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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES  
                                NUCLEAR REGULATORY COMMISSION
NUCLEAR REGULATORY COMMISSION  
                                                REGION II
REGION II  
                            245 PEACHTREE CENTER AVENUE NE, SUITE 1200
245 PEACHTREE CENTER AVENUE NE, SUITE 1200  
                                      ATLANTA, GEORGIA 30303-1257
ATLANTA, GEORGIA 30303-1257  
                                          February 7, 2014
Mr. Joseph W. Shea
February 7, 2014  
Vice President, Nuclear Licensing
Tennessee Valley Authority
1101 Market Street, LP 3D-C
Chattanooga, TN 37402-2801
Mr. Joseph W. Shea  
SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT
Vice President, Nuclear Licensing  
            05000327/2013005 AND 05000328/2013005
Tennessee Valley Authority  
Dear Mr. Shea:
1101 Market Street, LP 3D-C  
On December 31, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an
Chattanooga, TN 37402-2801
inspection at your Sequoyah Nuclear Plant, Units 1 and 2. On January 13, 2014, the NRC
inspectors discussed the results of this inspection with Mr. Carlin and other members of your
SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT  
staff. Inspectors documented the results of this inspection in the enclosed inspection report.
05000327/2013005 AND 05000328/2013005
NRC inspectors documented one self-revealing finding of very low safety significance (Green) in
this report. This finding involved a violation of NRC requirements. The NRC is treating this
Dear Mr. Shea:  
violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the NRC Enforcement
Policy.
On December 31, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an  
If you contest the violation or significance of this NCV, you should provide a response within 30
inspection at your Sequoyah Nuclear Plant, Units 1 and 2. On January 13, 2014, the NRC  
days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
inspectors discussed the results of this inspection with Mr. Carlin and other members of your  
Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001; with
staff. Inspectors documented the results of this inspection in the enclosed inspection report.  
copies to the Regional Administrator, Region II; the Director, Office of Enforcement, U.S.
Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident
NRC inspectors documented one self-revealing finding of very low safety significance (Green) in  
Inspector at the Sequoyah Nuclear Plant.
this report. This finding involved a violation of NRC requirements. The NRC is treating this  
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the NRC Enforcement  
response within 30 days of the date of this inspection report, with the basis for your
Policy.
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the
Sequoyah Nuclear Plant.
If you contest the violation or significance of this NCV, you should provide a response within 30  
As a result of the Safety Culture Common Language Initiative, the terminology and coding of
days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear  
cross-cutting aspects were revised beginning in calendar year (CY) 2014. New cross-cutting
Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001; with  
aspects identified in CY 2014 will be coded under the latest revision to Inspection Manual
copies to the Regional Administrator, Region II; the Director, Office of Enforcement, U.S.  
Chapter (IMC) 0310. Cross-cutting aspects identified in the last six months of 2013 using the
Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident  
Inspector at the Sequoyah Nuclear Plant.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a  
response within 30 days of the date of this inspection report, with the basis for your  
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the  
Sequoyah Nuclear Plant.  
As a result of the Safety Culture Common Language Initiative, the terminology and coding of  
cross-cutting aspects were revised beginning in calendar year (CY) 2014. New cross-cutting  
aspects identified in CY 2014 will be coded under the latest revision to Inspection Manual  
Chapter (IMC) 0310. Cross-cutting aspects identified in the last six months of 2013 using the  
previous terminology will be converted to the latest revision in accordance with the cross-
previous terminology will be converted to the latest revision in accordance with the cross-
reference in IMC 0310. The revised cross-cutting aspects will be evaluated for cross-cutting
reference in IMC 0310. The revised cross-cutting aspects will be evaluated for cross-cutting  
themes and potential substantive cross-cutting issues in accordance with IMC 0305 starting with
themes and potential substantive cross-cutting issues in accordance with IMC 0305 starting with  
the CY 2014 mid-cycle assessment review.
the CY 2014 mid-cycle assessment review.  


J. Shea                                     2
J. Shea  
In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections,
2  
Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections,  
NRCs Public Document Room or from the Publicly Available Records (PARS) component of
Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of this letter, its  
NRCs Agencywide Documents Access and Management System (ADAMS). ADAMS is
enclosure, and your response (if any) will be available electronically for public inspection in the  
accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public
NRCs Public Document Room or from the Publicly Available Records (PARS) component of  
Electronic Reading Room).
NRCs Agencywide Documents Access and Management System (ADAMS). ADAMS is  
                                              Sincerely,
accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public  
                                                /RA/
Electronic Reading Room).  
                                              Jonathan H. Bartley, Chief
                                              Reactor Projects Branch 6
Sincerely,  
                                              Division of Reactor Projects
Docket Nos.: 50-327, 50-328
License Nos.: DPR-77, DPR-79
Enclosure: Inspection Report 05000327/2013005, 05000328/2013005
                w/Attachment: Supplementary Information
/RA/  
Jonathan H. Bartley, Chief  
Reactor Projects Branch 6  
Division of Reactor Projects  
Docket Nos.: 50-327, 50-328  
License Nos.: DPR-77, DPR-79  
Enclosure: Inspection Report 05000327/2013005, 05000328/2013005  
w/Attachment: Supplementary Information  
cc: via ListServ distribution
cc: via ListServ distribution




_________________________                 SUNSI REVIEW COMPLETE   FORM 665 ATTACHED
_________________________  
OFFICE         RII:DRP       RII:DRP       RII:DRS     RII:DRS       RII:DRS       RII:DRS     RII:DRP       RII:DRP
SIGNATURE     JHB /RA for/ Via email     BRB /RA for/ ORL /RA for/   BRB /RA for/   BRB /RA for/ JDH /RA/     JHB /RA/
SUNSI REVIEW COMPLETE  
NAME           GSmith       WDeschaine   MSpeck       LLake         RHamilton     RKellner     JHamman       JBartley
FORM 665 ATTACHED  
DATE             02/07/2014   02/07/2014   02/07/2014   02/07/2014     02/07/2014   02/07/2014   02/07/2014   02/07/2014
OFFICE  
E-MAIL COPY?    YES   NO   YES     NO   YES      NO  YES     NO   YES     NO   YES     NO                 YES     NO
RII:DRP  
       
RII:DRP  
J. Shea                                    3
RII:DRS  
Letter to J.W. Shea from Jonathan H. Bartley dated February 7, 2014
RII:DRS  
SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT
RII:DRS  
            05000327/2013005 AND 05000328/2013005
RII:DRS  
Distribution w/encl:
RII:DRP  
C. Evans, RII
RII:DRP  
L. Douglas, RII
SIGNATURE  
OE Mail
JHB /RA for/  
RIDSNRRDIRS
Via email  
PUBLIC
BRB /RA for/  
RidsNrrPMSequoyah Resource
ORL /RA for/  
BRB /RA for/  
BRB /RA for/  
JDH /RA/  
JHB /RA/  
NAME  
GSmith  
WDeschaine  
MSpeck  
LLake  
RHamilton  
RKellner  
JHamman  
JBartley  
DATE  
02/07/2014  
02/07/2014  
02/07/2014  
02/07/2014  
02/07/2014  
02/07/2014  
02/07/2014  
02/07/2014  
E-MAIL COPY?  
     YES  
NO       YES  
NO       YES  
NO     YES  
NO     YES  
NO    
  YES  
NO       
  YES
NO   


              U. S. NUCLEAR REGULATORY COMMISSION
J. Shea
                                REGION II
3
Docket Nos.:        50-327, 50-328
License Nos.:       DPR-77, DPR-79
Letter to J.W. Shea from Jonathan H. Bartley dated February 7, 2014
Report Nos.:        05000327/2013005, 05000328/2013005
Licensee:          Tennessee Valley Authority (TVA)
SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT
Facility:          Sequoyah Nuclear Plant, Units 1 and 2
05000327/2013005 AND 05000328/2013005  
Location:           Sequoyah Access Road
                    Soddy-Daisy, TN 37379
Distribution w/encl:  
Dates:              October 1 - December 31, 2013
C. Evans, RII
Inspectors:        G. Smith, Senior Resident Inspector
L. Douglas, RII 
                    W. Deschaine, Resident Inspector
OE Mail
                    M. Speck, Senior Emergency Preparedness Inspector (Sections
RIDSNRRDIRS
                      1R04.1 and 1R05)
PUBLIC
                    L. Lake, Senior Reactor Inspector (Section 1R08)
RidsNrrPMSequoyah Resource
                    R. Hamilton, Senior Health Physicist (Section 2RS8)
                    R. Kellner, Health Physicist (Sections 2RS1, 4OA1)
Approved by:        Jonathan H. Bartley, Chief
                    Reactor Projects Branch 6
                    Division of Reactor Projects
                                                                        Enclosure


                                              SUMMARY
IR 05000327/2013-005, 05000328/2013-005; 10/1/2013 - 12/31/2013; Sequoyah Nuclear Plant,
Enclosure
Units 1 and 2; Other Activities
U. S. NUCLEAR REGULATORY COMMISSION
The report covered a three-month period of inspection by resident inspectors and announced
inspections by regional inspectors. One self-revealing finding was identified. The significance
REGION II
of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual
Chapter (IMC) 0609, "Significance Determination Process," (SDP) dated June 2, 2011. Cross-
cutting aspects are determined using IMC 0310, Components Within the Cross-Cutting Areas,
Docket Nos.: 
dated October 28, 2011. The NRC's program for overseeing the safe operation of commercial
50-327, 50-328
nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4,
dated December 2006.
A.      NRC-Identified and Self-Revealing Findings
License Nos.: 
        Cornerstone: Mitigating Systems
DPR-77, DPR-79
        Green: A self-revealing non-cited violation of 10 CFR 50 Appendix B, Criterion XVI,
        Corrective Action, was identified for the licensees failure to promptly correct a
        condition adverse to quality within a reasonable time. Timely corrective actions were not
Report Nos.:
        taken to correct a dual position indication (open and closed lights both illuminated) on
05000327/2013005, 05000328/2013005
        the Unit 1 A train residual heat removal (RHR) containment sump suction flow control
        valve (FCV) 1-FCV-63-72. This licensee entered this issue into the corrective action
        program as problem evaluation report (PER) 772193 and performed repairs to the valve
        to restore the system to operable status.
        This finding was determined to be more than minor because it was associated with the
        Design Control attribute of the Mitigating Systems cornerstone and adversely affected
        the cornerstones objective to ensure the availability, reliability, and capability of systems
Licensee:
        that respond to initiating events to prevent undesirable consequences (i.e., core
        damage). Specifically, the finding reduced the reliability and capability of the A train
Tennessee Valley Authority (TVA)
        RHR system to perform its safety function as designed. The finding required a detailed
        risk analysis as the A RHR system was inoperable beyond its allowed outage time of 72
        hours. The detailed risk analysis concluded that the finding was of very low safety
Facility:
        significance (Green). This finding was determined to have a cross-cutting aspect
        relating to the proper classification, prioritization, and evaluation of operability and
Sequoyah Nuclear Plant, Units 1 and 2  
        reportability of conditions adverse to quality in the Corrective Action component of the
        Problem Identification and Resolution area. [P.1(c)] (Section 4OA5)
B.      Licensee-Identified Violations
Location:
        None
                                                                                              Enclosure
Sequoyah Access Road
Soddy-Daisy, TN 37379
Dates: 
October 1 - December 31, 2013
Inspectors:  
G. Smith, Senior Resident Inspector
W. Deschaine, Resident Inspector
M. Speck, Senior Emergency Preparedness Inspector (Sections 
1R04.1 and 1R05)  
L. Lake, Senior Reactor Inspector (Section 1R08)  
R. Hamilton, Senior Health Physicist (Section 2RS8)  
R. Kellner, Health Physicist (Sections 2RS1, 4OA1)  
Approved by: 
Jonathan H. Bartley, Chief
Reactor Projects Branch 6
Division of Reactor Projects


                                        REPORT DETAILS
Summary of Plant Status:
Unit 1 operated at or near 100 percent rated thermal power (RTP) until September 9, 2013,
Enclosure
when the unit entered a power coast down period until October 14 when the unit shut down for a
SUMMARY
refueling outage. Unit 1 returned to 100 percent RTP on November 24 where it operated for the
remainder of the inspection period.
IR 05000327/2013-005, 05000328/2013-005; 10/1/2013 - 12/31/2013; Sequoyah Nuclear Plant,
Unit 2 operated at or near 100 percent RTP for the entire inspection period.
Units 1 and 2; Other Activities
1.      REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
The report covered a three-month period of inspection by resident inspectors and announced
1R01 Adverse Weather Protection
inspections by regional inspectors.  One self-revealing finding was identified.  The significance
  a.   Inspection Scope
of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual
.1      Readiness for Seasonal Extreme Weather Conditions
Chapter (IMC) 0609, "Significance Determination Process," (SDP) dated June 2, 2011.  Cross-
        The inspectors reviewed design features and licensee preparations for protecting the
cutting aspects are determined using IMC 0310, Components Within the Cross-Cutting Areas,
        essential raw cooling water (ERCW) intake structure and both Unit 1 and 2 refueling
dated October 28, 2011. The NRC's program for overseeing the safe operation of commercial
        water storage tanks (RWSTs) from extreme cold and freezing conditions. The
nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4,
        inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) and Technical
dated December 2006.  
        Specifications (TS), reviewed implementation of licensee freeze protection procedures,
        walked down portions of the systems to assess deficiencies and system readiness for
A.  
        extreme cold weather, and discussed prioritization and status of correcting deficiencies
NRC-Identified and Self-Revealing Findings 
        with licensee personnel. Documents reviewed are listed in the Attachment. The
        inspectors completed one sample.
  b.   Findings
        No findings were identified.
Cornerstone: Mitigating Systems  
1R04 Equipment Alignment
.1      Partial System Walkdown
Green: A self-revealing non-cited violation of 10 CFR 50 Appendix B, Criterion XVI,  
  a.  Inspection Scope
Corrective Action, was identified for the licensees failure to promptly correct a
        The inspectors performed partial walkdowns of the following three systems to verify the
condition adverse to quality within a reasonable time. Timely corrective actions were not
        operability of redundant or diverse trains and components when safety equipment was
taken to correct a dual position indication (open and closed lights both illuminated) on
        inoperable. The inspectors focused on identification of discrepancies that could impact
the Unit 1 A train residual heat removal (RHR) containment sump suction flow control
        the function of the system and, therefore, potentially increase risk. The inspectors
valve (FCV) 1-FCV-63-72. This licensee entered this issue into the corrective action
        reviewed applicable operating procedures, walked down control system components,
program as problem evaluation report (PER) 772193 and performed repairs to the valve
        and determined whether selected breakers, valves, and support equipment were in the
to restore the system to operable status. 
        correct position to support system operation. The inspectors also verified that the
        licensee had properly identified and resolved equipment alignment problems that could
This finding was determined to be more than minor because it was associated with the
                                                                                        Enclosure
Design Control attribute of the Mitigating Systems cornerstone and adversely affected
the cornerstones objective to ensure the availability, reliability, and capability of systems
that respond to initiating events to prevent undesirable consequences (i.e., core
damage). Specifically, the finding reduced the reliability and capability of the A train
RHR system to perform its safety function as designed. The finding required a detailed
risk analysis as the A RHR system was inoperable beyond its allowed outage time of 72
hours. The detailed risk analysis concluded that the finding was of very low safety
significance (Green). This finding was determined to have a cross-cutting aspect
relating to the proper classification, prioritization, and evaluation of operability and  
reportability of conditions adverse to quality in the Corrective Action component of the  
Problem Identification and Resolution area. [P.1(c)] (Section 4OA5)
B.
Licensee-Identified Violations
None


                                            4
      cause initiating events or impact the capability of mitigating systems or barriers and
      entered them into the corrective action program (CAP). Documents reviewed are listed
Enclosure
      in the Attachment. The inspectors completed 3 samples.
REPORT DETAILS
      *    Spent fuel pool cooling during core empty period of U1R19
      *    1A emergency core cooling train while 1B 669 penetration cooler out-of-service
Summary of Plant Status:
      *    2A auxiliary feed-water and 2A emergency diesel generator while 2B under-voltage
          coils out-of-service
Unit 1 operated at or near 100 percent rated thermal power (RTP) until September 9, 2013,
.2    Complete System Walkdown
when the unit entered a power coast down period until October 14 when the unit shut down for a
   a. Inspection Scope
refueling outage.  Unit 1 returned to 100 percent RTP on November 24 where it operated for the
      The inspectors performed a complete system walkdown of the: 1) emergency gas
remainder of the inspection period.  
      treatment system/auxiliary building gas treatment system (ABGTS); and 2) auxiliary
      building ventilation/control building ventilation systems. The purpose of this inspection
Unit 2 operated at or near 100 percent RTP for the entire inspection period.  
      was to verify proper equipment alignment, to identify any discrepancies that could impact
      the function of the system and increase risk, and to verify that the licensee properly
1.  
      identified and resolved equipment alignment problems that could cause events or impact
REACTOR SAFETY
      the functional capability of the system.
      The inspectors reviewed the UFSAR, system procedures, system drawings, and system
Cornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity
      design documents to determine the correct lineup and then examined system
      components and their configuration to identify any discrepancies between the existing
1R01 Adverse Weather Protection
      system equipment lineup and the correct lineup. During the walkdown, the inspectors
      reviewed the following:
   a.
      *   Dampers were correctly positioned.
Inspection Scope  
      *    Electrical power was available as required.
      *    Hangers and supports were correctly installed and functional.
.1
      *    Essential support systems were operational.
Readiness for Seasonal Extreme Weather Conditions
      *    Ancillary equipment or debris did not interfere with system performance.
      *   Breakers were correctly positioned.
The inspectors reviewed design features and licensee preparations for protecting the  
      *    Major system components were correctly labeled.
essential raw cooling water (ERCW) intake structure and both Unit 1 and 2 refueling
      *    Cabinets, cable trays, and conduits were correctly installed and functional.
water storage tanks (RWSTs) from extreme cold and freezing conditions. The  
      *    Visible cabling appeared to be in good material condition.
inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) and Technical
      In addition, the inspectors reviewed corrective action items and design issues associated
Specifications (TS), reviewed implementation of licensee freeze protection procedures,  
      with the systems to determine whether any condition described in those documents
walked down portions of the systems to assess deficiencies and system readiness for
      could adversely impact current system operability. Documents reviewed are listed in the
extreme cold weather, and discussed prioritization and status of correcting deficiencies
      Attachment. The inspectors completed two samples.
with licensee personnel.  Documents reviewed are listed in the Attachment. The
  b. Findings
inspectors completed one sample.
      No findings were identified.
                                                                                        Enclosure
   b.
Findings
No findings were identified.  
1R04 Equipment Alignment
.1
Partial System Walkdown
   a.  
Inspection Scope 
The inspectors performed partial walkdowns of the following three systems to verify the
operability of redundant or diverse trains and components when safety equipment was
inoperable.  The inspectors focused on identification of discrepancies that could impact  
the function of the system and, therefore, potentially increase risk. The inspectors
reviewed applicable operating procedures, walked down control system components,
and determined whether selected breakers, valves, and support equipment were in the  
correct position to support system operation. The inspectors also verified that the
licensee had properly identified and resolved equipment alignment problems that could


                                          5
1R05 Fire Protection
4
.1    Fire Protection Tours
  a. Inspection Scope
Enclosure
      The inspectors conducted a tour of the six areas important to safety listed below to
      assess the material condition and operational status of fire protection features. The
cause initiating events or impact the capability of mitigating systems or barriers and  
      inspectors evaluated whether: combustibles and ignition sources were controlled in
entered them into the corrective action program (CAP). Documents reviewed are listed  
      accordance with the licensees administrative procedures; fire detection and suppression
in the Attachment. The inspectors completed 3 samples.  
      equipment was available for use; passive fire barriers were maintained in good material
      condition; and compensatory measures for out-of-service, degraded, or inoperable fire
*  
      protection equipment were implemented in accordance with the licensees fire plan.
Spent fuel pool cooling during core empty period of U1R19
      Documents reviewed are listed in the Attachment. The inspectors completed six
*  
      samples.
1A emergency core cooling train while 1B 669 penetration cooler out-of-service
      *   Unit 1 Lower Containment Building
*  
      *   Unit 1 Upper Containment Building
2A auxiliary feed-water and 2A emergency diesel generator while 2B under-voltage
      *  Control Building Elevation 685 (Auxiliary Instrument Room)
coils out-of-service
      *   Control Building Elevation 706 (Cable Spreading Room)
      *  ERCW Building - Elevations 688/704/720
.2
      *  Turbine Building - Elevations 662/685
Complete System Walkdown
  b. Findings
      No findings were identified.
   a.  
1R06 Flood Protection Measures
Inspection Scope  
.1    Internal Flooding
   a. Inspection Scope
The inspectors performed a complete system walkdown of the:  1) emergency gas
      The inspectors examined internal flood protection measures associated with the 1A and
treatment system/auxiliary building gas treatment system (ABGTS); and 2) auxiliary
      1B safety injection (SI) pump rooms internal flood design in order to verify that flood
building ventilation/control building ventilation systems.  The purpose of this inspection
      mitigation plans were consistent with the design requirements and risk analysis
was to verify proper equipment alignment, to identify any discrepancies that could impact
      assumptions. The inspectors verified that equipment essential for reactor shutdown was
the function of the system and increase risk, and to verify that the licensee properly
      properly protected from a flood caused by pipe breaks in the 1A & 1B SI pump room.
identified and resolved equipment alignment problems that could cause events or impact
      Specifically, the inspectors reviewed the licensees moderate energy line break flooding
the functional capability of the system.
      study to fully understand the licensees flood mitigation strategy, reviewed licensee
      drawings and then verified that the assumptions and results remained valid. The
The inspectors reviewed the UFSAR, system procedures, system drawings, and system
      inspectors walked down the 1A & 1B SI pump room to verify the assumed flooding
design documents to determine the correct lineup and then examined system
      sources, adequacy of common area drainage, and flood detection instrumentation to
components and their configuration to identify any discrepancies between the existing
      ensure that a flooding event would not impact reactor shutdown capabilities. The
system equipment lineup and the correct lineup.  During the walkdown, the inspectors
      inspectors completed one sample.
reviewed the following:
                                                                                        Enclosure
*
Dampers were correctly positioned.
*
Electrical power was available as required.
*
Hangers and supports were correctly installed and functional.
*
Essential support systems were operational.
*
Ancillary equipment or debris did not interfere with system performance.
*
Breakers were correctly positioned.
*
Major system components were correctly labeled.
*
Cabinets, cable trays, and conduits were correctly installed and functional.  
*
Visible cabling appeared to be in good material condition.
In addition, the inspectors reviewed corrective action items and design issues associated
with the systems to determine whether any condition described in those documents
could adversely impact current system operability.  Documents reviewed are listed in the
Attachment. The inspectors completed two samples.
  b.  
Findings 
No findings were identified.


                                            6
  b. Findings
5
    No findings were identified.
   
1R08 Non-Destructive Examination Activities and Welding Activities
Enclosure
  a. Inspection Scope
1R05 Fire Protection
    From October 21-25, 2013, the inspectors conducted an on-site review of the
   
    implementation of the licensees in-service inspection (ISI) Program for monitoring
.1
    degradation of the reactor coolant system; emergency feedwater systems, risk-
Fire Protection Tours
    significant piping and components, and containment systems in Unit 1.
   
    The inspectors activities included a review of non-destructive examinations (NDEs) to
  a.  
    evaluate compliance with the applicable edition of the American Society of Mechanical
Inspection Scope  
    Engineers (ASME) Boiler and Pressure Vessel Code, Section XI, and to verify that
    indications and defects were appropriately evaluated and dispositioned in accordance
The inspectors conducted a tour of the six areas important to safety listed below to
    with the requirements of the ASME Code, Section XI, acceptance standards or NRC
assess the material condition and operational status of fire protection features.  The
    approved alternative requirement.
inspectors evaluated whether: combustibles and ignition sources were controlled in  
    The inspectors directly observed or reviewed records of the following NDEs mandated
accordance with the licensees administrative procedures; fire detection and suppression
    by the ASME Code to evaluate compliance with the ASME Code Section XI and Section
equipment was available for use; passive fire barriers were maintained in good material
    V requirements, and if any indications and defects were detected. Inspectors also
condition; and compensatory measures for out-of-service, degraded, or inoperable fire
    reviewed evaluations of results that were dispositioned in accordance with the ASME
protection equipment were implemented in accordance with the licensees fire plan.
    Code or an NRC-approved alternative requirement.
Documents reviewed are listed in the Attachment.  The inspectors completed six
    *   Directly observed:
samples.  
        o Ultrasonic testing (UT) examinations of the reactor pressure vessel head to shell
            flange studs
*
        o General visual examination of the outside surface of the containment shell
Unit 1 Lower Containment Building
    *   Reviewed records:
*
        o UT examinations of reactor coolant pump #4 bolting
Unit 1 Upper Containment Building 
        o VT-3 visual examination of containment penetration bolting
*  
        o Work Order 113312025 modification of component cooling water system piping
Control Building Elevation 685 (Auxiliary Instrument Room)  
    The inspectors reviewed documentation for the repair/replacement of the following
*
    pressure boundary welds. The inspectors evaluated if the licensee applied the pre-
Control Building Elevation 706 (Cable Spreading Room)
    service non-destructive examinations and acceptance criteria required by the
*  
    Construction Code. In addition, the inspectors reviewed the welding procedure
ERCW Building - Elevations 688/704/720
    specifications, welder qualifications, welding material certifications, and supporting weld
*
    procedure qualification records to evaluate if the weld procedures were qualified in
Turbine Building - Elevations 662/685
    accordance with the requirements of the Construction Code and the ASME Code
    Section XI.
  b.
                                                                                      Enclosure
Findings
No findings were identified.
1R06 Flood Protection Measures
.1
Internal Flooding 
  a.
Inspection Scope 
The inspectors examined internal flood protection measures associated with the 1A and
1B safety injection (SI) pump rooms internal flood design in order to verify that flood
mitigation plans were consistent with the design requirements and risk analysis
assumptions. The inspectors verified that equipment essential for reactor shutdown was
properly protected from a flood caused by pipe breaks in the 1A & 1B SI pump room. 
Specifically, the inspectors reviewed the licensees moderate energy line break flooding
study to fully understand the licensees flood mitigation strategy, reviewed licensee
drawings and then verified that the assumptions and results remained valid.  The
inspectors walked down the 1A & 1B SI pump room to verify the assumed flooding
sources, adequacy of common area drainage, and flood detection instrumentation to
ensure that a flooding event would not impact reactor shutdown capabilities.  The
inspectors completed one sample.  


                                      7
PWR Vessel Upper Head Penetration (VUHP) Inspection Activities: For the Unit 1
6
vessel head, a bare metal visual examination and a volumetric examination required in
accordance with the requirements of ASME Code Case N-729-1 and 10 CFR
Enclosure
50.55a(g)(6)(ii)(D) were conducted in the previous outage and therefore not required to
  b.  
be performed this outage.
Findings 
Boric Acid Corrosion Control (BACC) Inspection Activities: The inspectors reviewed the
licensees BACC program activities to ensure implementation with commitments made in
No findings were identified. 
response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor
Pressure Boundary, and applicable industry guidance documents. Specifically, the
1R08 Non-Destructive Examination Activities and Welding Activities
inspectors performed an on-site record review of procedures and the results of the
licensees containment walkdown inspections performed during the current refueling
  a.  
outage. The inspectors also reviewed Focused Self-Assessment CRP-ENG-F-13-031 of
Inspection Scope
the Boric Acid Program.
The inspectors also interviewed the BACC program owner, conducted an independent
From October 21-25, 2013, the inspectors conducted an on-site review of the  
walkdown of containment to evaluate compliance with licensees BACC program
implementation of the licensees in-service inspection (ISI) Program for monitoring
requirements, and verified that degraded or non-conforming conditions, such as boric
degradation of the reactor coolant system; emergency feedwater systems, risk-
acid leaks, were properly identified and corrected in accordance with the licensees
significant piping and components, and containment systems in Unit 1.  
BACC and corrective action programs.
The inspectors reviewed the following evaluations and corrective actions related to
The inspectors activities included a review of non-destructive examinations (NDEs) to  
evidence of boric acid leakage to evaluate if the corrective actions completed were
evaluate compliance with the applicable edition of the American Society of Mechanical
consistent with the requirements of the ASME Code Section XI and 10 CFR Part 50,
Engineers (ASME) Boiler and Pressure Vessel Code, Section XI, and to verify that  
Appendix B, Criterion XVI.
indications and defects were appropriately evaluated and dispositioned in accordance  
*  Problem Event Report (PER) 618770 - Boron buildup on 1B-B SI pump pedestal
with the requirements of the ASME Code, Section XI, acceptance standards or NRC
*   PER 691545 - Boric acid build up and wet boric acid are present on transmitter
approved alternative requirement.  
    sensing line 1-FT-72-41
Steam Generator (SG) Tube Inspection Activities:
The inspectors directly observed or reviewed records of the following NDEs mandated
There were no SG tube eddy current examinations conducted during this outage. The
by the ASME Code to evaluate compliance with the ASME Code Section XI and Section
inspectors reviewed the following documentation and evaluated them against the
V requirements, and if any indications and defects were detected. Inspectors also
licensees TS, commitments made to the NRC, ASME Section XI, and Nuclear Energy
reviewed evaluations of results that were dispositioned in accordance with the ASME
Institute (NEI) 97-06, Steam Generator Program Guidelines, to ensure that the licensee
Code or an NRC-approved alternative requirement.
was in compliance with the schedule to skip the SG eddy current testing inspections for
the 1R19 outage:
*  
*  AREVA document # 51-9178898-001, Sequoyah Unit Condition Monitoring for Cycle
Directly observed:
    18 and Operational Assessment for Cycles 19, 20 and 21
o Ultrasonic testing (UT) examinations of the reactor pressure vessel head to shell
Identification and Resolution of Problems:
flange studs
The inspectors performed a review of selected ISI-related problems that were identified
o General visual examination of the outside surface of the containment shell
by the licensee and entered into the corrective action program as PERs. The inspectors
reviewed the PERs to confirm the licensee had appropriately described the scope of the
*
problem and had initiated corrective actions. The review also included the licensees
Reviewed records:  
                                                                                Enclosure
o UT examinations of reactor coolant pump #4 bolting
o VT-3 visual examination of containment penetration bolting 
o Work Order 113312025 modification of component cooling water system piping
The inspectors reviewed documentation for the repair/replacement of the following
pressure boundary welds.  The inspectors evaluated if the licensee applied the pre-
service non-destructive examinations and acceptance criteria required by the  
Construction Code. In addition, the inspectors reviewed the welding procedure
specifications, welder qualifications, welding material certifications, and supporting weld
procedure qualification records to evaluate if the weld procedures were qualified in
accordance with the requirements of the Construction Code and the ASME Code
Section XI.  


                                              8
      consideration and assessment of operating experience events applicable to the plant.
7
      The inspectors performed this review to ensure compliance with 10 CFR Part 50,
      Appendix B, Criterion XVI, Corrective Action, requirements. Documents reviewed are
Enclosure
      listed in the Attachment.
PWR Vessel Upper Head Penetration (VUHP) Inspection Activities:  For the Unit 1
  b. Findings
vessel head, a bare metal visual examination and a volumetric examination required in
      No findings were identified.
accordance with the requirements of ASME Code Case N-729-1 and 10 CFR  
1R11 Licensed Operator Requalification Program
50.55a(g)(6)(ii)(D) were conducted in the previous outage and therefore not required to
.1    Quarterly Review of Licensed Operator Requalification
be performed this outage.  
  a. Inspection Scope
      The inspectors performed one licensed operator requalification program review. The
      inspectors observed a simulator session on October 9, 2013. The training scenario
Boric Acid Corrosion Control (BACC) Inspection Activities:  The inspectors reviewed the
      involved Just-In-Time Training for Pre-Refueling Outage risk significant activities such as
licensees BACC program activities to ensure implementation with commitments made in
      placing the RHR system in service. The inspectors observed crew performance in terms
response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor
      of communications; ability to take timely and proper actions; prioritizing, interpreting, and
Pressure Boundary, and applicable industry guidance documents. Specifically, the
      verifying alarms; correct use and implementation of procedures, including the alarm
inspectors performed an on-site record review of procedures and the results of the
      response procedures; timely control board operation and manipulation, including high
licensees containment walkdown inspections performed during the current refueling
      risk operator actions; oversight and direction provided by shift manager, including the
outage. The inspectors also reviewed Focused Self-Assessment CRP-ENG-F-13-031 of
      ability to identify and implement appropriate TS action; and, group dynamics involved in
the Boric Acid Program.
      crew performance. The inspectors also observed the evaluators critique and reviewed
      simulator fidelity to verify that it matched actual plant response. Documents reviewed
The inspectors also interviewed the BACC program owner, conducted an independent
      are listed in the Attachment. The inspectors completed one sample.
walkdown of containment to evaluate compliance with licensees BACC program
  b. Findings
requirements, and verified that degraded or non-conforming conditions, such as boric
      No findings were identified.
acid leaks, were properly identified and corrected in accordance with the licensees
.2    Quarterly Review of Licensed Operator Performance
BACC and corrective action programs.
  a. Inspection Scope
      The inspectors observed and assessed licensed operator performance in the main
The inspectors reviewed the following evaluations and corrective actions related to
      control room during periods of heightened activity or risk. The inspectors reviewed
evidence of boric acid leakage to evaluate if the corrective actions completed were
      various licensee policies and procedures such as OPDP-1, Conduct of Operations,
consistent with the requirements of the ASME Code Section XI and 10 CFR Part 50,
      NPG-SPP-10.0, Plant Operations, and 0-GO-5, Normal Power Operation. The
Appendix B, Criterion XVI.  
      inspectors utilized activities such as post-maintenance testing, surveillance testing,
      unplanned transients, infrequent plant evolutions, plant startups and shutdowns, reactor
*
      power and turbine load changes, and refueling and other outage activities to focus on
Problem Event Report (PER) 618770 - Boron buildup on 1B-B SI pump pedestal
      the following conduct of operations as appropriate:
*
      *    operator compliance and use of procedures
PER 691545 - Boric acid build up and wet boric acid are present on transmitter
      *    control board manipulations
sensing line 1-FT-72-41
      *    communication between crew members
                                                                                        Enclosure
Steam Generator (SG) Tube Inspection Activities:
There were no SG tube eddy current examinations conducted during this outage. The  
inspectors reviewed the following documentation and evaluated them against the
licensees TS, commitments made to the NRC, ASME Section XI, and Nuclear Energy
Institute (NEI) 97-06, Steam Generator Program Guidelines, to ensure that the licensee
was in compliance with the schedule to skip the SG eddy current testing inspections for
the 1R19 outage:
*
AREVA document # 51-9178898-001, Sequoyah Unit Condition Monitoring for Cycle
18 and Operational Assessment for Cycles 19, 20 and 21 
Identification and Resolution of Problems:  
The inspectors performed a review of selected ISI-related problems that were identified
by the licensee and entered into the corrective action program as PERs.  The inspectors
reviewed the PERs to confirm the licensee had appropriately described the scope of the
problem and had initiated corrective actions.  The review also included the licensees


                                            9
      *  use and interpretation of plant instruments, indications, and alarms
8
      *  use of human error prevention techniques
      *  documentation of activities, including initials and sign-offs in procedures
Enclosure
      *  supervision of activities, including risk and reactivity management
consideration and assessment of operating experience events applicable to the plant
      *  pre-job briefs
The inspectors performed this review to ensure compliance with 10 CFR Part 50,  
      Specifically, the inspectors observed licensed operator performance during the following
Appendix B, Criterion XVI, Corrective Action, requirements.  Documents reviewed are  
      activities:
listed in the Attachment.  
      *  Unit 1 reactor shutdown and plant cool down/depressurization
      *  Unit 1 refueling and other outage activities
   b.  
      *  Unit 1 startup, including Mode changes
Findings  
      *  Unit 2 down power with turbine in manual for valve testing
      Documents reviewed are listed in the Attachment. The inspectors completed one
No findings were identified.  
      sample.
   b. Findings
1R11 Licensed Operator Requalification Program   
      No findings were identified.
.3    Annual Review of Licensee Requalification Examination Results
.
   a. Inspection Scope
Quarterly Review of Licensed Operator Requalification
      On September 13, 2013, the licensee completed the annual requalification operating
      examinations required to be administered to all licensed operators in accordance with 10
   a.  
      CFR 55.59(a)(2), Requalification requirements, of the NRCs Operators Licenses.
Inspection Scope  
      The inspectors performed an in-office review of the overall pass/fail results of the
      individual operating examinations and the crew simulator operating examinations in
The inspectors performed one licensed operator requalification program review.  The
      accordance with Inspection Procedure (IP) 71111.11, Licensed Operator Requalification
inspectors observed a simulator session on October 9, 2013.  The training scenario
      Program and Licensed Operator Performance. The results were compared to the
involved Just-In-Time Training for Pre-Refueling Outage risk significant activities such as
      thresholds established in Section 3.02, Requalification Examination Results, of IP
placing the RHR system in service. The inspectors observed crew performance in terms
      71111.11.
of communications; ability to take timely and proper actions; prioritizing, interpreting, and
   b. Findings
verifying alarms; correct use and implementation of procedures, including the alarm
      No findings were identified.
response procedures; timely control board operation and manipulation, including high
1R12 Maintenance Effectiveness
risk operator actions; oversight and direction provided by shift manager, including the  
   a. Inspection Scope
ability to identify and implement appropriate TS action; and, group dynamics involved in
      The inspectors reviewed five maintenance activities, issues, and/or systems listed below
crew performance. The inspectors also observed the evaluators critique and reviewed
      to verify the effectiveness of the licensees activities in terms of: appropriate work
simulator fidelity to verify that it matched actual plant response. Documents reviewed
      practices; identifying and addressing common cause failures; scoping in accordance
are listed in the Attachment. The inspectors completed one sample.  
      with 10 CFR 50.65(b); characterizing reliability issues for performance; trending key
   
                                                                                          Enclosure
   b.  
Findings  
No findings were identified.
.2
Quarterly Review of Licensed Operator Performance
   a.  
Inspection Scope  
The inspectors observed and assessed licensed operator performance in the main
control room during periods of heightened activity or risk.  The inspectors reviewed  
various licensee policies and procedures such as OPDP-1, Conduct of Operations,
NPG-SPP-10.0, Plant Operations, and 0-GO-5, Normal Power Operation.  The
inspectors utilized activities such as post-maintenance testing, surveillance testing,
unplanned transients, infrequent plant evolutions, plant startups and shutdowns, reactor
power and turbine load changes, and refueling and other outage activities to focus on
the following conduct of operations as appropriate:  
*
operator compliance and use of procedures
*
control board manipulations
*
communication between crew members


                                          10
    parameters for condition monitoring; charging unavailability for performance;
9
    classification in accordance with 10 CFR 50.65(a)(1) or (a)(2); appropriateness of
    performance criteria for structures, systems, or components (SSCs) and functions
Enclosure
    classified as (a)(2); and appropriateness of goals and corrective actions for SSCs and
*
    functions classified as (a)(1). Documents reviewed are listed in the Attachment. The
use and interpretation of plant instruments, indications, and alarms
    inspectors completed 5 samples.
*
    *  MR 11th Periodic Assessment Report (PE sample)
use of human error prevention techniques
    *  Cause Determination and Evaluation (CDE) #2700, FCV-63-72 Failure
*
    *  CDE #2696, EBGTS B Fan Failure
documentation of activities, including initials and sign-offs in procedures
    *  CDE #2686, A Shutdown Boardroom Chiller Failure
*
    *  CDE #2674, B Main Condenser Test Connection Failure
supervision of activities, including risk and reactivity management
  b.  Findings
*
    No findings were identified.
pre-job briefs
1R13 Maintenance Risk Assessments and Emergent Work Control
  a. Inspection Scope
Specifically, the inspectors observed licensed operator performance during the following
    The inspectors reviewed the following activities to determine whether appropriate risk
activities:
    assessments were performed prior to removing equipment from service for
    maintenance. The inspectors evaluated whether risk assessments were performed as
*
    required by 10 CFR 50.65(a)(4), and were accurate and complete. When emergent
Unit 1 reactor shutdown and plant cool down/depressurization
    work was performed, the inspectors reviewed whether plant risk was promptly
*
    reassessed and managed. The inspectors also assessed whether the licensees risk
Unit 1 refueling and other outage activities
    assessment tool use and risk categories were in accordance with Standard Programs
*
    and Processes Procedure NPG-SPP-07.1, On-Line Work Management, Revision 3,
Unit 1 startup, including Mode changes
    and Instruction 0-TI-DSM-000-007.1, Risk Assessment Guidelines, Revision 9.
*
    Documents reviewed are listed in the Attachment. The inspectors completed 2 samples.
Unit 2 down power with turbine in manual for valve testing
    *  Review U1R19 Outage Schedule
    *  Review of risk during ABGTS outage
Documents reviewed are listed in the Attachment. The inspectors completed one
  b. Findings
sample.
    No findings were identified.
1R15 Operability Determinations and Functionality Assessments
  b.
  a. Inspection Scope
Findings
    For the eight operability evaluations described in the PERs listed below, the inspectors
    evaluated the technical adequacy of the evaluations to ensure that TS operability was
   
    properly justified and the subject component or system remained available, such that no
No findings were identified.
    unrecognized increase in risk occurred. The inspectors compared the operability
                                                                                      Enclosure
.3
Annual Review of Licensee Requalification Examination Results
   
  a.  
Inspection Scope  
On September 13, 2013, the licensee completed the annual requalification operating
examinations required to be administered to all licensed operators in accordance with 10
CFR 55.59(a)(2), Requalification requirements, of the NRCs Operators Licenses. 
The inspectors performed an in-office review of the overall pass/fail results of the  
individual operating examinations and the crew simulator operating examinations in  
accordance with Inspection Procedure (IP) 71111.11, Licensed Operator Requalification
Program and Licensed Operator Performance.  The results were compared to the
thresholds established in Section 3.02, Requalification Examination Results, of IP
71111.11.  
  b.
Findings
   
   
No findings were identified.
1R12 Maintenance Effectiveness
   
  a.  
Inspection Scope  
The inspectors reviewed five maintenance activities, issues, and/or systems listed below  
to verify the effectiveness of the licensees activities in terms of: appropriate work
practices; identifying and addressing common cause failures; scoping in accordance
with 10 CFR 50.65(b); characterizing reliability issues for performance; trending key


                                            11
      evaluations to UFSAR descriptions to determine if the system or components intended
10
      function(s) were adversely impacted. In addition, the inspectors reviewed compensatory
      measures implemented to determine whether the compensatory measures worked as
Enclosure
      stated and the measures were adequately controlled. The inspectors also reviewed a
parameters for condition monitoring; charging unavailability for performance;
      sampling of PERs to assess whether the licensee was identifying and correcting any
classification in accordance with 10 CFR 50.65(a)(1) or (a)(2); appropriateness of
      deficiencies associated with operability evaluations. Documents reviewed are listed in
performance criteria for structures, systems, or components (SSCs) and functions
      the Attachment. The inspectors completed 8 samples.
classified as (a)(2); and appropriateness of goals and corrective actions for SSCs and  
      *   PER 789552 - Unit 2 Turbine Controls in Manual
functions classified as (a)(1). Documents reviewed are listed in the Attachment. The  
      *   PER 795451 - POE WO 113223153 T1 motor lead pinch
inspectors completed 5 samples.  
      *    PER 799097 - POE TS LCO 3.7.4 action for FCV-67-146
      *   PER 800432 - POE (ABSCE boundary issue)
*  
      *   PER 795433 - PDO (During U1R19 water found leaking out of conduit in bioshield
MR 11th Periodic Assessment Report (PE sample)
          wall)
*  
      *   PER 801415 - PDO EDG 1B 2 sec load sequence
Cause Determination and Evaluation (CDE) #2700, FCV-63-72 Failure
      *    PER 803833 - PDO U-1 Rx Head Vent Valve Stroke
*  
      *    PERs 816731, 815638, 817841 - FEs associated with the Unit 1 loose parts alarm
CDE #2696, EBGTS B Fan Failure
   b. Findings
*  
      No findings were identified.
CDE #2686, A Shutdown Boardroom Chiller Failure
1R18 Plant Modifications
*  
.1    Permanent Modifications
CDE #2674, B Main Condenser Test Connection Failure
   a. Inspection Scope
      The inspectors reviewed the modification listed below and the associated 10 CFR 50.59
   b.  
      screening, and compared it against the UFSAR and TS to verify whether the
Findings  
      modification affected operability or availability of the affected system.
      *    DCN 22643 - Replace Pressurizer Power Operated Relief Valves (PORVs)
No findings were identified.  
      Following installation and testing, the inspectors observed indications affected by the
      modification, discussed them with operators, and verified that the modification was
1R13 Maintenance Risk Assessments and Emergent Work Control
      installed properly and its operation did not adversely affect safety system functions. The
      inspectors did note that, ultimately, the installed PORVs did not meet the acceptance
   a.  
      criteria associated with the close stroke time. As a result, the licensee chose to cut
Inspection Scope  
      out/remove the new style PORVs and reinstall the original PORVs prior to plant startup
      in November 2013. Documents reviewed are listed in the Attachment. The inspectors
The inspectors reviewed the following activities to determine whether appropriate risk
      completed one sample.
assessments were performed prior to removing equipment from service for
   b. Findings
maintenance.  The inspectors evaluated whether risk assessments were performed as
      No findings were identified.
required by 10 CFR 50.65(a)(4), and were accurate and complete. When emergent
                                                                                        Enclosure
work was performed, the inspectors reviewed whether plant risk was promptly
reassessed and managed. The inspectors also assessed whether the licensees risk
assessment tool use and risk categories were in accordance with Standard Programs
and Processes Procedure NPG-SPP-07.1, On-Line Work Management, Revision 3,  
and Instruction 0-TI-DSM-000-007.1, Risk Assessment Guidelines, Revision 9. 
Documents reviewed are listed in the Attachment. The inspectors completed 2 samples.  
*
Review U1R19 Outage Schedule 
*
Review of risk during ABGTS outage 
   b.  
Findings  
No findings were identified.  
1R15  Operability Determinations and Functionality Assessments
  a.
Inspection Scope
For the eight operability evaluations described in the PERs listed below, the inspectors
evaluated the technical adequacy of the evaluations to ensure that TS operability was
properly justified and the subject component or system remained available, such that no
unrecognized increase in risk occurred.  The inspectors compared the operability


                                            12
1R19 Post Maintenance Testing
11
  a. Inspection Scope
      The inspectors reviewed the post maintenance tests associated with the nine work
Enclosure
      orders (WO) listed below to assess whether procedures and test activities ensured
evaluations to UFSAR descriptions to determine if the system or components intended
      system operability and functional capability. The inspectors reviewed the licensees test
function(s) were adversely impacted. In addition, the inspectors reviewed compensatory
      procedure to evaluate whether: the procedure adequately tested the safety function(s)
measures implemented to determine whether the compensatory measures worked as
      that may have been affected by the maintenance activity; the acceptance criteria in the
stated and the measures were adequately controlled. The inspectors also reviewed a
      procedure were consistent with information in the applicable licensing basis and/or
sampling of PERs to assess whether the licensee was identifying and correcting any
      design basis documents; and the procedure had been properly reviewed and approved.
deficiencies associated with operability evaluations. Documents reviewed are listed in  
      The inspectors also witnessed the test or reviewed the test data to determine whether
the Attachment. The inspectors completed 8 samples.  
      test results adequately demonstrated restoration of the affected safety function(s).
      Documents reviewed are listed in the Attachment. The inspectors completed nine
*  
      samples.
PER 789552 - Unit 2 Turbine Controls in Manual
      *   WO 113377829 - Repack Valve (1-LCV-3-175) and perform AIRCET test
*  
      *   WO 112096045 - Repair isolation check valve (1-VLV-026-1296)
PER 795451 - POE WO 113223153 T1 motor lead pinch
      *   WO 111234712 - 5 year PM to swap 480V Shutdown board breaker with a
*  
          refurbished breaker
PER 799097 - POE TS LCO 3.7.4 action for FCV-67-146
      *  WO 113806636 - Perform 0-MI-EPM-317-102.0 on CCS pump C-S and
*
          clean/replace motor air filter
PER 800432 - POE (ABSCE boundary issue)  
      *  WO 114560807 - Centrifugal charging pump (CCP) room cooler fan motor current
*  
          check, bearing lubrication and cleaning
PER 795433 - PDO (During U1R19 water found leaking out of conduit in bioshield
      *   WO 114198329 - EQ maintenance and inspection
wall)
      *  WO 113408190 - Change out electrolytic capacitors in the Woodward 2301A
*  
          governor card
PER 801415 - PDO EDG 1B 2 sec load sequence
      *   WOs 114306842, 114306841, 114325805, 114325799 - Aux Feedwater valves -
*
          836 & 837
PER 803833 - PDO U-1 Rx Head Vent Valve Stroke
      *  WO 113756597 - PORVs - PCV-68-340 & PCV-68-334
*
   b. Findings
PERs 816731, 815638, 817841 - FEs associated with the Unit 1 loose parts alarm
      No findings were identified.
1R20 Refueling and Other Outage Activities
   b.  
.1   Unit 1 Refueling Outage Cycle 19
Findings  
   a. Inspection Scope
      For the Unit 1 refueling outage that began on October 14, 2013, the inspectors
      evaluated licensee activities to verify that the licensee considered risk in developing
No findings were identified.  
      outage schedules, followed risk reduction methods developed to control plant
      configuration, developed mitigation strategies for the loss of key safety functions, and
1R18 Plant Modifications
      adhered to operating license and TS requirements that ensure defense-in-depth. The
      inspectors also walked down portions of Unit 1 not normally accessible during at-power
.1  
                                                                                        Enclosure
Permanent Modifications
   a.  
Inspection Scope  
The inspectors reviewed the modification listed below and the associated 10 CFR 50.59
screening, and compared it against the UFSAR and TS to verify whether the
modification affected operability or availability of the affected system.
*
DCN 22643 - Replace Pressurizer Power Operated Relief Valves (PORVs) 
Following installation and testing, the inspectors observed indications affected by the
modification, discussed them with operators, and verified that the modification was
installed properly and its operation did not adversely affect safety system functions.  The
inspectors did note that, ultimately, the installed PORVs did not meet the acceptance
criteria associated with the close stroke time.  As a result, the licensee chose to cut
out/remove the new style PORVs and reinstall the original PORVs prior to plant startup
in November 2013.  Documents reviewed are listed in the Attachment. The inspectors
completed one sample.
  b.
Findings
No findings were identified.


                                      13
operations to verify that safety-related and risk-significant SSCs were maintained in an
12
operable condition. Specifically, between October 14 and November 21, the inspectors
performed inspections and reviews of the following outage activities. Documents
Enclosure
reviewed are listed in the Attachment. The inspectors completed one sample.
1R19 Post Maintenance Testing
*   Outage Plan. The inspectors reviewed the outage safety plan and contingency plans
    to confirm that the licensee had appropriately considered risk, industry experience,
  a.
    and previous site-specific problems in developing and implementing a plan that
Inspection Scope
    assured maintenance of defense-in-depth.
*   Reactor Shutdown. The inspectors observed the shutdown in the control room from
The inspectors reviewed the post maintenance tests associated with the nine work
    the time the reactor was tripped until operators placed it on the RHR system for
orders (WO) listed below to assess whether procedures and test activities ensured
    decay heat removal to verify that TS cool down restrictions were followed. The
system operability and functional capability.  The inspectors reviewed the licensees test
    inspectors also toured the lower containment as soon as practicable after reactor
procedure to evaluate whether:  the procedure adequately tested the safety function(s)
    shutdown to observe the general condition of the reactor coolant system (RCS) and
that may have been affected by the maintenance activity; the acceptance criteria in the
    emergency core cooling system components and to look for indications of previously
procedure were consistent with information in the applicable licensing basis and/or
    unidentified leakage inside the polar crane wall.
design basis documents; and the procedure had been properly reviewed and approved. 
*   Licensee Control of Outage Activities. On a daily basis, the inspectors attended the
The inspectors also witnessed the test or reviewed the test data to determine whether
    licensee outage turnover meeting, reviewed PERs, and reviewed the defense-in-
test results adequately demonstrated restoration of the affected safety function(s).
    depth status sheets to verify that status control was commensurate with the outage
Documents reviewed are listed in the Attachment. The inspectors completed nine
    safety plan and in compliance with the applicable TS when taking equipment out of
samples.  
    service. The inspectors further toured the main control room and areas of the plant
    daily to ensure that the following key safety functions were maintained in accordance
*  
    with the outage safety plan and TS: electrical power, decay heat removal, spent fuel
WO 113377829 - Repack Valve (1-LCV-3-175) and perform AIRCET test
    cooling, inventory control, reactivity control, and containment closure. The
*
    inspectors also observed a tag-out of the B Train CCP system to verify that the
WO 112096045 - Repair isolation check valve (1-VLV-026-1296)
    equipment was appropriately configured to safely support the work and testing. To
*  
    ensure that RCS level instrumentation was properly installed and configured to give
WO 111234712 - 5 year PM to swap 480V Shutdown board breaker with a
    accurate information, the inspectors reviewed the installation of the Mansell level
refurbished breaker
    monitoring system. Specifically, the inspectors discussed the system with
*
    engineering, walked it down to verify that it was installed in accordance with
WO 113806636 - Perform 0-MI-EPM-317-102.0 on CCS pump C-S and
    procedures and adequately protected from inadvertent damage, verified that Mansell
clean/replace motor air filter
    indication properly overlapped with pressurizer level instruments during pressurizer
*
    drain-down, verified that operators properly set level alarms to procedurally required
WO 114560807 - Centrifugal charging pump (CCP) room cooler fan motor current
    set-points, and verified that the system consistently tracked RCS level while lowering
check, bearing lubrication and cleaning
    to reduced inventory conditions. The inspectors also observed operators compare
*
    the Mansell indications with locally-installed ultrasonic level indicators during entry
WO 114198329 - EQ maintenance and inspection
    into reduced inventory conditions.
*
                                                                                    Enclosure
WO 113408190 - Change out electrolytic capacitors in the Woodward 2301A
governor card
*  
WOs 114306842, 114306841, 114325805, 114325799 - Aux Feedwater valves -  
836 & 837
*
WO 113756597 - PORVs - PCV-68-340 & PCV-68-334
  b.  
Findings
No findings were identified.
1R20 Refueling and Other Outage Activities
.1
Unit 1 Refueling Outage Cycle 19
  a.
Inspection Scope
For the Unit 1 refueling outage that began on October 14, 2013, the inspectors  
evaluated licensee activities to verify that the licensee considered risk in developing
outage schedules, followed risk reduction methods developed to control plant
configuration, developed mitigation strategies for the loss of key safety functions, and  
adhered to operating license and TS requirements that ensure defense-in-depth. The  
inspectors also walked down portions of Unit 1 not normally accessible during at-power


                                          14
    *  Refueling Activities. The inspectors observed fuel movement at the spent fuel pool
13
        and at the refueling cavity in order to verify compliance with TS and that each
        assembly was properly tracked from core offload to core reload. In order to verify
Enclosure
        proper licensee control of foreign material, the inspectors verified that personnel
operations to verify that safety-related and risk-significant SSCs were maintained in an
        were properly checked before entering any foreign material exclusion (FME) areas,
operable condition. Specifically, between October 14 and November 21, the inspectors
        reviewed FME procedures, and verified that the licensee followed the procedures.
performed inspections and reviews of the following outage activities.  Documents
        To ensure that fuel assemblies were loaded in the core locations specified by the
reviewed are listed in the Attachment.  The inspectors completed one sample.
        design, the inspectors independently reviewed the recording of the licensees final
        core verification.
*
    *   Reduced Inventory and Mid-Loop Conditions. Prior to the outage, the inspectors
Outage Plan.  The inspectors reviewed the outage safety plan and contingency plans
        reviewed the licensees commitments to Generic Letter 88-17. Before entering
to confirm that the licensee had appropriately considered risk, industry experience,
        reduced inventory conditions the inspectors verified that these commitments were in
and previous site-specific problems in developing and implementing a plan that  
        place, that plant configuration was in accordance with those commitments, and that
assured maintenance of defense-in-depth.
        distractions from unexpected conditions or emergent work did not affect operator
        ability to maintain the required reactor vessel level. Mid-loop conditions were not
*
        entered during this outage since SG eddy current testing was not required.
Reactor Shutdown.  The inspectors observed the shutdown in the control room from
    *  Heat-up and Start-up Activities. The inspectors toured the containment prior to
the time the reactor was tripped until operators placed it on the RHR system for
        reactor startup to verify that debris that could affect the performance of the
decay heat removal to verify that TS cool down restrictions were followed.  The
        containment sump had not been left in the containment. The inspectors reviewed
inspectors also toured the lower containment as soon as practicable after reactor
        the licensees mode-change checklists to verify that appropriate prerequisites were
shutdown to observe the general condition of the reactor coolant system (RCS) and
        met prior to changing TS modes. To verify RCS integrity and containment integrity,
emergency core cooling system components and to look for indications of previously
        the inspectors further reviewed the licensees RCS leakage calculations and
unidentified leakage inside the polar crane wall.  
        containment isolation valve lineups. In order to verify that core operating limit
        parameters were consistent with core design, the inspectors also examined portions
*  
        of the low power physics testing surveillance.
Licensee Control of Outage Activities. On a daily basis, the inspectors attended the
bFindings
licensee outage turnover meeting, reviewed PERs, and reviewed the defense-in-
    No findings were identified.
depth status sheets to verify that status control was commensurate with the outage  
1R22 Surveillance Testing
safety plan and in compliance with the applicable TS when taking equipment out of
a.  Inspection Scope
service. The inspectors further toured the main control room and areas of the plant
    For the twelve surveillance tests identified below, the inspectors assessed whether the
daily to ensure that the following key safety functions were maintained in accordance
    SSCs involved in these tests satisfied the requirements described in the TS surveillance
with the outage safety plan and TS:  electrical power, decay heat removal, spent fuel
    requirements, the UFSAR, applicable licensee procedures, and whether the tests
cooling, inventory control, reactivity control, and containment closure. The  
    demonstrated that the SSCs were capable of performing their intended safety functions.
inspectors also observed a tag-out of the B Train CCP system to verify that the
    This was accomplished by witnessing testing and/or reviewing the test data. Documents
equipment was appropriately configured to safely support the work and testing. To  
    reviewed are listed in the Attachment. The inspectors completed twelve samples.
ensure that RCS level instrumentation was properly installed and configured to give
                                                                                        Enclosure
accurate information, the inspectors reviewed the installation of the Mansell level
monitoring systemSpecifically, the inspectors discussed the system with
engineering, walked it down to verify that it was installed in accordance with
procedures and adequately protected from inadvertent damage, verified that Mansell
indication properly overlapped with pressurizer level instruments during pressurizer
drain-down, verified that operators properly set level alarms to procedurally required
set-points, and verified that the system consistently tracked RCS level while lowering
to reduced inventory conditions. The inspectors also observed operators compare
the Mansell indications with locally-installed ultrasonic level indicators during entry
into reduced inventory conditions.  


                                          15
    In-Service Tests:
14
    *   1-SI-SXP-003-202.B, Motor Driven Auxiliary Feedwater Pump 1B-B Comprehensive
        Performance Test, Revision 7
Enclosure
    *  1-SI-SXP-074-202.0, RHR Pump 1A-A and 1B-B Comprehensive Performance and
*  
        Check Valve Test, Revision 10
Refueling Activities.  The inspectors observed fuel movement at the spent fuel pool
    RCS leakage test:
and at the refueling cavity in order to verify compliance with TS and that each
    *   0-SI-OPS-068-137.0, Reactor Coolant System Water Inventory, Revision 32
assembly was properly tracked from core offload to core reload. In order to verify
    Routine Surveillance Tests:
proper licensee control of foreign material, the inspectors verified that personnel
    *  1-SI-OPS-088-001.0, Phase A Isolation Test, Revision 14
were properly checked before entering any foreign material exclusion (FME) areas,  
    *  1-SI-OPS-082-026A, Loss of Offsite Power with Safety Injection D/G 1A-A Test,
reviewed FME procedures, and verified that the licensee followed the procedures. 
        Revision 46
To ensure that fuel assemblies were loaded in the core locations specified by the
    *  0-SI-SFT-072-138.0, Unit 1 Containment Spray - Spray Nozzle Test, Revision 6
design, the inspectors independently reviewed the recording of the licensees final
    *  0-SI-SXV-063-203.2, Full Stroking of Safety Injection Cold Leg Accumulator Isolation
core verification.
        Valves, Revision 1
    Ice Condenser Surveillance Test:
*  
    *  0-SI-MIN-061-105.0, Ice Condenser Ice Weighing, Revision 11
Reduced Inventory and Mid-Loop Conditions. Prior to the outage, the inspectors
    Containment Isolation Valve (CIV) Surveillance Tests:
reviewed the licensees commitments to Generic Letter 88-17. Before entering
    *  0-SI-SLT-067-258.2, Containment Isolation Valve Local Leak Rate Test Lower
reduced inventory conditions the inspectors verified that these commitments were in
        Compartment Essential Raw Cooling Water, Revision 13
place, that plant configuration was in accordance with those commitments, and that
    *  0-SI-SLT-088-259.4, Upper Personnel Airlock Interlock Operability Test, Revision 2
distractions from unexpected conditions or emergent work did not affect operator
    *  0-SI-SLT-088-259.1, Upper Personnel Airlock Overall Leak Rate Test and General
ability to maintain the required reactor vessel level. Mid-loop conditions were not
        Inspection, Revision 6
entered during this outage since SG eddy current testing was not required.  
    *  0-SI-SLT-081-258.1, Containment Isolation Valve Local Leak Rate Test Primary
        Water System, Revision 5
*
  b.  Findings
Heat-up and Start-up Activities. The inspectors toured the containment prior to
    No findings were identified.
reactor startup to verify that debris that could affect the performance of the
    Cornerstone: Emergency Preparedness
containment sump had not been left in the containment. The inspectors reviewed
1EP2 Alert and Notification System Evaluation
the licensees mode-change checklists to verify that appropriate prerequisites were
  a. Inspection Scope
met prior to changing TS modes. To verify RCS integrity and containment integrity,  
    The inspectors evaluated the adequacy of the licensees methods for testing and
the inspectors further reviewed the licensees RCS leakage calculations and
    maintaining the alert and notification system in accordance with NRC Inspection
containment isolation valve lineups. In order to verify that core operating limit
    Procedure 71114, Attachment 02, Alert and Notification System Evaluation. The
parameters were consistent with core design, the inspectors also examined portions
                                                                                  Enclosure
of the low power physics testing surveillance.  
   
  b.  
Findings
   
No findings were identified.  
1R22 Surveillance Testing
   
  a.  
Inspection Scope  
For the twelve surveillance tests identified below, the inspectors assessed whether the
SSCs involved in these tests satisfied the requirements described in the TS surveillance
requirements, the UFSAR, applicable licensee procedures, and whether the tests
demonstrated that the SSCs were capable of performing their intended safety functions. 
This was accomplished by witnessing testing and/or reviewing the test data.  Documents
reviewed are listed in the Attachment. The inspectors completed twelve samples.


                                          16
    applicable planning standard, 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50,
15
    Appendix E, Section IV.D requirements were used as reference criteria. The criteria
    contained in NUREG-0654, Criteria for Preparation and Evaluation of Radiological
Enclosure
    Emergency Response Plans and Preparedness in Support of Nuclear Power Plants,
In-Service Tests:
    Revision 1, were also used as a reference.
    The inspectors reviewed various documents which are listed in the Attachment,
*
    interviewed personnel responsible for system performance, and observed aspects of
1-SI-SXP-003-202.B, Motor Driven Auxiliary Feedwater Pump 1B-B Comprehensive
    periodic siren maintenance and testing. This inspection activity satisfied one inspection
Performance Test, Revision 7
    sample for the alert and notification system on a biennial basis.
*
  b. Findings
1-SI-SXP-074-202.0, RHR Pump 1A-A and 1B-B Comprehensive Performance and  
    No findings were identified.
Check Valve Test, Revision 10
1EP3 Emergency Response Organization Staffing and Augmentation System
   
  a.  Inspection Scope
RCS leakage test:
    The inspectors reviewed the licensees Emergency Response Organization (ERO)
   
    augmentation staffing requirements and process for notifying the ERO to ensure the
*
    readiness of key staff for responding to an event and timely facility activation. The
0-SI-OPS-068-137.0, Reactor Coolant System Water Inventory, Revision 32
    qualification records of key position ERO personnel were reviewed to ensure all ERO
   
    qualifications were current. A sample of problems identified from augmentation drills or
Routine Surveillance Tests:
    system tests performed since the last inspection was reviewed to assess the
    effectiveness of corrective actions.
*
    The inspection was conducted in accordance with NRC Inspection Procedure 71114,
1-SI-OPS-088-001.0, Phase A Isolation Test, Revision 14
    Attachment 03, Emergency Response Organization Staffing and Augmentation System.
*
    The applicable planning standard, 10 CFR 50.47(b)(2), and its related 10 CFR 50,
1-SI-OPS-082-026A, Loss of Offsite Power with Safety Injection D/G 1A-A Test,  
    Appendix E requirements were used as reference criteria.
Revision 46
    The inspectors reviewed various documents which are listed in the Attachment. This
*
    inspection activity satisfied one inspection sample for the ERO staffing and
0-SI-SFT-072-138.0, Unit 1 Containment Spray - Spray Nozzle Test, Revision 6
    augmentation system on a biennial basis.
*
  b.  Findings
0-SI-SXV-063-203.2, Full Stroking of Safety Injection Cold Leg Accumulator Isolation
    No findings were identified.
Valves, Revision 1
1EP4 Emergency Action Level and Emergency Plan Changes
  a. Inspection Scope
Ice Condenser Surveillance Test:
    The NRC Office of Nuclear Security and Incident Response headquarters staff
    performed an in-office review of the latest revisions of various Emergency Plan
*
    Implementing Procedures (EPIPs) and the Emergency Plan located under ADAMS
0-SI-MIN-061-105.0, Ice Condenser Ice Weighing, Revision 11
                                                                                      Enclosure
Containment Isolation Valve (CIV) Surveillance Tests:
*
0-SI-SLT-067-258.2, Containment Isolation Valve Local Leak Rate Test Lower
Compartment Essential Raw Cooling Water, Revision 13
*
0-SI-SLT-088-259.4, Upper Personnel Airlock Interlock Operability Test, Revision 2
*
0-SI-SLT-088-259.1, Upper Personnel Airlock Overall Leak Rate Test and General
Inspection, Revision 6
*
0-SI-SLT-081-258.1, Containment Isolation Valve Local Leak Rate Test Primary
Water System, Revision 5
   
  b.  
Findings
   
No findings were identified.  
Cornerstone:  Emergency Preparedness
1EP2 Alert and Notification System Evaluation
   
  a.  
Inspection Scope  
The inspectors evaluated the adequacy of the licensees methods for testing and  
maintaining the alert and notification system in accordance with NRC Inspection
Procedure 71114, Attachment 02, Alert and Notification System Evaluation.  The


                                          17
    Accession numbers ML12326A678, ML12353A050, ML13025A102, ML13070A025,
16
    ML13219A022, and ML13246A091.
    The licensee determined that in accordance with 10 CFR 50.54(q), the changes made in
Enclosure
    the revisions resulted in no reduction in the effectiveness of the Plan, and that the
applicable planning standard, 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50,
    revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to
Appendix E, Section IV.D requirements were used as reference criteria. The criteria
    10 CFR Part 50. The NRC review was not documented in a safety evaluation report and
contained in NUREG-0654, Criteria for Preparation and Evaluation of Radiological
    did not constitute approval of licensee-generated changes; therefore, these revisions are
Emergency Response Plans and Preparedness in Support of Nuclear Power Plants,  
    subject to future inspection. Documents reviewed are listed in the Attachment. The
Revision 1, were also used as a reference.  
    inspectors completed one sample.
  b.  Findings
The inspectors reviewed various documents which are listed in the Attachment,
    No findings were identified.
interviewed personnel responsible for system performance, and observed aspects of
1EP5 Maintenance of Emergency Preparedness
periodic siren maintenance and testing. This inspection activity satisfied one inspection
  a. Inspection Scope
sample for the alert and notification system on a biennial basis.  
    The inspectors reviewed the corrective actions identified through the Emergency
   
    Preparedness program to determine the significance of the issues, the completeness
  b.  
    and effectiveness of corrective actions, and to determine if issues were recurring. The
Findings
    licensees post-event after action reports, self-assessments, and audits were reviewed to
   
    assess the licensees ability to be self-critical, thus avoiding complacency and
No findings were identified.  
    degradation of their emergency preparedness program. Inspectors reviewed the
    licensees 10 CFR 50.54(q) change process, personnel training, and selected
1EP3 Emergency Response Organization Staffing and Augmentation System
    screenings and evaluations to assess adequacy. The inspectors toured facilities and
   
    reviewed equipment and facility maintenance records to assess licensees adequacy in
  a.  
    maintaining them. The inspectors evaluated the capabilities of selected radiation
Inspection Scope  
    monitoring instrumentation to adequately support Emergency Action Level (EAL)
    declarations.
The inspectors reviewed the licensees Emergency Response Organization (ERO)
    The inspection was conducted in accordance with NRC Inspection Procedure 71114.05,
augmentation staffing requirements and process for notifying the ERO to ensure the  
    Maintenance of Emergency Preparedness. The applicable planning standards, related
readiness of key staff for responding to an event and timely facility activation. The  
    10 CFR 50, Appendix E requirements, and 10 CFR 50.54(q) and (t) were used as
qualification records of key position ERO personnel were reviewed to ensure all ERO
    reference criteria.
qualifications were current.  A sample of problems identified from augmentation drills or
    The inspectors reviewed various documents which are listed in the Attachment. This
system tests performed since the last inspection was reviewed to assess the
    inspection activity satisfied one inspection sample for the maintenance of emergency
effectiveness of corrective actions.  
    preparedness on a biennial basis.
  b.  Findings
The inspection was conducted in accordance with NRC Inspection Procedure 71114,  
    No findings were identified.
Attachment 03, Emergency Response Organization Staffing and Augmentation System.
                                                                                        Enclosure
The applicable planning standard, 10 CFR 50.47(b)(2), and its related 10 CFR 50,  
Appendix E requirements were used as reference criteria.  
The inspectors reviewed various documents which are listed in the Attachment. This  
inspection activity satisfied one inspection sample for the ERO staffing and
augmentation system on a biennial basis.  
   
  b.  
Findings
   
No findings were identified.  
1EP4 Emergency Action Level and Emergency Plan Changes
  a.
Inspection Scope
The NRC Office of Nuclear Security and Incident Response headquarters staff
performed an in-office review of the latest revisions of various Emergency Plan
Implementing Procedures (EPIPs) and the Emergency Plan located under ADAMS 


                                            18
2.    RADIATION SAFETY (RS)
17
      Cornerstones: Occupational Radiation Safety (OS) and Public Radiation Safety (PS)
2RS1 Radiological Hazard Assessment and Exposure Controls
Enclosure
  a. Inspection Scope
Accession numbers ML12326A678, ML12353A050, ML13025A102, ML13070A025,
      Hazard Assessment and Instructions to Workers: During facility tours, the inspectors
ML13219A022, and ML13246A091.
      directly observed labeling of radioactive material and postings for radiation areas, high
      radiation areas (HRAs), and airborne radioactivity areas established within the
The licensee determined that in accordance with 10 CFR 50.54(q), the changes made in
      radiologically controlled area (RCA) of the Unit 1 containment, Unit 1 and Unit 2 auxiliary
the revisions resulted in no reduction in the effectiveness of the Plan, and that the
      buildings, Independent Spent Fuel Storage Installation (ISFSI), and radioactive waste
revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to
      (radwaste) processing and storage locations. The inspectors independently measured
10 CFR Part 50. The NRC review was not documented in a safety evaluation report and
      radiation dose rates or directly observed conduct of licensee radiation surveys for RCA
did not constitute approval of licensee-generated changes; therefore, these revisions are
      areas in the Unit 1 containment, Unit 1 and Unit 2 Auxiliary buildings, and ISFSI. The
subject to future inspection.  Documents reviewed are listed in the Attachment. The  
      inspectors reviewed survey records for several plant areas including surveys for alpha
inspectors completed one sample.
      emitters, airborne radioactivity, and pre-job surveys for selected Unit 1 Refueling Outage
      19 (U1R19) tasks. The inspectors also discussed changes to plant operations that could
  b.
      contribute to changing radiological conditions since the last inspection and reviewed
Findings
      U1R19 crud burst results and post crud burst dose rate surveys. For selected U1R19
      outage jobs, the inspectors attended, or reviewed, pre-job briefings and radiation work
No findings were identified.
      permit (RWP) details to assess communication of radiological control requirements and
      current radiological conditions to workers. Selected U1R19 work activities included Unit
1EP5 Maintenance of Emergency Preparedness
      1 control rod drive mechanism duct work, Unit 1 Refueling Activities, Unit 1 Head O-ring
      Surface Work & Inspection, and work in the Unit 1 Equipment Pit and transfer canal.
  a.   Inspection Scope
      Hazard Control and Work Practices: The inspectors evaluated access barrier
      effectiveness for selected Unit 1 and Unit 2 Locked High Radiation Area (LHRA) and
The inspectors reviewed the corrective actions identified through the Emergency
      Very High Radiation Area (VHRA) locations. Changes to procedural guidance for LHRA
Preparedness program to determine the significance of the issues, the completeness
      and VHRA controls were discussed with health physics (HP) supervisors. Controls and
and effectiveness of corrective actions, and to determine if issues were recurring. The
      their implementation for storage of irradiated material within the spent fuel pool (SFP)
licensees post-event after action reports, self-assessments, and audits were reviewed to
      were reviewed and discussed in detail. Established radiological controls (including
assess the licensees ability to be self-critical, thus avoiding complacency and  
      airborne controls) were evaluated for selected U1R19 tasks including refueling and
degradation of their emergency preparedness program.  Inspectors reviewed the
      reactor cavity work activities, work in auxiliary building HRAs, and radwaste processing
licensees 10 CFR 50.54(q) change process, personnel training, and selected
      and storage. In addition, licensee controls for areas where dose rates could change
screenings and evaluations to assess adequacy. The inspectors toured facilities and
      significantly as a result of plant shutdown and refueling operations were reviewed and
reviewed equipment and facility maintenance records to assess licensees adequacy in  
      discussed.
maintaining them. The inspectors evaluated the capabilities of selected radiation
      Occupational workers adherence to selected RWPs and HP technician (HPT)
monitoring instrumentation to adequately support Emergency Action Level (EAL)  
      proficiency in providing job coverage were evaluated through direct observations and
declarations.  
      interviews with licensee staff. Electronic dosimeter (ED) alarm set points and worker
      stay times were evaluated against area radiation survey results for refueling and reactor
The inspection was conducted in accordance with NRC Inspection Procedure 71114.05,
      cavity work. ED alarm logs were reviewed and worker response to dose and dose rate
Maintenance of Emergency Preparedness. The applicable planning standards, related
      alarms during selected work activities was evaluated. For HRA tasks involving
10 CFR 50, Appendix E requirements, and 10 CFR 50.54(q) and (t) were used as
      significant dose rate gradients, e.g. reactor head O-ring work, the inspectors evaluated
reference criteria.
      the use and placement of whole body and extremity dosimetry to monitor worker
      exposure.
The inspectors reviewed various documents which are listed in the Attachment. This
                                                                                        Enclosure
inspection activity satisfied one inspection sample for the maintenance of emergency
preparedness on a biennial basis.  
  b.  
Findings
No findings were identified.  


                                            19
    Control of Radioactive Material: The inspectors observed surveys of material and
18
    personnel being released from the RCA using small article monitor, personnel
    contamination monitor, and portal monitor instruments. The inspectors reviewed the last
Enclosure
    two calibration records for selected release point survey instruments and discussed
2.
    equipment sensitivity, alarm set points, and release program guidance with licensee
RADIATION SAFETY (RS)
    staff. The inspectors compared recent 10 CFR Part 61 results for the Dry Active Waste
 
    (DAW) radioactive waste stream with radionuclides used in calibration sources to
Cornerstones:  Occupational Radiation Safety (OS) and Public Radiation Safety (PS)
    evaluate the appropriateness and accuracy of release survey instrumentation. The
    inspectors also reviewed records of leak tests on selected sealed sources and discussed
2RS1 Radiological Hazard Assessment and Exposure Controls
    nationally tracked source transactions with licensee staff.
 
    Problem Identification and Resolution: PERs associated with radiological hazard
  a.
    assessment and control were reviewed and assessed. The inspectors evaluated the
Inspection Scope
    licensees ability to identify and resolve the issues in accordance with procedure NPG-
    SPP-22.300, Corrective Action Program, Rev. 0. The inspectors also evaluated the
    scope of the licensees internal audit program and reviewed recent assessment results.
Hazard Assessment and Instructions to Workers: During facility tours, the inspectors  
    Radiation protection activities were evaluated against the requirements of UFSAR
directly observed labeling of radioactive material and postings for radiation areas, high
    Section 12; TS Sections 6.8 and 6.12; 10 CFR Parts 19 and 20; and approved licensee
radiation areas (HRAs), and airborne radioactivity areas established within the  
    procedures. Licensee programs for monitoring materials and personnel released from
radiologically controlled area (RCA) of the Unit 1 containment, Unit 1 and Unit 2 auxiliary
    the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of
buildings, Independent Spent Fuel Storage Installation (ISFSI), and radioactive waste
    Radioactively Contaminated Material. Documents reviewed are listed in the
(radwaste) processing and storage locations. The inspectors independently measured
    Attachment. The inspectors completed one sample.
radiation dose rates or directly observed conduct of licensee radiation surveys for RCA
bFindings
areas in the Unit 1 containment, Unit 1 and Unit 2 Auxiliary buildings, and ISFSI. The  
    No findings were identified.
inspectors reviewed survey records for several plant areas including surveys for alpha
2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and
emitters, airborne radioactivity, and pre-job surveys for selected Unit 1 Refueling Outage
    Transportation
19 (U1R19) tasks. The inspectors also discussed changes to plant operations that could
aInspection Scope
contribute to changing radiological conditions since the last inspection and reviewed  
    Waste Processing and Characterization: During inspector walkdowns, accessible
U1R19 crud burst results and post crud burst dose rate surveys. For selected U1R19
    sections of the liquid and solid radwaste processing systems were assessed for material
outage jobs, the inspectors attended, or reviewed, pre-job briefings and radiation work
    condition and conformance with system design diagrams. Inspected equipment included
permit (RWP) details to assess communication of radiological control requirements and  
    radwaste storage tanks; resin transfer piping, resin, and filter packaging components;
current radiological conditions to workers. Selected U1R19 work activities included Unit
    and abandoned boric acid evaporator equipment. The inspectors discussed component
1 control rod drive mechanism duct work, Unit 1 Refueling Activities, Unit 1 Head O-ring
    function, processing system changes, and radwaste program implementation with
Surface Work & Inspection, and work in the Unit 1 Equipment Pit and transfer canal.  
    licensee staff.
    The radionuclide characterizations for 2010, and 2012, for selected waste streams were
Hazard Control and Work Practices:  The inspectors evaluated access barrier
    reviewed and discussed with Radwaste/Transportation staff. For primary resin, reactor
effectiveness for selected Unit 1 and Unit 2 Locked High Radiation Area (LHRA) and  
    coolant system filters, and DAW, the inspectors evaluated analyses for hard-to-detect
Very High Radiation Area (VHRA) locations. Changes to procedural guidance for LHRA
    nuclides, reviewed the use of scaling factors, and examined quality assurance
and VHRA controls were discussed with health physics (HP) supervisors.  Controls and  
    comparison results between licensee waste stream characterizations and outside
their implementation for storage of irradiated material within the spent fuel pool (SFP)
    laboratory data. Waste stream mixing and concentration averaging methodology for
were reviewed and discussed in detailEstablished radiological controls (including
    resins and filters was evaluated and discussed with Radwaste/Transportation staff. The
airborne controls) were evaluated for selected U1R19 tasks including refueling and
                                                                                      Enclosure
reactor cavity work activities, work in auxiliary building HRAs, and radwaste processing
and storageIn addition, licensee controls for areas where dose rates could change
significantly as a result of plant shutdown and refueling operations were reviewed and
discussed.  
Occupational workers adherence to selected RWPs and HP technician (HPT)
proficiency in providing job coverage were evaluated through direct observations and  
interviews with licensee staff. Electronic dosimeter (ED) alarm set points and worker
stay times were evaluated against area radiation survey results for refueling and reactor
cavity work.  ED alarm logs were reviewed and worker response to dose and dose rate
alarms during selected work activities was evaluated. For HRA tasks involving
significant dose rate gradients, e.g. reactor head O-ring work, the inspectors evaluated  
the use and placement of whole body and extremity dosimetry to monitor worker
exposure.  


                                        20
  inspectors also reviewed the licensees procedural guidance for monitoring changes in
19
  waste stream isotopic mixtures. The 10 CFR 61 analysis results were also discussed
  with Chemistry personnel.
Enclosure
  Radioactive Material Storage: During walkdowns of indoor and outdoor radioactive
  material storage areas, the inspectors observed the physical condition and labeling of
Control of Radioactive Material: The inspectors observed surveys of material and  
  storage containers and the posting of Radioactive Material Areas. The inspectors also
personnel being released from the RCA using small article monitor, personnel
  reviewed licensee procedural guidance for storage and monitoring of radioactive
contamination monitor, and portal monitor instruments. The inspectors reviewed the last
  material.
two calibration records for selected release point survey instruments and discussed
  Transportation: The inspectors observed a shipment of vendor equipment during the
equipment sensitivity, alarm set points, and release program guidance with licensee  
  week of inspection. The inspectors reviewed shipping procedure requirements and
staff. The inspectors compared recent 10 CFR Part 61 results for the Dry Active Waste
  discussed preparation of shipping documents, package marking and labeling, and
(DAW) radioactive waste stream with radionuclides used in calibration sources to
  interviewed shipping technicians regarding Department of Transportation (DOT)
evaluate the appropriateness and accuracy of release survey instrumentation. The
  regulations.
inspectors also reviewed records of leak tests on selected sealed sources and discussed
  Selected shipping records were reviewed for consistency with licensee procedures and
nationally tracked source transactions with licensee staff.
  compliance with NRC and DOT regulations. The inspectors reviewed emergency
  response information, DOT shipping package classification, waste classification,
Problem Identification and Resolution: PERs associated with radiological hazard
  radiation survey results, and evaluated whether receiving licensees were authorized to
assessment and control were reviewed and assessed. The inspectors evaluated the  
  accept the packages. Licensee procedures for handling shipping containers were
licensees ability to identify and resolve the issues in accordance with procedure NPG-
  compared to Certificate of Compliance requirements and manufacturer
SPP-22.300, Corrective Action Program, Rev. 0.  The inspectors also evaluated the  
  recommendations. In addition, training records for selected individuals currently
scope of the licensees internal audit program and reviewed recent assessment results.  
  qualified to ship radioactive material were reviewed.
  Radwaste processing activities and equipment configuration were reviewed for
Radiation protection activities were evaluated against the requirements of UFSAR
  compliance with the licensees Process Control Program and UFSAR, Chapter 11.
Section 12; TS Sections 6.8 and 6.12; 10 CFR Parts 19 and 20; and approved licensee
  Waste stream characterization analyses were reviewed against regulations detailed in
procedures.  Licensee programs for monitoring materials and personnel released from
  10 CFR Part 20, 10 CFR Part 61, and guidance provided in the Branch Technical
the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of
  Position on Waste Classification (1983). Radioactive material and waste storage
Radioactively Contaminated Material.  Documents reviewed are listed in the  
  activities were reviewed against the requirements of 10 CFR Part 20. Transportation
Attachment. The inspectors completed one sample.  
  program implementation was reviewed against regulations detailed in 10 CFR Part 20,
  10 CFR Part 71, 49 CFR Parts 172-178, as well as the guidance provided in NUREG-
  b.
  1608. Training activities were assessed against 49 CFR Part 172, Subpart H.
Findings  
  Problem Identification and Resolution: The inspectors reviewed PERs in the area of
  radwaste processing and transportation. The inspectors evaluated the licensees ability
No findings were identified.  
  to identify and resolve the issues in accordance with procedure NPG-SPP-22.300,. The
  inspectors also evaluated the scope of the licensees internal audit program and
2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and
  reviewed recent assessment results. Documents reviewed are listed in the Attachment.
Transportation
  The inspectors completed one sample.
b. Findings
  a.
  No findings were identified.
Inspection Scope
                                                                                  Enclosure
Waste Processing and Characterization:  During inspector walkdowns, accessible
sections of the liquid and solid radwaste processing systems were assessed for material
condition and conformance with system design diagrams.  Inspected equipment included
radwaste storage tanks; resin transfer piping, resin, and filter packaging components;
and abandoned boric acid evaporator equipment.  The inspectors discussed component
function, processing system changes, and radwaste program implementation with
licensee staff.
The radionuclide characterizations for 2010, and 2012, for selected waste streams were
reviewed and discussed with Radwaste/Transportation staff.  For primary resin, reactor
coolant system filters, and DAW, the inspectors evaluated analyses for hard-to-detect
nuclides, reviewed the use of scaling factors, and examined quality assurance
comparison results between licensee waste stream characterizations and outside
laboratory data.  Waste stream mixing and concentration averaging methodology for
resins and filters was evaluated and discussed with Radwaste/Transportation staff.  The


                                            21
4.    OTHER ACTIVITIES
20
4OA1 Performance Indicator (PI) Verification
  a. Inspection Scope
Enclosure
      Occupational Radiation Safety Cornerstone: The inspectors reviewed the Occupational
inspectors also reviewed the licensees procedural guidance for monitoring changes in
      Exposure Control Effectiveness PI results for the Occupational Radiation Safety
waste stream isotopic mixtures.  The 10 CFR 61 analysis results were also discussed
      Cornerstone from October 2012 through October 2013. For the assessment period, the
with Chemistry personnel.
      inspectors reviewed ED alarm logs and selected PERs related to controls for exposure
      significant areas. The inspectors also reviewed licensee procedural guidance for
      collecting and documenting PI data. Documents reviewed are listed in the Attachment.
Radioactive Material Storage:  During walkdowns of indoor and outdoor radioactive
      The inspectors completed one sample.
material storage areas, the inspectors observed the physical condition and labeling of
      Emergency Preparedness Cornerstone:
storage containers and the posting of Radioactive Material Areas. The inspectors also  
      *    Drill/Exercise Performance (DEP)
reviewed licensee procedural guidance for storage and monitoring of radioactive
      *    Emergency Response Organization Drill Participation (ERO)
material.  
      *    Alert and Notification System Reliability (ANS)
      For the specified review period, the inspectors examined data reported to the NRC,
      procedural guidance for reporting PI information, and records used by the licensee to
Transportation:  The inspectors observed a shipment of vendor equipment during the  
      identify potential PI occurrences. The inspectors verified the accuracy of the PI for ERO
week of inspection. The inspectors reviewed shipping procedure requirements and
      drill and exercise performance through review of a sample of drill and event records.
discussed preparation of shipping documents, package marking and labeling, and
      The inspectors reviewed selected training records to verify the accuracy of the PI for
interviewed shipping technicians regarding Department of Transportation (DOT)  
      ERO drill participation for personnel assigned to key positions in the ERO. The
regulations.
      inspectors verified the accuracy of the PI for alert and notification system reliability
      through review of a sample of the licensees records of periodic system tests. The
      inspectors also interviewed the licensee personnel who were responsible for collecting
Selected shipping records were reviewed for consistency with licensee procedures and
      and evaluating the PI data. Documents reviewed are listed in the Attachment. This
compliance with NRC and DOT regulations.  The inspectors reviewed emergency
      inspection satisfied three inspection samples for PI verification on an annual basis.
response information, DOT shipping package classification, waste classification,  
  b. Findings
radiation survey results, and evaluated whether receiving licensees were authorized to  
      No findings were identified.
accept the packages. Licensee procedures for handling shipping containers were
4OA2 Problem Identification and Resolution
compared to Certificate of Compliance requirements and manufacturer
.1    Routine Review
recommendations. In addition, training records for selected individuals currently
  a. Inspection Scope
qualified to ship radioactive material were reviewed.  
      As required by IP 71152, Problem Identification and Resolution, and in order to help
      identify repetitive equipment failures or specific human performance issues for follow-up,
Radwaste processing activities and equipment configuration were reviewed for  
      the inspectors performed a daily screening of items entered into the licensees CAP.
compliance with the licensees Process Control Program and UFSAR, Chapter 11.
      This was accomplished by reviewing the description of each new PER and attending
Waste stream characterization analyses were reviewed against regulations detailed in
      daily management review committee meetings.
10 CFR Part 20, 10 CFR Part 61, and guidance provided in the Branch Technical
                                                                                        Enclosure
Position on Waste Classification (1983). Radioactive material and waste storage
activities were reviewed against the requirements of 10 CFR Part 20. Transportation
program implementation was reviewed against regulations detailed in 10 CFR Part 20,
10 CFR Part 71, 49 CFR Parts 172-178, as well as the guidance provided in NUREG-
1608. Training activities were assessed against 49 CFR Part 172, Subpart H.  
Problem Identification and Resolution:  The inspectors reviewed PERs in the area of
radwaste processing and transportation. The inspectors evaluated the licensees ability
to identify and resolve the issues in accordance with procedure NPG-SPP-22.300,.  The
inspectors also evaluated the scope of the licensees internal audit program and
reviewed recent assessment results.  Documents reviewed are listed in the Attachment. 
The inspectors completed one sample.
  b.  
Findings
No findings were identified.  


                                              22
  b. Findings
21
      No findings were identified.
.2    Annual Follow-up of Selected Issues
Enclosure
   a. Inspection Scope
4.  
      The inspectors performed an in-depth review of PER 665633, NRC identified freeze
OTHER ACTIVITIES
      protection issues. The inspectors reviewed the actions taken to determine if the
      licensee had adequately addressed the following attributes. Documents reviewed are
4OA1 Performance Indicator (PI) Verification
      listed in the Attachment. The inspectors completed one sample for Annual Follow-up of
      Selected Issues.
   a.  
      *   Complete, accurate and timely identification of the problem
Inspection Scope  
      *    Evaluation and disposition of operability and reportability issues
      *    Consideration of previous failures, extent of condition, generic or common cause
Occupational Radiation Safety Cornerstone:  The inspectors reviewed the Occupational
          implications
Exposure Control Effectiveness PI results for the Occupational Radiation Safety
      *    Prioritization and resolution of the issue commensurate with safety significance
Cornerstone from October 2012 through October 2013.  For the assessment period, the
      *    Identification of the root cause and contributing causes of the problem
inspectors reviewed ED alarm logs and selected PERs related to controls for exposure
      *    Identification and implementation of corrective actions commensurate with the safety
significant areas. The inspectors also reviewed licensee procedural guidance for
          significance of the issue
collecting and documenting PI data. Documents reviewed are listed in the Attachment.
   b. Findings
The inspectors completed one sample.
      No findings were identified.
.3    Semiannual Trend Review
Emergency Preparedness Cornerstone:
   a. Inspection Scope
      As required by IP 71152, the inspectors performed a review of the licensees corrective
      action program and associated documents to identify trends that could indicate the
*
      existence of a more significant safety issue. The inspectors review was focused on
Drill/Exercise Performance (DEP)
      repetitive equipment issues, but also included licensee trending efforts and licensee
*
      human performance results. The inspectors review nominally considered the twelve-
Emergency Response Organization Drill Participation (ERO)
      month period of January 2013 through December 2013, although some examples
*  
      expanded beyond those dates when the scope of the trend warranted. Specifically, the
Alert and Notification System Reliability (ANS)
      inspectors considered the results of daily inspector screening discussed in Section
      4OA2.1 and reviewed licensee trend reports for the period in order to determine the
For the specified review period, the inspectors examined data reported to the NRC,
      existence of any adverse trends that the licensee may not have previously identified.
procedural guidance for reporting PI information, and records used by the licensee to
      Documents reviewed are listed in the Attachment. The inspectors completed one
identify potential PI occurrences.  The inspectors verified the accuracy of the PI for ERO
      sample for Semiannual Trend Review.
drill and exercise performance through review of a sample of drill and event records. 
   b. Findings and Observations
The inspectors reviewed selected training records to verify the accuracy of the PI for
      No findings were identified. In general, the licensee had identified trends and
ERO drill participation for personnel assigned to key positions in the ERO.  The
                                                                                        Enclosure
inspectors verified the accuracy of the PI for alert and notification system reliability
through review of a sample of the licensees records of periodic system tests.  The
inspectors also interviewed the licensee personnel who were responsible for collecting
and evaluating the PI data.  Documents reviewed are listed in the Attachment.  This
inspection satisfied three inspection samples for PI verification on an annual basis.
   b.  
Findings  
No findings were identified.  
4OA2 Problem Identification and Resolution
.1
Routine Review  
   a.  
Inspection Scope  
As required by IP 71152, Problem Identification and Resolution, and in order to help
identify repetitive equipment failures or specific human performance issues for follow-up,  
the inspectors performed a daily screening of items entered into the licensees CAP.
This was accomplished by reviewing the description of each new PER and attending
daily management review committee meetings.     


                                            23
      appropriately addressed them in their CAP. The inspectors evaluated the licensee
22
      trending methodology and observed that the licensee had performed a detailed review.
      The licensee routinely reviewed cause codes, involved organizations, key words, and
Enclosure
      system links to identify potential trends in their data. The inspectors compared the
  b.  
      licensee process results with the results of the inspectors daily screening. No
Findings
      previously unidentified trends of significance were identified.
.4    Annual Follow-up of Operator Workarounds
   a. Inspection Scope
No findings were identified.
      The inspectors reviewed the operator workaround (OWA) program to verify that OWAs
      were identified at an appropriate threshold, were entered into the CAP, and that
.2
      corrective actions were appropriate and timely. Specifically, the inspectors reviewed the
Annual Follow-up of Selected Issues
      licensees workaround lists and repair schedules, reviewed CAP word searches,
      conducted tours and interviewed operators and operations department support staff.
   a.  
      Additionally, the inspectors checked for undocumented workarounds by observing
Inspection Scope  
      operators perform rounds, reviewed operator deficiency lists, reviewed appropriate
      system health documents, attended plant health committee meetings, and verified that
The inspectors performed an in-depth review of PER 665633, NRC identified freeze
      identified program deficiencies were corrected. The inspectors evaluated all
protection issues. The inspectors reviewed the actions taken to determine if the  
      workarounds for their aggregate impact. Documents reviewed are listed in the
licensee had adequately addressed the following attributes. Documents reviewed are  
      Attachment. The inspectors completed one sample for Annual Follow-up of Operator
listed in the Attachment. The inspectors completed one sample for Annual Follow-up of  
      Workarounds.
Selected Issues.  
   b. Findings
      No findings were identified.
*
4OA5 Other Activities
Complete, accurate and timely identification of the problem
.1    (Closed) Unresolved Item (URI) 050000327/2013004-01, Water Intrusion into Actuator of
*
      Valve 1-FCV-63-72
Evaluation and disposition of operability and reportability issues
   a. Inspection Scope
*
      The inspectors opened this URI as a result of water intrusion into the actuator of 1-FCV-
Consideration of previous failures, extent of condition, generic or common cause
      63-72, which is the A train containment sump suction for the Unit 1 A RHR train. This
implications
      issue was noted during an operability inspection conducted last quarter. The inspectors
*
      determined more inspection was required in order to resolve the issue. On August 8,
Prioritization and resolution of the issue commensurate with safety significance
      2013, an operator noted the valve exhibited dual indication and on August 14, a related
*
      valve, 1-FCV-74-3, failed its periodic stroke test. The following day, 1-FCV-63-72 was
Identification of the root cause and contributing causes of the problem
      noted to be failed as well due to a large of amount of water buildup in the actuator. A
*
      subsequent root cause of the failure was completed during this inspection period and
Identification and implementation of corrective actions commensurate with the safety
      concluded the water intrusion was due to groundwater which migrated through the wall
significance of the issue
      of the RHR valve vault room and into the valve conduit. Although the circumstances
      regarding the water intrusion may have been beyond the licensees ability to predict, the
   b.  
                                                                                      Enclosure
Findings  
No findings were identified.  
.3
Semiannual Trend Review 
   a.  
Inspection Scope  
As required by IP 71152, the inspectors performed a review of the licensees corrective
action program and associated documents to identify trends that could indicate the  
existence of a more significant safety issue. The inspectors review was focused on
repetitive equipment issues, but also included licensee trending efforts and licensee
human performance results. The inspectors review nominally considered the twelve-
month period of January 2013 through December 2013, although some examples
expanded beyond those dates when the scope of the trend warranted. Specifically, the
inspectors considered the results of daily inspector screening discussed in Section
4OA2.1 and reviewed licensee trend reports for the period in order to determine the  
existence of any adverse trends that the licensee may not have previously identified. 
Documents reviewed are listed in the Attachment. The inspectors completed one
sample for Semiannual Trend Review. 
  b.
Findings and Observations
No findings were identified.  In general, the licensee had identified trends and


                                        24
  inspectors noted there were opportunities before August 14 to identify and correct the
23
  deficient condition. Thus, the inspectors identified the following non-cited violation
  (NCV) as discussed below. Documents reviewed are listed in the Attachment.
Enclosure
b. Findings
appropriately addressed them in their CAP.  The inspectors evaluated the licensee
  Introduction: A self-revealing Green NCV of 10 CFR 50 Appendix B, Criterion XVI,
trending methodology and observed that the licensee had performed a detailed review. 
   Corrective Action, was identified for the licensees failure to correct a condition adverse
The licensee routinely reviewed cause codes, involved organizations, key words, and
  to quality within a reasonable amount of time. Timely corrective actions were not taken
system links to identify potential trends in their data. The inspectors compared the  
  to correct a dual position indication (open and closed lights both illuminated) on the Unit
licensee process results with the results of the inspectors daily screening. No
  1 A train RHR containment sump suction flow control valve 1-FCV-63-72.
previously unidentified trends of significance were identified.  
  Description: On August 8 at 0709, the Unit 1 control room operator noted that valve 1-
  FCV-63-72 showed dual position indication on the control board. This valve is the A
.4
  train RHR suction valve from the reactor containment sump and is normally closed,
Annual Follow-up of Operator Workarounds
  showing only a single position indication lamp on the control board. Valve 1-FCV-63-72
   was verified to be locally closed. No other activities were noted that would have caused
   a.
  the valve to come off its closed seat. Initial troubleshooting for the dual indication
Inspection Scope
  consisted of: 1) a visual inspection of the valve; 2) a visual inspection of the motor
  control center (MCC) cubicle during an attempted closure of the valve; 3) a review of the
The inspectors reviewed the operator workaround (OWA) program to verify that OWAs
  wiring diagram by a troubleshooting team; 4) replacement of the MCC light indicating
were identified at an appropriate threshold, were entered into the CAP, and that
  bulb; and 5) a visual inspection of the main control room (MCR) hand switch. Based on
corrective actions were appropriate and timely.  Specifically, the inspectors reviewed the
  the troubleshooting teams analysis of the wiring diagrams, no impact was expected on
licensees workaround lists and repair schedules, reviewed CAP word searches,
  the interlocks associated with 1-FCV-63-72. The team initially concluded that the most
conducted tours and interviewed operators and operations department support staff.
   likely cause of the indication was a short circuit in the control power indication in the
Additionally, the inspectors checked for undocumented workarounds by observing
  MCR valve hand switch. Based on this conclusion, plus the fact that the valve is not
operators perform rounds, reviewed operator deficiency lists, reviewed appropriate
  normally stroked at power (due to concerns of accidently transferring borated water from
system health documents, attended plant health committee meetings, and verified that  
  the RWST to the containment sump), the licensee chose not to immediately stroke test
identified program deficiencies were corrected. The inspectors evaluated all
  1-FCV-63-72. Instead, the licensee declared the position indication for the valve
workarounds for their aggregate impact.  Documents reviewed are listed in the  
  inoperable per Post Accident Monitoring requirements as delineated in TS 3.9.1. This
Attachment. The inspectors completed one sample for Annual Follow-up of Operator
  was a 30 day limiting condition for operation. The licensee then began development of a
Workarounds.
  troubleshooting plan which would require more intrusive troubleshooting of the issue
  starting the following week.
   b.  
  On August 14 at 2315, during a routine quarterly inservice testing valve stroke activity,
Findings
  valve 1-FCV-74-3 failed to stroke in the closed direction from the control room. This
  valve is the A train RHR suction valve from the RWST and is normally open. Valve 1-
No findings were identified. 
  FCV-74-3 was immediately declared out of service and the 72-hour Emergency Core
  Cooling Systems (ECCS) TS 3.5.2 action statement was entered. During
4OA5 Other Activities
  troubleshooting, operators attempted to close valve 1-FCV-74-3 remotely from the MCC
  cubicle. This action blew control power fuses. The licensee then attempted local
.1  
  manual operation and noted 1-FVC-74-3 could be manually closed without binding.
(Closed) Unresolved Item (URI) 050000327/2013004-01, Water Intrusion into Actuator of  
  Valve 1-FCV-74-3 was partially manually closed and then reopened from the MCC
Valve 1-FCV-63-72  
  without incident. Due to the relationship between valves 1-FCV-63-72 and 1-FCV-74-3
  (interlocks, shared wiring in junction boxes, etc.) the licensee suspected that the failure
   a.
  of valve 1-FCV-74-3 to close and valve 1-FCV-63-72 dual position indication were
Inspection Scope
  related.
                                                                                      Enclosure
The inspectors opened this URI as a result of water intrusion into the actuator of 1-FCV-
63-72, which is the A train containment sump suction for the Unit 1 A RHR train. This  
issue was noted during an operability inspection conducted last quarter. The inspectors
determined more inspection was required in order to resolve the issue.  On August 8,
2013, an operator noted the valve exhibited dual indication and on August 14, a related
valve, 1-FCV-74-3, failed its periodic stroke test. The following day, 1-FCV-63-72 was  
noted to be failed as well due to a large of amount of water buildup in the actuator. A
subsequent root cause of the failure was completed during this inspection period and  
concluded the water intrusion was due to groundwater which migrated through the wall
of the RHR valve vault room and into the valve conduit. Although the circumstances
regarding the water intrusion may have been beyond the licensees ability to predict, the 


                                        25
The licensee subsequently opened the 1-FCV-63-72 actuator and noted that a
24
significant amount of water had accumulated inside the actuator. This water caused
significant electrical shorting in the valve control circuit and rendered the valve
Enclosure
inoperable. Also, the water affected valve 1-FCV-74-3, as this valve utilizes contacts
inspectors noted there were opportunities before August 14 to identify and correct the
from valve 1-FCV-63-72 circuitry. It was noted that a low current short caused the failure
deficient condition.  Thus, the inspectors identified the following non-cited violation
of the closing coil for valve 1-FCV-74-3. Following repairs to both 1-FCV-63-72 and
(NCV) as discussed below.  Documents reviewed are listed in the Attachment.
1-FCV-74-3, the ECCS system was returned to operable status on August 17 at 0200.
  b.
Findings
Introduction:  A self-revealing Green NCV of 10 CFR 50 Appendix B, Criterion XVI,
Corrective Action, was identified for the licensees failure to correct a condition adverse
to quality within a reasonable amount of time.  Timely corrective actions were not taken
to correct a dual position indication (open and closed lights both illuminated) on the Unit
1 A train RHR containment sump suction flow control valve 1-FCV-63-72.   
Description:  On August 8 at 0709, the Unit 1 control room operator noted that valve 1-
FCV-63-72 showed dual position indication on the control board.  This valve is the A
train RHR suction valve from the reactor containment sump and is normally closed,
showing only a single position indication lamp on the control board.  Valve 1-FCV-63-72
was verified to be locally closed.  No other activities were noted that would have caused
the valve to come off its closed seat.  Initial troubleshooting for the dual indication
consisted of:  1) a visual inspection of the valve; 2) a visual inspection of the motor
control center (MCC) cubicle during an attempted closure of the valve; 3) a review of the
wiring diagram by a troubleshooting team; 4) replacement of the MCC light indicating
bulb; and 5) a visual inspection of the main control room (MCR) hand switch.  Based on
the troubleshooting teams analysis of the wiring diagrams, no impact was expected on
the interlocks associated with 1-FCV-63-72.  The team initially concluded that the most
likely cause of the indication was a short circuit in the control power indication in the
MCR valve hand switch.  Based on this conclusion, plus the fact that the valve is not
normally stroked at power (due to concerns of accidently transferring borated water from
the RWST to the containment sump), the licensee chose not to immediately stroke test
1-FCV-63-72.  Instead, the licensee declared the position indication for the valve
inoperable per Post Accident Monitoring requirements as delineated in TS 3.9.1.  This
was a 30 day limiting condition for operation.  The licensee then began development of a
troubleshooting plan which would require more intrusive troubleshooting of the issue
starting the following week.
On August 14 at 2315, during a routine quarterly inservice testing valve stroke activity,
valve 1-FCV-74-3 failed to stroke in the closed direction from the control room.  This
valve is the A train RHR suction valve from the RWST and is normally open.  Valve 1-
FCV-74-3 was immediately declared out of service and the 72-hour Emergency Core
Cooling Systems (ECCS) TS 3.5.2 action statement was entered.  During
troubleshooting, operators attempted to close valve 1-FCV-74-3 remotely from the MCC
cubicle.  This action blew control power fuses.  The licensee then attempted local
manual operation and noted 1-FVC-74-3 could be manually closed without binding. 
Valve 1-FCV-74-3 was partially manually closed and then reopened from the MCC
without incident.  Due to the relationship between valves 1-FCV-63-72 and 1-FCV-74-3
(interlocks, shared wiring in junction boxes, etc.) the licensee suspected that the failure
of valve 1-FCV-74-3 to close and valve 1-FCV-63-72 dual position indication were
related. 
 
25  
Enclosure
The licensee subsequently opened the 1-FCV-63-72 actuator and noted that a  
significant amount of water had accumulated inside the actuator. This water caused  
significant electrical shorting in the valve control circuit and rendered the valve  
inoperable. Also, the water affected valve 1-FCV-74-3, as this valve utilizes contacts  
from valve 1-FCV-63-72 circuitry. It was noted that a low current short caused the failure  
of the closing coil for valve 1-FCV-74-3. Following repairs to both 1-FCV-63-72 and    
1-FCV-74-3, the ECCS system was returned to operable status on August 17 at 0200.  
The licensees past operability determination concluded that 1-FCV-63-72 and 1-FCV-
The licensees past operability determination concluded that 1-FCV-63-72 and 1-FCV-
74-3 were likely inoperable beginning on August 8 when 1-FCV-63-72 was noted to have
74-3 were likely inoperable beginning on August 8 when 1-FCV-63-72 was noted to have  
a dual indication. Thus the A train ECCS system was most likely inoperable for
a dual indication. Thus the A train ECCS system was most likely inoperable for  
approximately nine days, which exceeded the TS allowable outage time. On October
approximately nine days, which exceeded the TS allowable outage time. On October  
21, 2013, Licensee Event Report 50-327/2013-003 was submitted as a result of this
21, 2013, Licensee Event Report 50-327/2013-003 was submitted as a result of this  
issue. The licensee concluded that the source of the water was ground water that had
issue. The licensee concluded that the source of the water was ground water that had  
migrated through the concrete ceiling that housed the valve and actuator cables. The
migrated through the concrete ceiling that housed the valve and actuator cables. The  
ground water leaked through the threaded penetration seal and inside the conduit and
ground water leaked through the threaded penetration seal and inside the conduit and  
flowed down into the valve actuator. During the most recent Unit 1 refueling outage in
flowed down into the valve actuator. During the most recent Unit 1 refueling outage in  
November 2013, the licensee redesigned the conduit penetration to prevent the intrusion
November 2013, the licensee redesigned the conduit penetration to prevent the intrusion  
of moisture into the conduit. The licensee noted the rate of moisture intrusion was most
of moisture into the conduit. The licensee noted the rate of moisture intrusion was most  
likely higher in the recent months due to a higher than normal amount of rainfall that
likely higher in the recent months due to a higher than normal amount of rainfall that  
temporarily raised the water table in the vicinity of the plant. The inspectors also noted
temporarily raised the water table in the vicinity of the plant. The inspectors also noted  
that on February 29, 2012, the licensee discovered water buildup in the actuator of 1-
that on February 29, 2012, the licensee discovered water buildup in the actuator of 1-
FCV-63-72. This deficiency was entered into the CAP; however it appears that this
FCV-63-72. This deficiency was entered into the CAP; however it appears that this  
precursor was not adequately evaluated such that continued water intrusion ultimately
precursor was not adequately evaluated such that continued water intrusion ultimately  
led to the failure noted on August 8, 2013.
led to the failure noted on August 8, 2013.  
Analysis: The licensees failure to take timely actions to correct a condition adverse to
   
quality was a performance deficiency. The inspectors concluded that testing and
Analysis: The licensees failure to take timely actions to correct a condition adverse to  
inspection could have determined that valve 1-FCV-63-72 was inoperable much earlier
quality was a performance deficiency. The inspectors concluded that testing and  
than August 14 when it was noted that RHR suction valve to the RWST, 1-FCV-74-3, did
inspection could have determined that valve 1-FCV-63-72 was inoperable much earlier  
not pass its routine surveillance test. This finding was determined to be more than minor
than August 14 when it was noted that RHR suction valve to the RWST, 1-FCV-74-3, did  
because it was associated with the Design Control attribute of the Mitigating Systems
not pass its routine surveillance test. This finding was determined to be more than minor  
cornerstone and adversely affected the cornerstones objective to ensure the availability,
because it was associated with the Design Control attribute of the Mitigating Systems  
reliability, and capability of systems that respond to initiating events to prevent
cornerstone and adversely affected the cornerstones objective to ensure the availability,  
undesirable consequences (i.e., core damage). Specifically, the finding reduced the
reliability, and capability of systems that respond to initiating events to prevent  
reliability and capability of the A train RHR system to perform its safety function as
undesirable consequences (i.e., core damage). Specifically, the finding reduced the  
designed. Using IMC 0609.04, Initial Characterization of Findings, dated June 19,
reliability and capability of the A train RHR system to perform its safety function as  
2012, and IMC 0609, Appendix A, Exhibit 4 - External Events Screening Questions,
designed. Using IMC 0609.04, Initial Characterization of Findings, dated June 19,  
dated June 19, 2012, the finding required a detailed risk analysis as the A RHR system
2012, and IMC 0609, Appendix A, Exhibit 4 - External Events Screening Questions,  
was inoperable beyond its TS-allowed outage time of 72 hours. The detailed risk
dated June 19, 2012, the finding required a detailed risk analysis as the A RHR system  
analysis concluded that the finding was of very low safety significance (Green).
was inoperable beyond its TS-allowed outage time of 72 hours. The detailed risk  
A Phase 3 analysis was performed by the regional Senior Reactor Analyst to determine
analysis concluded that the finding was of very low safety significance (Green).  
the impact of the finding. The analysis assumed a recoverable failure of the 1-FCV-63-
72 valve, along with a dependent failure of the 1-FCV-74-3 valve. The major impacts
A Phase 3 analysis was performed by the regional Senior Reactor Analyst to determine  
were in the swapover from the RWST to the containment sump as the source of water to
the impact of the finding. The analysis assumed a recoverable failure of the 1-FCV-63-
                                                                                    Enclosure
72 valve, along with a dependent failure of the 1-FCV-74-3 valve. The major impacts  
were in the swapover from the RWST to the containment sump as the source of water to


                                              26
      mitigate medium and smaller LOCA sequences. Because of the low exposure time, the
26  
      availability of the opposite train, and the ability of the operations staff to operate the
      effected valves manually, the finding was determined to be Green.
Enclosure
      The cause of this finding was determined to have a cross-cutting aspect relating to the
mitigate medium and smaller LOCA sequences. Because of the low exposure time, the  
      proper classification, prioritization, and evaluation of operability and reportability of
availability of the opposite train, and the ability of the operations staff to operate the  
      conditions adverse to quality in the Corrective Action component of the Problem
effected valves manually, the finding was determined to be Green.  
      Identification and Resolution area, in that, on February 29, 2012, the licensee discovered
      water buildup in the actuator of 1-FCV-63-72 and did not adequately evaluated the
The cause of this finding was determined to have a cross-cutting aspect relating to the  
      condition adverse to quality such that continued water intrusion ultimately led to the
proper classification, prioritization, and evaluation of operability and reportability of  
      failure noted on August 8, 2013. [P.1(c)]
conditions adverse to quality in the Corrective Action component of the Problem  
      Enforcement: Title 10 of the Code of Federal Regulations Part 50, Appendix B, Criterion
Identification and Resolution area, in that, on February 29, 2012, the licensee discovered  
      XVI, Corrective Action, requires, in part, that measures shall be established to assure
water buildup in the actuator of 1-FCV-63-72 and did not adequately evaluated the  
      that conditions adverse to quality, such as failures, malfunctions, deficiencies,
condition adverse to quality such that continued water intrusion ultimately led to the  
      deviations, defective material and equipment, and non-conformances are promptly
failure noted on August 8, 2013. [P.1(c)]  
      identified and corrected. Contrary to the above, from August 8 through August 17, 2013,
      the licensee failed to assure that a condition adverse to quality, the failure of valve FCV-
      63-72, was corrected in a timely manner. Specifically, the licensee failed to sufficiently
Enforcement: Title 10 of the Code of Federal Regulations Part 50, Appendix B, Criterion  
      evaluate and correct a moisture intrusion problem associated with the RHR containment
XVI, Corrective Action, requires, in part, that measures shall be established to assure  
      suction motor-operated valve. Corrective actions taken by the licensee included
that conditions adverse to quality, such as failures, malfunctions, deficiencies,  
      redesigning and modifying the conduit penetration to prevent the intrusion of moisture
deviations, defective material and equipment, and non-conformances are promptly  
      into the conduit. The violation was entered into the licensees CAP as PER 772193.
identified and corrected. Contrary to the above, from August 8 through August 17, 2013,  
      This violation is being treated as an NCV, consistent with Section 2.3.2 of the
the licensee failed to assure that a condition adverse to quality, the failure of valve FCV-
      Enforcement Policy and will be identified as NCV 05000327/2013005-01, Unit 1 Train
63-72, was corrected in a timely manner. Specifically, the licensee failed to sufficiently  
      A RHR Containment Suction Valve Failure.
evaluate and correct a moisture intrusion problem associated with the RHR containment  
.2   Quarterly Resident Inspector Observations of Security Personnel and Activities
suction motor-operated valve. Corrective actions taken by the licensee included  
   a. Inspection Scope
redesigning and modifying the conduit penetration to prevent the intrusion of moisture  
      During the inspection period, the inspectors conducted observations of security force
into the conduit. The violation was entered into the licensees CAP as PER 772193.
      personnel and activities to ensure that the activities were consistent with licensee
This violation is being treated as an NCV, consistent with Section 2.3.2 of the  
      security procedures and regulatory requirements relating to nuclear plant security.
Enforcement Policy and will be identified as NCV 05000327/2013005-01, Unit 1 Train  
      These observations took place during both normal and off-normal plant working hours.
A RHR Containment Suction Valve Failure.  
      These quarterly resident inspector observations of security force personnel and activities
      did not constitute any additional inspection samples. Rather, they were considered an
.2  
      integral part of the inspectors normal plant status review and inspection activities.
Quarterly Resident Inspector Observations of Security Personnel and Activities  
   b. Findings
      No findings were identified.
   a.  
                                                                                            Enclosure
Inspection Scope  
During the inspection period, the inspectors conducted observations of security force  
personnel and activities to ensure that the activities were consistent with licensee  
security procedures and regulatory requirements relating to nuclear plant security.
These observations took place during both normal and off-normal plant working hours.  
These quarterly resident inspector observations of security force personnel and activities  
did not constitute any additional inspection samples. Rather, they were considered an  
integral part of the inspectors normal plant status review and inspection activities.  
   b.  
Findings  
No findings were identified.  


                                          27
.3   Review of the Operation of an Independent Spent Fuel Storage Installation (ISFSI)
27  
      (60855.1)
   a. Inspection Scope
Enclosure
      The inspectors performed a walkdown with the field operator of the ISFSI storage pad on
.3  
      December 26, 2013, to verify that operations were conducted in a safe manner in
Review of the Operation of an Independent Spent Fuel Storage Installation (ISFSI)  
      accordance with approved procedures and without undue risk to the health and safety of
(60855.1)  
      the public. The inspectors noted that there were 40 multi-purpose canisters (MPCs)
      positioned on the ISFSI pad. The inspectors verified the MPC vents were in good
   a.  
      condition and free of obstruction. The inspectors also verified natural circulation within
Inspection Scope  
      the MPCs. The inspectors verified that any ISFSI problems were placed in the CAP.
      The inspectors also reviewed ISFSI document control practices to verify that changes to
The inspectors performed a walkdown with the field operator of the ISFSI storage pad on  
      the required ISFSI procedures and equipment were performed in accordance with
December 26, 2013, to verify that operations were conducted in a safe manner in  
      guidelines established in local procedures and 10 CFR 72.48. Documents reviewed are
accordance with approved procedures and without undue risk to the health and safety of  
      listed in the Attachment.
the public. The inspectors noted that there were 40 multi-purpose canisters (MPCs)  
   b. Findings
positioned on the ISFSI pad. The inspectors verified the MPC vents were in good  
      No findings were identified.
condition and free of obstruction. The inspectors also verified natural circulation within  
4OA6 Meetings
the MPCs. The inspectors verified that any ISFSI problems were placed in the CAP.
.1   Exit Meeting Summary
The inspectors also reviewed ISFSI document control practices to verify that changes to  
      On January 13, 2014, the resident inspectors presented the inspection results to Mr.
the required ISFSI procedures and equipment were performed in accordance with  
      Carlin and other members of his staff, who acknowledged the finding. The inspectors
guidelines established in local procedures and 10 CFR 72.48. Documents reviewed are  
      asked the licensee whether any of the material examined during the inspection should
listed in the Attachment.  
      be considered proprietary. No proprietary information was identified.
      ATTACHMENT: SUPPLEMENTARY INFORMATION
   b.  
                                                                                        Enclosure
Findings  
No findings were identified.  
4OA6 Meetings  
.1  
Exit Meeting Summary  
On January 13, 2014, the resident inspectors presented the inspection results to Mr.  
Carlin and other members of his staff, who acknowledged the finding. The inspectors  
asked the licensee whether any of the material examined during the inspection should  
be considered proprietary. No proprietary information was identified.  
ATTACHMENT: SUPPLEMENTARY INFORMATION


                                SUPPLEMENTARY INFORMATION
                                    KEY POINTS OF CONTACT
Attachment
Licensee personnel
SUPPLEMENTARY INFORMATION  
J. Alfultis, Director of Modifications & Projects
J. Carlin, Site Vice President
KEY POINTS OF CONTACT  
J. Cross, Chemistry Manager
A. Day, Radiation Protection Manager
Licensee personnel  
D. Erb, Work Control Manager
J. Alfultis, Director of Modifications & Projects  
M. Henderson, ISI Program Engineer
J. Carlin, Site Vice President  
H. Hill, Rad Waste Superintendent
J. Cross, Chemistry Manager  
J. Johnson, Program Manager Licensing
A. Day, Radiation Protection Manager  
A. Little, Site Security Manager
D. Erb, Work Control Manager  
K. Loomis, Boric Acid Program Engineer
M. Henderson, ISI Program Engineer  
T. Marshall, Operations Manager
H. Hill, Rad Waste Superintendent  
M. McBrearty, Licensing Manager
J. Johnson, Program Manager Licensing  
S. McCamy, Quality Assurance Manager
A. Little, Site Security Manager  
S. Mohorn, Rad Waste Superintendent
K. Loomis, Boric Acid Program Engineer  
P. Noe, Director Safety and Licensing
T. Marshall, Operations Manager  
C. Owens, Rad Waste HP
M. McBrearty, Licensing Manager  
W. Pierce, Site Engineering Director
S. McCamy, Quality Assurance Manager  
P. Pratt, Manager, Maintenance
S. Mohorn, Rad Waste Superintendent  
J. Rolph, Radiation Protection Technical Support Superintendent
P. Noe, Director Safety and Licensing  
P. Simmons, Plant Manager
C. Owens, Rad Waste HP  
K. Smith, Director of Training
W. Pierce, Site Engineering Director  
D. Sutton, Licensing
P. Pratt, Manager, Maintenance  
J. Stamey, Rad Waste Health Physicist
J. Rolph, Radiation Protection Technical Support Superintendent  
J. Stewart, Chemist
P. Simmons, Plant Manager  
NRC personnel
K. Smith, Director of Training  
S. Lingam, Project Manager, Office of Nuclear Reactor Regulation
D. Sutton, Licensing  
                      LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
J. Stamey, Rad Waste Health Physicist  
Opened and Closed
J. Stewart, Chemist  
05000327/2013005-01                     NCV       Unit 1 Train A RHR Containment Suction
                                                  Valve Failure (Section 4OA5)
Closed
NRC personnel  
05000327/2013004-01                     URI       Water Intrusion Into Actuator of Valve 1-
S. Lingam, Project Manager, Office of Nuclear Reactor Regulation  
                                                  FCV-63-72 (Section 4OA5)
                                                                                    Attachment
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
Opened and Closed  
05000327/2013005-01  
NCV  
Unit 1 Train A RHR Containment Suction  
Valve Failure (Section 4OA5)  
Closed  
05000327/2013004-01  
URI  
Water Intrusion Into Actuator of Valve 1-  
FCV-63-72 (Section 4OA5)  


                              LIST OF DOCUMENTS REVIEWED
Section 1R01: Adverse Weather Protection
Procedures
Enclosure
0-PI-OPS-006.0, Freeze Protection, Rev. 55
LIST OF DOCUMENTS REVIEWED  
Service Requests (SRs)
SR 807550
Section 1R01: Adverse Weather Protection  
SR 825408
SR 821489
Section 1R04: Equipment Alignment
Partial System Walkdowns
Procedures
0-GO-16, System Operability Checklists, Rev. 4
Procedures  
Other documents
0-PI-OPS-006.0, Freeze Protection, Rev. 55  
UFSAR Section 9
Procedures
Service Requests (SRs)  
0-SI-OPS-030-021.A, Auxiliary Building Gas Treatment System Train A, Rev. 6
SR 807550  
0-SI-OPS-030-021.B, Auxiliary Building Gas Treatment System Train B, Rev. 6
SR 825408  
0-SO-30-18, Auxiliary Building Gas Treatment System, Rev. 14
SR 821489  
0-SO-65-1, Emergency Gas Treatment System Air Cleanup and Annulus Vacuum, Rev. 27
0-SO-30-1, Control Building Heating, Air Conditioning, and Ventilation, Rev. 39
Section 1R04: Equipment Alignment  
0-SO-30-10, Auxiliary Building Ventilation Systems, Rev. 54
Partial System Walkdowns  
Section 1R05: Fire Protection
Procedures
Procedures  
FPDP-1, Conduct of Fire Protection, Rev. 2
0-GO-16, System Operability Checklists, Rev. 4  
0-PI-FPU-317-299.W, Att. 8, Shift Check List, Rev. 32
NPG-SPP-18.4.7, Control of Transient Combustibles, Rev. 0
Other documents  
EITP-100, Environmental Compliance, Rev. 6
UFSAR Section 9  
0-SI-FPU-410-703.0, Inspection of FPR Required Fire Doors, Rev. 5
SQN-FPR-Part-II, SQN Fire Protection Report Part II - Fire Protection Plan, Rev. 28
Procedures  
Other documents
0-SI-OPS-030-021.A, Auxiliary Building Gas Treatment System Train A, Rev. 6  
Fire Protection Pre-Fire Plans for Unit 1 Lower Containment Building
0-SI-OPS-030-021.B, Auxiliary Building Gas Treatment System Train B, Rev. 6  
Fire Protection Pre-Fire Plans for Unit 2 Lower Containment Building
0-SO-30-18, Auxiliary Building Gas Treatment System, Rev. 14  
Fire Protection Pre-Fire Plans for Control Building Elevation 685 (Auxiliary Instrument Room)
0-SO-65-1, Emergency Gas Treatment System Air Cleanup and Annulus Vacuum, Rev. 27  
Fire Protection Pre-Fire Plans for Control Building Elevation 706 (Cable Spreading Room)
0-SO-30-1, Control Building Heating, Air Conditioning, and Ventilation, Rev. 39  
Fire Protection Pre-Fire Plans for ERCW Building - Elevations 688/704/720
0-SO-30-10, Auxiliary Building Ventilation Systems, Rev. 54  
Fire Protection Pre-Fire Plans for Turbine Building - Elevations 662/685
Section 1R06: Flood Protection Measures
Section 1R05: Fire Protection  
Work Orders
Procedures  
FPDP-1, Conduct of Fire Protection, Rev. 2  
0-PI-FPU-317-299.W, Att. 8, Shift Check List, Rev. 32  
NPG-SPP-18.4.7, Control of Transient Combustibles, Rev. 0  
EITP-100, Environmental Compliance, Rev. 6  
0-SI-FPU-410-703.0, Inspection of FPR Required Fire Doors, Rev. 5  
SQN-FPR-Part-II, SQN Fire Protection Report Part II - Fire Protection Plan, Rev. 28  
Other documents  
Fire Protection Pre-Fire Plans for Unit 1 Lower Containment Building  
Fire Protection Pre-Fire Plans for Unit 2 Lower Containment Building
Fire Protection Pre-Fire Plans for Control Building Elevation 685 (Auxiliary Instrument Room)  
Fire Protection Pre-Fire Plans for Control Building Elevation 706 (Cable Spreading Room)  
Fire Protection Pre-Fire Plans for ERCW Building - Elevations 688/704/720  
Fire Protection Pre-Fire Plans for Turbine Building - Elevations 662/685  
Section 1R06: Flood Protection Measures  
Work Orders  
WO 11108121224, Check Standing Water Level in Manholes/Handholes
WO 11108121224, Check Standing Water Level in Manholes/Handholes
                                                                                        Enclosure


                                            3
Other documents
3  
TVA letter to NRC dated May 4, 2007. TVA response to GL 2007-01
Section 1R08: Inservice Inspection Activities
Attachment
Procedures
Other documents  
N-VT-15 - Visual Examination of Class MC and Metallic Liners of Class CC Components of
TVA letter to NRC dated May 4, 2007. TVA response to GL 2007-01  
Light-Water cooled Plants, Rev. 11
N-VT-16 - General Visual Examination Containment Vessel Integrity Verification, Rev. 05
Section 1R08: Inservice Inspection Activities  
N-UT-67 - Generic Procedure for Straight Beam Ultrasonic Examination of Bolts and Studs,
Procedures  
Rev. 05
N-VT-15 - Visual Examination of Class MC and Metallic Liners of Class CC Components of  
PDI-UT-5 - Generic Procedure for Straight Beam Ultrasonic Examination of Bolts and Studs,
Light-Water cooled Plants, Rev. 11  
Rev. D34
N-VT-16 - General Visual Examination Containment Vessel Integrity Verification, Rev. 05  
IEP-200 - Qualification and Certification Requirements for TVA Inspection Services
N-UT-67 - Generic Procedure for Straight Beam Ultrasonic Examination of Bolts and Studs,  
Organization (ISO) Nondestructive (NDE) Personnel, Rev. 13
Rev. 05  
Corrective Action Documents
PDI-UT-5 - Generic Procedure for Straight Beam Ultrasonic Examination of Bolts and Studs,  
PER 618770 - Boron buildup on 1B-B SIS Pump Pedestal
Rev. D34  
PER 691545 - Boric acid build up and wet boric acid are present on transmitter sensing line
IEP-200 - Qualification and Certification Requirements for TVA Inspection Services  
1-ft-72-41
Organization (ISO) Nondestructive (NDE) Personnel, Rev. 13  
PER 01-010244 - Minor concrete voids in U1C11 Vt-3 inspection
PER 169175 - Airline cracks in ceiling beneath reactor cavity and reactor wall
Corrective Action Documents  
SR 797854 - Hairline cracking in the concrete beneath the fuel transfer canal in lower
PER 618770 - Boron buildup on 1B-B SIS Pump Pedestal  
containment
PER 691545 - Boric acid build up and wet boric acid are present on transmitter sensing line      
SR 526607 - Spalling on baseplate of Protection Device No. 1 on Drawing 48N1701-17.
1-ft-72-41  
SR 797166 - Boric acid on Reactor Coolant Pump #1 on #3 seal
PER 01-010244 - Minor concrete voids in U1C11 Vt-3 inspection  
SR 797061 - Boric acid on valve 1-FCV-063-0098
PER 169175 - Airline cracks in ceiling beneath reactor cavity and reactor wall  
SR 797072 - Two areas of white deposit in Fan Room 2
SR 797854 - Hairline cracking in the concrete beneath the fuel transfer canal in lower  
Other documents
containment  
Periodic Instruction 0-PI-DXI-000-116.2, ASME Section XI IWE/IWL Containment Inservice
SR 526607 - Spalling on baseplate of Protection Device No. 1 on Drawing 48N1701-17.  
Inspection (CSI) Program, Rev. 05
SR 797166 - Boric acid on Reactor Coolant Pump #1 on #3 seal  
Q-NIC-100 - Written Practice for the Qualification and Certification of Nondestructive
SR 797061 - Boric acid on valve 1-FCV-063-0098  
Examination (NDE0 Personnel, Rev. 20-TVA
SR 797072 - Two areas of white deposit in Fan Room 2  
IHI Southwest Technologies, Inc. Operating Procedure 2.0-NDES-001, Nondestructive
Examination Personnel Qualification and Certification, Rev. 06
Other documents  
WO 113312025 - Modify Component Cooling Piping to eliminate interference with actuator for
Periodic Instruction 0-PI-DXI-000-116.2, ASME Section XI IWE/IWL Containment Inservice  
1-FC-063-011
Inspection (CSI) Program, Rev. 05  
Section 1R12: Maintenance Effectiveness
Q-NIC-100 - Written Practice for the Qualification and Certification of Nondestructive  
Procedures
Examination (NDE0 Personnel, Rev. 20-TVA  
TI-4, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -
IHI Southwest Technologies, Inc. Operating Procedure 2.0-NDES-001, Nondestructive  
10CFR50.65, Rev. 23
Examination Personnel Qualification and Certification, Rev. 06  
Other documents
WO 113312025 - Modify Component Cooling Piping to eliminate interference with actuator for  
MR 11th Periodic Assessment Report (PE sample)
1-FC-063-011  
Cause Determination and Evaluation (CDE) #2700, FCV-63-72 Failure
CDE #2696, EBGTS B Fan Failure
Section 1R12: Maintenance Effectiveness  
                                                                                      Attachment
Procedures  
TI-4, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -  
10CFR50.65, Rev. 23  
Other documents  
MR 11th Periodic Assessment Report (PE sample)  
Cause Determination and Evaluation (CDE) #2700, FCV-63-72 Failure  
CDE #2696, EBGTS B Fan Failure  


                                          4
CDE #2686, A Shutdown Boardroom Chiller Failure
4  
CDE #2674, B Main Condenser Test Connection Failure
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
Attachment
Procedures
CDE #2686, A Shutdown Boardroom Chiller Failure  
0-TI-DSM-000-007.1, Risk Assessment Guidelines, Rev. 9
CDE #2674, B Main Condenser Test Connection Failure  
NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 3
NPG-SPP-07.2.4, Forced Outage or Short Duration Planned Outage Management, Rev. 0
Section 1R13: Maintenance Risk Assessments and Emergent Work Control  
NPG-SPP-07.2, Outage Management, Rev. 0
Procedures  
GOI-6, Apparatus Operations, Rev. 142
0-TI-DSM-000-007.1, Risk Assessment Guidelines, Rev. 9  
Section 1R15: Operability Determinations and Functionality Assessments
NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 3  
Procedures
NPG-SPP-07.2.4, Forced Outage or Short Duration Planned Outage Management, Rev. 0  
NEDP-22, Functional Evaluations, Rev. 9
NPG-SPP-07.2, Outage Management, Rev. 0
OPDP-8, Limiting Conditions for Operation Tracking, Rev. 5
GOI-6, Apparatus Operations, Rev. 142  
NPG-SPP-03.5, Regulatory Reporting Requirements, Rev. 2
PERs
Section 1R15: Operability Determinations and Functionality Assessments  
789552 - Unit 2 Turbine Controls in Manual
Procedures  
795451 - POE WO 113223153 T1 motor lead pinch
NEDP-22, Functional Evaluations, Rev. 9  
799097 - POE TS LCO 3.7.4 action for FCV-67-146
OPDP-8, Limiting Conditions for Operation Tracking, Rev. 5  
800432 - POE (ABSCE boundary issue)
NPG-SPP-03.5, Regulatory Reporting Requirements, Rev. 2  
795433 - PDO (During U1R19 water found leaking out of conduit in bioshield wall)
801415 - PDO EDG 1B 2 sec load sequence
PERs  
803833 - PDO U-1 Rx Head Vent Valve Stroke
789552 - Unit 2 Turbine Controls in Manual  
816731, 815638, 817841 - FEs associated with the Unit 1 loose parts alarm
795451 - POE WO 113223153 T1 motor lead pinch  
Section 1R18: Plant Modifications
799097 - POE TS LCO 3.7.4 action for FCV-67-146  
Procedures
800432 - POE (ABSCE boundary issue)  
NPG-SPP-09.3, Plant Modifications and Engineering Change Control, Rev. 4
795433 - PDO (During U1R19 water found leaking out of conduit in bioshield wall)  
NPG-SPP-09.4, 10 CFR 50.59 Evaluations of Changes, Tests, and Experiments, Rev. 1
801415 - PDO EDG 1B 2 sec load sequence  
NPG-SPP-09.5, Temporary Alterations, Rev. 0
803833 - PDO U-1 Rx Head Vent Valve Stroke  
Other documents
816731, 815638, 817841 - FEs associated with the Unit 1 loose parts alarm  
DCN 22643 - Replace Pressurizer PORVs
Section 1R19: Post Maintenance Testing
Section 1R18: Plant Modifications  
Procedures
Procedures  
MMDP-1, Maintenance Management System, Rev. 20
NPG-SPP-09.3, Plant Modifications and Engineering Change Control, Rev. 4  
MMDP-3, Guidelines for Planning and Execution of Troubleshooting Activities, Rev. 6
NPG-SPP-09.4, 10 CFR 50.59 Evaluations of Changes, Tests, and Experiments, Rev. 1  
NPG-SPP-6.5, Foreign Material Control, Rev. 0
NPG-SPP-09.5, Temporary Alterations, Rev. 0  
NPG-SPP-6.1, Work Order Process Initiation, Rev. 0
NPG-SPP-06.3, Pre-/Post-Maintenance Testing, Rev. 0
Other documents  
NPG-SPP-06.9, Testing Programs, Rev. 0
DCN 22643 - Replace Pressurizer PORVs  
NPG-SPP-06.9.1, Conduct of Testing, Rev. 1
NPG-SPP-06.9.3, Post-Modification Testing, Rev. 0
Section 1R19: Post Maintenance Testing  
                                                                                  Attachment
Procedures  
MMDP-1, Maintenance Management System, Rev. 20  
MMDP-3, Guidelines for Planning and Execution of Troubleshooting Activities, Rev. 6  
NPG-SPP-6.5, Foreign Material Control, Rev. 0  
NPG-SPP-6.1, Work Order Process Initiation, Rev. 0  
NPG-SPP-06.3, Pre-/Post-Maintenance Testing, Rev. 0  
NPG-SPP-06.9, Testing Programs, Rev. 0  
NPG-SPP-06.9.1, Conduct of Testing, Rev. 1  
NPG-SPP-06.9.3, Post-Modification Testing, Rev. 0  


                                          5
Work Orders
5  
114306842 - Disassemble and reassemble valve in support of 113716425
114306841 - Remove actuator, install actuator, set up calibration in support of 113716425
Attachment
114325805 - Disassemble and reassemble valve in support of 113716459
Work Orders  
114325799 - Remove and install actuator in support of 113716459
114306842 - Disassemble and reassemble valve in support of 113716425  
113756597 - PORVs - PCV-68-340 & pcv-68-334 Replacement activities
114306841 - Remove actuator, install actuator, set up calibration in support of 113716425  
113377829 - Repack Valve (1-LCV-3-175) and perform AIRCET test
114325805 - Disassemble and reassemble valve in support of 113716459  
112096045 - Repair isolation check valve (1-VLV-026-1296)
114325799 - Remove and install actuator in support of 113716459  
111234712 - 5 year PM to swap 480V Shutdown board breaker with a refurbished breaker
113756597 - PORVs - PCV-68-340 & pcv-68-334 Replacement activities  
113806636 - Perform 0-MI-EPM-317-102.0 on CCS pump C-S and clean/replace motor air filter
113377829 - Repack Valve (1-LCV-3-175) and perform AIRCET test  
114560807 - CCP room cooler fan motor current check, bearing lubrication and cleaning
112096045 - Repair isolation check valve (1-VLV-026-1296)  
114198329 - EQ maintenance and inspection
111234712 - 5 year PM to swap 480V Shutdown board breaker with a refurbished breaker  
113408190 - Change out electrolytic capacitors in the Woodward 2301A governor card
113806636 - Perform 0-MI-EPM-317-102.0 on CCS pump C-S and clean/replace motor air filter  
Section 1R20: Refueling and Other Outage Activities
114560807 - CCP room cooler fan motor current check, bearing lubrication and cleaning  
Procedures
114198329 - EQ maintenance and inspection  
FHI-3, Movement of Fuel, Rev. 65
113408190 - Change out electrolytic capacitors in the Woodward 2301A governor card  
0-GO-15, Containment Closure Control, Rev. 34
0-GO-13, Reactor Coolant System Drain and Fill Operations, Rev. 71
Section 1R20: Refueling and Other Outage Activities  
NPG-SPP-08.1, Nuclear Fuel Management, Rev. 00
Procedures  
0-PI-OPS-000-011.0, Containment Access Control During Modes 1-4, Rev. 1
FHI-3, Movement of Fuel, Rev. 65  
Section 1R22: Surveillance Testing
0-GO-15, Containment Closure Control, Rev. 34  
Procedures
0-GO-13, Reactor Coolant System Drain and Fill Operations, Rev. 71  
NPG-SPP-06.9.1, Conduct of Testing, Rev. 8
NPG-SPP-08.1, Nuclear Fuel Management, Rev. 00  
0-SI-SXV-072-266.0, ASME Code Valve Testing, Rev. 12
0-PI-OPS-000-011.0, Containment Access Control During Modes 1-4, Rev. 1  
0-SI-OPS-068-137.0, Reactor Coolant System Water Inventory, Rev. 32
0-SI-SFT-072-138.0, Unit 1 Containment Spray - Spray Nozzle Test, Rev. 6
Section 1R22: Surveillance Testing  
0-SI-SLT-081-258.1, Unit 1 Primary Water LLRT, Rev. 5
Procedures  
0-SI-SLT-088-259.1, Upper Personnel Airlock Overall Leak Rate Test and General Inspection,
NPG-SPP-06.9.1, Conduct of Testing, Rev. 8  
Rev. 6
0-SI-SXV-072-266.0, ASME Code Valve Testing, Rev. 12  
0-SI-SLT-088-259.4, Upper Personnel Airlock Interlock Operability Test, Rev. 2
0-SI-OPS-068-137.0, Reactor Coolant System Water Inventory, Rev. 32  
1-SI-SXP-003-202.B, Motor Driven Auxiliary Feedwater Pump 1B-B Comprehensive
0-SI-SFT-072-138.0, Unit 1 Containment Spray - Spray Nozzle Test, Rev. 6  
Performance Test, Rev. 7
0-SI-SLT-081-258.1, Unit 1 Primary Water LLRT, Rev. 5  
1-SI-SXP-074-202.0, RHR Pump 1A-A and 1B-B Comprehensive Performance and Check
0-SI-SLT-088-259.1, Upper Personnel Airlock Overall Leak Rate Test and General Inspection,  
Valve Test, Rev. 10
Rev. 6  
0-SI-OPS-068-137.0, Reactor Coolant System Water Inventory, Rev. 32
0-SI-SLT-088-259.4, Upper Personnel Airlock Interlock Operability Test, Rev. 2  
1-SI-OPS-088-001.0, Phase A Isolation Test, Rev. 14
1-SI-SXP-003-202.B, Motor Driven Auxiliary Feedwater Pump 1B-B Comprehensive  
1-SI-OPS-082-026A, Loss of Offsite Power with Safety Injection D/G 1A-A Test, Rev. 46
Performance Test, Rev. 7  
0-SI-SFT-072-138.0, Unit 1 Containment Spray - Spray Nozzle Test, Rev. 6
1-SI-SXP-074-202.0, RHR Pump 1A-A and 1B-B Comprehensive Performance and Check  
0-SI-SXV-063-203.2, Full Stroking of Safety Injection Cold Leg Accumulator Isolation Valves,
Valve Test, Rev. 10  
Rev. 1
0-SI-OPS-068-137.0, Reactor Coolant System Water Inventory, Rev. 32  
0-SI-MIN-061-105.0, Ice Condenser Ice Weighing, Rev. 11
1-SI-OPS-088-001.0, Phase A Isolation Test, Rev. 14  
0-SI-SLT-067-258.2, Containment Isolation Valve Local Leak Rate Test Lower Compartment
1-SI-OPS-082-026A, Loss of Offsite Power with Safety Injection D/G 1A-A Test, Rev. 46  
Essential Raw Cooling Water, Rev. 13
0-SI-SFT-072-138.0, Unit 1 Containment Spray - Spray Nozzle Test, Rev. 6  
PERs
0-SI-SXV-063-203.2, Full Stroking of Safety Injection Cold Leg Accumulator Isolation Valves,  
801081, FME concern while performing air flow test during core reload
Rev. 1  
                                                                                    Attachment
0-SI-MIN-061-105.0, Ice Condenser Ice Weighing, Rev. 11  
0-SI-SLT-067-258.2, Containment Isolation Valve Local Leak Rate Test Lower Compartment  
Essential Raw Cooling Water, Rev. 13  
PERs  
801081, FME concern while performing air flow test during core reload


                                            6
Other documents
6  
1-47W437-4, Mechanical Containment Spray System Piping, Rev. 1
1-47W437-5, Mechanical Containment Spray System Piping, Rev. 4
Attachment
1-47W812-1, Flow Diagram Containment Spray System, Rev. 45
Other documents  
Technical Specification Surveillance Requirement 4.6.2.1.1.d and 4.6.2.1.2.b
1-47W437-4, Mechanical Containment Spray System Piping, Rev. 1  
Section 1EP2: Alert and Notification System Evaluation
1-47W437-5, Mechanical Containment Spray System Piping, Rev. 4  
Procedures and Reports
1-47W812-1, Flow Diagram Containment Spray System, Rev. 45  
NP-REP, Appendix B, Sequoyah Nuclear Plant Radiological Emergency Plan, Rev. 101
Technical Specification Surveillance Requirement 4.6.2.1.1.d and 4.6.2.1.2.b  
EPFS-9, Inspection, Service, and Maintenance of the Prompt Notification System (PNS) at
Browns Ferry, Sequoyah, and Watts Bar Nuclear Plants, Rev. 8
Section 1EP2: Alert and Notification System Evaluation  
Sequoyah FEMA REP-10 Report, Revision 2
Procedures and Reports  
EPDP-10, Facilitation of the ANS and Notification Tests, Rev. 6
NP-REP, Appendix B, Sequoyah Nuclear Plant Radiological Emergency Plan, Rev. 101  
EPDP-14, Evaluation of Changes to Alert and Notification Systems (ANS), Rev 0
EPFS-9, Inspection, Service, and Maintenance of the Prompt Notification System (PNS) at  
Records and Data
Browns Ferry, Sequoyah, and Watts Bar Nuclear Plants, Rev. 8  
Weekly Silent Tests, 2011-September 2013
Sequoyah FEMA REP-10 Report, Revision 2  
Monthly Siren Tests, October 2011 - October 2013
EPDP-10, Facilitation of the ANS and Notification Tests, Rev. 6  
Corrective Action documents
EPDP-14, Evaluation of Changes to Alert and Notification Systems (ANS), Rev 0  
442747; During Monthly Siren Test Five Sirens Did Not Operate
521663; Siren Damaged by Storm
Records and Data  
591666; Two ANS Sirens Failed to Operate During Monthly Test
Weekly Silent Tests, 2011-September 2013  
701363; Siren Relocations Due to Land Owner Rejections
Monthly Siren Tests, October 2011 - October 2013  
711912; Loss of DC Power Indication for ANS Siren 12
727891; Loss of DC Power Indication for ANS Siren 26
Corrective Action documents  
751936; Two ANS Sirens Failed to Operate During Monthly Test
442747; During Monthly Siren Test Five Sirens Did Not Operate  
Section 1EP3: Emergency Response Organization Staffing and Augmentation System
521663; Siren Damaged by Storm  
Procedures
591666; Two ANS Sirens Failed to Operate During Monthly Test  
TRN-30, Radiological Emergency Preparedness Training, Rev. 24
701363; Siren Relocations Due to Land Owner Rejections  
EPDP-3, Emergency Plan Exercises and Preparedness Drills, Rev. 7
711912; Loss of DC Power Indication for ANS Siren 12  
EPDP-10, Facilitation of the Alert and Notification System and Pager Tests, Rev. 6
727891; Loss of DC Power Indication for ANS Siren 26  
EPIP-3, Alert, Rev 36
751936; Two ANS Sirens Failed to Operate During Monthly Test  
EPIP-6, Activation and Operation of the Technical Support Center, Rev. 49
EPIP-7, Activation and Operation of the Operations Support Center, Rev. 28
Section 1EP3: Emergency Response Organization Staffing and Augmentation System  
Records and Data
Procedures  
SQN-EP-S-13-02, snapshot self-assessment SCBA Qualification of Site Personnel, March 2013
TRN-30, Radiological Emergency Preparedness Training, Rev. 24  
EPT202.000, ERO Training Plan - TSC Training, Rev. 12
EPDP-3, Emergency Plan Exercises and Preparedness Drills, Rev. 7  
EPT900.010, ERO Training Plan, ERO Fundamentals, Rev. 4
EPDP-10, Facilitation of the Alert and Notification System and Pager Tests, Rev. 6  
Radiological Emergency Preparedness Training Oversight Committee minutes 2012/2013
EPIP-3, Alert, Rev 36  
2012/2013 ERO Augmentation test results
EPIP-6, Activation and Operation of the Technical Support Center, Rev. 49  
Results of periodic ERO notification tests
EPIP-7, Activation and Operation of the Operations Support Center, Rev. 28  
Corrective Action documents
786990; TRN error in CECC qualification requirement
Records and Data  
                                                                                  Attachment
SQN-EP-S-13-02, snapshot self-assessment SCBA Qualification of Site Personnel, March 2013  
EPT202.000, ERO Training Plan - TSC Training, Rev. 12  
EPT900.010, ERO Training Plan, ERO Fundamentals, Rev. 4  
Radiological Emergency Preparedness Training Oversight Committee minutes 2012/2013  
2012/2013 ERO Augmentation test results  
Results of periodic ERO notification tests  
Corrective Action documents
786990; TRN error in CECC qualification requirement  


                                          7
Section 1EP4: Emergency Action Level and Emergency Plan Changes
7  
Change Packages
TVA Radiological Emergency Plan, Revs. 99 and 100
Attachment
EPIP-1, Emergency Plan Classification Matrix, Revs. 48 and 49
Section 1EP4: Emergency Action Level and Emergency Plan Changes  
CECC EPIP-2, Operations Duty Specialist Procedure for Notification of Unusual Event,
Change Packages  
Rev. 43
TVA Radiological Emergency Plan, Revs. 99 and 100  
CECC EPIP-3, Operations Duty Specialist Procedure for Alert, Rev. 44
EPIP-1, Emergency Plan Classification Matrix, Revs. 48 and 49  
CECC EPIP-4, Operations Duty Specialist Procedure for Site Area Emergency, Rev. 45
CECC EPIP-2, Operations Duty Specialist Procedure for Notification of Unusual Event,    
CECC EPIP-5, Operations Duty Specialist Procedure for General Emergency, Rev. 50
Rev. 43  
CECC EPIP-7, CECC Radiological Assessment Staff Procedure for Alert, Site Area
CECC EPIP-3, Operations Duty Specialist Procedure for Alert, Rev. 44  
Emergency, and General Emergency, Rev. 34
CECC EPIP-4, Operations Duty Specialist Procedure for Site Area Emergency, Rev. 45  
TVA Radiological Emergency Plan, Rev. 101
CECC EPIP-5, Operations Duty Specialist Procedure for General Emergency, Rev. 50  
Evacuation Time Estimate Study Update
CECC EPIP-7, CECC Radiological Assessment Staff Procedure for Alert, Site Area  
Section 1EP5: Maintenance of Emergency Preparedness
Emergency, and General Emergency, Rev. 34  
Procedures
TVA Radiological Emergency Plan, Rev. 101  
CECC EPIP-9, Emergency Environmental Radiological Monitoring Procedures, Rev. 49
Evacuation Time Estimate Study Update  
EPDP-17, NPG Emergency Plan Effectiveness Review [10 CFR 50.54(q)], Rev. 3
NPG-SPP-7.1, On-Line Work Management, Rev. 10
Section 1EP5: Maintenance of Emergency Preparedness  
NPG-SPP-18.3.5, Designated Emergency Response Equipment (DERE), Rev. 0
Procedures  
NPG-SPP-22.300, Corrective Action Program, Rev. 0
CECC EPIP-9, Emergency Environmental Radiological Monitoring Procedures, Rev. 49  
Records and Data
EPDP-17, NPG Emergency Plan Effectiveness Review [10 CFR 50.54(q)], Rev. 3  
Drill and exercise reports 2011-2013
NPG-SPP-7.1, On-Line Work Management, Rev. 10  
TVA Quality Assurance Audit Report SSA 1203 dated April 16, 2012
NPG-SPP-18.3.5, Designated Emergency Response Equipment (DERE), Rev. 0  
TVA Quality Assurance Audit Report SSA 1305 dated June 17, 2013
NPG-SPP-22.300, Corrective Action Program, Rev. 0  
Focused Self-Assessment SQN-EP-F-13-001, NRC Inspection Preparation
SQN QA Quarterly Rating Report August 13, 2013
Records and Data  
Corrective Action documents
Drill and exercise reports 2011-2013  
571999; Maintenance Personnel Not Evacuated in a Timely Manner During REP Drill
TVA Quality Assurance Audit Report SSA 1203 dated April 16, 2012  
572584; RP Was Slow to Perform Airborne Sampling During REP Drill
TVA Quality Assurance Audit Report SSA 1305 dated June 17, 2013  
608785; Dose assessment error
Focused Self-Assessment SQN-EP-F-13-001, NRC Inspection Preparation  
581795; No Additional Fire Brigade Personnel Onsite During REP Drill
SQN QA Quarterly Rating Report August 13, 2013  
582858; TSC SED Filled Out Wrong Form Which Delayed CECC PAR Development
582751; MERT Failed 4 of 6 Drill Objectives
Corrective Action documents  
619808; RP Tech Left Team to Get Equipment During Graded Exercise
571999; Maintenance Personnel Not Evacuated in a Timely Manner During REP Drill  
619847; Inside Van Tech Did Not Grab All Equipment Required During Graded Exercise
572584; RP Was Slow to Perform Airborne Sampling During REP Drill
695758; MET Unavailable - Lessons Learned
608785; Dose assessment error  
704845; Evaluate EPIP-1 Classification of EAL 4.2 for Explosion
581795; No Additional Fire Brigade Personnel Onsite During REP Drill  
708940; Questioned CET Readings During Drill
582858; TSC SED Filled Out Wrong Form Which Delayed CECC PAR Development  
711961; REP Assignment Cannot Meet 1-Hour Requirement to Respond
582751; MERT Failed 4 of 6 Drill Objectives  
720352; 8 Personnel Were Not Accounted For During REP Drill
619808; RP Tech Left Team to Get Equipment During Graded Exercise  
722951; KI Tablets Should Be Evaluated for Issue Earlier Under Emergency Conditions
619847; Inside Van Tech Did Not Grab All Equipment Required During Graded Exercise  
732171; Clarify EPDP-11 regarding 10 CFR 50.54(t) requirements
695758; MET Unavailable - Lessons Learned  
751183; Wrong Pocket Ion Chambers in REP Van #3
704845; Evaluate EPIP-1 Classification of EAL 4.2 for Explosion  
                                                                                  Attachment
708940; Questioned CET Readings During Drill  
711961; REP Assignment Cannot Meet 1-Hour Requirement to Respond  
720352; 8 Personnel Were Not Accounted For During REP Drill  
722951; KI Tablets Should Be Evaluated for Issue Earlier Under Emergency Conditions  
732171; Clarify EPDP-11 regarding 10 CFR 50.54(t) requirements  
751183; Wrong Pocket Ion Chambers in REP Van #3  


                                          8
Section 2RS1: Radiological Hazard Assessment and Exposure Controls
8  
Procedures, Guidance Documents, and Manuals
NPG-SPP-05.1.1, Alpha Radiation Monitoring Program, Rev. 3
Attachment
NPG-SPP-05.6, Controlling Byproduct and Source Material, Rev. 2
Section 2RS1: Radiological Hazard Assessment and Exposure Controls  
NPG-SPP-22.300, Corrective Action Program, Rev. 0
Procedures, Guidance Documents, and Manuals  
RCDP-1, Conduct of Radiological Controls, Rev. 5
NPG-SPP-05.1.1, Alpha Radiation Monitoring Program, Rev. 3  
RCI-01, Radiation Protection Program, Rev. 78
NPG-SPP-05.6, Controlling Byproduct and Source Material, Rev. 2  
RCI-14, Radiation Work Permit (RWP) Program, Rev. 57
NPG-SPP-22.300, Corrective Action Program, Rev. 0  
RCI-15, Radiological Postings, Rev. 24
RCDP-1, Conduct of Radiological Controls, Rev. 5
RCI-17, Control of Byproduct and Source Material, Rev. 19
RCI-01, Radiation Protection Program, Rev. 78  
RCI-18, Vacuum Cleaner Control Within the Radiologically Controlled Area, Rev. 9
RCI-14, Radiation Work Permit (RWP) Program, Rev. 57  
RCI-21, Control of Radioactive Materials, Rev. 19
RCI-15, Radiological Postings, Rev. 24  
RCI-29, Control of Radiation Protection Keys, Rev. 15
RCI-17, Control of Byproduct and Source Material, Rev. 19  
RCI-101, Radiation Operations Routines, Rev. 3
RCI-18, Vacuum Cleaner Control Within the Radiologically Controlled Area, Rev. 9  
RCI-106, Radiation Protection Standards and Expectations, Rev. 3
RCI-21, Control of Radioactive Materials, Rev. 19  
RCI-201, Radiation and Contamination Surveys, Rev. 13
RCI-29, Control of Radiation Protection Keys, Rev. 15  
RCI-202, Airborne Radioactivity Surveys, Rev. 7
RCI-101, Radiation Operations Routines, Rev. 3  
RCI-204, Radiological Surveys of Equipment and Materials Leaving the RCA, Rev. 7
RCI-106, Radiation Protection Standards and Expectations, Rev. 3  
RCI-209, Radiological Surveys of Personnel Leaving the RCA or Protected Area, Rev. 3
RCI-201, Radiation and Contamination Surveys, Rev. 13  
RCI-301, Radionuclide Tracking and Assessment (RTA) Program, Rev. 2
RCI-412, Radiation Protection Surveys during Initial Spent Fuel Assembly Movement, Rev. 1
RCI-202, Airborne Radioactivity Surveys, Rev. 7  
RCI-417, Radiological Monitoring of the Hydrogen Peroxide Injection Crud Burst, Rev. 1
RCI-204, Radiological Surveys of Equipment and Materials Leaving the RCA, Rev. 7  
RCTP-106, Special Dosimetry Operations, Rev. 2
RCI-209, Radiological Surveys of Personnel Leaving the RCA or Protected Area, Rev. 3  
0-TI-NUC-000-002.0, Storing Material in Spent Fuel Pool or New Fuel Vault, Rev. 21
RCI-301, Radionuclide Tracking and Assessment (RTA) Program, Rev. 2  
Records and Data
RCI-412, Radiation Protection Surveys during Initial Spent Fuel Assembly Movement, Rev. 1  
Air Sample Detail Report for 10/13/2013 thru 11/5/2013, 11/5/2103
RCI-417, Radiological Monitoring of the Hydrogen Peroxide Injection Crud Burst, Rev. 1  
Air Sample 101713018, U1 Equipment Pit, 10/17/2013
RCTP-106, Special Dosimetry Operations, Rev. 2  
Air Sample 101813018, U1 734 RFF GA, 10/18/2013
0-TI-NUC-000-002.0, Storing Material in Spent Fuel Pool or New Fuel Vault, Rev. 21  
Air Sample 102313006, U1 Rx Head Stand, 10/23/2013
Air Sample 102313014, U1 653 1B RHR Pump Room, 10/23/2013
Records and Data  
Air Sample 102313023, U1 653 1B RHR Pump Room, 10/23/2013
Air Sample Detail Report for 10/13/2013 thru 11/5/2013, 11/5/2103  
Air Sample 102613003, U1 Upper Rx Head O-ring Cleaning, 10/26/2013
Air Sample 101713018, U1 Equipment Pit, 10/17/2013  
Air Sample 110213012, U1 Upper GA, 11/2/2013
Air Sample 101813018, U1 734 RFF GA, 10/18/2013  
ALARA Plan 2013-010, Refueling Operations
Air Sample 102313006, U1 Rx Head Stand, 10/23/2013  
ALARA Plan 2013-011, Mechanical Maintenance Group (MMG)
Air Sample 102313014, U1 653 1B RHR Pump Room, 10/23/2013  
ALARA Plan 2013-018, MODS - Ice Condenser/Snubbers/Insulation/Scaffolds/Painting
Air Sample 102313023, U1 653 1B RHR Pump Room, 10/23/2013  
Instrument Calibration/Check Source Certificates:
Air Sample 102613003, U1 Upper Rx Head O-ring Cleaning, 10/26/2013  
  Vendor Source No. I3-328, TVA No. 2530, 7/29/2011
Air Sample 110213012, U1 Upper GA, 11/2/2013  
  Vendor Source No. I3-329, TVA No. 2531, 7/29/2011
ALARA Plan 2013-010, Refueling Operations  
  Vendor Source No. I3-330, TVA No. 2532, 7/29/2011
ALARA Plan 2013-011, Mechanical Maintenance Group (MMG)  
  Vendor Source No.G4-975, TVA No. 2483, 10/9/2009
ALARA Plan 2013-018, MODS - Ice Condenser/Snubbers/Insulation/Scaffolds/Painting  
  Vendor Source No. 92421, TVA No. 2571, 12/7/2012
Instrument Calibration/Check Source Certificates:  
  Vendor Source No. 52736-185D2, TVA No. 2245, 5/19/2003
Vendor Source No. I3-328, TVA No. 2530, 7/29/2011  
Instrument Calibration Records:
Vendor Source No. I3-329, TVA No. 2531, 7/29/2011  
  Canberra GEM-5 Personnel Monitor, Serial No. 0909-179, 3/23/2012 and 3/18/2013
Vendor Source No. I3-330, TVA No. 2532, 7/29/2011  
  ARGOS-5AB Personnel Monitor, Instrument No. 860587, 5/11/2012 and 5/2/2013
Vendor Source No.G4-975, TVA No. 2483, 10/9/2009  
  iSolo, Instrument No. 860494, 12/6/2012 and 10/11/13
Vendor Source No. 92421, TVA No. 2571, 12/7/2012  
                                                                                  Attachment
Vendor Source No. 52736-185D2, TVA No. 2245, 5/19/2003  
Instrument Calibration Records:  
Canberra GEM-5 Personnel Monitor, Serial No. 0909-179, 3/23/2012 and 3/18/2013  
ARGOS-5AB Personnel Monitor, Instrument No. 860587, 5/11/2012 and 5/2/2013  
iSolo, Instrument No. 860494, 12/6/2012 and 10/11/13  


                                            9
  Small Article Monitor (Cronos 11), Instrument No. 860653, 8/17/2012 and 7/16/2013
9  
  Small Article Monitor (SAM-11), Instrument No. 860325, 7/6/2012 and 11/17/2012
List of Active SQN Temporary Shielding Request Forms (TSRFs), 11/6/2013
Attachment
National Source Tracking System Annual Inventory Reconciliation Confirmation, 1/24/2013
Small Article Monitor (Cronos 11), Instrument No. 860653, 8/17/2012 and 7/16/2013  
National Source Tracking System Inventory Report, Sequoyah Nuclear Plant, 1/24/2013
Small Article Monitor (SAM-11), Instrument No. 860325, 7/6/2012 and 11/17/2012  
RWP Dose by Work Step Report for ALARA Plans 2013-010 to 2013-021 for the period
List of Active SQN Temporary Shielding Request Forms (TSRFs), 11/6/2013  
10/14/2013 thru 11/6/2013
National Source Tracking System Annual Inventory Reconciliation Confirmation, 1/24/2013  
RWP Total Dose, Hours and Dose Rate Report for the period 10/14/2013 thru 11/5/2013
National Source Tracking System Inventory Report, Sequoyah Nuclear Plant, 1/24/2013  
RWP Work Step Dose and Dose Rate Alarm Setpoints for RWP 13140052, 11/5/2013
RWP Dose by Work Step Report for ALARA Plans 2013-010 to 2013-021 for the period  
RWP 13120122, U1 Seal Table work
10/14/2013 thru 11/6/2013  
RWP 13140002, U1 Upper Containment High Rad Area Mechanical Maintenance
RWP Total Dose, Hours and Dose Rate Report for the period 10/14/2013 thru 11/5/2013  
RWP 13140052, HRA U1 Refueling Activities for AREVA and Boilermakers
RWP Work Step Dose and Dose Rate Alarm Setpoints for RWP 13140052, 11/5/2013  
RWP 13140072, U1 HRA MODS Work: Snubbers, Scaffold, Insulation, Painting
RWP 13120122, U1 Seal Table work  
RWP 13140172, U1 Rx Head Insulation
RWP 13140002, U1 Upper Containment High Rad Area Mechanical Maintenance  
RWP 13140252, HRA U1 Upper Containment Rx Cavity
RWP 13140052, HRA U1 Refueling Activities for AREVA and Boilermakers  
RWP 13140352, U1 HRA Head O-Ring Surface Work & Inspection (Multibadging)
RWP 13140072, U1 HRA MODS Work: Snubbers, Scaffold, Insulation, Painting  
RWP 13140353, U1 Equipment Pit - LHRA Vortex Suppressors
RWP 13140172, U1 Rx Head Insulation  
RWP 13140453, U1 Upper Containment, Rx Cavity, LHRA, CRDM duct work, (Multibadging)
RWP 13140252, HRA U1 Upper Containment Rx Cavity  
Radiological Survey SQN-M-20131014-23 and SQN-M-20131104-2, U1 Containment
RWP 13140352, U1 HRA Head O-Ring Surface Work & Inspection (Multibadging)  
Equipment Pit
RWP 13140353, U1 Equipment Pit - LHRA Vortex Suppressors  
Radiological Survey SQN-M-20131021-3, SQN-M-20131014-6, SQN-M-20131014-15, and
RWP 13140453, U1 Upper Containment, Rx Cavity, LHRA, CRDM duct work, (Multibadging)  
SQN-M-20131014-22, U1 Containment Accumulator Rooms #1, #2, #3, and #4
Radiological Survey SQN-M-20131014-23 and SQN-M-20131104-2, U1 Containment  
Radiological Survey SQN-M-20131014-32 and SQN-M-20131017-9, U1 Containment Top of
Equipment Pit  
Pressurizer
Radiological Survey SQN-M-20131021-3, SQN-M-20131014-6, SQN-M-20131014-15, and  
Radiological Survey SQN-M-20130909-1 and SQN-M-20131014-8, U1 Containment Raceway
SQN-M-20131014-22, U1 Containment Accumulator Rooms #1, #2, #3, and #4
Radiological Survey SQN-M-20131014-14, SQN-M-20131014-7, and SQN-M-20131014-5, U1
Radiological Survey SQN-M-20131014-32 and SQN-M-20131017-9, U1 Containment Top of  
Containment Steam Generator Primary Platform #1, #2, and #3
Pressurizer  
Radiological Survey SQN-M-20131014-17 and SQN-M-20131020-7, U1 Containment Inside
Radiological Survey SQN-M-20130909-1 and SQN-M-20131014-8, U1 Containment Raceway  
Polar Crane Wall
Radiological Survey SQN-M-20131014-14, SQN-M-20131014-7, and SQN-M-20131014-5, U1  
Radiological Survey SQN-M-20131021-21, SQN-M-20131014-10, and SQN-M-20131014-18,
Containment Steam Generator Primary Platform #1, #2, and #3  
U1 Containment RCP Platform #1, #2, and #3
Radiological Survey SQN-M-20131014-17 and SQN-M-20131020-7, U1 Containment Inside  
Radiological Survey SQN-M-20131020-16, SQN ISFSI Pad
Polar Crane Wall  
Radiological Survey SQN-M-20121212-8, U2 Letdown Heat Exchanger Room
Radiological Survey SQN-M-20131021-21, SQN-M-20131014-10, and SQN-M-20131014-18,  
Radiological Survey SQN-M-20131014-26, U1 Letdown Heat Exchanger Room
U1 Containment RCP Platform #1, #2, and #3
Radiological Survey SQN-M-20130502-11 and SQN-M-20131005-1, U1 651' Waste Evaporator
Radiological Survey SQN-M-20131020-16, SQN ISFSI Pad  
Feed Pump Room
Radiological Survey SQN-M-20121212-8, U2 Letdown Heat Exchanger Room  
Radiological Survey SQN-M-20131018-1 and SQN-M-20131025-1, Radiochemistry Lab
Radiological Survey SQN-M-20131014-26, U1 Letdown Heat Exchanger Room  
Radiological Survey SQN-M-20130617-3, SQN-M-20131007-1, and SQN-M-20131104-4,
Radiological Survey SQN-M-20130502-11 and SQN-M-20131005-1, U1 651' Waste Evaporator  
  Equipment Decon Room
Feed Pump Room  
Radiological Survey SQN-M-20130823-3, and SQN-M-20131016-24, Spent Fuel Heat
Radiological Survey SQN-M-20131018-1 and SQN-M-20131025-1, Radiochemistry Lab  
  Exchanger Room
Radiological Survey SQN-M-20130617-3, SQN-M-20131007-1, and SQN-M-20131104-4,  
Radiological Survey SQN-M-20130920-5, SQN-M-20131020-4, and SQN-M-20131028-7, Spent
Equipment Decon Room  
  Fuel Pool Area
Radiological Survey SQN-M-20130823-3, and SQN-M-20131016-24, Spent Fuel Heat  
Radiological Survey SQN-M-20131015-8, SQN-M-20131020-9, and SQN-M-20131024-7, 1A
Exchanger Room  
  RHR Pump Room
Radiological Survey SQN-M-20130920-5, SQN-M-20131020-4, and SQN-M-20131028-7, Spent  
Radiological Survey SQN-M-20131015-11, SQN-M-20131022-8, and SQN-M-20131023-10, 1B
Fuel Pool Area  
  RHR Pump Room
Radiological Survey SQN-M-20131015-8, SQN-M-20131020-9, and SQN-M-20131024-7, 1A  
Radiological Survey SQN-M-20131101-10, 2B RHR Pump Room
RHR Pump Room  
                                                                                  Attachment
Radiological Survey SQN-M-20131015-11, SQN-M-20131022-8, and SQN-M-20131023-10, 1B  
RHR Pump Room  
Radiological Survey SQN-M-20131101-10, 2B RHR Pump Room  


                                          10
Radioactive Sealed Source Leak Test Certification, Source ID 0413-00-00, 7/23/09 and 1/25/10
10  
Sequoyah Nuclear Plant Annual Radionuclide Trending and Assessment Report for 2011,
  6/30/2012
Attachment
Sequoyah Nuclear Plant Annual Radionuclide Trending and Assessment Report for 2012,
Radioactive Sealed Source Leak Test Certification, Source ID 0413-00-00, 7/23/09 and 1/25/10  
  4/18/2013
Sequoyah Nuclear Plant Annual Radionuclide Trending and Assessment Report for 2011,  
U1R19 Radiation Protection Status Report, 11/5/2013
6/30/2012  
U1R19 RCS Shutdown Co-58 Activity Graphs (Crud Burst Cleanup), 11/5/2013
Sequoyah Nuclear Plant Annual Radionuclide Trending and Assessment Report for 2012,  
U1R19 Crud Burst Cleanup Dose Rate Trending Graphs (1A and 1B RHR Pump and Heat
4/18/2013  
  Exchanger rooms, and 690 and 669 Pipe Chases near RHR Lines), 11/5/2013
U1R19 Radiation Protection Status Report, 11/5/2013  
Waste Stream Report (10 CFR Part 61 Waste Characterization), DAW 10-22-2010, 5/11/2011
U1R19 RCS Shutdown Co-58 Activity Graphs (Crud Burst Cleanup), 11/5/2013  
Waste Stream Report (10 CFR Part 61 Waste Characterization), DAW 3-22-2012, 11/4/2012
U1R19 Crud Burst Cleanup Dose Rate Trending Graphs (1A and 1B RHR Pump and Heat  
WO 114067330, 0-SI-RCI-000-056.0 Byproduct Material Inventory and Sealed Source Leak
Exchanger rooms, and 690 and 669 Pipe Chases near RHR Lines), 11/5/2013
  Test, 7/8/2013
Waste Stream Report (10 CFR Part 61 Waste Characterization), DAW 10-22-2010, 5/11/2011  
WO 114139751, 0-SI-RCI-000-056.0 Byproduct Material Inventory and Sealed Source Leak
Waste Stream Report (10 CFR Part 61 Waste Characterization), DAW 3-22-2012, 11/4/2012  
  Test, 12/17/2012
WO 114067330, 0-SI-RCI-000-056.0 Byproduct Material Inventory and Sealed Source Leak  
CAP Documents
Test, 7/8/2013  
Apparent Cause Evaluation PER Report, SQN PER 782859, 10/20/2013
WO 114139751, 0-SI-RCI-000-056.0 Byproduct Material Inventory and Sealed Source Leak  
Site Audit Report SSA1309, Radiation Protection Sequoyah Nuclear Plant, 9/16/2013
Test, 12/17/2012  
TVA Nuclear Power Group Benchmarking Report SQN-RP-I-13-BM09, 8/23/2013
PERs
CAP Documents  
PER 626962
Apparent Cause Evaluation PER Report, SQN PER 782859, 10/20/2013
PER 629341
Site Audit Report SSA1309, Radiation Protection Sequoyah Nuclear Plant, 9/16/2013  
PER 657724
TVA Nuclear Power Group Benchmarking Report SQN-RP-I-13-BM09, 8/23/2013  
PER 659369
PER 782859
PERs
PER 788604
PER 626962  
PER 790597
PER 629341  
PER 793236
PER 657724  
PER 793935
PER 659369  
PER 799256
PER 782859  
PER 802329
PER 788604  
Section 2RS8: Radioactive Solid Waste Processing and Radioactive Material Handling,
PER 790597  
Storage, and Transportation
PER 793236  
Procedures, Manuals, and Guides
PER 793935  
Energy Solutions Cask Book for Model 8-120B USA/9168/B(U)
PER 799256  
NPG-SPP-05.7, Radwaste Management, Rev. 0
PER 802329  
Process Control Program (PCP), Rev. 4
Radioactive Material Shipment Manual (RMSM, Vol.II -Radioactive Material Shipment, Rev. 42
Section 2RS8: Radioactive Solid Waste Processing and Radioactive Material Handling,  
Radioactive Material Shipment Manual (RMSM, Vol.III -Radwaste Shipment, Rev. 39
Storage, and Transportation  
RCI-06, Receipt of Radioactive Materials, Rev. 19
Procedures, Manuals, and Guides  
RCI-21 Control of Radioactive Materials, Rev. 19
Energy Solutions Cask Book for Model 8-120B USA/9168/B(U)  
RHSI-1, Packaging Dry Active Waste for Shipment to a Waste Processor/Broker or a
NPG-SPP-05.7, Radwaste Management, Rev. 0  
  Commercial Radwaste Burial Facility, Rev. 10
Process Control Program (PCP), Rev. 4
RHSI-1.1, Packaging Filters and Items of High Levels of Radiation, Rev. 6
Radioactive Material Shipment Manual (RMSM, Vol.II -Radioactive Material Shipment, Rev. 42  
                                                                                  Attachment
Radioactive Material Shipment Manual (RMSM, Vol.III -Radwaste Shipment, Rev. 39  
RCI-06, Receipt of Radioactive Materials, Rev. 19  
RCI-21 Control of Radioactive Materials, Rev. 19  
RHSI-1, Packaging Dry Active Waste for Shipment to a Waste Processor/Broker or a  
Commercial Radwaste Burial Facility, Rev. 10  
RHSI-1.1, Packaging Filters and Items of High Levels of Radiation, Rev. 6  


                                              11
RHSI-6, Bead Resin Activated Carbon Dewatering Procedure for Energy Solutions 14-215 or
11  
  Smaller Liners, Rev. 8
RHSI-7, Utilization of Polyethylene High Integrity Containers (HICs) and HIC Overpacks, Rev. 9
Attachment
RHSI-11, Control of Radioactive Material and Training, Rev. 6
RHSI-6, Bead Resin Activated Carbon Dewatering Procedure for Energy Solutions 14-215 or  
RHSI-13, Administration and Control of Onsite Storage of Low Level Radioactive Waste, Rev. 4
Smaller Liners, Rev. 8  
RWTP-100 Attachment A, Radwaste Training Program, Rev. 3
RHSI-7, Utilization of Polyethylene High Integrity Containers (HICs) and HIC Overpacks, Rev. 9  
RWTP-100, Radioactive Material/Waste Shipments, Rev. 7
RHSI-11, Control of Radioactive Material and Training, Rev. 6  
RWTP-101, 10 CFR 61 Waste Characterization, Rev. 2
RHSI-13, Administration and Control of Onsite Storage of Low Level Radioactive Waste, Rev. 4  
RWTP-102, Use of Casks, Rev. 2
RWTP-100 Attachment A, Radwaste Training Program, Rev. 3  
0-SO-77-29, Waste Processing, Rev. 9
RWTP-100, Radioactive Material/Waste Shipments, Rev. 7  
0-VI-RCI-077-001.0, Operating Procedure for Duratek Modular Fluidized Transfer Demineralizer
RWTP-101, 10 CFR 61 Waste Characterization, Rev. 2  
  System (MFTDS), Rev. 2
RWTP-102, Use of Casks, Rev. 2  
Shipping Records and Radwaste Data
0-SO-77-29, Waste Processing, Rev. 9  
Two Design Change Notices were reviewed and both have been accomplished. The first
0-VI-RCI-077-001.0, Operating Procedure for Duratek Modular Fluidized Transfer Demineralizer  
moved Radwaste liquid processing from the railroad bay into the drumming room that was in
System (MFTDS), Rev. 2  
effect at the start of the period which included back to November 2010 and the second
established a lift system to be used for the steam generator replacement in 2012 with a closure
Shipping Records and Radwaste Data  
date of 8/13/2013.
Two Design Change Notices were reviewed and both have been accomplished. The first  
The licensee provided several drawings delineating abandoned equipment. The inspector
moved Radwaste liquid processing from the railroad bay into the drumming room that was in  
chose the abandoned boric acid evaporator system to review.
effect at the start of the period which included back to November 2010 and the second  
Shipments:
established a lift system to be used for the steam generator replacement in 2012 with a closure  
  SNP-12-0111 (LQ)
date of 8/13/2013.  
  SNP-13-0105 (SCO)
  SNP-13-0109 (Type B)
The licensee provided several drawings delineating abandoned equipment. The inspector  
  SNP-13-0307 (LSA)
chose the abandoned boric acid evaporator system to review.  
  SNP-13-0504 (Type A)
Shipments:  
CAP Documents
SNP-12-0111 (LQ)  
Site Audit Report SSA1309, Radiation Protection, August 19 through August 30, 2013
SNP-13-0105 (SCO)  
Snapshot Self-Assessment Report SQN-RP-S-13-004, Radioactive Solid Waste Processing and
SNP-13-0109 (Type B)  
Radioactive Material Handling, Storage and Transportation, July 29 through August 9, 2013
PERs
SNP-13-0307 (LSA)  
412285
SNP-13-0504 (Type A)  
431332
488136
CAP Documents  
635127
Site Audit Report SSA1309, Radiation Protection, August 19 through August 30, 2013  
735591
Snapshot Self-Assessment Report SQN-RP-S-13-004, Radioactive Solid Waste Processing and  
765281
Radioactive Material Handling, Storage and Transportation, July 29 through August 9, 2013  
767526
783784
PERs
                                                                                    Attachment
412285  
431332  
488136  
635127  
735591  
765281  
767526  
783784  


                                          12
Section 4OA1: Performance Indicator Verification
12  
Procedures, Manuals, and Guides
NSDP-29, Tracking and Trending and NRC Performance Indicators, Rev. 6
Attachment
NPG-SPP-02.2, Performance Indicator Program, Rev. 5
Section 4OA1: Performance Indicator Verification  
RCI-151, Radiation Protection Functional Area Performance Indicators, Rev. 1
Procedures, Manuals, and Guides  
PERs
NSDP-29, Tracking and Trending and NRC Performance Indicators, Rev. 6  
621990
NPG-SPP-02.2, Performance Indicator Program, Rev. 5  
623246
RCI-151, Radiation Protection Functional Area Performance Indicators, Rev. 1  
626962
653648
PERs
655642
621990  
788604
623246  
793921
626962  
794437
653648  
Section 4OA2: Problem Identification and Resolution
655642  
Procedures
788604  
NPG-SPP-03.1, Corrective Action Program, Rev. 1
793921  
Section 4OA5: Other Activities
794437  
0-GO-17, Spent Fuel/Dry Cask Operations, Rev. 5
NPG-SPP-01.2, Administration of Site Technical Procedures, Rev. 9
Section 4OA2: Problem Identification and Resolution  
NFTP-100, Fuel Selection for Dry MPC Storage, Rev. 5 completed for campaign #6
Procedures  
10CFR 72.48 Screening/Evaluation: EDC E22443C
NPG-SPP-03.1, Corrective Action Program, Rev. 1  
SQN-DCS-300.11, Supplemental Cooling System Operation, Rev. 9
CTP-DCS-100.0, Dry Cask Storage Campaign Guidelines, Rev. 15
Section 4OA5: Other Activities  
SQN-DCS-200.0, Dry Cask Campaign Review Program, Rev. 4
0-GO-17, Spent Fuel/Dry Cask Operations, Rev. 5  
SQN-DCS-200.2, SQN-MPC-Loading and Transport Operations, Rev. 35
NPG-SPP-01.2, Administration of Site Technical Procedures, Rev. 9  
                                                                              Attachment
NFTP-100, Fuel Selection for Dry MPC Storage, Rev. 5 completed for campaign #6  
10CFR 72.48 Screening/Evaluation: EDC E22443C  
SQN-DCS-300.11, Supplemental Cooling System Operation, Rev. 9  
CTP-DCS-100.0, Dry Cask Storage Campaign Guidelines, Rev. 15  
SQN-DCS-200.0, Dry Cask Campaign Review Program, Rev. 4  
SQN-DCS-200.2, SQN-MPC-Loading and Transport Operations, Rev. 35  


                                LIST OF ACRONYMS
ABGTS   auxiliary building gas treatment system
Attachment
ALARA   as low as reasonably achievable
LIST OF ACRONYMS  
ASME     American Society of Mechanical Engineers
BACC     boric acid corrosion control
ABGTS  
CAP     corrective action program
auxiliary building gas treatment system  
CCP     centrifugal charging pump
ALARA  
CDE     cause determination evaluation
as low as reasonably achievable  
CFR     Code of Federal Regulations
ASME  
CIV     containment isolation valve
American Society of Mechanical Engineers  
DAW     dry active waste
BACC  
DOT     Department of Transportation
boric acid corrosion control  
ECCS     emergency core cooling system
CAP  
ED       electronic dosimeter
corrective action program  
ERCW     essential raw cooling water
CCP  
FCV     flow control valve
centrifugal charging pump  
FME     foreign material exclusion
CDE  
HRA     high radiation areas
cause determination evaluation  
IMC     inspection manual chapter
CFR  
IP       inspection procedure
Code of Federal Regulations  
ISFSI   independent spent fuel storage installation
CIV  
ISI     in-service inspection
containment isolation valve  
MCC     motor control center
DAW  
MPC     multi-purpose canister
dry active waste  
NCV     non-cited violation
DOT  
NDE     non-destructive examination
Department of Transportation  
NEI     Nuclear Energy Institute
ECCS  
PER     problem evaluation report
emergency core cooling system  
PORV     power operated relief valve
ED  
Radwaste radioactive waste
electronic dosimeter  
RCA     radiologically controlled area
ERCW
Rev     revision
essential raw cooling water
RHR     residual heat removal
FCV  
RS       radiation safety
RTP     rated thermal power
flow control valve  
RWP     radiation work permit
FME  
RWST     refueling water storage tank
foreign material exclusion  
SDP     significance determination process
HRA  
SI       safety injection
high radiation areas  
SR       service request
IMC  
SSC     structure, system, or component
inspection manual chapter  
TS       technical specification
IP  
TVA     Tennessee Valley Authority
inspection procedure  
URI     unresolved item
ISFSI  
UT       ultrasonic testing
independent spent fuel storage installation  
UFSAR   Updated Final Safety Analysis Report
ISI  
WO       work order
in-service inspection  
                                                    Attachment
MCC  
motor control center  
MPC  
multi-purpose canister  
NCV  
non-cited violation  
NDE  
non-destructive examination  
NEI  
Nuclear Energy Institute  
PER  
problem evaluation report  
PORV  
power operated relief valve  
Radwaste  
radioactive waste  
RCA  
radiologically controlled area  
Rev  
revision  
RHR  
residual heat removal  
RS  
radiation safety  
RTP  
rated thermal power  
RWP  
radiation work permit  
RWST  
refueling water storage tank  
SDP  
significance determination process  
SI  
safety injection  
SR  
service request  
SSC  
structure, system, or component
TS  
technical specification  
TVA
Tennessee Valley Authority  
URI  
unresolved item  
UT  
ultrasonic testing  
UFSAR  
Updated Final Safety Analysis Report  
WO  
work order
}}
}}

Latest revision as of 23:21, 10 January 2025

IR 05000327-13-005, 05000328-13-005; 10/1/2013 - 12/31/2013; Sequoyah Nuclear Plant, Units 1 and 2; Other Activities
ML14038A346
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 02/07/2014
From: Bartley J
Reactor Projects Region 2 Branch 6
To: James Shea
Tennessee Valley Authority
References
IR-13-005
Download: ML14038A346 (44)


See also: IR 05000327/2013005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

February 7, 2014

Mr. Joseph W. Shea

Vice President, Nuclear Licensing

Tennessee Valley Authority

1101 Market Street, LP 3D-C

Chattanooga, TN 37402-2801

SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT

05000327/2013005 AND 05000328/2013005

Dear Mr. Shea:

On December 31, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Sequoyah Nuclear Plant, Units 1 and 2. On January 13, 2014, the NRC

inspectors discussed the results of this inspection with Mr. Carlin and other members of your

staff. Inspectors documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented one self-revealing finding of very low safety significance (Green) in

this report. This finding involved a violation of NRC requirements. The NRC is treating this

violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the NRC Enforcement

Policy.

If you contest the violation or significance of this NCV, you should provide a response within 30

days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001; with

copies to the Regional Administrator, Region II; the Director, Office of Enforcement, U.S.

Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident

Inspector at the Sequoyah Nuclear Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the

Sequoyah Nuclear Plant.

As a result of the Safety Culture Common Language Initiative, the terminology and coding of

cross-cutting aspects were revised beginning in calendar year (CY) 2014. New cross-cutting

aspects identified in CY 2014 will be coded under the latest revision to Inspection Manual

Chapter (IMC) 0310. Cross-cutting aspects identified in the last six months of 2013 using the

previous terminology will be converted to the latest revision in accordance with the cross-

reference in IMC 0310. The revised cross-cutting aspects will be evaluated for cross-cutting

themes and potential substantive cross-cutting issues in accordance with IMC 0305 starting with

the CY 2014 mid-cycle assessment review.

J. Shea

2

In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections,

Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRCs Public Document Room or from the Publicly Available Records (PARS) component of

NRCs Agencywide Documents Access and Management System (ADAMS). ADAMS is

accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

Jonathan H. Bartley, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Docket Nos.: 50-327, 50-328

License Nos.: DPR-77, DPR-79

Enclosure: Inspection Report 05000327/2013005, 05000328/2013005

w/Attachment: Supplementary Information

cc: via ListServ distribution

_________________________

SUNSI REVIEW COMPLETE

FORM 665 ATTACHED

OFFICE

RII:DRP

RII:DRP

RII:DRS

RII:DRS

RII:DRS

RII:DRS

RII:DRP

RII:DRP

SIGNATURE

JHB /RA for/

Via email

BRB /RA for/

ORL /RA for/

BRB /RA for/

BRB /RA for/

JDH /RA/

JHB /RA/

NAME

GSmith

WDeschaine

MSpeck

LLake

RHamilton

RKellner

JHamman

JBartley

DATE

02/07/2014

02/07/2014

02/07/2014

02/07/2014

02/07/2014

02/07/2014

02/07/2014

02/07/2014

E-MAIL COPY?

YES

NO YES

NO YES

NO YES

NO YES

NO

YES

NO

YES

NO

J. Shea

3

Letter to J.W. Shea from Jonathan H. Bartley dated February 7, 2014

SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT

05000327/2013005 AND 05000328/2013005

Distribution w/encl:

C. Evans, RII

L. Douglas, RII

OE Mail

RIDSNRRDIRS

PUBLIC

RidsNrrPMSequoyah Resource

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.:

50-327, 50-328

License Nos.:

DPR-77, DPR-79

Report Nos.:

05000327/2013005, 05000328/2013005

Licensee:

Tennessee Valley Authority (TVA)

Facility:

Sequoyah Nuclear Plant, Units 1 and 2

Location:

Sequoyah Access Road

Soddy-Daisy, TN 37379

Dates:

October 1 - December 31, 2013

Inspectors:

G. Smith, Senior Resident Inspector

W. Deschaine, Resident Inspector

M. Speck, Senior Emergency Preparedness Inspector (Sections

1R04.1 and 1R05)

L. Lake, Senior Reactor Inspector (Section 1R08)

R. Hamilton, Senior Health Physicist (Section 2RS8)

R. Kellner, Health Physicist (Sections 2RS1, 4OA1)

Approved by:

Jonathan H. Bartley, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Enclosure

SUMMARY

IR 05000327/2013-005, 05000328/2013-005; 10/1/2013 - 12/31/2013; Sequoyah Nuclear Plant,

Units 1 and 2; Other Activities

The report covered a three-month period of inspection by resident inspectors and announced

inspections by regional inspectors. One self-revealing finding was identified. The significance

of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual

Chapter (IMC) 0609, "Significance Determination Process," (SDP) dated June 2, 2011. Cross-

cutting aspects are determined using IMC 0310, Components Within the Cross-Cutting Areas,

dated October 28, 2011. The NRC's program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4,

dated December 2006.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green: A self-revealing non-cited violation of 10 CFR 50 Appendix B, Criterion XVI,

Corrective Action, was identified for the licensees failure to promptly correct a

condition adverse to quality within a reasonable time. Timely corrective actions were not

taken to correct a dual position indication (open and closed lights both illuminated) on

the Unit 1 A train residual heat removal (RHR) containment sump suction flow control

valve (FCV) 1-FCV-63-72. This licensee entered this issue into the corrective action

program as problem evaluation report (PER) 772193 and performed repairs to the valve

to restore the system to operable status.

This finding was determined to be more than minor because it was associated with the

Design Control attribute of the Mitigating Systems cornerstone and adversely affected

the cornerstones objective to ensure the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences (i.e., core

damage). Specifically, the finding reduced the reliability and capability of the A train

RHR system to perform its safety function as designed. The finding required a detailed

risk analysis as the A RHR system was inoperable beyond its allowed outage time of 72

hours. The detailed risk analysis concluded that the finding was of very low safety

significance (Green). This finding was determined to have a cross-cutting aspect

relating to the proper classification, prioritization, and evaluation of operability and

reportability of conditions adverse to quality in the Corrective Action component of the

Problem Identification and Resolution area. P.1(c) (Section 4OA5)

B.

Licensee-Identified Violations

None

Enclosure

REPORT DETAILS

Summary of Plant Status:

Unit 1 operated at or near 100 percent rated thermal power (RTP) until September 9, 2013,

when the unit entered a power coast down period until October 14 when the unit shut down for a

refueling outage. Unit 1 returned to 100 percent RTP on November 24 where it operated for the

remainder of the inspection period.

Unit 2 operated at or near 100 percent RTP for the entire inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

a.

Inspection Scope

.1

Readiness for Seasonal Extreme Weather Conditions

The inspectors reviewed design features and licensee preparations for protecting the

essential raw cooling water (ERCW) intake structure and both Unit 1 and 2 refueling

water storage tanks (RWSTs) from extreme cold and freezing conditions. The

inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) and Technical

Specifications (TS), reviewed implementation of licensee freeze protection procedures,

walked down portions of the systems to assess deficiencies and system readiness for

extreme cold weather, and discussed prioritization and status of correcting deficiencies

with licensee personnel. Documents reviewed are listed in the Attachment. The

inspectors completed one sample.

b.

Findings

No findings were identified.

1R04 Equipment Alignment

.1

Partial System Walkdown

a.

Inspection Scope

The inspectors performed partial walkdowns of the following three systems to verify the

operability of redundant or diverse trains and components when safety equipment was

inoperable. The inspectors focused on identification of discrepancies that could impact

the function of the system and, therefore, potentially increase risk. The inspectors

reviewed applicable operating procedures, walked down control system components,

and determined whether selected breakers, valves, and support equipment were in the

correct position to support system operation. The inspectors also verified that the

licensee had properly identified and resolved equipment alignment problems that could

4

Enclosure

cause initiating events or impact the capability of mitigating systems or barriers and

entered them into the corrective action program (CAP). Documents reviewed are listed

in the Attachment. The inspectors completed 3 samples.

Spent fuel pool cooling during core empty period of U1R19

1A emergency core cooling train while 1B 669 penetration cooler out-of-service

2A auxiliary feed-water and 2A emergency diesel generator while 2B under-voltage

coils out-of-service

.2

Complete System Walkdown

a.

Inspection Scope

The inspectors performed a complete system walkdown of the: 1) emergency gas

treatment system/auxiliary building gas treatment system (ABGTS); and 2) auxiliary

building ventilation/control building ventilation systems. The purpose of this inspection

was to verify proper equipment alignment, to identify any discrepancies that could impact

the function of the system and increase risk, and to verify that the licensee properly

identified and resolved equipment alignment problems that could cause events or impact

the functional capability of the system.

The inspectors reviewed the UFSAR, system procedures, system drawings, and system

design documents to determine the correct lineup and then examined system

components and their configuration to identify any discrepancies between the existing

system equipment lineup and the correct lineup. During the walkdown, the inspectors

reviewed the following:

Dampers were correctly positioned.

Electrical power was available as required.

Hangers and supports were correctly installed and functional.

Essential support systems were operational.

Ancillary equipment or debris did not interfere with system performance.

Breakers were correctly positioned.

Major system components were correctly labeled.

Cabinets, cable trays, and conduits were correctly installed and functional.

Visible cabling appeared to be in good material condition.

In addition, the inspectors reviewed corrective action items and design issues associated

with the systems to determine whether any condition described in those documents

could adversely impact current system operability. Documents reviewed are listed in the

Attachment. The inspectors completed two samples.

b.

Findings

No findings were identified.

5

Enclosure

1R05 Fire Protection

.1

Fire Protection Tours

a.

Inspection Scope

The inspectors conducted a tour of the six areas important to safety listed below to

assess the material condition and operational status of fire protection features. The

inspectors evaluated whether: combustibles and ignition sources were controlled in

accordance with the licensees administrative procedures; fire detection and suppression

equipment was available for use; passive fire barriers were maintained in good material

condition; and compensatory measures for out-of-service, degraded, or inoperable fire

protection equipment were implemented in accordance with the licensees fire plan.

Documents reviewed are listed in the Attachment. The inspectors completed six

samples.

Unit 1 Lower Containment Building

Unit 1 Upper Containment Building

Control Building Elevation 685 (Auxiliary Instrument Room)

Control Building Elevation 706 (Cable Spreading Room)

ERCW Building - Elevations 688/704/720

Turbine Building - Elevations 662/685

b.

Findings

No findings were identified.

1R06 Flood Protection Measures

.1

Internal Flooding

a.

Inspection Scope

The inspectors examined internal flood protection measures associated with the 1A and

1B safety injection (SI) pump rooms internal flood design in order to verify that flood

mitigation plans were consistent with the design requirements and risk analysis

assumptions. The inspectors verified that equipment essential for reactor shutdown was

properly protected from a flood caused by pipe breaks in the 1A & 1B SI pump room.

Specifically, the inspectors reviewed the licensees moderate energy line break flooding

study to fully understand the licensees flood mitigation strategy, reviewed licensee

drawings and then verified that the assumptions and results remained valid. The

inspectors walked down the 1A & 1B SI pump room to verify the assumed flooding

sources, adequacy of common area drainage, and flood detection instrumentation to

ensure that a flooding event would not impact reactor shutdown capabilities. The

inspectors completed one sample.

6

Enclosure

b.

Findings

No findings were identified.

1R08 Non-Destructive Examination Activities and Welding Activities

a.

Inspection Scope

From October 21-25, 2013, the inspectors conducted an on-site review of the

implementation of the licensees in-service inspection (ISI) Program for monitoring

degradation of the reactor coolant system; emergency feedwater systems, risk-

significant piping and components, and containment systems in Unit 1.

The inspectors activities included a review of non-destructive examinations (NDEs) to

evaluate compliance with the applicable edition of the American Society of Mechanical

Engineers (ASME) Boiler and Pressure Vessel Code,Section XI, and to verify that

indications and defects were appropriately evaluated and dispositioned in accordance

with the requirements of the ASME Code,Section XI, acceptance standards or NRC

approved alternative requirement.

The inspectors directly observed or reviewed records of the following NDEs mandated

by the ASME Code to evaluate compliance with the ASME Code Section XI and Section

V requirements, and if any indications and defects were detected. Inspectors also

reviewed evaluations of results that were dispositioned in accordance with the ASME

Code or an NRC-approved alternative requirement.

Directly observed:

o Ultrasonic testing (UT) examinations of the reactor pressure vessel head to shell

flange studs

o General visual examination of the outside surface of the containment shell

Reviewed records:

o UT examinations of reactor coolant pump #4 bolting

o VT-3 visual examination of containment penetration bolting

o Work Order 113312025 modification of component cooling water system piping

The inspectors reviewed documentation for the repair/replacement of the following

pressure boundary welds. The inspectors evaluated if the licensee applied the pre-

service non-destructive examinations and acceptance criteria required by the

Construction Code. In addition, the inspectors reviewed the welding procedure

specifications, welder qualifications, welding material certifications, and supporting weld

procedure qualification records to evaluate if the weld procedures were qualified in

accordance with the requirements of the Construction Code and the ASME Code

Section XI.

7

Enclosure

PWR Vessel Upper Head Penetration (VUHP) Inspection Activities: For the Unit 1

vessel head, a bare metal visual examination and a volumetric examination required in

accordance with the requirements of ASME Code Case N-729-1 and 10 CFR

50.55a(g)(6)(ii)(D) were conducted in the previous outage and therefore not required to

be performed this outage.

Boric Acid Corrosion Control (BACC) Inspection Activities: The inspectors reviewed the

licensees BACC program activities to ensure implementation with commitments made in

response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor

Pressure Boundary, and applicable industry guidance documents. Specifically, the

inspectors performed an on-site record review of procedures and the results of the

licensees containment walkdown inspections performed during the current refueling

outage. The inspectors also reviewed Focused Self-Assessment CRP-ENG-F-13-031 of

the Boric Acid Program.

The inspectors also interviewed the BACC program owner, conducted an independent

walkdown of containment to evaluate compliance with licensees BACC program

requirements, and verified that degraded or non-conforming conditions, such as boric

acid leaks, were properly identified and corrected in accordance with the licensees

BACC and corrective action programs.

The inspectors reviewed the following evaluations and corrective actions related to

evidence of boric acid leakage to evaluate if the corrective actions completed were

consistent with the requirements of the ASME Code Section XI and 10 CFR Part 50,

Appendix B, Criterion XVI.

Problem Event Report (PER) 618770 - Boron buildup on 1B-B SI pump pedestal

PER 691545 - Boric acid build up and wet boric acid are present on transmitter

sensing line 1-FT-72-41

Steam Generator (SG) Tube Inspection Activities:

There were no SG tube eddy current examinations conducted during this outage. The

inspectors reviewed the following documentation and evaluated them against the

licensees TS, commitments made to the NRC, ASME Section XI, and Nuclear Energy

Institute (NEI) 97-06, Steam Generator Program Guidelines, to ensure that the licensee

was in compliance with the schedule to skip the SG eddy current testing inspections for

the 1R19 outage:

AREVA document # 51-9178898-001, Sequoyah Unit Condition Monitoring for Cycle

18 and Operational Assessment for Cycles 19, 20 and 21

Identification and Resolution of Problems:

The inspectors performed a review of selected ISI-related problems that were identified

by the licensee and entered into the corrective action program as PERs. The inspectors

reviewed the PERs to confirm the licensee had appropriately described the scope of the

problem and had initiated corrective actions. The review also included the licensees

8

Enclosure

consideration and assessment of operating experience events applicable to the plant.

The inspectors performed this review to ensure compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. Documents reviewed are

listed in the Attachment.

b.

Findings

No findings were identified.

1R11 Licensed Operator Requalification Program

.1

Quarterly Review of Licensed Operator Requalification

a.

Inspection Scope

The inspectors performed one licensed operator requalification program review. The

inspectors observed a simulator session on October 9, 2013. The training scenario

involved Just-In-Time Training for Pre-Refueling Outage risk significant activities such as

placing the RHR system in service. The inspectors observed crew performance in terms

of communications; ability to take timely and proper actions; prioritizing, interpreting, and

verifying alarms; correct use and implementation of procedures, including the alarm

response procedures; timely control board operation and manipulation, including high

risk operator actions; oversight and direction provided by shift manager, including the

ability to identify and implement appropriate TS action; and, group dynamics involved in

crew performance. The inspectors also observed the evaluators critique and reviewed

simulator fidelity to verify that it matched actual plant response. Documents reviewed

are listed in the Attachment. The inspectors completed one sample.

b.

Findings

No findings were identified.

.2

Quarterly Review of Licensed Operator Performance

a.

Inspection Scope

The inspectors observed and assessed licensed operator performance in the main

control room during periods of heightened activity or risk. The inspectors reviewed

various licensee policies and procedures such as OPDP-1, Conduct of Operations,

NPG-SPP-10.0, Plant Operations, and 0-GO-5, Normal Power Operation. The

inspectors utilized activities such as post-maintenance testing, surveillance testing,

unplanned transients, infrequent plant evolutions, plant startups and shutdowns, reactor

power and turbine load changes, and refueling and other outage activities to focus on

the following conduct of operations as appropriate:

operator compliance and use of procedures

control board manipulations

communication between crew members

9

Enclosure

use and interpretation of plant instruments, indications, and alarms

use of human error prevention techniques

documentation of activities, including initials and sign-offs in procedures

supervision of activities, including risk and reactivity management

pre-job briefs

Specifically, the inspectors observed licensed operator performance during the following

activities:

Unit 1 reactor shutdown and plant cool down/depressurization

Unit 1 refueling and other outage activities

Unit 1 startup, including Mode changes

Unit 2 down power with turbine in manual for valve testing

Documents reviewed are listed in the Attachment. The inspectors completed one

sample.

b.

Findings

No findings were identified.

.3

Annual Review of Licensee Requalification Examination Results

a.

Inspection Scope

On September 13, 2013, the licensee completed the annual requalification operating

examinations required to be administered to all licensed operators in accordance with 10

CFR 55.59(a)(2), Requalification requirements, of the NRCs Operators Licenses.

The inspectors performed an in-office review of the overall pass/fail results of the

individual operating examinations and the crew simulator operating examinations in

accordance with Inspection Procedure (IP) 71111.11, Licensed Operator Requalification

Program and Licensed Operator Performance. The results were compared to the

thresholds established in Section 3.02, Requalification Examination Results, of IP

71111.11.

b.

Findings

No findings were identified.

1R12 Maintenance Effectiveness

a.

Inspection Scope

The inspectors reviewed five maintenance activities, issues, and/or systems listed below

to verify the effectiveness of the licensees activities in terms of: appropriate work

practices; identifying and addressing common cause failures; scoping in accordance

with 10 CFR 50.65(b); characterizing reliability issues for performance; trending key

10

Enclosure

parameters for condition monitoring; charging unavailability for performance;

classification in accordance with 10 CFR 50.65(a)(1) or (a)(2); appropriateness of

performance criteria for structures, systems, or components (SSCs) and functions

classified as (a)(2); and appropriateness of goals and corrective actions for SSCs and

functions classified as (a)(1). Documents reviewed are listed in the Attachment. The

inspectors completed 5 samples.

MR 11th Periodic Assessment Report (PE sample)

Cause Determination and Evaluation (CDE) #2700, FCV-63-72 Failure

CDE #2696, EBGTS B Fan Failure

CDE #2686, A Shutdown Boardroom Chiller Failure

CDE #2674, B Main Condenser Test Connection Failure

b.

Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a.

Inspection Scope

The inspectors reviewed the following activities to determine whether appropriate risk

assessments were performed prior to removing equipment from service for

maintenance. The inspectors evaluated whether risk assessments were performed as

required by 10 CFR 50.65(a)(4), and were accurate and complete. When emergent

work was performed, the inspectors reviewed whether plant risk was promptly

reassessed and managed. The inspectors also assessed whether the licensees risk

assessment tool use and risk categories were in accordance with Standard Programs

and Processes Procedure NPG-SPP-07.1, On-Line Work Management, Revision 3,

and Instruction 0-TI-DSM-000-007.1, Risk Assessment Guidelines, Revision 9.

Documents reviewed are listed in the Attachment. The inspectors completed 2 samples.

Review U1R19 Outage Schedule

Review of risk during ABGTS outage

b.

Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a.

Inspection Scope

For the eight operability evaluations described in the PERs listed below, the inspectors

evaluated the technical adequacy of the evaluations to ensure that TS operability was

properly justified and the subject component or system remained available, such that no

unrecognized increase in risk occurred. The inspectors compared the operability

11

Enclosure

evaluations to UFSAR descriptions to determine if the system or components intended

function(s) were adversely impacted. In addition, the inspectors reviewed compensatory

measures implemented to determine whether the compensatory measures worked as

stated and the measures were adequately controlled. The inspectors also reviewed a

sampling of PERs to assess whether the licensee was identifying and correcting any

deficiencies associated with operability evaluations. Documents reviewed are listed in

the Attachment. The inspectors completed 8 samples.

PER 789552 - Unit 2 Turbine Controls in Manual

PER 795451 - POE WO 113223153 T1 motor lead pinch

PER 799097 - POE TS LCO 3.7.4 action for FCV-67-146

PER 800432 - POE (ABSCE boundary issue)

PER 795433 - PDO (During U1R19 water found leaking out of conduit in bioshield

wall)

PER 801415 - PDO EDG 1B 2 sec load sequence

PER 803833 - PDO U-1 Rx Head Vent Valve Stroke

PERs 816731, 815638, 817841 - FEs associated with the Unit 1 loose parts alarm

b.

Findings

No findings were identified.

1R18 Plant Modifications

.1

Permanent Modifications

a.

Inspection Scope

The inspectors reviewed the modification listed below and the associated 10 CFR 50.59

screening, and compared it against the UFSAR and TS to verify whether the

modification affected operability or availability of the affected system.

DCN 22643 - Replace Pressurizer Power Operated Relief Valves (PORVs)

Following installation and testing, the inspectors observed indications affected by the

modification, discussed them with operators, and verified that the modification was

installed properly and its operation did not adversely affect safety system functions. The

inspectors did note that, ultimately, the installed PORVs did not meet the acceptance

criteria associated with the close stroke time. As a result, the licensee chose to cut

out/remove the new style PORVs and reinstall the original PORVs prior to plant startup

in November 2013. Documents reviewed are listed in the Attachment. The inspectors

completed one sample.

b.

Findings

No findings were identified.

12

Enclosure

1R19 Post Maintenance Testing

a.

Inspection Scope

The inspectors reviewed the post maintenance tests associated with the nine work

orders (WO) listed below to assess whether procedures and test activities ensured

system operability and functional capability. The inspectors reviewed the licensees test

procedure to evaluate whether: the procedure adequately tested the safety function(s)

that may have been affected by the maintenance activity; the acceptance criteria in the

procedure were consistent with information in the applicable licensing basis and/or

design basis documents; and the procedure had been properly reviewed and approved.

The inspectors also witnessed the test or reviewed the test data to determine whether

test results adequately demonstrated restoration of the affected safety function(s).

Documents reviewed are listed in the Attachment. The inspectors completed nine

samples.

WO 113377829 - Repack Valve (1-LCV-3-175) and perform AIRCET test

WO 112096045 - Repair isolation check valve (1-VLV-026-1296)

WO 111234712 - 5 year PM to swap 480V Shutdown board breaker with a

refurbished breaker

WO 113806636 - Perform 0-MI-EPM-317-102.0 on CCS pump C-S and

clean/replace motor air filter

WO 114560807 - Centrifugal charging pump (CCP) room cooler fan motor current

check, bearing lubrication and cleaning

WO 114198329 - EQ maintenance and inspection

WO 113408190 - Change out electrolytic capacitors in the Woodward 2301A

governor card

WOs 114306842, 114306841, 114325805, 114325799 - Aux Feedwater valves -

836 & 837

WO 113756597 - PORVs - PCV-68-340 & PCV-68-334

b.

Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

.1

Unit 1 Refueling Outage Cycle 19

a.

Inspection Scope

For the Unit 1 refueling outage that began on October 14, 2013, the inspectors

evaluated licensee activities to verify that the licensee considered risk in developing

outage schedules, followed risk reduction methods developed to control plant

configuration, developed mitigation strategies for the loss of key safety functions, and

adhered to operating license and TS requirements that ensure defense-in-depth. The

inspectors also walked down portions of Unit 1 not normally accessible during at-power

13

Enclosure

operations to verify that safety-related and risk-significant SSCs were maintained in an

operable condition. Specifically, between October 14 and November 21, the inspectors

performed inspections and reviews of the following outage activities. Documents

reviewed are listed in the Attachment. The inspectors completed one sample.

Outage Plan. The inspectors reviewed the outage safety plan and contingency plans

to confirm that the licensee had appropriately considered risk, industry experience,

and previous site-specific problems in developing and implementing a plan that

assured maintenance of defense-in-depth.

Reactor Shutdown. The inspectors observed the shutdown in the control room from

the time the reactor was tripped until operators placed it on the RHR system for

decay heat removal to verify that TS cool down restrictions were followed. The

inspectors also toured the lower containment as soon as practicable after reactor

shutdown to observe the general condition of the reactor coolant system (RCS) and

emergency core cooling system components and to look for indications of previously

unidentified leakage inside the polar crane wall.

Licensee Control of Outage Activities. On a daily basis, the inspectors attended the

licensee outage turnover meeting, reviewed PERs, and reviewed the defense-in-

depth status sheets to verify that status control was commensurate with the outage

safety plan and in compliance with the applicable TS when taking equipment out of

service. The inspectors further toured the main control room and areas of the plant

daily to ensure that the following key safety functions were maintained in accordance

with the outage safety plan and TS: electrical power, decay heat removal, spent fuel

cooling, inventory control, reactivity control, and containment closure. The

inspectors also observed a tag-out of the B Train CCP system to verify that the

equipment was appropriately configured to safely support the work and testing. To

ensure that RCS level instrumentation was properly installed and configured to give

accurate information, the inspectors reviewed the installation of the Mansell level

monitoring system. Specifically, the inspectors discussed the system with

engineering, walked it down to verify that it was installed in accordance with

procedures and adequately protected from inadvertent damage, verified that Mansell

indication properly overlapped with pressurizer level instruments during pressurizer

drain-down, verified that operators properly set level alarms to procedurally required

set-points, and verified that the system consistently tracked RCS level while lowering

to reduced inventory conditions. The inspectors also observed operators compare

the Mansell indications with locally-installed ultrasonic level indicators during entry

into reduced inventory conditions.

14

Enclosure

Refueling Activities. The inspectors observed fuel movement at the spent fuel pool

and at the refueling cavity in order to verify compliance with TS and that each

assembly was properly tracked from core offload to core reload. In order to verify

proper licensee control of foreign material, the inspectors verified that personnel

were properly checked before entering any foreign material exclusion (FME) areas,

reviewed FME procedures, and verified that the licensee followed the procedures.

To ensure that fuel assemblies were loaded in the core locations specified by the

design, the inspectors independently reviewed the recording of the licensees final

core verification.

Reduced Inventory and Mid-Loop Conditions. Prior to the outage, the inspectors

reviewed the licensees commitments to Generic Letter 88-17. Before entering

reduced inventory conditions the inspectors verified that these commitments were in

place, that plant configuration was in accordance with those commitments, and that

distractions from unexpected conditions or emergent work did not affect operator

ability to maintain the required reactor vessel level. Mid-loop conditions were not

entered during this outage since SG eddy current testing was not required.

Heat-up and Start-up Activities. The inspectors toured the containment prior to

reactor startup to verify that debris that could affect the performance of the

containment sump had not been left in the containment. The inspectors reviewed

the licensees mode-change checklists to verify that appropriate prerequisites were

met prior to changing TS modes. To verify RCS integrity and containment integrity,

the inspectors further reviewed the licensees RCS leakage calculations and

containment isolation valve lineups. In order to verify that core operating limit

parameters were consistent with core design, the inspectors also examined portions

of the low power physics testing surveillance.

b.

Findings

No findings were identified.

1R22 Surveillance Testing

a.

Inspection Scope

For the twelve surveillance tests identified below, the inspectors assessed whether the

SSCs involved in these tests satisfied the requirements described in the TS surveillance

requirements, the UFSAR, applicable licensee procedures, and whether the tests

demonstrated that the SSCs were capable of performing their intended safety functions.

This was accomplished by witnessing testing and/or reviewing the test data. Documents

reviewed are listed in the Attachment. The inspectors completed twelve samples.

15

Enclosure

In-Service Tests:

1-SI-SXP-003-202.B, Motor Driven Auxiliary Feedwater Pump 1B-B Comprehensive

Performance Test, Revision 7

1-SI-SXP-074-202.0, RHR Pump 1A-A and 1B-B Comprehensive Performance and

Check Valve Test, Revision 10

RCS leakage test:

0-SI-OPS-068-137.0, Reactor Coolant System Water Inventory, Revision 32

Routine Surveillance Tests:

1-SI-OPS-088-001.0, Phase A Isolation Test, Revision 14

1-SI-OPS-082-026A, Loss of Offsite Power with Safety Injection D/G 1A-A Test,

Revision 46

0-SI-SFT-072-138.0, Unit 1 Containment Spray - Spray Nozzle Test, Revision 6

0-SI-SXV-063-203.2, Full Stroking of Safety Injection Cold Leg Accumulator Isolation

Valves, Revision 1

Ice Condenser Surveillance Test:

0-SI-MIN-061-105.0, Ice Condenser Ice Weighing, Revision 11

Containment Isolation Valve (CIV) Surveillance Tests:

0-SI-SLT-067-258.2, Containment Isolation Valve Local Leak Rate Test Lower

Compartment Essential Raw Cooling Water, Revision 13

0-SI-SLT-088-259.4, Upper Personnel Airlock Interlock Operability Test, Revision 2

0-SI-SLT-088-259.1, Upper Personnel Airlock Overall Leak Rate Test and General

Inspection, Revision 6

0-SI-SLT-081-258.1, Containment Isolation Valve Local Leak Rate Test Primary

Water System, Revision 5

b.

Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System Evaluation

a.

Inspection Scope

The inspectors evaluated the adequacy of the licensees methods for testing and

maintaining the alert and notification system in accordance with NRC Inspection

Procedure 71114, Attachment 02, Alert and Notification System Evaluation. The

16

Enclosure

applicable planning standard, 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50,

Appendix E,Section IV.D requirements were used as reference criteria. The criteria

contained in NUREG-0654, Criteria for Preparation and Evaluation of Radiological

Emergency Response Plans and Preparedness in Support of Nuclear Power Plants,

Revision 1, were also used as a reference.

The inspectors reviewed various documents which are listed in the Attachment,

interviewed personnel responsible for system performance, and observed aspects of

periodic siren maintenance and testing. This inspection activity satisfied one inspection

sample for the alert and notification system on a biennial basis.

b.

Findings

No findings were identified.

1EP3 Emergency Response Organization Staffing and Augmentation System

a.

Inspection Scope

The inspectors reviewed the licensees Emergency Response Organization (ERO)

augmentation staffing requirements and process for notifying the ERO to ensure the

readiness of key staff for responding to an event and timely facility activation. The

qualification records of key position ERO personnel were reviewed to ensure all ERO

qualifications were current. A sample of problems identified from augmentation drills or

system tests performed since the last inspection was reviewed to assess the

effectiveness of corrective actions.

The inspection was conducted in accordance with NRC Inspection Procedure 71114,

Attachment 03, Emergency Response Organization Staffing and Augmentation System.

The applicable planning standard, 10 CFR 50.47(b)(2), and its related 10 CFR 50,

Appendix E requirements were used as reference criteria.

The inspectors reviewed various documents which are listed in the Attachment. This

inspection activity satisfied one inspection sample for the ERO staffing and

augmentation system on a biennial basis.

b.

Findings

No findings were identified.

1EP4 Emergency Action Level and Emergency Plan Changes

a.

Inspection Scope

The NRC Office of Nuclear Security and Incident Response headquarters staff

performed an in-office review of the latest revisions of various Emergency Plan

Implementing Procedures (EPIPs) and the Emergency Plan located under ADAMS

17

Enclosure

Accession numbers ML12326A678, ML12353A050, ML13025A102, ML13070A025,

ML13219A022, and ML13246A091.

The licensee determined that in accordance with 10 CFR 50.54(q), the changes made in

the revisions resulted in no reduction in the effectiveness of the Plan, and that the

revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to

10 CFR Part 50. The NRC review was not documented in a safety evaluation report and

did not constitute approval of licensee-generated changes; therefore, these revisions are

subject to future inspection. Documents reviewed are listed in the Attachment. The

inspectors completed one sample.

b.

Findings

No findings were identified.

1EP5 Maintenance of Emergency Preparedness

a. Inspection Scope

The inspectors reviewed the corrective actions identified through the Emergency

Preparedness program to determine the significance of the issues, the completeness

and effectiveness of corrective actions, and to determine if issues were recurring. The

licensees post-event after action reports, self-assessments, and audits were reviewed to

assess the licensees ability to be self-critical, thus avoiding complacency and

degradation of their emergency preparedness program. Inspectors reviewed the

licensees 10 CFR 50.54(q) change process, personnel training, and selected

screenings and evaluations to assess adequacy. The inspectors toured facilities and

reviewed equipment and facility maintenance records to assess licensees adequacy in

maintaining them. The inspectors evaluated the capabilities of selected radiation

monitoring instrumentation to adequately support Emergency Action Level (EAL)

declarations.

The inspection was conducted in accordance with NRC Inspection Procedure 71114.05,

Maintenance of Emergency Preparedness. The applicable planning standards, related

10 CFR 50, Appendix E requirements, and 10 CFR 50.54(q) and (t) were used as

reference criteria.

The inspectors reviewed various documents which are listed in the Attachment. This

inspection activity satisfied one inspection sample for the maintenance of emergency

preparedness on a biennial basis.

b.

Findings

No findings were identified.

18

Enclosure

2.

RADIATION SAFETY (RS)

Cornerstones: Occupational Radiation Safety (OS) and Public Radiation Safety (PS)

2RS1 Radiological Hazard Assessment and Exposure Controls

a.

Inspection Scope

Hazard Assessment and Instructions to Workers: During facility tours, the inspectors

directly observed labeling of radioactive material and postings for radiation areas, high

radiation areas (HRAs), and airborne radioactivity areas established within the

radiologically controlled area (RCA) of the Unit 1 containment, Unit 1 and Unit 2 auxiliary

buildings, Independent Spent Fuel Storage Installation (ISFSI), and radioactive waste

(radwaste) processing and storage locations. The inspectors independently measured

radiation dose rates or directly observed conduct of licensee radiation surveys for RCA

areas in the Unit 1 containment, Unit 1 and Unit 2 Auxiliary buildings, and ISFSI. The

inspectors reviewed survey records for several plant areas including surveys for alpha

emitters, airborne radioactivity, and pre-job surveys for selected Unit 1 Refueling Outage

19 (U1R19) tasks. The inspectors also discussed changes to plant operations that could

contribute to changing radiological conditions since the last inspection and reviewed

U1R19 crud burst results and post crud burst dose rate surveys. For selected U1R19

outage jobs, the inspectors attended, or reviewed, pre-job briefings and radiation work

permit (RWP) details to assess communication of radiological control requirements and

current radiological conditions to workers. Selected U1R19 work activities included Unit

1 control rod drive mechanism duct work, Unit 1 Refueling Activities, Unit 1 Head O-ring

Surface Work & Inspection, and work in the Unit 1 Equipment Pit and transfer canal.

Hazard Control and Work Practices: The inspectors evaluated access barrier

effectiveness for selected Unit 1 and Unit 2 Locked High Radiation Area (LHRA) and

Very High Radiation Area (VHRA) locations. Changes to procedural guidance for LHRA

and VHRA controls were discussed with health physics (HP) supervisors. Controls and

their implementation for storage of irradiated material within the spent fuel pool (SFP)

were reviewed and discussed in detail. Established radiological controls (including

airborne controls) were evaluated for selected U1R19 tasks including refueling and

reactor cavity work activities, work in auxiliary building HRAs, and radwaste processing

and storage. In addition, licensee controls for areas where dose rates could change

significantly as a result of plant shutdown and refueling operations were reviewed and

discussed.

Occupational workers adherence to selected RWPs and HP technician (HPT)

proficiency in providing job coverage were evaluated through direct observations and

interviews with licensee staff. Electronic dosimeter (ED) alarm set points and worker

stay times were evaluated against area radiation survey results for refueling and reactor

cavity work. ED alarm logs were reviewed and worker response to dose and dose rate

alarms during selected work activities was evaluated. For HRA tasks involving

significant dose rate gradients, e.g. reactor head O-ring work, the inspectors evaluated

the use and placement of whole body and extremity dosimetry to monitor worker

exposure.

19

Enclosure

Control of Radioactive Material: The inspectors observed surveys of material and

personnel being released from the RCA using small article monitor, personnel

contamination monitor, and portal monitor instruments. The inspectors reviewed the last

two calibration records for selected release point survey instruments and discussed

equipment sensitivity, alarm set points, and release program guidance with licensee

staff. The inspectors compared recent 10 CFR Part 61 results for the Dry Active Waste

(DAW) radioactive waste stream with radionuclides used in calibration sources to

evaluate the appropriateness and accuracy of release survey instrumentation. The

inspectors also reviewed records of leak tests on selected sealed sources and discussed

nationally tracked source transactions with licensee staff.

Problem Identification and Resolution: PERs associated with radiological hazard

assessment and control were reviewed and assessed. The inspectors evaluated the

licensees ability to identify and resolve the issues in accordance with procedure NPG-

SPP-22.300, Corrective Action Program, Rev. 0. The inspectors also evaluated the

scope of the licensees internal audit program and reviewed recent assessment results.

Radiation protection activities were evaluated against the requirements of UFSAR

Section 12; TS Sections 6.8 and 6.12; 10 CFR Parts 19 and 20; and approved licensee

procedures. Licensee programs for monitoring materials and personnel released from

the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of

Radioactively Contaminated Material. Documents reviewed are listed in the

Attachment. The inspectors completed one sample.

b.

Findings

No findings were identified.

2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and

Transportation

a.

Inspection Scope

Waste Processing and Characterization: During inspector walkdowns, accessible

sections of the liquid and solid radwaste processing systems were assessed for material

condition and conformance with system design diagrams. Inspected equipment included

radwaste storage tanks; resin transfer piping, resin, and filter packaging components;

and abandoned boric acid evaporator equipment. The inspectors discussed component

function, processing system changes, and radwaste program implementation with

licensee staff.

The radionuclide characterizations for 2010, and 2012, for selected waste streams were

reviewed and discussed with Radwaste/Transportation staff. For primary resin, reactor

coolant system filters, and DAW, the inspectors evaluated analyses for hard-to-detect

nuclides, reviewed the use of scaling factors, and examined quality assurance

comparison results between licensee waste stream characterizations and outside

laboratory data. Waste stream mixing and concentration averaging methodology for

resins and filters was evaluated and discussed with Radwaste/Transportation staff. The

20

Enclosure

inspectors also reviewed the licensees procedural guidance for monitoring changes in

waste stream isotopic mixtures. The 10 CFR 61 analysis results were also discussed

with Chemistry personnel.

Radioactive Material Storage: During walkdowns of indoor and outdoor radioactive

material storage areas, the inspectors observed the physical condition and labeling of

storage containers and the posting of Radioactive Material Areas. The inspectors also

reviewed licensee procedural guidance for storage and monitoring of radioactive

material.

Transportation: The inspectors observed a shipment of vendor equipment during the

week of inspection. The inspectors reviewed shipping procedure requirements and

discussed preparation of shipping documents, package marking and labeling, and

interviewed shipping technicians regarding Department of Transportation (DOT)

regulations.

Selected shipping records were reviewed for consistency with licensee procedures and

compliance with NRC and DOT regulations. The inspectors reviewed emergency

response information, DOT shipping package classification, waste classification,

radiation survey results, and evaluated whether receiving licensees were authorized to

accept the packages. Licensee procedures for handling shipping containers were

compared to Certificate of Compliance requirements and manufacturer

recommendations. In addition, training records for selected individuals currently

qualified to ship radioactive material were reviewed.

Radwaste processing activities and equipment configuration were reviewed for

compliance with the licensees Process Control Program and UFSAR, Chapter 11.

Waste stream characterization analyses were reviewed against regulations detailed in

10 CFR Part 20, 10 CFR Part 61, and guidance provided in the Branch Technical

Position on Waste Classification (1983). Radioactive material and waste storage

activities were reviewed against the requirements of 10 CFR Part 20. Transportation

program implementation was reviewed against regulations detailed in 10 CFR Part 20,

10 CFR Part 71, 49 CFR Parts 172-178, as well as the guidance provided in NUREG-

1608. Training activities were assessed against 49 CFR Part 172, Subpart H.

Problem Identification and Resolution: The inspectors reviewed PERs in the area of

radwaste processing and transportation. The inspectors evaluated the licensees ability

to identify and resolve the issues in accordance with procedure NPG-SPP-22.300,. The

inspectors also evaluated the scope of the licensees internal audit program and

reviewed recent assessment results. Documents reviewed are listed in the Attachment.

The inspectors completed one sample.

b.

Findings

No findings were identified.

21

Enclosure

4.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

a.

Inspection Scope

Occupational Radiation Safety Cornerstone: The inspectors reviewed the Occupational

Exposure Control Effectiveness PI results for the Occupational Radiation Safety

Cornerstone from October 2012 through October 2013. For the assessment period, the

inspectors reviewed ED alarm logs and selected PERs related to controls for exposure

significant areas. The inspectors also reviewed licensee procedural guidance for

collecting and documenting PI data. Documents reviewed are listed in the Attachment.

The inspectors completed one sample.

Emergency Preparedness Cornerstone:

Drill/Exercise Performance (DEP)

Emergency Response Organization Drill Participation (ERO)

Alert and Notification System Reliability (ANS)

For the specified review period, the inspectors examined data reported to the NRC,

procedural guidance for reporting PI information, and records used by the licensee to

identify potential PI occurrences. The inspectors verified the accuracy of the PI for ERO

drill and exercise performance through review of a sample of drill and event records.

The inspectors reviewed selected training records to verify the accuracy of the PI for

ERO drill participation for personnel assigned to key positions in the ERO. The

inspectors verified the accuracy of the PI for alert and notification system reliability

through review of a sample of the licensees records of periodic system tests. The

inspectors also interviewed the licensee personnel who were responsible for collecting

and evaluating the PI data. Documents reviewed are listed in the Attachment. This

inspection satisfied three inspection samples for PI verification on an annual basis.

b.

Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1

Routine Review

a.

Inspection Scope

As required by IP 71152, Problem Identification and Resolution, and in order to help

identify repetitive equipment failures or specific human performance issues for follow-up,

the inspectors performed a daily screening of items entered into the licensees CAP.

This was accomplished by reviewing the description of each new PER and attending

daily management review committee meetings.

22

Enclosure

b.

Findings

No findings were identified.

.2

Annual Follow-up of Selected Issues

a.

Inspection Scope

The inspectors performed an in-depth review of PER 665633, NRC identified freeze

protection issues. The inspectors reviewed the actions taken to determine if the

licensee had adequately addressed the following attributes. Documents reviewed are

listed in the Attachment. The inspectors completed one sample for Annual Follow-up of

Selected Issues.

Complete, accurate and timely identification of the problem

Evaluation and disposition of operability and reportability issues

Consideration of previous failures, extent of condition, generic or common cause

implications

Prioritization and resolution of the issue commensurate with safety significance

Identification of the root cause and contributing causes of the problem

Identification and implementation of corrective actions commensurate with the safety

significance of the issue

b.

Findings

No findings were identified.

.3

Semiannual Trend Review

a.

Inspection Scope

As required by IP 71152, the inspectors performed a review of the licensees corrective

action program and associated documents to identify trends that could indicate the

existence of a more significant safety issue. The inspectors review was focused on

repetitive equipment issues, but also included licensee trending efforts and licensee

human performance results. The inspectors review nominally considered the twelve-

month period of January 2013 through December 2013, although some examples

expanded beyond those dates when the scope of the trend warranted. Specifically, the

inspectors considered the results of daily inspector screening discussed in Section

4OA2.1 and reviewed licensee trend reports for the period in order to determine the

existence of any adverse trends that the licensee may not have previously identified.

Documents reviewed are listed in the Attachment. The inspectors completed one

sample for Semiannual Trend Review.

b.

Findings and Observations

No findings were identified. In general, the licensee had identified trends and

23

Enclosure

appropriately addressed them in their CAP. The inspectors evaluated the licensee

trending methodology and observed that the licensee had performed a detailed review.

The licensee routinely reviewed cause codes, involved organizations, key words, and

system links to identify potential trends in their data. The inspectors compared the

licensee process results with the results of the inspectors daily screening. No

previously unidentified trends of significance were identified.

.4

Annual Follow-up of Operator Workarounds

a.

Inspection Scope

The inspectors reviewed the operator workaround (OWA) program to verify that OWAs

were identified at an appropriate threshold, were entered into the CAP, and that

corrective actions were appropriate and timely. Specifically, the inspectors reviewed the

licensees workaround lists and repair schedules, reviewed CAP word searches,

conducted tours and interviewed operators and operations department support staff.

Additionally, the inspectors checked for undocumented workarounds by observing

operators perform rounds, reviewed operator deficiency lists, reviewed appropriate

system health documents, attended plant health committee meetings, and verified that

identified program deficiencies were corrected. The inspectors evaluated all

workarounds for their aggregate impact. Documents reviewed are listed in the

Attachment. The inspectors completed one sample for Annual Follow-up of Operator

Workarounds.

b.

Findings

No findings were identified.

4OA5 Other Activities

.1

(Closed) Unresolved Item (URI) 050000327/2013004-01, Water Intrusion into Actuator of

Valve 1-FCV-63-72

a.

Inspection Scope

The inspectors opened this URI as a result of water intrusion into the actuator of 1-FCV-

63-72, which is the A train containment sump suction for the Unit 1 A RHR train. This

issue was noted during an operability inspection conducted last quarter. The inspectors

determined more inspection was required in order to resolve the issue. On August 8,

2013, an operator noted the valve exhibited dual indication and on August 14, a related

valve, 1-FCV-74-3, failed its periodic stroke test. The following day, 1-FCV-63-72 was

noted to be failed as well due to a large of amount of water buildup in the actuator. A

subsequent root cause of the failure was completed during this inspection period and

concluded the water intrusion was due to groundwater which migrated through the wall

of the RHR valve vault room and into the valve conduit. Although the circumstances

regarding the water intrusion may have been beyond the licensees ability to predict, the

24

Enclosure

inspectors noted there were opportunities before August 14 to identify and correct the

deficient condition. Thus, the inspectors identified the following non-cited violation

(NCV) as discussed below. Documents reviewed are listed in the Attachment.

b.

Findings

Introduction: A self-revealing Green NCV of 10 CFR 50 Appendix B, Criterion XVI,

Corrective Action, was identified for the licensees failure to correct a condition adverse

to quality within a reasonable amount of time. Timely corrective actions were not taken

to correct a dual position indication (open and closed lights both illuminated) on the Unit

1 A train RHR containment sump suction flow control valve 1-FCV-63-72.

Description: On August 8 at 0709, the Unit 1 control room operator noted that valve 1-

FCV-63-72 showed dual position indication on the control board. This valve is the A

train RHR suction valve from the reactor containment sump and is normally closed,

showing only a single position indication lamp on the control board. Valve 1-FCV-63-72

was verified to be locally closed. No other activities were noted that would have caused

the valve to come off its closed seat. Initial troubleshooting for the dual indication

consisted of: 1) a visual inspection of the valve; 2) a visual inspection of the motor

control center (MCC) cubicle during an attempted closure of the valve; 3) a review of the

wiring diagram by a troubleshooting team; 4) replacement of the MCC light indicating

bulb; and 5) a visual inspection of the main control room (MCR) hand switch. Based on

the troubleshooting teams analysis of the wiring diagrams, no impact was expected on

the interlocks associated with 1-FCV-63-72. The team initially concluded that the most

likely cause of the indication was a short circuit in the control power indication in the

MCR valve hand switch. Based on this conclusion, plus the fact that the valve is not

normally stroked at power (due to concerns of accidently transferring borated water from

the RWST to the containment sump), the licensee chose not to immediately stroke test

1-FCV-63-72. Instead, the licensee declared the position indication for the valve

inoperable per Post Accident Monitoring requirements as delineated in TS 3.9.1. This

was a 30 day limiting condition for operation. The licensee then began development of a

troubleshooting plan which would require more intrusive troubleshooting of the issue

starting the following week.

On August 14 at 2315, during a routine quarterly inservice testing valve stroke activity,

valve 1-FCV-74-3 failed to stroke in the closed direction from the control room. This

valve is the A train RHR suction valve from the RWST and is normally open. Valve 1-

FCV-74-3 was immediately declared out of service and the 72-hour Emergency Core

Cooling Systems (ECCS) TS 3.5.2 action statement was entered. During

troubleshooting, operators attempted to close valve 1-FCV-74-3 remotely from the MCC

cubicle. This action blew control power fuses. The licensee then attempted local

manual operation and noted 1-FVC-74-3 could be manually closed without binding.

Valve 1-FCV-74-3 was partially manually closed and then reopened from the MCC

without incident. Due to the relationship between valves 1-FCV-63-72 and 1-FCV-74-3

(interlocks, shared wiring in junction boxes, etc.) the licensee suspected that the failure

of valve 1-FCV-74-3 to close and valve 1-FCV-63-72 dual position indication were

related.

25

Enclosure

The licensee subsequently opened the 1-FCV-63-72 actuator and noted that a

significant amount of water had accumulated inside the actuator. This water caused

significant electrical shorting in the valve control circuit and rendered the valve

inoperable. Also, the water affected valve 1-FCV-74-3, as this valve utilizes contacts

from valve 1-FCV-63-72 circuitry. It was noted that a low current short caused the failure

of the closing coil for valve 1-FCV-74-3. Following repairs to both 1-FCV-63-72 and

1-FCV-74-3, the ECCS system was returned to operable status on August 17 at 0200.

The licensees past operability determination concluded that 1-FCV-63-72 and 1-FCV-

74-3 were likely inoperable beginning on August 8 when 1-FCV-63-72 was noted to have

a dual indication. Thus the A train ECCS system was most likely inoperable for

approximately nine days, which exceeded the TS allowable outage time. On October

21, 2013, Licensee Event Report 50-327/2013-003 was submitted as a result of this

issue. The licensee concluded that the source of the water was ground water that had

migrated through the concrete ceiling that housed the valve and actuator cables. The

ground water leaked through the threaded penetration seal and inside the conduit and

flowed down into the valve actuator. During the most recent Unit 1 refueling outage in

November 2013, the licensee redesigned the conduit penetration to prevent the intrusion

of moisture into the conduit. The licensee noted the rate of moisture intrusion was most

likely higher in the recent months due to a higher than normal amount of rainfall that

temporarily raised the water table in the vicinity of the plant. The inspectors also noted

that on February 29, 2012, the licensee discovered water buildup in the actuator of 1-

FCV-63-72. This deficiency was entered into the CAP; however it appears that this

precursor was not adequately evaluated such that continued water intrusion ultimately

led to the failure noted on August 8, 2013.

Analysis: The licensees failure to take timely actions to correct a condition adverse to

quality was a performance deficiency. The inspectors concluded that testing and

inspection could have determined that valve 1-FCV-63-72 was inoperable much earlier

than August 14 when it was noted that RHR suction valve to the RWST, 1-FCV-74-3, did

not pass its routine surveillance test. This finding was determined to be more than minor

because it was associated with the Design Control attribute of the Mitigating Systems

cornerstone and adversely affected the cornerstones objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences (i.e., core damage). Specifically, the finding reduced the

reliability and capability of the A train RHR system to perform its safety function as

designed. Using IMC 0609.04, Initial Characterization of Findings, dated June 19,

2012, and IMC 0609, Appendix A, Exhibit 4 - External Events Screening Questions,

dated June 19, 2012, the finding required a detailed risk analysis as the A RHR system

was inoperable beyond its TS-allowed outage time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The detailed risk

analysis concluded that the finding was of very low safety significance (Green).

A Phase 3 analysis was performed by the regional Senior Reactor Analyst to determine

the impact of the finding. The analysis assumed a recoverable failure of the 1-FCV-63-

72 valve, along with a dependent failure of the 1-FCV-74-3 valve. The major impacts

were in the swapover from the RWST to the containment sump as the source of water to

26

Enclosure

mitigate medium and smaller LOCA sequences. Because of the low exposure time, the

availability of the opposite train, and the ability of the operations staff to operate the

effected valves manually, the finding was determined to be Green.

The cause of this finding was determined to have a cross-cutting aspect relating to the

proper classification, prioritization, and evaluation of operability and reportability of

conditions adverse to quality in the Corrective Action component of the Problem

Identification and Resolution area, in that, on February 29, 2012, the licensee discovered

water buildup in the actuator of 1-FCV-63-72 and did not adequately evaluated the

condition adverse to quality such that continued water intrusion ultimately led to the

failure noted on August 8, 2013. P.1(c)

Enforcement: Title 10 of the Code of Federal Regulations Part 50, Appendix B, Criterion

XVI, Corrective Action, requires, in part, that measures shall be established to assure

that conditions adverse to quality, such as failures, malfunctions, deficiencies,

deviations, defective material and equipment, and non-conformances are promptly

identified and corrected. Contrary to the above, from August 8 through August 17, 2013,

the licensee failed to assure that a condition adverse to quality, the failure of valve FCV-

63-72, was corrected in a timely manner. Specifically, the licensee failed to sufficiently

evaluate and correct a moisture intrusion problem associated with the RHR containment

suction motor-operated valve. Corrective actions taken by the licensee included

redesigning and modifying the conduit penetration to prevent the intrusion of moisture

into the conduit. The violation was entered into the licensees CAP as PER 772193.

This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy and will be identified as NCV 05000327/2013005-01, Unit 1 Train

A RHR Containment Suction Valve Failure.

.2

Quarterly Resident Inspector Observations of Security Personnel and Activities

a.

Inspection Scope

During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors normal plant status review and inspection activities.

b.

Findings

No findings were identified.

27

Enclosure

.3

Review of the Operation of an Independent Spent Fuel Storage Installation (ISFSI)

(60855.1)

a.

Inspection Scope

The inspectors performed a walkdown with the field operator of the ISFSI storage pad on

December 26, 2013, to verify that operations were conducted in a safe manner in

accordance with approved procedures and without undue risk to the health and safety of

the public. The inspectors noted that there were 40 multi-purpose canisters (MPCs)

positioned on the ISFSI pad. The inspectors verified the MPC vents were in good

condition and free of obstruction. The inspectors also verified natural circulation within

the MPCs. The inspectors verified that any ISFSI problems were placed in the CAP.

The inspectors also reviewed ISFSI document control practices to verify that changes to

the required ISFSI procedures and equipment were performed in accordance with

guidelines established in local procedures and 10 CFR 72.48. Documents reviewed are

listed in the Attachment.

b.

Findings

No findings were identified.

4OA6 Meetings

.1

Exit Meeting Summary

On January 13, 2014, the resident inspectors presented the inspection results to Mr.

Carlin and other members of his staff, who acknowledged the finding. The inspectors

asked the licensee whether any of the material examined during the inspection should

be considered proprietary. No proprietary information was identified.

ATTACHMENT: SUPPLEMENTARY INFORMATION

Attachment

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

J. Alfultis, Director of Modifications & Projects

J. Carlin, Site Vice President

J. Cross, Chemistry Manager

A. Day, Radiation Protection Manager

D. Erb, Work Control Manager

M. Henderson, ISI Program Engineer

H. Hill, Rad Waste Superintendent

J. Johnson, Program Manager Licensing

A. Little, Site Security Manager

K. Loomis, Boric Acid Program Engineer

T. Marshall, Operations Manager

M. McBrearty, Licensing Manager

S. McCamy, Quality Assurance Manager

S. Mohorn, Rad Waste Superintendent

P. Noe, Director Safety and Licensing

C. Owens, Rad Waste HP

W. Pierce, Site Engineering Director

P. Pratt, Manager, Maintenance

J. Rolph, Radiation Protection Technical Support Superintendent

P. Simmons, Plant Manager

K. Smith, Director of Training

D. Sutton, Licensing

J. Stamey, Rad Waste Health Physicist

J. Stewart, Chemist

NRC personnel

S. Lingam, Project Manager, Office of Nuclear Reactor Regulation

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed 05000327/2013005-01

NCV

Unit 1 Train A RHR Containment Suction

Valve Failure (Section 4OA5)

Closed 05000327/2013004-01

URI

Water Intrusion Into Actuator of Valve 1-

FCV-63-72 (Section 4OA5)

Enclosure

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

0-PI-OPS-006.0, Freeze Protection, Rev. 55

Service Requests (SRs)

SR 807550

SR 825408

SR 821489

Section 1R04: Equipment Alignment

Partial System Walkdowns

Procedures

0-GO-16, System Operability Checklists, Rev. 4

Other documents

UFSAR Section 9

Procedures

0-SI-OPS-030-021.A, Auxiliary Building Gas Treatment System Train A, Rev. 6

0-SI-OPS-030-021.B, Auxiliary Building Gas Treatment System Train B, Rev. 6

0-SO-30-18, Auxiliary Building Gas Treatment System, Rev. 14

0-SO-65-1, Emergency Gas Treatment System Air Cleanup and Annulus Vacuum, Rev. 27

0-SO-30-1, Control Building Heating, Air Conditioning, and Ventilation, Rev. 39

0-SO-30-10, Auxiliary Building Ventilation Systems, Rev. 54

Section 1R05: Fire Protection

Procedures

FPDP-1, Conduct of Fire Protection, Rev. 2

0-PI-FPU-317-299.W, Att. 8, Shift Check List, Rev. 32

NPG-SPP-18.4.7, Control of Transient Combustibles, Rev. 0

EITP-100, Environmental Compliance, Rev. 6

0-SI-FPU-410-703.0, Inspection of FPR Required Fire Doors, Rev. 5

SQN-FPR-Part-II, SQN Fire Protection Report Part II - Fire Protection Plan, Rev. 28

Other documents

Fire Protection Pre-Fire Plans for Unit 1 Lower Containment Building

Fire Protection Pre-Fire Plans for Unit 2 Lower Containment Building

Fire Protection Pre-Fire Plans for Control Building Elevation 685 (Auxiliary Instrument Room)

Fire Protection Pre-Fire Plans for Control Building Elevation 706 (Cable Spreading Room)

Fire Protection Pre-Fire Plans for ERCW Building - Elevations 688/704/720

Fire Protection Pre-Fire Plans for Turbine Building - Elevations 662/685

Section 1R06: Flood Protection Measures

Work Orders

WO 11108121224, Check Standing Water Level in Manholes/Handholes

3

Attachment

Other documents

TVA letter to NRC dated May 4, 2007. TVA response to GL 2007-01

Section 1R08: Inservice Inspection Activities

Procedures

N-VT-15 - Visual Examination of Class MC and Metallic Liners of Class CC Components of

Light-Water cooled Plants, Rev. 11

N-VT-16 - General Visual Examination Containment Vessel Integrity Verification, Rev. 05

N-UT-67 - Generic Procedure for Straight Beam Ultrasonic Examination of Bolts and Studs,

Rev. 05

PDI-UT-5 - Generic Procedure for Straight Beam Ultrasonic Examination of Bolts and Studs,

Rev. D34

IEP-200 - Qualification and Certification Requirements for TVA Inspection Services

Organization (ISO) Nondestructive (NDE) Personnel, Rev. 13

Corrective Action Documents

PER 618770 - Boron buildup on 1B-B SIS Pump Pedestal

PER 691545 - Boric acid build up and wet boric acid are present on transmitter sensing line

1-ft-72-41

PER 01-010244 - Minor concrete voids in U1C11 Vt-3 inspection

PER 169175 - Airline cracks in ceiling beneath reactor cavity and reactor wall

SR 797854 - Hairline cracking in the concrete beneath the fuel transfer canal in lower

containment

SR 526607 - Spalling on baseplate of Protection Device No. 1 on Drawing 48N1701-17.

SR 797166 - Boric acid on Reactor Coolant Pump #1 on #3 seal

SR 797061 - Boric acid on valve 1-FCV-063-0098

SR 797072 - Two areas of white deposit in Fan Room 2

Other documents

Periodic Instruction 0-PI-DXI-000-116.2, ASME Section XI IWE/IWL Containment Inservice

Inspection (CSI) Program, Rev. 05

Q-NIC-100 - Written Practice for the Qualification and Certification of Nondestructive

Examination (NDE0 Personnel, Rev. 20-TVA

IHI Southwest Technologies, Inc. Operating Procedure 2.0-NDES-001, Nondestructive

Examination Personnel Qualification and Certification, Rev. 06

WO 113312025 - Modify Component Cooling Piping to eliminate interference with actuator for

1-FC-063-011

Section 1R12: Maintenance Effectiveness

Procedures

TI-4, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -

10CFR50.65, Rev. 23

Other documents

MR 11th Periodic Assessment Report (PE sample)

Cause Determination and Evaluation (CDE) #2700, FCV-63-72 Failure

CDE #2696, EBGTS B Fan Failure

4

Attachment

CDE #2686, A Shutdown Boardroom Chiller Failure

CDE #2674, B Main Condenser Test Connection Failure

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

0-TI-DSM-000-007.1, Risk Assessment Guidelines, Rev. 9

NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 3

NPG-SPP-07.2.4, Forced Outage or Short Duration Planned Outage Management, Rev. 0

NPG-SPP-07.2, Outage Management, Rev. 0

GOI-6, Apparatus Operations, Rev. 142

Section 1R15: Operability Determinations and Functionality Assessments

Procedures

NEDP-22, Functional Evaluations, Rev. 9

OPDP-8, Limiting Conditions for Operation Tracking, Rev. 5

NPG-SPP-03.5, Regulatory Reporting Requirements, Rev. 2

PERs

789552 - Unit 2 Turbine Controls in Manual

795451 - POE WO 113223153 T1 motor lead pinch

799097 - POE TS LCO 3.7.4 action for FCV-67-146

800432 - POE (ABSCE boundary issue)

795433 - PDO (During U1R19 water found leaking out of conduit in bioshield wall)

801415 - PDO EDG 1B 2 sec load sequence

803833 - PDO U-1 Rx Head Vent Valve Stroke

816731, 815638, 817841 - FEs associated with the Unit 1 loose parts alarm

Section 1R18: Plant Modifications

Procedures

NPG-SPP-09.3, Plant Modifications and Engineering Change Control, Rev. 4

NPG-SPP-09.4, 10 CFR 50.59 Evaluations of Changes, Tests, and Experiments, Rev. 1

NPG-SPP-09.5, Temporary Alterations, Rev. 0

Other documents

DCN 22643 - Replace Pressurizer PORVs

Section 1R19: Post Maintenance Testing

Procedures

MMDP-1, Maintenance Management System, Rev. 20

MMDP-3, Guidelines for Planning and Execution of Troubleshooting Activities, Rev. 6

NPG-SPP-6.5, Foreign Material Control, Rev. 0

NPG-SPP-6.1, Work Order Process Initiation, Rev. 0

NPG-SPP-06.3, Pre-/Post-Maintenance Testing, Rev. 0

NPG-SPP-06.9, Testing Programs, Rev. 0

NPG-SPP-06.9.1, Conduct of Testing, Rev. 1

NPG-SPP-06.9.3, Post-Modification Testing, Rev. 0

5

Attachment

Work Orders

114306842 - Disassemble and reassemble valve in support of 113716425

114306841 - Remove actuator, install actuator, set up calibration in support of 113716425

114325805 - Disassemble and reassemble valve in support of 113716459

114325799 - Remove and install actuator in support of 113716459

113756597 - PORVs - PCV-68-340 & pcv-68-334 Replacement activities

113377829 - Repack Valve (1-LCV-3-175) and perform AIRCET test

112096045 - Repair isolation check valve (1-VLV-026-1296)

111234712 - 5 year PM to swap 480V Shutdown board breaker with a refurbished breaker

113806636 - Perform 0-MI-EPM-317-102.0 on CCS pump C-S and clean/replace motor air filter

114560807 - CCP room cooler fan motor current check, bearing lubrication and cleaning

114198329 - EQ maintenance and inspection

113408190 - Change out electrolytic capacitors in the Woodward 2301A governor card

Section 1R20: Refueling and Other Outage Activities

Procedures

FHI-3, Movement of Fuel, Rev. 65

0-GO-15, Containment Closure Control, Rev. 34

0-GO-13, Reactor Coolant System Drain and Fill Operations, Rev. 71

NPG-SPP-08.1, Nuclear Fuel Management, Rev. 00

0-PI-OPS-000-011.0, Containment Access Control During Modes 1-4, Rev. 1

Section 1R22: Surveillance Testing

Procedures

NPG-SPP-06.9.1, Conduct of Testing, Rev. 8

0-SI-SXV-072-266.0, ASME Code Valve Testing, Rev. 12

0-SI-OPS-068-137.0, Reactor Coolant System Water Inventory, Rev. 32

0-SI-SFT-072-138.0, Unit 1 Containment Spray - Spray Nozzle Test, Rev. 6

0-SI-SLT-081-258.1, Unit 1 Primary Water LLRT, Rev. 5

0-SI-SLT-088-259.1, Upper Personnel Airlock Overall Leak Rate Test and General Inspection,

Rev. 6

0-SI-SLT-088-259.4, Upper Personnel Airlock Interlock Operability Test, Rev. 2

1-SI-SXP-003-202.B, Motor Driven Auxiliary Feedwater Pump 1B-B Comprehensive

Performance Test, Rev. 7

1-SI-SXP-074-202.0, RHR Pump 1A-A and 1B-B Comprehensive Performance and Check

Valve Test, Rev. 10

0-SI-OPS-068-137.0, Reactor Coolant System Water Inventory, Rev. 32

1-SI-OPS-088-001.0, Phase A Isolation Test, Rev. 14

1-SI-OPS-082-026A, Loss of Offsite Power with Safety Injection D/G 1A-A Test, Rev. 46

0-SI-SFT-072-138.0, Unit 1 Containment Spray - Spray Nozzle Test, Rev. 6

0-SI-SXV-063-203.2, Full Stroking of Safety Injection Cold Leg Accumulator Isolation Valves,

Rev. 1

0-SI-MIN-061-105.0, Ice Condenser Ice Weighing, Rev. 11

0-SI-SLT-067-258.2, Containment Isolation Valve Local Leak Rate Test Lower Compartment

Essential Raw Cooling Water, Rev. 13

PERs

801081, FME concern while performing air flow test during core reload

6

Attachment

Other documents

1-47W437-4, Mechanical Containment Spray System Piping, Rev. 1

1-47W437-5, Mechanical Containment Spray System Piping, Rev. 4

1-47W812-1, Flow Diagram Containment Spray System, Rev. 45

Technical Specification Surveillance Requirement 4.6.2.1.1.d and 4.6.2.1.2.b

Section 1EP2: Alert and Notification System Evaluation

Procedures and Reports

NP-REP, Appendix B, Sequoyah Nuclear Plant Radiological Emergency Plan, Rev. 101

EPFS-9, Inspection, Service, and Maintenance of the Prompt Notification System (PNS) at

Browns Ferry, Sequoyah, and Watts Bar Nuclear Plants, Rev. 8

Sequoyah FEMA REP-10 Report, Revision 2

EPDP-10, Facilitation of the ANS and Notification Tests, Rev. 6

EPDP-14, Evaluation of Changes to Alert and Notification Systems (ANS), Rev 0

Records and Data

Weekly Silent Tests, 2011-September 2013

Monthly Siren Tests, October 2011 - October 2013

Corrective Action documents

442747; During Monthly Siren Test Five Sirens Did Not Operate

521663; Siren Damaged by Storm

591666; Two ANS Sirens Failed to Operate During Monthly Test

701363; Siren Relocations Due to Land Owner Rejections

711912; Loss of DC Power Indication for ANS Siren 12

727891; Loss of DC Power Indication for ANS Siren 26

751936; Two ANS Sirens Failed to Operate During Monthly Test

Section 1EP3: Emergency Response Organization Staffing and Augmentation System

Procedures

TRN-30, Radiological Emergency Preparedness Training, Rev. 24

EPDP-3, Emergency Plan Exercises and Preparedness Drills, Rev. 7

EPDP-10, Facilitation of the Alert and Notification System and Pager Tests, Rev. 6

EPIP-3, Alert, Rev 36

EPIP-6, Activation and Operation of the Technical Support Center, Rev. 49

EPIP-7, Activation and Operation of the Operations Support Center, Rev. 28

Records and Data

SQN-EP-S-13-02, snapshot self-assessment SCBA Qualification of Site Personnel, March 2013

EPT202.000, ERO Training Plan - TSC Training, Rev. 12

EPT900.010, ERO Training Plan, ERO Fundamentals, Rev. 4

Radiological Emergency Preparedness Training Oversight Committee minutes 2012/2013

2012/2013 ERO Augmentation test results

Results of periodic ERO notification tests

Corrective Action documents

786990; TRN error in CECC qualification requirement

7

Attachment

Section 1EP4: Emergency Action Level and Emergency Plan Changes

Change Packages

TVA Radiological Emergency Plan, Revs. 99 and 100

EPIP-1, Emergency Plan Classification Matrix, Revs. 48 and 49

CECC EPIP-2, Operations Duty Specialist Procedure for Notification of Unusual Event,

Rev. 43

CECC EPIP-3, Operations Duty Specialist Procedure for Alert, Rev. 44

CECC EPIP-4, Operations Duty Specialist Procedure for Site Area Emergency, Rev. 45

CECC EPIP-5, Operations Duty Specialist Procedure for General Emergency, Rev. 50

CECC EPIP-7, CECC Radiological Assessment Staff Procedure for Alert, Site Area

Emergency, and General Emergency, Rev. 34

TVA Radiological Emergency Plan, Rev. 101

Evacuation Time Estimate Study Update

Section 1EP5: Maintenance of Emergency Preparedness

Procedures

CECC EPIP-9, Emergency Environmental Radiological Monitoring Procedures, Rev. 49

EPDP-17, NPG Emergency Plan Effectiveness Review [10 CFR 50.54(q)], Rev. 3

NPG-SPP-7.1, On-Line Work Management, Rev. 10

NPG-SPP-18.3.5, Designated Emergency Response Equipment (DERE), Rev. 0

NPG-SPP-22.300, Corrective Action Program, Rev. 0

Records and Data

Drill and exercise reports 2011-2013

TVA Quality Assurance Audit Report SSA 1203 dated April 16, 2012

TVA Quality Assurance Audit Report SSA 1305 dated June 17, 2013

Focused Self-Assessment SQN-EP-F-13-001, NRC Inspection Preparation

SQN QA Quarterly Rating Report August 13, 2013

Corrective Action documents

571999; Maintenance Personnel Not Evacuated in a Timely Manner During REP Drill

572584; RP Was Slow to Perform Airborne Sampling During REP Drill

608785; Dose assessment error

581795; No Additional Fire Brigade Personnel Onsite During REP Drill

582858; TSC SED Filled Out Wrong Form Which Delayed CECC PAR Development

582751; MERT Failed 4 of 6 Drill Objectives

619808; RP Tech Left Team to Get Equipment During Graded Exercise

619847; Inside Van Tech Did Not Grab All Equipment Required During Graded Exercise

695758; MET Unavailable - Lessons Learned

704845; Evaluate EPIP-1 Classification of EAL 4.2 for Explosion

708940; Questioned CET Readings During Drill

711961; REP Assignment Cannot Meet 1-Hour Requirement to Respond

720352; 8 Personnel Were Not Accounted For During REP Drill

722951; KI Tablets Should Be Evaluated for Issue Earlier Under Emergency Conditions

732171; Clarify EPDP-11 regarding 10 CFR 50.54(t) requirements

751183; Wrong Pocket Ion Chambers in REP Van #3

8

Attachment

Section 2RS1: Radiological Hazard Assessment and Exposure Controls

Procedures, Guidance Documents, and Manuals

NPG-SPP-05.1.1, Alpha Radiation Monitoring Program, Rev. 3

NPG-SPP-05.6, Controlling Byproduct and Source Material, Rev. 2

NPG-SPP-22.300, Corrective Action Program, Rev. 0

RCDP-1, Conduct of Radiological Controls, Rev. 5

RCI-01, Radiation Protection Program, Rev. 78

RCI-14, Radiation Work Permit (RWP) Program, Rev. 57

RCI-15, Radiological Postings, Rev. 24

RCI-17, Control of Byproduct and Source Material, Rev. 19

RCI-18, Vacuum Cleaner Control Within the Radiologically Controlled Area, Rev. 9

RCI-21, Control of Radioactive Materials, Rev. 19

RCI-29, Control of Radiation Protection Keys, Rev. 15

RCI-101, Radiation Operations Routines, Rev. 3

RCI-106, Radiation Protection Standards and Expectations, Rev. 3

RCI-201, Radiation and Contamination Surveys, Rev. 13

RCI-202, Airborne Radioactivity Surveys, Rev. 7

RCI-204, Radiological Surveys of Equipment and Materials Leaving the RCA, Rev. 7

RCI-209, Radiological Surveys of Personnel Leaving the RCA or Protected Area, Rev. 3

RCI-301, Radionuclide Tracking and Assessment (RTA) Program, Rev. 2

RCI-412, Radiation Protection Surveys during Initial Spent Fuel Assembly Movement, Rev. 1

RCI-417, Radiological Monitoring of the Hydrogen Peroxide Injection Crud Burst, Rev. 1

RCTP-106, Special Dosimetry Operations, Rev. 2

0-TI-NUC-000-002.0, Storing Material in Spent Fuel Pool or New Fuel Vault, Rev. 21

Records and Data

Air Sample Detail Report for 10/13/2013 thru 11/5/2013, 11/5/2103

Air Sample 101713018, U1 Equipment Pit, 10/17/2013

Air Sample 101813018, U1 734 RFF GA, 10/18/2013

Air Sample 102313006, U1 Rx Head Stand, 10/23/2013

Air Sample 102313014, U1 653 1B RHR Pump Room, 10/23/2013

Air Sample 102313023, U1 653 1B RHR Pump Room, 10/23/2013

Air Sample 102613003, U1 Upper Rx Head O-ring Cleaning, 10/26/2013

Air Sample 110213012, U1 Upper GA, 11/2/2013

ALARA Plan 2013-010, Refueling Operations

ALARA Plan 2013-011, Mechanical Maintenance Group (MMG)

ALARA Plan 2013-018, MODS - Ice Condenser/Snubbers/Insulation/Scaffolds/Painting

Instrument Calibration/Check Source Certificates:

Vendor Source No. I3-328, TVA No. 2530, 7/29/2011

Vendor Source No. I3-329, TVA No. 2531, 7/29/2011

Vendor Source No. I3-330, TVA No. 2532, 7/29/2011

Vendor Source No.G4-975, TVA No. 2483, 10/9/2009

Vendor Source No. 92421, TVA No. 2571, 12/7/2012

Vendor Source No. 52736-185D2, TVA No. 2245, 5/19/2003

Instrument Calibration Records:

Canberra GEM-5 Personnel Monitor, Serial No. 0909-179, 3/23/2012 and 3/18/2013

ARGOS-5AB Personnel Monitor, Instrument No. 860587, 5/11/2012 and 5/2/2013

iSolo, Instrument No. 860494, 12/6/2012 and 10/11/13

9

Attachment

Small Article Monitor (Cronos 11), Instrument No. 860653, 8/17/2012 and 7/16/2013

Small Article Monitor (SAM-11), Instrument No. 860325, 7/6/2012 and 11/17/2012

List of Active SQN Temporary Shielding Request Forms (TSRFs), 11/6/2013

National Source Tracking System Annual Inventory Reconciliation Confirmation, 1/24/2013

National Source Tracking System Inventory Report, Sequoyah Nuclear Plant, 1/24/2013

RWP Dose by Work Step Report for ALARA Plans 2013-010 to 2013-021 for the period

10/14/2013 thru 11/6/2013

RWP Total Dose, Hours and Dose Rate Report for the period 10/14/2013 thru 11/5/2013

RWP Work Step Dose and Dose Rate Alarm Setpoints for RWP 13140052, 11/5/2013

RWP 13120122, U1 Seal Table work

RWP 13140002, U1 Upper Containment High Rad Area Mechanical Maintenance

RWP 13140052, HRA U1 Refueling Activities for AREVA and Boilermakers

RWP 13140072, U1 HRA MODS Work: Snubbers, Scaffold, Insulation, Painting

RWP 13140172, U1 Rx Head Insulation

RWP 13140252, HRA U1 Upper Containment Rx Cavity

RWP 13140352, U1 HRA Head O-Ring Surface Work & Inspection (Multibadging)

RWP 13140353, U1 Equipment Pit - LHRA Vortex Suppressors

RWP 13140453, U1 Upper Containment, Rx Cavity, LHRA, CRDM duct work, (Multibadging)

Radiological Survey SQN-M-20131014-23 and SQN-M-20131104-2, U1 Containment

Equipment Pit

Radiological Survey SQN-M-20131021-3, SQN-M-20131014-6, SQN-M-20131014-15, and

SQN-M-20131014-22, U1 Containment Accumulator Rooms #1, #2, #3, and #4

Radiological Survey SQN-M-20131014-32 and SQN-M-20131017-9, U1 Containment Top of

Pressurizer

Radiological Survey SQN-M-20130909-1 and SQN-M-20131014-8, U1 Containment Raceway

Radiological Survey SQN-M-20131014-14, SQN-M-20131014-7, and SQN-M-20131014-5, U1

Containment Steam Generator Primary Platform #1, #2, and #3

Radiological Survey SQN-M-20131014-17 and SQN-M-20131020-7, U1 Containment Inside

Polar Crane Wall

Radiological Survey SQN-M-20131021-21, SQN-M-20131014-10, and SQN-M-20131014-18,

U1 Containment RCP Platform #1, #2, and #3

Radiological Survey SQN-M-20131020-16, SQN ISFSI Pad

Radiological Survey SQN-M-20121212-8, U2 Letdown Heat Exchanger Room

Radiological Survey SQN-M-20131014-26, U1 Letdown Heat Exchanger Room

Radiological Survey SQN-M-20130502-11 and SQN-M-20131005-1, U1 651' Waste Evaporator

Feed Pump Room

Radiological Survey SQN-M-20131018-1 and SQN-M-20131025-1, Radiochemistry Lab

Radiological Survey SQN-M-20130617-3, SQN-M-20131007-1, and SQN-M-20131104-4,

Equipment Decon Room

Radiological Survey SQN-M-20130823-3, and SQN-M-20131016-24, Spent Fuel Heat

Exchanger Room

Radiological Survey SQN-M-20130920-5, SQN-M-20131020-4, and SQN-M-20131028-7, Spent

Fuel Pool Area

Radiological Survey SQN-M-20131015-8, SQN-M-20131020-9, and SQN-M-20131024-7, 1A

RHR Pump Room

Radiological Survey SQN-M-20131015-11, SQN-M-20131022-8, and SQN-M-20131023-10, 1B

RHR Pump Room

Radiological Survey SQN-M-20131101-10, 2B RHR Pump Room

10

Attachment

Radioactive Sealed Source Leak Test Certification, Source ID 0413-00-00, 7/23/09 and 1/25/10

Sequoyah Nuclear Plant Annual Radionuclide Trending and Assessment Report for 2011,

6/30/2012

Sequoyah Nuclear Plant Annual Radionuclide Trending and Assessment Report for 2012,

4/18/2013

U1R19 Radiation Protection Status Report, 11/5/2013

U1R19 RCS Shutdown Co-58 Activity Graphs (Crud Burst Cleanup), 11/5/2013

U1R19 Crud Burst Cleanup Dose Rate Trending Graphs (1A and 1B RHR Pump and Heat

Exchanger rooms, and 690 and 669 Pipe Chases near RHR Lines), 11/5/2013

Waste Stream Report (10 CFR Part 61 Waste Characterization), DAW 10-22-2010, 5/11/2011

Waste Stream Report (10 CFR Part 61 Waste Characterization), DAW 3-22-2012, 11/4/2012

WO 114067330, 0-SI-RCI-000-056.0 Byproduct Material Inventory and Sealed Source Leak

Test, 7/8/2013

WO 114139751, 0-SI-RCI-000-056.0 Byproduct Material Inventory and Sealed Source Leak

Test, 12/17/2012

CAP Documents

Apparent Cause Evaluation PER Report, SQN PER 782859, 10/20/2013

Site Audit Report SSA1309, Radiation Protection Sequoyah Nuclear Plant, 9/16/2013

TVA Nuclear Power Group Benchmarking Report SQN-RP-I-13-BM09, 8/23/2013

PERs

PER 626962

PER 629341

PER 657724

PER 659369

PER 782859

PER 788604

PER 790597

PER 793236

PER 793935

PER 799256

PER 802329

Section 2RS8: Radioactive Solid Waste Processing and Radioactive Material Handling,

Storage, and Transportation

Procedures, Manuals, and Guides

Energy Solutions Cask Book for Model 8-120B USA/9168/B(U)

NPG-SPP-05.7, Radwaste Management, Rev. 0

Process Control Program (PCP), Rev. 4

Radioactive Material Shipment Manual (RMSM, Vol.II -Radioactive Material Shipment, Rev. 42

Radioactive Material Shipment Manual (RMSM, Vol.III -Radwaste Shipment, Rev. 39

RCI-06, Receipt of Radioactive Materials, Rev. 19

RCI-21 Control of Radioactive Materials, Rev. 19

RHSI-1, Packaging Dry Active Waste for Shipment to a Waste Processor/Broker or a

Commercial Radwaste Burial Facility, Rev. 10

RHSI-1.1, Packaging Filters and Items of High Levels of Radiation, Rev. 6

11

Attachment

RHSI-6, Bead Resin Activated Carbon Dewatering Procedure for Energy Solutions14-215 or

Smaller Liners, Rev. 8

RHSI-7, Utilization of Polyethylene High Integrity Containers (HICs) and HIC Overpacks, Rev. 9

RHSI-11, Control of Radioactive Material and Training, Rev. 6

RHSI-13, Administration and Control of Onsite Storage of Low Level Radioactive Waste, Rev. 4

RWTP-100 Attachment A, Radwaste Training Program, Rev. 3

RWTP-100, Radioactive Material/Waste Shipments, Rev. 7

RWTP-101, 10 CFR 61 Waste Characterization, Rev. 2

RWTP-102, Use of Casks, Rev. 2

0-SO-77-29, Waste Processing, Rev. 9

0-VI-RCI-077-001.0, Operating Procedure for Duratek Modular Fluidized Transfer Demineralizer

System (MFTDS), Rev. 2

Shipping Records and Radwaste Data

Two Design Change Notices were reviewed and both have been accomplished. The first

moved Radwaste liquid processing from the railroad bay into the drumming room that was in

effect at the start of the period which included back to November 2010 and the second

established a lift system to be used for the steam generator replacement in 2012 with a closure

date of 8/13/2013.

The licensee provided several drawings delineating abandoned equipment. The inspector

chose the abandoned boric acid evaporator system to review.

Shipments:

SNP-12-0111 (LQ)

SNP-13-0105 (SCO)

SNP-13-0109 (Type B)

SNP-13-0307 (LSA)

SNP-13-0504 (Type A)

CAP Documents

Site Audit Report SSA1309, Radiation Protection, August 19 through August 30, 2013

Snapshot Self-Assessment Report SQN-RP-S-13-004, Radioactive Solid Waste Processing and

Radioactive Material Handling, Storage and Transportation, July 29 through August 9, 2013

PERs

412285

431332

488136

635127

735591

765281

767526

783784

12

Attachment

Section 4OA1: Performance Indicator Verification

Procedures, Manuals, and Guides

NSDP-29, Tracking and Trending and NRC Performance Indicators, Rev. 6

NPG-SPP-02.2, Performance Indicator Program, Rev. 5

RCI-151, Radiation Protection Functional Area Performance Indicators, Rev. 1

PERs

621990

623246

626962

653648

655642

788604

793921

794437

Section 4OA2: Problem Identification and Resolution

Procedures

NPG-SPP-03.1, Corrective Action Program, Rev. 1

Section 4OA5: Other Activities

0-GO-17, Spent Fuel/Dry Cask Operations, Rev. 5

NPG-SPP-01.2, Administration of Site Technical Procedures, Rev. 9

NFTP-100, Fuel Selection for Dry MPC Storage, Rev. 5 completed for campaign #6

10CFR 72.48 Screening/Evaluation: EDC E22443C

SQN-DCS-300.11, Supplemental Cooling System Operation, Rev. 9

CTP-DCS-100.0, Dry Cask Storage Campaign Guidelines, Rev. 15

SQN-DCS-200.0, Dry Cask Campaign Review Program, Rev. 4

SQN-DCS-200.2, SQN-MPC-Loading and Transport Operations, Rev. 35

Attachment

LIST OF ACRONYMS

ABGTS

auxiliary building gas treatment system

ALARA

as low as reasonably achievable

ASME

American Society of Mechanical Engineers

BACC

boric acid corrosion control

CAP

corrective action program

CCP

centrifugal charging pump

CDE

cause determination evaluation

CFR

Code of Federal Regulations

CIV

containment isolation valve

DAW

dry active waste

DOT

Department of Transportation

ECCS

emergency core cooling system

ED

electronic dosimeter

ERCW

essential raw cooling water

FCV

flow control valve

FME

foreign material exclusion

HRA

high radiation areas

IMC

inspection manual chapter

IP

inspection procedure

ISFSI

independent spent fuel storage installation

ISI

in-service inspection

MCC

motor control center

MPC

multi-purpose canister

NCV

non-cited violation

NDE

non-destructive examination

NEI

Nuclear Energy Institute

PER

problem evaluation report

PORV

power operated relief valve

Radwaste

radioactive waste

RCA

radiologically controlled area

Rev

revision

RHR

residual heat removal

RS

radiation safety

RTP

rated thermal power

RWP

radiation work permit

RWST

refueling water storage tank

SDP

significance determination process

SI

safety injection

SR

service request

SSC

structure, system, or component

TS

technical specification

TVA

Tennessee Valley Authority

URI

unresolved item

UT

ultrasonic testing

UFSAR

Updated Final Safety Analysis Report

WO

work order