hatches for the RCFCs was a

performance deficiency that required an evaluation using the SDP. The inspectors

concluded that this second example of a finding was more than minor in accordance with

Appendix B, Issue Screening, of IMC 0612, Power Reactor Inspection Reports,

because the finding was associated with the Configuration Control attribute of the Barrier

Integrity Cornerstone and adversely affected the cornerstone objective of providing

reasonable assurance that physical design barriers, including the containment, protect

the public from radionuclide releases caused by accidents and events. Specifically, this

issue decreased the availability and reliability of the RCFCs for use during a design

basis accident.

The inspectors completed a significance determination of this issue using IMC 0609,

Appendix A, Significance Determination of Reactor Inspection Findings for At Power

Situations, Phase 1 Screening. The inspectors determined that because the finding did

not represent a degradation of the radiological barrier function, did not represent a

degradation of the barrier function of the control room, did not represent an actual open

pathway in the physical integrity of reactor containment, and did not involve an actual

reduction in the function of hydrogen igniters in the reactor containment, the issue was of

very low safety significance (Green). In addition, the inspectors contacted the Region III

Senior Risk Analysts (SRAs) and requested that a Phase 2 determination be performed.

The SRA also determined that the issue was of very low safety significance (Green).

This finding had a cross-cutting aspect in the Work Practices component of the Human

Performance cross-cutting area because licensee personnel failed to utilize human error

prevention techniques, such as documenting which internal hatches had been removed

for maintenance so as to ensure that all hatches were reinstalled at the conclusion of the

refueling outage H.4(a).

Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, required, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures or drawings of a type appropriate to the

circumstances and shall include appropriate quantitative or qualitative acceptance

criteria for determining that important activities have been satisfactorily accomplished.

Licensee work instructions and safety-related drawings M-1254, Revision F, RCFC

Partial Plan, and M-1250 Revision V, RCFC Partial Plan, were developed in

accordance with 10 CFR Part 50, Appendix B, to accomplish an activity affecting quality.

Contrary to the above, as of March 29, 2012, the licensees work instructions for the

repair of RCFCs, an activity affecting quality, failed to have instructions and drawings of

a type appropriate to the circumstances. Specifically, drawings M-1254, Revision F; and

M-1250, Revision V, failed to adequately identify the internal hatches necessary to

accomplish repair activities. Because this violation was of very low safety significance

and because this issue was entered into the licensees CAP as IR 1347450, this second

example of a violation is being treated as a NCV, consistent with Section 2.3.2 of the

NRC Enforcement Policy. This is the second example of the NCV.

(NCV 05000454/2012002-02; Failure to Have Instructions Appropriate to the

Circumstances)

24

Enclosure

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

.1

(Closed) Licensee Event Report 05000454/2012002-00: One Train of Containment

Cooling System Inoperable Longer Than Allowed by Technical Specifications Due to

Inadequate Work Instructions

The licensee submitted this Licensee Event Report (LER) on May 29, 2012, as an event

that could have prevented the fulfillment of a safety system. The inspectors performed

follow up on the LER and documented the results of the followup in Paragraph 4OA2 as

the second example of a self-revealed example of an NCV.

This LER is closed to NCV 05000454/2012003-02 above.

4OA5 Other Activities

.1

Pre-operational Testing of an Independent Spent Fuel Storage Facility Installation at

Operating Plants (60854.1)

a.

Inspection Scope

Dry Run Activities

The licensee performed pre-operational dry run activities to fulfill the requirements of the

Certificate of Compliance (CoC). Specifically, the licensee performed forced helium

dehydration and supplemental cooling system pre-operational testing and training

exercises prior to the second Independent Spent Fuel Storage Facility Installation

(ISFSI) campaign. These operations had not been performed prior to the first loading

campaign as the first campaigns spent nuclear fuel characteristics did not necessitate

use of the equipment. The inspectors were on site to observe dry run activities on

February 24, 2012, and March 16, 2012.

The inspectors reviewed loading procedures to ensure that they contained commitments

and requirements specified in the license, the TS, the Final Safety Analysis Report

(FSAR), and Title 10 of the Code of Federal Regulations (CFR) Part 72.

b.

Findings

No violations of NRC requirements were identified.

.2

Review of 10 CFR 72.212(b) Evaluations at Operating Plants (60856.1)

a.

Inspection Scope

Review of Site Characteristics Against Safety Analysis Report and Safety Evaluation

Report

The inspectors evaluated the licensees compliance with the requirements of

10 CFR 72.212 and 10 CFR 72.48. The inspection consisted of interviews with

cognizant personnel and review of documentation.

During the licensees initial loading campaign Holtec HI-STORM 100 CoC 1014,

Amendment 3, was used under the general license process; however, for the licensees

25

Enclosure

second campaign HI-STORM 100 CoC 1014, Amendment 7 was used. A written

evaluation was required per 10 CFR 72.212(b)(5), prior to use, to establish that the

conditions of the CoC have been met. Byron Nuclear Power Station, Units 1 and 2,

10 CFR 72.212 Evaluation Report, Revision 3, dated February 2012, documented the

evaluations performed by the licensee.

The inspectors reviewed and assessed the licensees 10 CFR 72.212 Evaluation Report.

The inspectors determined whether applicable reactor site parameters, such as fire and

explosions, tornadoes, wind-generated missile impacts, seismic qualifications, lightning,

flooding and temperature, had been evaluated for acceptability with bounding values

specified in the Holtec HI-STORM 100 FSAR and associated analyses.

b.

Findings

No violations of NRC requirements were identified.

.2

Operation of an Independent Spent Fuel Storage Facility Installation at Operating Plants

(60855.1)

a.

Inspection Scope

The inspectors observed and evaluated the licensees loading of the second canister

during the licensees second ISFSI loading campaign to verify compliance with the CoC,

TS, regulations, and associated procedures.

The inspectors observed the heavy load movement of the transfer cask (HI-TRAC) from

the spent fuel pool to the dry decontamination pit inside the Fuel Handling Building. The

inspectors also observed multi-purpose canister (MPC) processing operations, including

decontamination and surveying, MPC welding, non-destructive weld examinations, MPC

draining, forced helium dehydration, helium backfilling, and the use of the supplemental

cooling system.

During performance of these activities, the inspectors evaluated the licensee staffs

familiarity with procedures, supervisory oversight, and communication and coordination

between the groups involved. The inspectors reviewed loading and monitoring

procedures and evaluated the licensees adherence to these procedures.

The inspectors performed tours of the ISFSI pad to assess the material condition of the

pad and the loaded storage casks (HI-STORM). The inspectors reviewed

documentation of the licensees ISFSI radiation monitoring program. Additionally, the

inspectors performed independent radiation surveys around the ISFSI pad and loaded

HI-STORM casks. The inspectors reviewed the contamination and radiation levels from

a previously loaded MPC during the campaign to determine whether they were below

the regulatory limits. The inspectors also reviewed the As-Low-As-Is-Reasonably-

Achievable (ALARA) Work-In-Progress Review for the loading of the previous cask to

determine the adequacy of the licensees radiological controls and to ensure that

radiation worker doses were ALARA and that project dose goals could be achieved.

The inspectors attended licensee briefings to assess the licensees ability to identify

critical steps of the evolution, potential failure scenarios, and tools to prevent errors.

26

Enclosure

The inspectors reviewed the licensees program associated with fuel characterization

and selection for storage. The inspectors reviewed cask fuel selection packages to

verify that the licensee was loading fuel in accordance with the CoC TS. The licensee

did not plan to load any damaged fuel assemblies during this campaign.

The inspectors reviewed issue reports and the associated follow-up actions that were

generated since the licensees last loading campaign. The inspectors reviewed the

licensees 10 CFR 72.48 screenings.

b.

Findings

No findings were identified.

4OA6 Management Meetings

.1

Exit Meeting Summary

On July 2, 2012, the inspectors presented the inspection results to Mr. T. Tulon, and

other members of the licensee staff.

The licensee acknowledged the issues presented. The inspectors confirmed that none

of the potential report input discussed was considered proprietary.

.2

Interim Exit Meetings

On April 13, 2012, the inspectors presented the inspection results of the ISFSI

inspection to members of the licensee management and staff. Licensee personnel

acknowledged the issues presented. The inspectors confirmed that none of the potential

report input discussed was considered proprietary. Proprietary material received during

the inspection was returned to the licensee.

On June 27, 2012, the inspectors presented inspection results of the licensed operator

examination security issue to Mr. S. Gackstetter and other members of the licensee

staff. No proprietary information was identified during the interim exit.

On June 30, 2012, the inspectors presented the inspection results of the Emergency

Preparedness Program inspection to members of licensee management and staff. No

proprietary information was identified during the interim exit.

4OA7 Licensee-Identified Violation

The following violation of very low significance (Green) or Severity Level IV was

identified by the licensee and is a violation of NRC requirements which meet the criteria

of Section VI of the NRC Enforcement Policy for being dispositioned as an NCV:

Title 10 CFR 55.49, Integrity of Examinations and Tests, requires, in part,

that the licensee shall not engage in activities that compromises the integrity

of any application, test, or examination required by 10 CFR Part 55. Contrary

to the above, on March 30, 2012, at the Clinton Power Station, the licensee

identified activities that compromised the integrity of the examinations required

by 10 CFR Part 55. Specifically, the licensee identified that the control room

simulators plant process computer model was saving sequence of events files

27

Enclosure

on a routine basis, which contained examination materials related to

examinations required by 10 CFR Part 55. A licensee investigation determined

that the same condition existed at other Midwest Exelon sites, including the

Byron Station. The licensee determined that some of the files contained

examination materials related to examinations required by 10 CFR Part 55.

The integrity of a test or examination is considered compromised if any activity,

regardless of intent, affected, or, but for detection, would have affected the

equitable and consistent administration of the test or examination.

Although the examination materials were available for scrutiny by unauthorized

personnel, (compromised), the licensee was able to demonstrate that the files

were not readily viewable, required interpretation and additional administrative

controls were in place that would likely inhibit access to, and reconstruction of

simulator events. No individuals had an unfair advantage in taking any

NRC-related examinations. Therefore, this finding was of very low safety

significance (Green). This issue was documented in the facilitys corrective

action program as IR 1350674. Corrective actions for this issue included revising

the simulators software to delete data from the sequence of events files being

generated by the simulator upon reset of the simulator.

ATTACHMENT: SUPPLEMENTAL INFORMATION

1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

B. Youman, Plant Manager

D. Gudger, Regulatory Assurance Manager

J. Langan, Regulatory Assurance Licensing Engineer

B. Spahr, Maintenance Director

D. Drawbaugh, Emergency Preparedness Manager

B. Kartheiser, Emergency Preparedness Coordinator

S. Kerr, Work Management Manager

D. Spitizer, Regulatory Assurance

T. Eliakis, ISFSI Project Manager

T. Hulbert, Regulatory Assurance Assistant

S. Briggs, Operations Director

Nuclear Regulatory Commission

E. Duncan, Chief, Branch 3, Division of Reactor Projects

2

Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened 05000454/2012003-01

NCV

Leakage Detection Trough with Large Accumulation of Boric

Acid Identified (Section 1R15)05000454/2012003-02

NCV

Failure to Have Instructions Appropriate to the

Circumstances (Section 4OA2)

Closed 05000454/2012002-02

URI

Potential Under-Torque of Valve 1RC8042B (Section 4OA2)05000454/2012002-03

URI

Boric Acid Accumulation Identified in Leakage Detection

Trough (Section 1R15)05000454/2012003-01

NCV

Leakage Detection Trough with Large Accumulation of Boric

Acid Identified (Section 1R15)05000454/2012003-02

NCV

Failure to Have Instructions Appropriate to the

Circumstances (Section 4OA2)

05000454/2012-002-00

LER

One Train of Containment Cooling System Inoperable Longer

Than Allowed by Technical Specifications Due to Inadequate

Work Instructions

Discussed

None

3

Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 1R01: Adverse Weather Protection (Quarterly)

- IR 1360541; Not Enough Charcoal Filters on Hand for Summer Readiness, April 30, 2012

- IR 1360553; Byron Summer Readiness Maintenance Review Results, April 30, 2012

- IR 1361366; Summer Readiness Contingency Work Packages Not Ready, April 26, 2012

- IR 1365484; 2012 Transformer Replacement Summer Readiness Exceptions, May 11, 2012

- WC-AA-107; Summer Seasonal Readiness, June 1 through August 31, 2012

- Plant System Readiness Review; System AP, Revision 9

- IR 1360510; Summer Readiness Contingency WO Review Gaps, April 28, 2012

- System Engineer System Summary Sheet/Recommendation Form

- Certification of 2012 Summer Readiness, May 15, 2012

- OP-AA-108-107-1001; Station Response to Grid Capacity Conditions, Revision 4

- OP-AA-108-107-1002; Interface Procedure Between ComEd/PRCO and Exelon Generation

(Nuclear/Power) for Transmission Operations, Revision 6

- WC-AA-107; Seasonal Readiness, Revision 9

Section 1R05: Fire Protection (Quarterly)

- FZ 5.4-2; Auxiliary Building 451-0 Elevation, Division 22 Miscellaneous Electrical Equipment

and Battery Room, Rev.0

- A-269; Drawing, Auxiliary Building Main Floor Area 4, Rev. AP

- S-1328; Drawing, Auxiliary Building Roof Framing Plan Area 4, Rev. AJ

Corrective Action Documents As a Result of NRC Inspection

- IR 1367933; NRC Observed Fire Drill, May 17, 2012

Section 1R06: Flooding

- 0BOSR WF-SA1; Auxiliary Building Floor Drain Semi-Annual Surveillance, Rev. 6

- A-223; Auxiliary Building Upper Basement, Floor Plan EL. 364-0 Area 6, Rev. BM

Corrective Action Documents As a Result of NRC Inspection

- IR 1362200; 0BOSR WF-SA1 Acceptance Criteria Needs Engineering Calc., May 3, 2012

Section 1R12: Maintenance Effectiveness (Quarterly)

- IR 1349587; Investigate Unit 1 & 2 CW Flume Temperature Differences, April 3, 2012

- IR 1352076; 2E NDCT Riser Pipe Rupture, April 10, 2012

- IR 1353164; Leak at U1 NDCT 1B Riser at Clamp, April 12, 2012

- IR 1357297; U2 NDCT Cold Basin Water Lapping Out West Door Area, April 23, 2012

- IR 1358209; U2 NDCT Cold Basin Water Wave Lapping Out West Door Area, April 25, 2012

4

Attachment

- IR 1361821; Rapid Rise in U1 NDCT Debris Fence Delta Level, May 3, 2012

- IR 1363647; U1 NDCT 1B Riser Leak, May 7, 2012

- IR 1363702; Recommend Temporary Set Point Change, May 7, 2012

- IR 1364085; What is the Plan for CW Blowdown, May 8, 2012

- IR 1364405; Safety Concerns with the Operation of CW PP Intakes, May 9, 2012

- IR 1366347; U1 NDCT Debris Fence Level at 1.5 Feet, May 14, 2012

- IR 1366348; U2 NDCT Debris Fence Level at 1.5 Feet, May 14, 2012

- IR 1366507; Adverse Trend Identified with Performance of the NDCT, May 15, 2012

- IR 1367711; Vendor Damaged 0C CW M/U Seal Injection Pipe Coupling, May 17, 2012

- IR 1369171; Improper Grouting of 0C CW M/U Base Plate to Foundation, May 21, 2012

- IR 1371687; Fill Damage to 2F NDCT Riser Pipe, May 29, 2012

- IR 1373743; Excessive CW Material in U1 Debris Fence, June 2, 2012

- IR 1373797; 1B CW Riser Piping Significantly Degraded, June 3, 2012

- IR 1374981; U2 CW Water Outfall Screen High Delta Level, June 6, 2012

- IR 1374981; U1 CW Water Outfall Screen High Delta Level, June 6, 2012

- IR 1379221; U2 NDCT Outfall Screen High Delta Level June 18, 2012

- IR 1380630; 1F NDCT Riser Leak, June 21, 2012

- IR 1381098; U2 CW Box DP Pegged High, Tube Sheet Fouling, June 22, 2012

- IR 1381376; Falling Concrete on North Side of U2 NDCT, June 24

- IR 1383022; U2 NDCT 2E Riser Leaking, June 28, 2012

- IR 1383848; 2E Riser Leakage has Worsened, June 30, 2012

Section 1R13: Maintenance Risk Assessments & Emergent Work control

- IR 1358649; DSA - Work Not Performed Due to OLR Not Evaluated, April 26, 2012

- IR 1378982; 2B SAC Tripped on Low Bearing Oil Pressure, Revision 21

- Online Risk Evaluation; Week of June 11, 2012, Revisions 0 through 6

- Online Risk Evaluation; Week of June 18, 2012, Revisions 0 through 9

Section 1R15: Operability Evaluations (Quarterly)

- BY-MISC-017; Risk Profile Improvements for Single Phase Conditions, Revision 0

- EC 374391 010; OP Eval 09-001, DOST-DG Vent Lines Crimp Vs Break, May 21, 2012

- EC 383599 003; BYR OP Eval 11-005, Turbine Building HELB Input Errors, October 05, 2011

- EC 387590 002; Potential Design Vulnerability in Switchyard Single Open Phase Detection,

May 18, 2012

- EC 389402 000; OP Eval 12-005, HELB Load Not Considered in Structural Calculation,

June 05, 2012

- 1BOSR Z.5.b.1-1; Unit One Containment Loose Debris Inspection, Rev. 15

- OP-AA-108-108-1001; Drywell / Containment Closeout, Rev. 1

- A-336; Drawing, Containment Building Basement Floor Plan Area 4, Rev. Q

- A-335; Drawing, Containment Building Basement Floor Plan Area 3, Rev. T

- A-334; Drawing, Containment Building Basement Floor Plan Area 2, Rev. U

- A-333; Drawing, Containment Building Basement Floor Plan Area 1, Rev. W

- IR 1378106; Potential Impact from Reduced SG PORV Relief Capacity, June 14, 2012

- IR 1359137; Probable Reduced SG PORV Capacity for Original Valves, April 26, 2012

- EC 367065; Op Eval 07-007, Main Steam PORV Steam Relief Capacity, Rev. 4

5

Attachment

Corrective Action Documents As a Result of NRC Inspection

- IR 1339957; 1PS9365B Has Leak From Either Packing Leak or Bonnet, March 12, 2012

- IR 1341380; NRC Identified Boric Acid Covering Floor, March 15, 2012

- IR 1382405; NRC (B1M03) Unit 1 IMB Drain Covered with Boric Acid, June 27, 2012

Section 1R19: Post Maintenance Testing (Quarterly)

- IR 1370582; PMT Run Required for B AF PP TS-1 Opening for Battery Test, May 25, 2012

- IR 1370734; Evaluate Test Frequency for 2AF01EA-B, May 25, 2012

- 2BOSR 0.5-2.SX.3-3; Unit 2 Position Indication Test of 2SX004, 2SX010, 2SX011, 2SX033,

2SX034, and 2SX136

- WO 1423904; OPS PMT: Stroke 2SX010 Using BOP SX-T3, May 23, 2012

- 1BOSR 6.3.5-19; Unit 1 Main Steam System Containment Isolation Valve Stroke Test, Rev. 4

- 1BOSR MS-R1; Unit 1 Manual Stroke of the S/G PORVs 18 Month Surveillance, Rev. 5

- 2BOSR 0.5-3.AF.1-2; Unit 2 ASME Surveillance Requirements for the B Train Auxiliary

Feedwater SX Supply Valves, Rev. 10

- 0BOSR 0.5-3.SX.1-3; Unit 0 Test of the Unit 0 Component Cooling Water Heat Exchangers

Essential Service Water Throttle and Outlet Isolation Valves, Rev. 3

Section 1R22: Surveillance Testing (Quarterly)

- 1359972; 1B AF STT and PIT Procedures Dont Work Together, April 28, 2012

- 1325427; Unit 1 & 2 AF013s Stem Lube Conflicts with C&T Level 4, February 10, 2012

- 1197504; 1AF013D Local Indication Shows 10% Open with Valve Closed, April 4, 2011

- 1197493; 1AF013A Local Indication Shows 70% Open with Valve Closed, April 4, 2012

- 1BOSR 0.5-2.AF.1-2; Unit 1 1AF013 E/F/G/H Stroke Test, Rev. 5

- 1BOSR 7.5.4-2; Unit 1 Diesel Driven Auxiliary Feedwater Pump Monthly Surveillance, Rev. 14

- 1BOSR 5.5.8.AF.5-2b; Unit 1 Group B Inservice Testing Requirements for Diesel Driven

Auxiliary Feedwater Pump 1AF01PB, Rev. 1

- 1BOSR 8.1.2-1; Unit 1 1A Diesel Generator Operability Surveillance, Rev. 20

- IR 1312027; 1A DG Lower JW Cooler Leaking from End Cover Bolting, January 11, 2012

- IR 1301853; 1A DG R-9 Fuel Injector Tell Tale Drain Leaking, December 31, 2011

- IR 1300657; 1A DG JW Heater Not Controlling Temperature in Automatic, December 10, 2011

- IR 1227745; 1A DG Possible Water in Crank Case, June 12, 2011

- IR 1212228; 1A DG Generic Letter 89-13 Inspection Relief Requested, May 5, 2011

- IR 1028474; 1A DG JW Leak at R-9 Supply Flange - 30 Drops Per Minute, February 10, 2010

1EP2 Alert and Notification (ANS) Evaluation

- Offsite Emergency Plan Alert and Notification System Addendum for Byron Station;

November 2009

- EP-AA-1000; Exelon Nuclear Standardized Radiological Emergency Plan Section E;

Revision 21

- EP-AA-1002; Exelon Nuclear Radiological Emergency Plan Annex for Byron Station,

Section 4; Revision 29

- Byron Station Warning System Annual Maintenance & Operational Reports; June 15, 2011

- Byron Station Monthly Siren Availability Reports; August 2010 - June 2012

- Exelon Semi-Annual Siren Reports; July 2010 and December 31, 2011

- IR 1254150; Semi-Annual Review of 1st Half of 2011 Siren Data; August 22, 2011

- IR 1245065; Single Siren Failures; July 28, 2011

6

Attachment

1EP3 Emergency Response Organization Augmentation Testing

- EP-AA-1000; Exelon Nuclear Standardized Radiological Emergency Plan, Sections B and N;

Revision 21

- EP-AA-1002; Exelon Nuclear Radiological Emergency Plan Annex for Byron Station,

Section 2; Revision 29

- EP-AA-112-100-F-06; Midwest ERO Notification or Augmentation; Revision O

- TQ-AA-113; ERO Training and Qualification; Revision 19

- Quarterly Unannounced Off-Hours Call-In Augmentation Drill Results; May 2010 - May 2012

- Emergency Response Organization Call-Out Roster; May 18, 2012

- IR 1367175; May 2021 Unannounced Off-Hours Call-In Augmentation Drill 2 Duty ERO Did

Not Respond; May 16, 2012

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies

- EP-AA-120; Section 4.4, Review of Actual Events; Revision 14

- EP-AA-120-1001; 10 CFR 50.54(q) Change Evaluation; Revision 7

- EP-AA-121; Emergency Response Facilities and Equipment Readiness; Revision 11

- EP-AA-121-F-02; Byron Station Equipment Matrix; Revision 1

- BRP 5800-3; Area Radiation Monitoring System Alert/High Alarm Setpoints; Revision 25

- BRP 5820-12; Response to Area and Process Radiation Monitor LCOARS or Out-of-Service

Conditions; Revision 29

- BRP 5820-14; Process Radiation Monitoring System Alert/High Alarm Setpoints; Revision 44

- LS-AA-126-1005; Check-In-Self-Assessment Emergency Preparedness Report; April 25, 2012

- NOSA-BYR-12-03; Emergency Preparedness Audit Report; April 27, 2012

- NOSA-BYR-11-03; Emergency Preparedness Audit Report; April 15, 2011

- 0BOSR CQ-1; Test of the Employee Alarm System; Revision 6

- WC-AA-106; Work Screening and Processing; Revision 19

- Monday Muster Meeting EP Weekly Newsletter; June 25, 2012

- Byron Station January 30, 2012, Unusual Event Report; February 27, 2012

- Byron Station February 28, 2012, Unusual Event Report; March 26, 2012

- List of Inaudible Public Address System Locations and Status; May 29, 2012

- Biennial Letters of Agreement; October 11, 2011

- Evacuation Time Estimates for the Byron Station; December 2003

- UFSAR, Table 11.5-1; Airborne Process and Effluent Monitors; Revision 7

- IR 1358442; NOS ID-Errors In Mailing List For EP Information Brochure; April 25, 2012

- IR 1353670; TSC HVAC Equipment Vulnerability; April 13, 2012

- IR 1320571; Byron Fire Department Response to Unusual Event; January 31, 2012

- IR 1319175; Additional Areas Are Deficient on the Quarterly Public Address Test;

January 27, 2012

- IR 1300315-10; NOS Objective Evidence Report; EP Offsite Agency Interface

- IR 1269312; MET Tower Wind Direction Erratic; September 28, 2011

- IR 1267919; Request For Additional Clarification For EAL HU6; September 25, 2011

- IR 1247327; Exercise-OSC Failed Demonstration Criteria; August 3, 2011

- IR 1237774; Pre-Exercise TSC Failed Demonstration Criteria; July 8, 2011

- IR 1130872-10; NOS Objective Evidence Report; EP Offsite Agency Interface

4OA1 Performance Indicator Verification

- LS-AA-2110; Monthly Data Elements for NRC ERO Drill Participation;

September 2011 - March 2012

7

Attachment

- LS-AA-2120; Monthly Data Elements for NRC Drill/Exercise Performance;

July 2011 - March 2012

- LS-AA-2130; Monthly Data Elements for NRC Alert and Notification System Reliability;

July 2011 - March 2012

- Byron ANS Test Reports; July 2011 - March 2012

- IR 1304945; Training-DEP Failures for LORT Annual Exam Cycle; December 20, 2011

Section 4OA2: Identification and Resolution of Problems (71152)

- IR 1071667; Non-Conservative Degraded Voltage Time Delay With a Due Date of

September 13, 2013, May 20, 2010

- IR 1237140; Non-Conservative Input to HELB Analysis, July 6, 2011

- IR 1275710; Braidwood NCV - Non-Conservative EQ Classification in HELB,

October 12, 2011

- IR 1288474; Potential Green NCV - Classification of EQ Zones from HELB,

November 8, 2011

- IR 1354220; Need to Replace Primary Rosettes on S.O#01Y017B4-7, April 16, 2012

- IR 1350467; Mass and Energy Analysis Could Impact UHS Temp and Inventory Limits,

April 8, 2012

- IR 1359137; Probable Reduced SG PORV Capacity for Original Valves, April 26, 2012

- IR 1359198; DG Full Load Reject Testing, April 26, 2012

- IR 1359686; Chillers in TSC Computer Room Not Providing Adequate Cooling, April 27, 2012

- IR 1360458; Recommended Work Not Performed Prior to RTS, April 30, 2012

- IR 1361284; 1CS001B STT Acceptance Criteria Data Sheet Not Revised, May 02, 2012

- IR 1361939; Chart Recorder Not Logged into Temporary Change Tracking Log, May 03, 2012

- IR 1362451; 2TO081 Found Closed, Valve Should Have Been Opened, May 04, 2012

Section 40A5: Other Activities

- ALARA Work-In-Progress Review; 2012 Dry Cask Storage Campaign; March 29, 2012

- BFP FH-20; Operation of Fuel Handling Building Crane; Revision 26

- BFP FH-35; Contingency Fuel Handling Building Crane Operations; Revision 0

- BFP FH-64; Transporter Operations; Revision 7

- BFP FH-65; Spent Fuel Cask Site Transportation; Revision 10

- BFP FH-68; HI-TRAC Preparation; Revision 3

- BFP FH-69; HI-TRAC Movement within the Fuel Building; Revision 10

- BFP FH-70; HI-TRAC Loading Operations; Revision 9

- BFP FH-71; MPC Processing; Revision 12, 13, 14 and 15

- BFP FH-72; HI-STORM Processing; Revision 2

- BFP FH-79; MPC Alternate Cooling; Revision 4

- BFP FH-83; Spent Fuel Cask Contingency Actions; Revision; Revision 3

- BHP 4200-101; General Inspection of Fuel Handling Building Overhead Crane 0HC03G;

Revision 0

- NF-AP-622; Fuel Selection and Documentation for Dry Cask Storage; Revision 4

- OP-AA-201-004; Fire Prevention for Hot Work; Revision 9

- PI-CNSTR-T-OP-220; Closure Welding of Holtec Multi-Purpose Canisters at Exelon Facilities;

Revision 2

- RP-BY-304-1001; HI-TRAC Radiation Survey; Revision 2

- RP-BY-304-1002; HI-STORM Radiation Survey; Revision 3

- 0BDCSR 3.1.1.1; Multi-Purpose Canister (MPC) Integrity Verification; Revision 1

- 0BDCSR 3.1.3.1; Multi-Purpose Canister (MPC) Cavity Pressure Verification; Revision 1

8

Attachment

- 0BDCSR 3.1.4.1; Supplemental Cooling System (SCS) Operability Verification; Revision 3

- 0BDCSR 3.2.2.1; MPC Surface Contamination Verification; Revision 1

- 0BDCSR 3.3.1.1; Wet Cask Pit/MPC Boron Concentration Verification; Revision 1

- Byron Dry Cask Storage Training Matrix, Revision 1

- Byron ISFSI Lessons Learned Readiness Brief; February 10, 2012

- Byron Nuclear Power Station, Units 1 and 2; 10 CFR 72.212 Evaluation Report; Revision 3

- BYR11-197; Fuel Selection Package BYR-0016 for MPC0187; Revision 0

- BYR11-198; Fuel Selection Package BYR-0017 for MPC0186; Revision 0

- BYR11-199; Fuel Selection Package BYR-0018 for MPC0183; Revision 0

- Forced Helium Dehydration System [Training], Revision 00

- Fuel Move Sheet Package 2012 Dry Cask - MPC0187; February 27, 2012

- Holtec Letter to Byron; FHD Dew Point Operability; March 22, 2012

- Holtec Report No. HI-2084113; Dose versus Distance from a HI-STORM 100S Version B

Containing the MPC-32 for Byron/Braidwood; Revision 7

- One Month Readiness Review, Byron Nuclear Station Dry Cask Storage 2012 Campaign;

February 6, 2012

- IR 01319213; Unclear Scope of Site Reactor Engineering Review for Fuel Selection

Packages; January 28, 2012

- IR 01319283; Dry Cask Storage Project Review for Process Alignment; January 28, 2012

- IR 01324010; HI-TRAC Trunnions Bound in HI-TRAC; February 7, 2012

- IR 01334080; Fuel Handling Building Crane 0HC03G Scoreboard Weight Readout;

February 29, 2012

- IR 01337745; Dry Cask Storage - Review of Holtec Information Bulletin 54 FHD Wiring;

March 7, 2012

- IR 01339936; DCS - MPC Number 187 Discovered to be Oblong; March 12, 2012

- IR 01342065; NRC Dry Cask Storage Results; March 16, 2012

- IR 01344618; Helium Supply Flow to FHD Skid Blocked; March 23, 2012

- IR 01345214; DCS Surveillance Change Needed for 0BDCSR 3.1.4.1; March 24, 2012

- IR 01349932; NRC IDD - DCS - Critique of Welding Operations; April 4, 2012

- IR 01350170; Dry Cask Process Recommendation - MPC Blowdown Phase; April 4, 2012

- IR 01350552; Procedure Documentation Incomplete; April 5, 2012

- IR 01350663; Procedure Revision Required - 0BDCSR 3.1.1.1; April 5, 2012

- IR 01350712; Vendor Welding Procedure Revision Requested; April 5, 2012

- IR 01350933; NRC Identified Bags of DAW Not Stored in Covered Carts; April 6, 2012

- WO 01322216; Fuel Handling Building Overhead Bridge Crane Electrical Inspection;

June 30, 2011

- WO 01323391, Fuel Handling Building Crane Mechanical Inspection; June 8, 2011

- WO 01437840; MPC Lift Cleat Inspection; February 8, 2012

- WO 01438159; Lift Yoke Inspection; February 6, 2012

- WO 01500091; Mechanical [Fuel Handling Building] Crane Inspection; January 18, 2012

- 72.48-032; Wet Cask Pit/MPC Boron Concentration Verification; September 14, 2011

- 72.48-033; MPC Surface Contamination Verification; September 14, 2011

- 72.48-038; Mating Device Modification; December 15, 2011

- 72.48-039; OU-AA-630; December 30, 2011

- 72.48-045; 72.212 Evaluation Changes for FSAR Revision 9 and CoC Amendment 7

9

Attachment

LIST OF ACRONYMNS USED

ADAMS

Agencywide Document Access and Management System

ALARA

As-Low-As-Is-Reasonably-Achievable

ANS

Alert and Notification System

ASME

American Society of Mechanical Engineers

CAP

Corrective Action Program

CFR

Code of Federal Regulations

CoC

Certificate of Compliance

CS

Containment Spray

DEP

Drill and Exercise Performance

EP

Emergency Preparedness

ERO

Emergency Response Organization

FSAR

Final Safety Analysis Report

HELB

High Energy Line Break

HI-STORM

Storage Cask

HI-TRAC

Transfer Cask

IMC

Inspection Manual Chapter

I/O

Input/Output

IP

Inspection Procedure

IR

Inspection Report

IR

Issue Report

ISFSI

Independent Spent Fuel Storage Installation

IST

Inservice Testing

LER

Licensee Event Report

MCID

Materials Control, ISFSI, and Decommissioning

MPC

Multi-Purpose Canister

NCV

Non-Cited Violation

NEi

Nuclear Energy Institute

NRC

U.S. Nuclear Regulatory Commission

PARS

Publicly Available Records System

PI

Performance Indicator

RCFC

Reactor Containment Fan Cooler

RCS

Reactor Coolant System

RH

Residual Heat Removal

RP

Radiation Protection

SDP

Significance Determination Process

SER

Safety Evaluation Report

SSC

Structure, System, and Component

SX

Essential Service Water

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

WO

Work Order

M. Pacilio

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Eric R. Duncan, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 50-454; 50-455; and 07200068

License Nos. NPF-37 and NPF-66

Enclosure:

Inspection Report No. 05000454/2012003 and 05000455/2012003;

07200068/2012001

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

DISTRIBUTION:

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To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE

RIII

RIII

NAME

Duncan

Ng

DATE

08/07/12

08/03/12

OFFICIAL RECORD COPY

Letter to M. Pacilio from E. Duncan dated August 7, 2012.

SUBJECT:

BYRON STATION, UNITS 1 AND 2, NRC INTEGRATED INSPECTION

REPORT 05000454/2012003; 05000455/2012003; 07200068/2012001

DISTRIBUTION:

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