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| {{#Wiki_filter:7 ~ ~.2 ....odify Plant Issue I *m Page 1 of-2 wStc\je j ýýe plant status daily enter daily plant status sat archives in Oconee Information for 09/29/2009 (Modify/Update) ovlr(W I'll Risk Si-g-nfi-ca-nt -Efferg-enU~ctWrnIs. | | {{#Wiki_filter:7~ ~ |
| C/2 httn://r2.nrc.izov/webapps/pita/Modifylssue.cfm?iid= | | .2 .... odify Plant Issue Page 1 of-2 I *m wStc\je j ýýe plant status daily enter daily plant status sat archives in Oconee Information for 09/29/2009 (Modify/Update) ovlr( |
| 15184&sname=Oconee 11/4/2010 w ; ....... ,Modify Plant Issue Page The tie-in work for the SSF ASW system began over the weekend. Unit 2 work is complete; i.e,, the new piping. is installed and pressure tested. All three old sections of piping are capped'in the outside hole. Tie-in on all 3 ASW pipes outside the building is complete and preparations are underway to start coating the pipes with the coal tar protection. | | I'll W |
| Inside the SSF building, tie-in work is underway for Unit 1 and 3. There have been fit-up issues with the final connections on both' units which may push completion until Wednesday morning. Following the tie7in inside the building, the "I headers willl have the VT-21 ,testing performedanrid'the operability test 'performed. | | Risk Si-g-nfi-ca-nt -Efferg-enU~ctWrnIs. |
| Refill of the hole will commenc eon e the testing is complete.Currently, Unit 2 is available and Unit 1 & 3 are inoperable in terms of the SSF.9:15mtg. C Yes ( No add attachment Outside of Scope 2 of 2 of L httn://r2.nrc.fiov/webapp~s/pita/ModifyIssue. | | C/2 httn://r2.nrc.izov/webapps/pita/Modifylssue.cfm?iid= 15184&sname=Oconee 11/4/2010 |
| cfm?iid= 5 l'84&sname=Oconee 11/4/2 0.10}} | | |
| | ** w ;....... *h* *JV |
| | ,Modify Plant Issue Page 2 of 2 The tie-in work for the SSF ASW system began over the weekend. Unit 2 work is complete; i.e,, the new piping. is installed and pressure tested. All three old sections of piping are capped'in the outside hole. Tie-in on all 3 ASW pipes outside the building is complete and preparations are underway to start coating the pipes with the coal tar protection. Inside the SSF building, tie-in work is underway for Unit 1 and 3. There have been fit-up issues with the final connections on both' units which may push completion until Wednesday morning. |
| | headers willl performed. |
| | Following the tie7in inside the building, the have the VT-21 ,testing performedanrid'the operability test Refill of the hole will commenc eon e the testing is complete. |
| | '"I Currently, Unit 2 is available and Unit 1 & 3 are inoperable in terms of the SSF. |
| | 9:15mtg. C Yes ( No [* |
| | add attachment Outside of Scope of L |
| | httn://r2.nrc.fiov/webapp~s/pita/ModifyIssue. cfm?iid= 5 l'84&sname=Oconee 11/4/2 0.10}} |
Latest revision as of 04:51, 13 November 2019
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Category:Status Report
MONTHYEARML24047A2092024-02-22022 February 2024 Calendar Year 2023 Baseline Inspection Completion RA-23-0036, Biennial Decommissioning Financial Assurance Reports2023-03-30030 March 2023 Biennial Decommissioning Financial Assurance Reports IR 05000269/20200062021-03-0303 March 2021 Annual Assessment Letter for Oconee Nuclear Station Units 1, 2, & 3 NRC Inspection Report 05000269/2020006, 05000270/2020006, & 05000287/2020006 RA-19-0159, Stations - Biennial Decommissioning Financial Assurance Reports2019-03-28028 March 2019 Stations - Biennial Decommissioning Financial Assurance Reports RA-17-0018, Duke Energy Carolinas, LLC - Biennial Decommissioning Financial Assurance Reports2017-03-29029 March 2017 Duke Energy Carolinas, LLC - Biennial Decommissioning Financial Assurance Reports ONS-2016-068, Seventh Six-Month Status Report in Response to March 12, 2012 Commission Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond Design-Basis External Events (Order Number EA-12-049)2016-08-26026 August 2016 Seventh Six-Month Status Report in Response to March 12, 2012 Commission Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond Design-Basis External Events (Order Number EA-12-049) ONS-2016-024, Sixth Six-Month Status Report in Response to March 12, 2012 Commission Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events (Order Number EA-12-049)2016-02-29029 February 2016 Sixth Six-Month Status Report in Response to March 12, 2012 Commission Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events (Order Number EA-12-049) RA-15-0010, Submits Required Biennial Decommissioning Financial Assurance Reports2015-03-30030 March 2015 Submits Required Biennial Decommissioning Financial Assurance Reports ONS-2015-023, Fourth Six-Month Status Report in Response to March 12, 2012 Commission Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events (Order Number EA-12-049)2015-02-27027 February 2015 Fourth Six-Month Status Report in Response to March 12, 2012 Commission Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events (Order Number EA-12-049) ONS-2014-029, Second Six-Month Status Report in Response to March 12, 2012 Commission Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events (Order Number EA-12-049)2014-02-28028 February 2014 Second Six-Month Status Report in Response to March 12, 2012 Commission Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events (Order Number EA-12-049) ML13246A0092013-08-29029 August 2013 First Six-Month Status Report in Response to Letter Dated March 12, 2012 ML13242A0092013-08-26026 August 2013 Duke Energy - First Six-Month Status Reports in Response to March 12, 2012, Commission Order Modifying Licenses with Regard to Reliable Spent Fuel Pool Instrumentation (Order Number EA-12-051) ML13091A0222013-03-28028 March 2013 Submittal of Biennial Decommissioning Financial Assurance Reports ML12024A3762011-12-28028 December 2011 State-of-the-Art Reactor Consequence Analyses, Current Status and Next Steps ML1100410072009-10-0707 October 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 10/07/2009 ML1100409702009-10-0606 October 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 10/06/2009 ML1100409692009-10-0505 October 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 10/05/2009 ML1100409682009-10-0202 October 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 10/02/2009 ML1100409672009-10-0101 October 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 0/01/2009 ML1100409662009-09-30030 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 9/30/2009 ML1100409652009-09-29029 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 9/29/2009 ML1100409642009-09-28028 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 9/28/2009 ML1100409632009-09-25025 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 9/25/2009 ML1100409622009-09-23023 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 9/23/2009 ML1100409612009-09-22022 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 09/22/2009 ML1100404392009-09-21021 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 9/21/2009 ML1100404382009-09-18018 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 9/18/2009 ML1100404372009-09-17017 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 9/17/2009 ML1100404342009-09-14014 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 09/14/2009 ML1100404332009-09-10010 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 09/10/2009 ML1100404322009-09-0909 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 09/09/2009 ML1100404312009-09-0808 September 2009 Plant Issue Tracking Application; Plant Status Daily - Oconee Information for 09/08/2009 ML0919004522009-03-30030 March 2009 Duke Energy Carolinas, LLC - Oconee Nuclear Station Units 1,2, and 3; McGuire Nuclear Station Units 1 and 2; Catawba Nuclear Station Units 1 and 2 - Decommisionings Financial Assurance Reports ML13057A6212009-02-0909 February 2009 Status of Oconee External Flooding Issue Briefing of Jack Grobe ML0711501992006-08-15015 August 2006 DPO-2006-002 Chronology and Status ML0711501952006-07-20020 July 2006 DPO-2006-002 Chronology and Status ML0623604652006-05-0909 May 2006 Duke Power Oconee Unit 3R EOC22 ECT Examination Status Report, Enclosure 2 to 05/09/2006 Meeting Summary for Conference Call Spring 2006 Steam Generator Inspection at Oconee, Unit 3 ML0505405242005-02-15015 February 2005 January 2005 Monthly Operating Report for Oconee McGuire and Catawba Nuclear Stations ML0224008422002-04-11011 April 2002 Advisory Committee on Reactor Safeguards 491st Meeting CRDM Penetration Cracking & RPV Head Degradation Room T-2B3, 11545 Rockville Pike, Rockville, MD, 04/11/2002 - Status Report ML0224007982002-02-0101 February 2002 E-mail from Beth Wetzel Bulletin 2001-01 Status Report ML0224007812002-01-18018 January 2002 E-mail from Jacob Zimmerman, Bulletin 2001-01 Status Report 2024-02-22
[Table view] |
Text
7~ ~
.2 .... odify Plant Issue Page 1 of-2 I *m wStc\je j ýýe plant status daily enter daily plant status sat archives in Oconee Information for 09/29/2009 (Modify/Update) ovlr(
I'll W
Risk Si-g-nfi-ca-nt -Efferg-enU~ctWrnIs.
C/2 httn://r2.nrc.izov/webapps/pita/Modifylssue.cfm?iid= 15184&sname=Oconee 11/4/2010
,Modify Plant Issue Page 2 of 2 The tie-in work for the SSF ASW system began over the weekend. Unit 2 work is complete; i.e,, the new piping. is installed and pressure tested. All three old sections of piping are capped'in the outside hole. Tie-in on all 3 ASW pipes outside the building is complete and preparations are underway to start coating the pipes with the coal tar protection. Inside the SSF building, tie-in work is underway for Unit 1 and 3. There have been fit-up issues with the final connections on both' units which may push completion until Wednesday morning.
headers willl performed.
Following the tie7in inside the building, the have the VT-21 ,testing performedanrid'the operability test Refill of the hole will commenc eon e the testing is complete.
'"I Currently, Unit 2 is available and Unit 1 & 3 are inoperable in terms of the SSF.
9:15mtg. C Yes ( No [*
add attachment Outside of Scope of L
httn://r2.nrc.fiov/webapp~s/pita/ModifyIssue. cfm?iid= 5 l'84&sname=Oconee 11/4/2 0.10