IR 05000498/2005005: Difference between revisions

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| issue date = 02/11/2006
| issue date = 02/11/2006
| title = IR 05000498-05-005 & 05000499-05-005, on 09/27-12/31/2005, South Texas Project Electric Generating Station
| title = IR 05000498-05-005 & 05000499-05-005, on 09/27-12/31/2005, South Texas Project Electric Generating Station
| author name = Johnson C E
| author name = Johnson C
| author affiliation = NRC/RGN-IV/DRP/RPB-A
| author affiliation = NRC/RGN-IV/DRP/RPB-A
| addressee name = Sheppard J J
| addressee name = Sheppard J
| addressee affiliation = South Texas Project Nuclear Operating Co
| addressee affiliation = South Texas Project Nuclear Operating Co
| docket = 05000498, 05000499
| docket = 05000498, 05000499
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:February 11, 2006James J. Sheppard, President and Chief Executive Officer STP Nuclear Operating Company P.O. Box 289 Wadsworth, Texas 77483SUBJECT:SOUTH TEXAS PROJECT ELECTRIC GENERATING STATION - NRCINTEGRATED INSPECTION REPORT 05000498/2005005 AND 05000499/2005005
[[Issue date::February 11, 2006]]
 
James J. Sheppard, President and Chief Executive Officer STP Nuclear Operating Company P.O. Box 289 Wadsworth, Texas 77483
 
SUBJECT: SOUTH TEXAS PROJECT ELECTRIC GENERATING STATION - NRCINTEGRATED INSPECTION REPORT 05000498/2005005 AND 05000499/2005005


==Dear Mr. Sheppard:==
==Dear Mr. Sheppard:==
Line 30: Line 25:
STP Nuclear Operating Company-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
STP Nuclear Operating Company-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/
Sincerely,
/RA/
Claude E. Johnson, ChiefProject Branch A Division of Reactor ProjectsDockets: 50-498  50-499 Licenses: NPF-76 NPF-80
Claude E. Johnson, ChiefProject Branch A Division of Reactor ProjectsDockets: 50-498  50-499 Licenses: NPF-76 NPF-80


===Enclosure:===
===Enclosure:===
NRC Inspection Report 05000498/2005005 and 05000499/2005005  
NRC Inspection Report 05000498/2005005 and 05000499/2005005 w/attachment: Supplemental Information


===w/attachment:===
REGION IV Dockets:50-498, 50-499 Licenses:NPF-76NPF-80Report No:05000498/200500505000499/2005005Licensee:STP Nuclear Operating Company Facility:South Texas Project Electric Generating Station, Units 1 and 2 Location:FM 521 - 8 miles west of Wadsworth Wadsworth, Texas 77483Dates:September 27 through December 31, 2005 Inspectors:J. Cruz, Senior Resident InspectorJ. Taylor, Resident Inspector H. Crouch, Reactor Engineer P. Goldberg, P.E., Reactor Inspector, Engineering Branch 2 J. Adams, Reactor Inspector, Engineering Branch 1 P. Elkmann, Emergency Preparedness Inspector T. McKernon, Senior Operations Engineer P. Gage, Senior Operations Engineer B. Tindell, Reactor InspectorApproved By:C. Johnson, ChiefProject Branch A Division of Reactor Projects-2-
Supplemental Informationcc w/enclosure:E. D. Halpin Vice President, Oversight STP Nuclear Operating Company P.O. Box 289 Wadsworth, TX 77483S. M. Head, Manager, LicensingSTP Nuclear Operating Company P.O. Box 289, Mail Code: N5014 Wadsworth, TX 77483C. Kirksey/C. M. CanadyCity of Austin Electric Utility Department 721 Barton Springs Road Austin, TX 78704 J. J. Nesrsta/R. K. TempleCity Public Service Board P.O. Box 1771 San Antonio, TX 78296Jack A. Fusco/Michael A. ReedTexas Genco, LP 12301 Kurland Drive Houston, TX 77034Jon C. WoodCox Smith Matthews 112 E. Pecan, Suite 1800 San Antonio, TX 78205A. H. Gutterman, Esq.Morgan, Lewis & Bockius 1111 Pennsylvania Avenue NW Washington, DC 20004INPORecords Center 700 Galleria Parkway Atlanta, GA 30339-3064 STP Nuclear Operating Company-3-Director, Division of Compliance &Inspection Bureau of Radiation Control Texas Department of State Health Services 1100 West 49th Street Austin, TX 78756Brian AlmonPublic Utility Commission William B. Travis Building P.O. Box 13326 1701 North Congress Avenue Austin, TX 78701-3326Environmental and Natural Resources Policy Director P.O. Box 12428 Austin, TX 78711-3189Judge, Matagorda CountyMatagorda County Courthouse 1700 Seventh Street Bay City, TX 77414Terry Parks, Chief InspectorTexas Department of Licensing and Regulation Boiler Program P.O. Box 12157 Austin, TX 78711Susan M. JablonskiOffice of Permitting, Remediation and Registration Texas Commission on Environmental Quality MC-122, P.O. Box 13087 Austin, TX 78711-3087Ted Enos4200 South Hulen Suite 630 Fort Worth, TX 76109 STP Nuclear Operating Company-4-Electronic distribution by RIV:Regional Administrator (BSM1)DRP Director (ATH)DRS Director (DDC)DRS Deputy Director (RJC1)Senior Resident Inspector (JXC2)Branch Chief, DRP/A (CEJ1)Senior Project Engineer, DRP/A (TRF)Team Leader, DRP/TSS (RLN1)RITS Coordinator (KEG)Only inspection reports to the following:DRS STA (DAP)J. Dixon-Herrity, OEDO RIV Coordinator (JLD)ROPreports STP Site Secretary (LAR)SUNSI Review Completed: _CEJ____ ADAMS: Yes G No Initials: __CEJ Publicly Available G Non-Publicly Available G Sensitive Non-SensitiveR:\REACTORS\ STP\2005\ST2005-05RP-JC.wpdRIV:RI:DRP/ASRI:DRP/AC:DRS/EBC:DRS/OBC:DRS/PEBJLTaylorJCruzJAClarkATGodyLJSmithE-CEJE-CEJ/RA//RA/DLProulx for2/2/062/2/061/30/061/31/061/27/06C:DRS/PSBC:DRP/AMPShannonCEJohnson/RA//RA/ 2/2/062/11/06OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax ENCLOSUREU.S. NUCLEAR REGULATORY COMMISSION REGION IV Dockets:50-498, 50-499 Licenses:NPF-76NPF-80Report No:05000498/200500505000499/2005005Licensee:STP Nuclear Operating Company Facility:South Texas Project Electric Generating Station, Units 1 and 2 Location:FM 521 - 8 miles west of Wadsworth Wadsworth, Texas 77483Dates:September 27 through December 31, 2005 Inspectors:J. Cruz, Senior Resident InspectorJ. Taylor, Resident Inspector H. Crouch, Reactor Engineer P. Goldberg, P.E., Reactor Inspector, Engineering Branch 2 J. Adams, Reactor Inspector, Engineering Branch 1 P. Elkmann, Emergency Preparedness Inspector T. McKernon, Senior Operations Engineer P. Gage, Senior Operations Engineer B. Tindell, Reactor InspectorApproved By:C. Johnson, ChiefProject Branch A Division of Reactor Projects  
-2-


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
Line 318: Line 312:
No findings of significance were identified.
No findings of significance were identified.


===Cornerstone:===
===Cornerstone: Emergency Preparedness1EP2Alert Notification System Testing (71114.02)
Emergency Preparedness1EP2Alert Notification System Testing (71114.02)


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors discussed with licensee staff the status of offsite siren and tone alertradio systems to determine the adequacy of licensee methods for testing the alert and notification system in accordance with 10 CFR Part 50, Appendix E. The licensee's alert and notification system testing program was compared with criteria in NUREG-0654, "Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants," Revision 1, Federal Emergency Management Agency (FEMA) Report REP-10, "Guide for the Evaluation of Alert and Notification Systems for Nuclear Power Plants," and the licensee's current FEMA-approved alert and notification system design report. The inspectors also reviewed Plant General Procedure 0PGP05-ZV-0006, "Emergency Notification and Response System," Revision 3, and Desktop Guide ZV-0013, "Alert Radio Maintenance and Distribution," Revision 0. The inspectors completed one sample during this inspection.
The inspectors discussed with licensee staff the status of offsite siren and tone alertradio systems to determine the adequacy of licensee methods for testing the alert and===
 
notification system in accordance with 10 CFR Part 50, Appendix E. The licensee's alert and notification system testing program was compared with criteria in NUREG-0654, "Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants," Revision 1, Federal Emergency Management Agency (FEMA) Report REP-10, "Guide for the Evaluation of Alert and Notification Systems for Nuclear Power Plants," and the licensee's current FEMA-approved alert and notification system design report. The inspectors also reviewed Plant General Procedure 0PGP05-ZV-0006, "Emergency Notification and Response System," Revision 3, and Desktop Guide ZV-0013, "Alert Radio Maintenance and Distribution," Revision 0. The inspectors completed one sample during this inspection.


====b. Findings====
====b. Findings====
Line 449: Line 444:
Opened and  
Opened and  
===Closed===
===Closed===
: [[Closes finding::05000499/FIN-2005005-01]]NCVInadvertent Letdown Relief Valve Opening(Section 1R20.1)
05000499/2005005-01NCVInadvertent Letdown Relief Valve Opening(Section 1R20.1)05000499/2005005-02NCV Improper Fuel Handling (Section 1R20.2)
: [[Closes finding::05000499/FIN-2005005-02]]NCV Improper Fuel Handling (Section 1R20.2)
: 05000499/2005005-03 NCVInoperability of Essential Cooling Water 2Aand 2B Trains(Section 4OA3)
: [[Closes finding::05000499/FIN-2005005-03]] NCVInoperability of Essential Cooling Water 2Aand 2B Trains(Section 4OA3)


===Closed===
===Closed===
: [[Closes finding::05000499/FIN-2005005-01]]NCVInadvertent Letdown Relief Valve Opening(Section 1R20.1)
0500499/2005-004-00LERInoperability of Essential Cooling Water 2Aand 2B Trains (Section 4OA3)0500499/2005-004-01LERInoperability of Essential Cooling Water 2Aand 2B Trains (Section 4OA3)05000498;499/2005004-01  URIPotential for Submerged Cables(Section 4OA5.1)
: [[Closes finding::05000499/FIN-2005005-02]]NCV Improper Fuel Handling (Section 1R20.2)
AttachmentA-3
: [[Closes finding::05000499/FIN-2005005-03]] NCVInoperability of Essential Cooling Water 2Aand 2B Trains(Section 4OA3)
 
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
In addition to the documents identified in the inspection report, the following documents wereselected and reviewed by the inspectors to accomplish the objectives and scope of the inspection and to support any findings:Heat Sink Performance (71111.07)Procedures0PCP01-ZA-0038, "Plant Chemistry Specifications," Revision 30
In addition to the documents identified in the inspection report, the following documents wereselected and reviewed by the inspectors to accomplish the objectives and scope of the
: 0PMP04-ZG-0011, "Heat Exchanger Cleaning (General Guidelines and Instructions)," Revision 60PE07-EW-0001, "Performance Test for Essential Cooling Heat Exchangers," Revision 6
: Condition Records05-707103-10566
: 04-11103
: 05-2294
: 05-1845
: 05-3995
: 03-13948
: 95-7568
: 99-741CalculationsMC-06482A, "Essential Chilled Water Minimum Flow Requirements For EAB, CRE. FBH &MAB Coolers," Revision 0DCP 00-5014-5, "Document Change Notice to Calculation MC-6482"
: 94E-0095-20, "Room Heat Loads," Revision 0 & Calculation Revision Notice
: EE-991864N201,dated August 28, 2000DCP 00-15286-03, "Document Change Notice to Procedure 0PG04-ZE-0309," Supplement 0
: DCP 05-255-8, "Document Change Notice to Procedure 0PG04-0309," dated May 12, 2005
: DCP 04-1238-40, "Document Change Notice to Procedure MC06482," dated December 16, 2004 
: AttachmentA-4Specifications3R209NS0033, "Specification for Component Cooling Water," Revision 2Testing Procedures, Calculations, and ResultsOPSP03-EW-0017, "Essential
: Cooling Water System Train A Testing," Revision 23
: OPSP03-EW-0018, "Essential Cooling Water System Train B Testing," Revision 33
: OPSP03-EW-0019, "Essential Cooling Water System Train C Testing," Revision 33
: 0PEP07-EW-001, "Performance Test for Essential Cooling Water Heat Exchangers," Revision 6
: Work OrdersMM-2-CH-97001689WAN-245552
: WAN- 60320
: WAN-211670
: WAN-433004
: WAN-245552
: WAN-182366
: WAN-127055
: WAN-242779
: WAN-132435
: WAN-151418
: WAN-85507MiscellaneousSTP letter to NRC, "Response to NRC Generic Letter 89-13, Service Water System ProblemsAffecting Safety Related Equipment," dated January 29,1990STP letter to NRC, "Service Water System Problems Affecting Safety Related Equipment,"dated April 3, 1991STP letter to NRC, "Service Water System Problems Affecting Safety Related Equipment,"dated March 27, 1991STP letter to NRC, "Service Water System Problems Affecting Safety Related Equipment,"dated May 15, 1991LER-2-2005-04, "Inoperability of Essential Cooling Water 2A and 2B Trains," Revision 0
: AttachmentA-5NRC Inspection Report 50-498;499/92-201, "South Texas Project Electric Generating StationService Water System Operational Performance Inspection," dated August 24,1992 Inservice Inspection Activities (71111.08)OPEP10-ZA-0001, "Qualification and Certification of Nondestructive Examination Personnel forExamination Methods Other than the Ultrasonic Examination Method for the Inservice Inspection Program" Revision 3OPEP10-ZA-0002, "Qualification and Certification of nondestructive Examination Personnel forthe Ultrasonic Examination Method for the Inservice Inspection Program," Revision 1OPEP-10-ZA-0004, "General Ultrasonic Examination," Revision 2
: OPEP10-ZA-0012, "Color Contrast Solvent Removable Liquid Penetrant Examination for ASMEXI PSI/ISI," Revision 2OPEP10-ZA-0018, "Dry Powder Magnetic Particle Examination for ASME XI PSI/ISI,"Revision 1OPEP10-ZA-0024, "ASME XI Examination for
: VT-1 and
: VT-3," Revision 1
: OPGP03-ZE-0027, "ASME Section XI Repair, Replacement and Postmaintenance PressureTesting," Revision 22OPGP03-ZE-0033, "RCS Pressure Boundary Inspection for Boric Acid Leaks," Revision 9
: SSI-A-005, "Qualification and Certification of Nondestructive Examination Personnel,"Revision 22SSI-A-013, "Qualification and Certification of Ultrasonic Examination personnel for ASME XIPSI/ISI Inspections," Revision 3UTI-057, "Modeling Component Configuration Profiles for Dissimilar Metal Welds," Revision 0
: UTI-PDI-UT-2, "PDI Generic Procedure for the Ultrasonic Examination of Austenitic PipeWelds," Revision 1Miscellaneous DocumentsNOC-AE-04001762, "Response to NRC Bulletin 2004-01, 'Inspection of "Alloy 82/182/600 Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping Connections at Pressurized-Water Reactors'" July 27, 2004
: AttachmentA-6NOC-AE-05001890, "Response to Nuclear Regulatory Commission Bulletin 2004-01,'Inspection of Alloy 82/182/600 Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping Connections at Pressurized-Water Reactors'" June 9, 2005"Examination Plan for the 2RE11 Inservice Inspection of Unit 2 South Texas Project ElectricGenerating Station" September 2005"Inservice Inspection Program Plan for Examination of Component Support, Containment MetalLiner, Repair/Replacement Activities, Steam Generator Tubing, System Pressure Testing and Weld Inspection Programs for the Second Inspection Interval of the South Texas Project Electric Generating Station Units 1 and 2" Revision 2Liquid Penetrant Examinations750620-PCW4RHARHS-2A-IWA2Ultrasonic Examinations12-RC-2212 BB112-RC-2221-BB1
: 2-RC-2312-BB1 Visual Examinations:Pressurizer upper head nozzle - N2 Spray Nozzle Pressurizer upper head nozzle  - N3 Safety Nozzle Pressurizer upper head nozzle  - N4A Relief Nozzle Pressurizer upper head nozzle  - N4B Safety Nozzle Pressurizer upper head nozzle  - N4C Safety Nozzle
: RPV Loop A outlet nozzle to safe end - 29-RC-2101, RPV2-N2ASE
: RPV Loop B outlet nozzle to safe end - 29-RC-2201, RPV2-N2BSE
: RPV Loop C outlet nozzle to safe end-
: 29-RC-2301, RPV2-N2CSE
: RPV Loop D outlet nozzle to safe end - 29-RC-2401, RPV2-N2DSE
: Safe End to RPV Loop A inlet nozzle - 27.5-RC-2103, RPV2-N2ASE
: Safe End to RPV Loop B inlet nozzle - 27.5-RC-2203, RPV2-N2BSE
: Safe End to RPV Loop C inlet nozzle - 27.5-RC-2303, RPV2-N2CSE
: Safe End to RPV Loop D inlet nozzle - 27.5-RC-2403,
: RPV2-N2DSECondition Reports04-427904-5109
: 04-5473
: 04-1197504-1675205-888
: 05-1854
: 05-197305-1200105-12073
: 05-12343
: AttachmentA-7Drawings:4C369PRC457, Reactor Coolant "RC", Revision 9A-RPV-1, "Reactor Pressure Vessel," Revision 0
: A-RPV-2, "Reactor Pressure Vessel," Revision 0Weld Certifications
:Weld Procedure Specification P8-T-Ag, 
===Procedure===
: Qualification Record 016Procedure Qualification Record 035
===Procedure===
: Qualification Record 037
===Procedure===
: Qualification Record 046
===Procedure===
: Qualification Record 197Welds:Drawing 4C369PRC0457, FW0011 PC 7B Pipe to Valve RC0057B, Weld FW007
: PC 7B Pipe to Valve RC0057B, Weld FW008Boric Acid Corrosion Control Examinations:BMI and lower RPV headLHSI 2C to RCS Loop 2C Hot Leg MOV
: Pzr Spray LP 2A,
: PCV-655C bypass valve
: RHR Pump 2A Suction First MOV
: RHR Pump 2C Suction First MOVLicensed Operator Requalification (71111.11)Procedures0PGP03-ZT-0132Licensed Operator RequalificationRevision 6LOR-GL-001LOR Training Program GuidelinesRevision 12
: LOR-GL-002Annual and Biennial Evaluation GuidelinesRevision 11LOR-GL-003Exam Bank GuidelinesRevision 2
: LOR-GL-004Two-Year Training Plan GuidelinesRevision 5
: LOR-GL-006Conduct of Simulator Training GuidelinesRevision 15
: AttachmentA-8Scenarios054-08054-15Job Performance Measures001.01.r8003.01.r8
: 011.02.r8014.01.r9028.02.r6
: 046.01.r9111.01.r2111.01.r3
: 115.01.r5120.02.r4143.02
: 145.02Reqaulification PlansLOR 2004-2005 Two-Year PlanLOR Simulator Sample Plan Cycle 054 Reqaulification ScheduleCycle Written ExamsLOR 051Written Exam 1LOR 051Written Exam 2
: LOR 051Written Exam 3
: LOR 051Written Exam 4LRO 051Written Exam Remediation Plans (8)
: LOR 041Written Exam 1LOR 041Written Exam 2
: LOR 041Written Exam 3LRO 041Written Exam Remediation Plans (1)
: LOR 043Written Exam 1LOR 043Written Exam 2
: LOR 043Written Exam 3Open Simulator DRs
: 28 1661
: 1662
: 1663
: 1673
: 1685
: 1686 1712 1717
: 1718
: 22
: 26
: 27
: 1739 1748 1753
: 1760
: 1763
: 1776
: 1784
: 1787 1789 1797
: 1800
: 1812
: 1815
: 1819 1820 1821
: 22
: 23
: 26
: 27
: AttachmentA-9Scenario-Based Test ChecklistsIST 403.27IST 403.12
: IST 403.03
: LOS 010.01
: IST 403.16IST 403.15IST 403.22
: IST 403.28
: IST 403.17
: IST 403.29IST 403.08IST 403.01
: IST 403.13
: IST 403.05IST 403.24IST 403.14
: IST 403.06
: IST 403.26Plant Events(Plant Condition Records also provided)DR 1608Charging flow following reactor trip mismatch of plant data & simulatorDR 1607Simulator test of feedwater pump trip (no startup pump available)(CR 03-3139)DR 1782Reactor trip, AFW actuation (CR 02-17080)
: CR 05-3171Solid plant operations
: CR 03-7772-1Reactor containment building atmosphere monitor
: CR 00-0500-35Loss of grid Section 71111.12 Maintenance Implementation (Condition Records reviewed)96-1046597-1249997-1325995-171899-1242600-79200-315202-518403-1854105-6342Section 1EP2South Texas Project Electric Generating Station, Site Specific Offsite Radiological EmergencyPreparedness Prompt Alert and Notification System Independent Technical Review, August 1989Addendum, Prompt Notification System for the South Texas Project Electric Generating Station,April 1997Final Report, South Texas Project Electric Generating Station Site Specific Offsite RadiologicalEmergency Preparedness Prompt Alert and Notification System Quality Assurance Review, April 1998
: AttachmentA-10Section 1EP30ERP01-ZV-IN03, "Emergency Response Organization Notification," Revision 120PGP05-ZV-0003, "Emergency Response Organization," Revision 8
: 0PGP05-ZV-0007, "Prompt Notification System," Revision 6
: 0PGP05-ZV-0016, "Prompt Notification System Implementation Procedure," Revision 3Drill Reports for:March 9, 2004, Call-In Drill October 28, 2004, Drive-In Drill August 30, 2005, Call-In DrillSection 1EP5Procedures:Desktop Guide
: ZV-0014, "Emergency Response Equipment Operability," Revision 0Drill Reports for:Combined Functional Drill, May 5, 2004
: Combined Functional Drill, June 22, 2004
: Combined Functional Drill, August 10, 2004
: Combined Functional Drill, August 31, 2004
: Combined Functional Drill, October 28, 2004
: Combined Functional Drill, January 5, 2005
: Combined Functional Drill, June 8, 2005
: Combined Functional Drill, July 26, 2005
: Field Monitoring Drill, December 1, 2004
: Medical Services Exercise, May 18, 2005Condition Reports:2003-13873, 14039, 15093
: 2004-254, 2247, 2650, 3177, 8997, 10494, 11148, 12265, 15103
: 2005-2585, 7997, 10886Other Reports:Quality Audit Report 04-01, Emergency Preparedness Quality Audit Report 05-01, Emergency Preparedness Quality Monitoring Report MN-05-0-5564
: Quality Monitoring Report MN-05-0-5696
: Quality Monitoring Report MN-05-0-5981
: Quality Monitoring Report MN-05-0-6002
: Quality Monitoring Report MN-05-0-7719
: Quality Monitoring Report MN-05-0-8242
: Quality Monitoring Report
: MN-05-0-8573
: AttachmentA-11Other Documents:50.54Q evaluation associated with CR2005-2585
: Lesson Plan EPT001.02, "Emergency Direction Part 2," Revision 7Section 4OA10ERP01-ZV-IN01, "Emergency Classifications," Revision 60ERP01-ZV-IN02, "Notifications to Offsite Agencies," Revision 18
: 0ERP01-ZV-IN07, 'Offsite Protective Action Recommendations," Revision 10
: 0ERP01-ZV-TP01, "Offsite Dose Calculations," Revision 16
: 0PGP05-ZV-0001, "Emergency Response Exercises and Drills," Revision 7Miscellaneous Documents0PGP03-ZV-0001, "Severe Weather Plan," Revision 12Section 4OA5 Other
: CRs03-18389
==LIST OF ACRONYMS==
ALARAAs Low As is Reasonably AchievedCCWcomponent cooling water
 
CFRCode of Federal RegulationsCRcondition report
ECWessential cooling water
EPZemergency planning zone
LERlicensee event report
NCVnoncited violation
PIperformance indicators
RCSreactor coolant system
SSCstructure, system, and component
: [[WAN]] [[work authorization number]]
}}
}}

Revision as of 23:34, 13 July 2019

IR 05000498-05-005 & 05000499-05-005, on 09/27-12/31/2005, South Texas Project Electric Generating Station
ML060440618
Person / Time
Site: South Texas  STP Nuclear Operating Company icon.png
Issue date: 02/11/2006
From: Clay Johnson
NRC/RGN-IV/DRP/RPB-A
To: Sheppard J
South Texas
References
IR-05-005
Download: ML060440618 (45)


Text

February 11, 2006James J. Sheppard, President and Chief Executive Officer STP Nuclear Operating Company P.O. Box 289 Wadsworth, Texas 77483SUBJECT:SOUTH TEXAS PROJECT ELECTRIC GENERATING STATION - NRCINTEGRATED INSPECTION REPORT 05000498/2005005 AND 05000499/2005005

Dear Mr. Sheppard:

On December 31, 2005, the US Nuclear Regulatory Commission (NRC) completed aninspection at your South Texas Project Electric Generating Station, Units 1 and 2, facility. The enclosed integrated report documents the inspection findings which were discussed on January 12, 2006, with you and members of your staff.The inspection examined activities conducted under your licenses as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your licenses. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.This report documents three findings of very low safety significance (Green), evaluated underthe risk significance determination process (SDP). These findings were determined to involve violations of NRC requirements. However, because of the very low safety significance and because they were entered into your corrective action program, the NRC is treating these findings as noncited violations (NCV) consistent with Section VI.A of the NRC Enforcement Policy. Additionally, two licensee-identified violations which were determined to be of very low safety significance are listed in this report. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at South Texas Project Electric Generating Station, Units 1 and 2, facility.

STP Nuclear Operating Company-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Claude E. Johnson, ChiefProject Branch A Division of Reactor ProjectsDockets: 50-498 50-499 Licenses: NPF-76 NPF-80

Enclosure:

NRC Inspection Report 05000498/2005005 and 05000499/2005005 w/attachment: Supplemental Information

REGION IV Dockets:50-498, 50-499 Licenses:NPF-76NPF-80Report No:05000498/200500505000499/2005005Licensee:STP Nuclear Operating Company Facility:South Texas Project Electric Generating Station, Units 1 and 2 Location:FM 521 - 8 miles west of Wadsworth Wadsworth, Texas 77483Dates:September 27 through December 31, 2005 Inspectors:J. Cruz, Senior Resident InspectorJ. Taylor, Resident Inspector H. Crouch, Reactor Engineer P. Goldberg, P.E., Reactor Inspector, Engineering Branch 2 J. Adams, Reactor Inspector, Engineering Branch 1 P. Elkmann, Emergency Preparedness Inspector T. McKernon, Senior Operations Engineer P. Gage, Senior Operations Engineer B. Tindell, Reactor InspectorApproved By:C. Johnson, ChiefProject Branch A Division of Reactor Projects-2-

SUMMARY OF FINDINGS

IR 05000498/2005005, 05000499/2005005; 09/27/05-12/31/05; South Texas Project ElectricGenerating Station; Units 1 & 2; Integrated Resident Report, Refueling Outage, Event FollowupThe report covered a three month period of inspection completed by the resident inspectors andproject engineers and announced inspections by regional inspectors. Three Green noncited violations were identified. The significance of most findings is indicated by their color (Green,White, Yellow, or Red) and was determined by the Significance Determination Process in Inspection Manual Chapter 0609. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review.

The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green.

A Green self-revealing noncited violation of Technical Specification 6.8.1.a andRegulatory Guide 1.33, Appendix A, was identified for failure to adhere to Plant Operating Procedure 0POP02-CV-004, "Chemical and Volume Control System Subsystem," Revision 41. The failure to follow procedure resulted in reactor coolant system inventory being diverted to the pressurizer relief tank when a letdown pressure relief valve opened during a letdown orifice swap. The licensee entered the performance deficiency into their corrective action program for resolution.This finding is greater than minor because it had the actual impact of lifting a relief valveand is associated with the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during power operations.

The finding is of very low safety significance because, assuming worst case degradation, the lifted relief valve would not have resulted in exceeding the Technical Specification limit for identified reactor coolant system leakage. The cause of the finding is related to the crosscutting element of human perform ance. (Section 1R20.1)

Cornerstone: Barrier Integrity

Green.

A Green self-revealing noncited violation of Technical Specification 6.8.1.a andRegulatory Guide 1.33, Appendix A, was identified for failure to adhere to Plant Operating Procedure 0POP08-FH-0003, "Fuel Transfer System," Revision 26. The failure to follow procedure resulted in fuel movers challenging the interlocks in the fuel transfer system. Specifically, a fuel mover attempted to lower a fuel assembly in the-3-upender while the upender was still rising. The interlock prevented the upender frommaking contact with the fuel assembly. The licensee entered the performance deficiency into their corrective action program for resolution.This finding is greater than minor, because it involved the potential damage to fuelassemblies. Because this issue involves fuel assembly handling, it is not suitable for evaluation under the NRC Significance Determination Process. Therefore, this finding was reviewed by NRC management and determined to be of low safety significance because the event did not result in damage to a fuel assembly. The cause of the finding is related to the crosscutting element of human performance.

(Section 1R20.2)

Cornerstone: Mitigating Systems

Green.

A Green self-revealing noncited violation of Technical Specification 3.7.4 wasidentified which requires in part, that with only two of three required essential cooling water loops operable, three loops be restored to operable within 7 days or be in at least hot standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Contrary to the above, an analysis of cavitation induced pipe cracking discovered by inspection had rendered essential cooling water Train 2B inoperable for an indeterminate time greater than 7 days while Unit 2 continued to operate at 100% power. The licensee entered the performance deficiency into their corrective action program for resolution.This finding is greater than minor because it affected the availability, reliability andcapability objectives of the mitigating systems reactor safety cornerstone. Engineering analysis determined that if a seismic event had occurred, essential cooling water Train 2B could have been rendered non-functional. The finding is only of very low safety significance because of the low frequency of occurrences of seismic events at the site and because the minimum required two trains of essential cooling water for accident mitigation was available. The cause of the finding is related to the crosscutting elementof problem identification and resolution. (Section 4OA3)

B.Licensee-Identified Violations

Violations of very low safety significance, which were identified by the licensee havebeen reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. These violations and corrective action tracking numbers are listed in Section 4OA7 of this report.

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REPORT DETAILS

Summary of Plant StatusUnit 1 operated at essentially 100 percent power throughout the inspection period.Unit 2 began the inspection period in coastdown at 93 percent power for scheduled RefuelingOutage 2RE11. The unit was shutdown on October 1, restarted on November 2 and achieved full power shortly thereafter. The unit operated at essentially 100 percent power for the remainder of the inspection period.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, Barrier Integrity1R04Equipment Alignment (71111.04)Partial System Walkdown

a. Inspection Scope

The inspectors:

(1) walked down portions of the two below listed risk important systemsand reviewed plant procedures and documents to verify that critical portions of the selected systems were correctly aligned; and
(2) compared deficiencies identified during the walk down to the licensee's corrective action program to ensure problems were being identified and corrected. *(Unit 2) The inspectors verified the condition of the Residual Heat Removalsystem Train A while the other two trains were in service using Plant Operating Procedure 0POP02-RH-001, " Residual Heat Removal System Operation,"

Revision 40, on October 6, 2005*(Unit 2) The inspectors verified the condition of the Spent Fuel Pool coolingsystem during core offload using Plant Operating Procedure 0POP02-FC-0001, "Spent Fuel Pool Cooling and Cleanup System", Revision 46, on October 11-14, 2005The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

Quarterly Inspection

a. Inspection Scope

The inspectors walked down the six below listed plant areas to assess the materialcondition of active and passive fire protection features and their operational lineup and readiness. The inspectors:

(1) verified that transient combustibles and hot work activities were controlled in accordance with plant procedures;
(2) observed the condition of fire detection devices to verify they remained functional;
(3) observed fire suppression systems to verify they remained functional;
(4) verified that fire extinguishers and hose stations were provided at their designated locations and that they were in a satisfactory condition;
(5) verified that passive fire protection features (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems) were in a satisfactory material condition;
(6) verified that adequate compensatory measures were established for degraded or inoperable fire protection features; and
(7) reviewed the corrective action program to determine if the licensee identified and corrected fire protection problems.
  • (Unit 2) Fuel Handling Building (Fire Zones Z310,317,318,322,330),September 29, 2005*(Unit 2) Fuel Handling Building (Fire Zones Z311), October 11, 2005
  • (Unit 2) Reactor Containment, Pressurizer Cubicle (Fire Zones Z224),October 20, 2005*(Unit 1,2) Essential Cooling Water Building (Fire Zones Z600-605),November 2, 2005*(Unit 1) Diesel Generator 13 Train "C" Emergency Ventilation Fan Room (FireZone 509), December 5, 2005*(Unit 2) Electrical Auxiliary Building 10' Elevation Corridor (Fire Zone Z016),December 7, 2005The inspectors completed six samples.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors:

(1) reviewed the Updated Safety Analysis Report, the flooding analysis,and plant procedures to assess seasonal susceptibilities involving external flooding;
(2) reviewed the corrective action program to determine if the licensee identified and corrected flooding problems;
(3) inspected underground bunkers/manholes to verify the adequacy of
(a) sump pumps,
(b) level alarm circuits,
(c) cable splices subject to submergence, and
(d) drainage for bunkers/manholes;
(4) verified that operator actions for coping with flooding can reasonably achieve the desired outcomes; and
(5) walked down the below listed areas to verify the adequacy of:
(a) equipment seals located below the floodline,
(b) floor and wall penetration seals,
(c) watertight door seals,
(d) common drain lines and sumps,
(e) sump pumps, level alarms, and control circuits, and
(f) temporary or removable flood barriers. (Units 1 and 2) On October 19-20, 2005, the inspectors reviewed the floodanalysis documentation and calculations for the intermediate valvecompartments. The inspectors also conducted a walkdown of the internal watertight doors and penetrations for both units. A loose door handle was reported tothe licensee and placed in the corrective action program.The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R07 Biennial Heat Sink Performance (71111.07B)

a. Inspection Scope

The inspectors reviewed design documents (e.g., calculations and performancespecifications), program documents, implementing documents (e.g., test and maintenance procedures), and corrective action documents. The inspectors reviewed heat exchanger testing and cleaning results, and design changes with licensee personnel. For heat exchangers directly connected to the safety-related service water system, theinspectors verified whether thermal performance testing, or heat exchanger inspection, maintenance and cleaning, and the chemistry monitoring program provided sufficient controls to ensure proper heat transfer. Specifically, the inspectors reviewed:

(1) heat exchanger test methods and test results from performance testing,
(2) heat exchanger inspection and cleaning methods and results,
(3) chemical water treatment and results, and
(4) verification of design including flow balancing to ensure sufficient heat exchanger flow.

For heat exchangers directly or indirectly connected to the safety-related service watersystem, the inspectors verified the:

(1) condition and operation were consistent with design assumptions in the heat transfer calculations,
(2) potential for water hammer, as applicable,
(3) chemistry controls for heat exchangers indirectly connected to the safety-related service water system, and
(4) redundant and infrequently used heat exchangers are flow tested periodically to ensure sufficient flow.If available, the inspectors reviewed additional nondestructive examination results forthe selected heat exchangers that demonstrated structural integrity. The inspectors selected three heat exchangers that ranked high in the plant specific riskassessment and were directly or indirectly connected to the safety-related service water system. The inspectors selected the following heat exchangers: *Unit 1 component cooling water/essential cooling water heat exchanger*Unit 1 residual heat removal heat exchanger, and
  • Unit 2 emergency diesel generator jacket water heat exchangerThe inspectors completed three heat exchangers which exceeded the minimum required sample size of two heat exchangers.The inspectors verified that the licensee had entered significant heat exchanger/heatsink problems into the corrective action program. The inspectors reviewed nine corrective action documents.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities (71111.08)

a. Inspection Scope

.1Performance of Nondestructive Examination Activities Other than Steam GeneratorTube Inspections The inspectors observed and reviewed 13 visual examinations, two surfaceexaminations, and three volumetric examinations. The two surface examinations were both liquid penetrant examinations. The three volumetric examinations were ultrasonic examinations. The inspectors also observed the ultrasonic system calibration. Of the examinations reviewed, none of them contained recordable indications that were accepted for continued service nor did any of the licensee-performed examinations since the last outage.

During the review of these examinations, the inspectors verified that the correctnondestructive examination procedures were used, examinations and conditions were as specified in the procedures, and test instrumentation or equipment was properly calibrated and within the allowable calibration period. The inspectors also reviewed the nondestructive examination certifications of personnel observed performing examinations or identified during review of completed examination packages.The inspectors also observed and reviewed three Class 1 welds and verified that theweld process and post-weld examinations were performed in accordance with the ASME

Code.The one sample for this step is comprised of reviewing two or three non-destructiveexamination types to ensure they were performed in accordance with the ASME code (three were reviewed); reviewing one or two examinations where relevant indications were left in service to ensure this was done in accordance with the ASME code (none were reviewed because no relevant indications were left in service); and reviewing one to three welds to ensure they were performed in accordance with the ASME code (three were reviewed). This sample was completed.

b. Findings

No findings of significance were identified.

.2 Pressurized Water Reactor Vessel Upper Head Penetration Inspection ActivitiesThe inspector did not perform this inspection step because the licensee did not performany activities in this area.The one sample for this step is comprised of reviewing the bare metal visual inspectionof the reactor vessel upper head penetrations and/or reviewing the volumetric/surface

examination of these penetrations to ensure the examinations were performed in a manner consistent with the ASME code; reviewing one or two recordable indications that were left in service to ensure this was done in accordance with the ASME code; and if weld repairs were performed, reviewing one to three weld repairs to ensure this was done in accordance with the ASME code. The licensee did not perform any of these activities so the inspectors did not perform this sample..3Boric Acid Corrosion Control Inspection Activities

a. Inspection Scope

The inspectors performed a review of the licensee's boric acid walkdown of the Unit 2reactor containment as documented. The inspectors verified that the visual inspections emphasized locations where boric acid leaks can cause degradation to safety significant components. The inspectors also reviewed five condition reports and associated workorders which documented the boric acid leaks identified during the walkdown.The one sample for this step is comprised of reviewing a sample of the boric acidwalkdown results performed by the licensee to verify that the inspections emphasize locations where boric acid leaks can cause degradation of safety significant components (the inspectors completed this); reviewing licensee response to one to three indications of boric acid leakage to verify that the licensee properly dispositioned them (the inspectors completed this); and reviewing one to three corrective actions associated with boric acid leaks to ensure they are consistent with the requirements of the ASME code and 10 CFR Part 50 Appendix B Criterion XVI (the inspectors completed this). The inspectors completed this sample.

b. Findings

No findings of significance were identified.

.4 Steam Generator Tube Inspection Activities

a. Inspection Scope

The inspectors did not perform this inspection step because the licensee did not performany activities in this area.The one sample for this step is comprised of reviewing in-situ pressure testing to ensureit is properly performed; comparing flaws detected during this outage against predictions; ensuring eddy current inspections conform to the various requirements; evaluating any new degradation mechanisms detected during the inspections to ensure they are properly dispositioned; ensuring the scope of eddy current inspections emphasizes locations where flaws are expected to occur; confirm that repair processes are consistent with the Technical Specifications requirements; evaluating the repair criteria to ensure they are consistent with requirements; assess whether the licensee has properly evaluated any significant primary to secondary leakage; evaluating licensee response to any foreign material in the secondary side; evaluating eddy current analysis, if there are concerns based on any of the above evaluations. The inspectors did not complete this sample because the licensee did not perform any of the activities in this area..5Identification and Resolution of Problems

a. Inspection Scope

The inspectors reviewed 11 inservice inspection-related condition reports issued duringthe current and past refueling outage, and verified that the licensee identified, evaluated, corrected, and trended problems. In this effort, the inspector evaluated theeffectiveness of the licensee's corrective action process, including the adequacy of the technical resolutions.There is no sample associated with this step.

b. Findings

No findings of significance were identified.

The inspectors completed the required samples for Section 1R08 (.1,

.2 , .3, and .4) byperforming two of the four samples - the other two could not be performed because the

licensee did not perform any activities in these areas.

1R11 Licensed Operator Requalification (71111.11).1Biennial Inspection (71111.11B)

a. Inspection Scope

The inspectors interviewed five personnel, including two operators, twoinstructors/evaluators, and an operations support person, regarding the policies and practices for administering requalification examinations. The inspectors also reviewed operator performance on the written and operating examinations. Examination results were assessed to determine if they were consistent with the guidance contained in NUREG 1021 and Manual Chapter 0609, Appendix I, "Operator Requalification Human Performance Significance Determination Process."The review included an assessment of 10 operating examination job performancemeasures (JPMs) and two scenarios that were used in the biennial requalification cycle to determine if they provided adequate discrimination at the minimum acceptable level of operator performance. The results of the examinations were assessed to determine the licensee's appraisal ofoperator performance and the feedback of performance analysis to the requalification training program. The inspectors interviewed members of the training department and reviewed minutes of training review group meetings to assess the responsiveness of the licensed operator requalification program. Additionally, the inspectors assessed the South Texas Project plant-referencedsimulator for compliance with 10 CFR 55.46, Simulator Facilities, using Baseline Inspection Procedure 71111.11 (Section 03.11). This assessment included the adequacy of the licensee's simulation facility for use in operator licensing examinations and for satisfying experience requirements as prescribed by 10 CFR 55.46. The inspectors reviewed a sample of simulator performance test records (transient tests, surveillance tests, and malfunction tests,) simulator deficiency report records, and processes for ensuring simulator fidelity commensurate with 10 CFR 55.46. Theinspectors reviewed selected simulator deficiency reports generated by the licensee that did not result in changes to the configuration of the simulator to assess the responsiveness of the licensee's simulator configuration management program. The inspectors also interviewed members of the licensee's simulator configuration control group as part of this review.

b. Findings

No findings of significance were identified..2Quarterly Inspection (71111.11Q)

a. Inspection Scope

On December 5, 2005, the inspectors observed testing and training of senior reactoroperators and reactor operators to identify deficiencies and discrepancies in the training,to assess operator performance, and to assess the evaluator's critique. The training scenario involved a failure of a steam generator feedwater pump concurrent with a large break loss of coolant accident. The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Implementation (71111.12)

a. Inspection Scope

The inspectors reviewed the two below listed maintenance activities to:

(1) verify theappropriate handling of structure, system, and component (SSC) performance or condition problems;
(2) verify the appropriate handling of degraded SSC functional performance;
(3) evaluate the role of work practices and common cause problems; and
(4) evaluate the handling of SSC issues reviewed under the requirements of the Maintenance Rule, 10 CFR Part 50 Appendix B, and the Technical Specifications. *(Unit 2) Steam generator feedwater pump corrective maintenance issues inresponse to high bearing temperatures, December 6, 2005*(Unit 2) Auxiliary feedwater Pump 22 maintenance activities in response todiscovery of foreign material in the re-circulation line, December 15, 2005 The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13).1Risk Assessment and Management of Risk

a. Inspection Scope

The inspectors reviewed the three below listed assessment activities to verify: (1)performance of risk assessments when required by 10 CFR 50.65 (a)(4) and licensee procedures prior to changes in plant configuration for maintenance activities and plant operations;

(2) the accuracy, adequacy, and completeness of the information considered in the risk assessment;
(3) that the licensee recognizes, and/or enters as applicable, the appropriate licensee-established risk category according to the risk assessment results and licensee procedures, and
(4) the licensee identified and corrected problems related to maintenance risk assessments.*(Unit 2) Evaluation of risk in accordance with Technical Specification 3.0.4.b priorto mode change conducted during refueling Outage 2RE11, October 31, 2005*(Common) Evaluation of risk for Diesel Generator 21 extended allowed outage,November 28, 2005*(Unit 2) Evaluation of risk for steam generator feedwater pump correctivemaintenance activities, December 6, 2005The inspectors completed three samples.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors:

(1) reviewed plant status documents such as operator shift logs,emergent work documentation, deferred modifications, and standing orders to determine if an operability evaluation was warranted for degraded components;
(2) referred to the Updated Safety Analysis Report and design basis documents to review the technical adequacy of licensee operability evaluations;
(3) evaluated compensatory measures associated with operability evaluations;
(4) determined degraded component impact on any Technical Specifications;
(5) used the SignificanceDetermination Process to evaluate the risk significance of degraded or inoperable equipment; and
(6) verified that the licensee has identified and implemented appropriate corrective actions associated with degraded components.*(Unit 1) Electrical Auxiliary Building HVAC backdraft damper failure to closewhen the supply fan was secured, October 13, 2005*(Unit 1) Auxiliary feedwater Pump 14 exhibiting increased vibrationmeasurements, October 22, 2005The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R16 Operator Workarounds (71111.16)Selected Operator Workarounds

a. Inspection Scope

The inspectors reviewed the one below listed operator workaround to:

(1) determine ifthe functional capability of the system or human reliability in responding to an initiating event is affected;
(2) evaluate the effect of the operator workaround on the operator's ability to implement abnormal or emergency operating procedures; and
(3) verify that the licensee has identified and implemented appropriate corrective actions associated with operator workarounds. *(Unit 1) Emergency Diesel Generator 12 jacket water level alarm switch out ofcalibration resulting in plant operators being required to adjust standpipe level while the diesel was running, December 7, 2005The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing

a. Inspection Scope

The inspectors selected the four below listed postmaintenance test activities of risksignificant systems or components. For each item, the inspectors:

(1) reviewed the applicable licensing basis and/or design-basis documents to determine the safety functions;
(2) evaluated the safety functions that may have been affected by the maintenance activity; and
(3) reviewed the test procedure to ensure it adequately tested the safety function that may have been affected. The inspectors either witnessed or reviewed test data to verify that acceptance criteria were met, plant impacts were evaluated, test equipment was calibrated, procedures were followed, jumpers were properly controlled, the test data results were complete and accurate, the test equipment was removed, the system was properly re-aligned, and deficiencies during testing were documented. The inspectors also reviewed the corrective action program to determine if the licensee identified and corrected problems related to postmaintenance testing. *(Unit 2) Work Authorization Number 298842 and Work Order 453058, postmaintenance testing associated with emergent maintenance in response to Safety Injection Accumulator 2B Fill Valve FV-3974 exhibiting leak-by, October 26, 2005
  • (Unit 1) Plant Maintenance Work Orders PM:MMD-1-91000010, Revision 07.0postmaintenance testing associated with Emergency Diesel Generator 12 planned maintenance, October 31, 2005*(Unit 2) Plant Operations Procedure 0POP02-RH-0001, "Residual Heat RemovalSystem Operation," Revision 40, postmaintenance testing associated with planned maintenance, November 2, 2005*(Unit 2) Plant Maintenance Work Orders PM:MM-2-88001972, Revision 08.0 andIC-2-05000278, Revision 00.0, postmaintenance testing associated with Auxiliary Feedwater Pump 24 planned maintenance, November 22, 2005The inspectors completed four samples.

b. Findings

No findings of significance were identified.

1R20 Refueling Outage

a. Inspection Scope

During September 27 through November 2, 2005, the inspectors reviewed the followingrisk significant refueling items or outage activities to verify defense in depth commensurate with the outage risk control plan and compliance with the Technical Specifications:

(1) the risk control plan;
(2) tagging/clearance activities;
(3) reactor coolant system instrumentation;
(4) electrical power;
(5) decay heat removal;
(6) spent fuel pool cooling;
(6) inventory control;
(7) reactivity control;
(8) containment closure;
(9) reduced inventory or mid-loop conditions;
(10) refueling activities;
(11) heatup and coldown activities; and
(12) licensee identification and implementation of appropriate corrective actions associated with refueling and outage activities.

b. Findings

.1Inadvertent Letdown Relief Valve OpeningIntroduction. A Green self-reveling noncited violation of Technical Specification 6.8.1.aand Regulatory Guide 1.33, Appendix A, was identified for failure to adhere to a procedure that resulted in a letdown pressure relief valve opening during a letdown orifice swap.Description. On October 2, 2005, Unit 2 was in the process of a plant shutdown andcooldown in support of refueling outage 2RE11. A reactor operator attempted to place the small letdown orifice in service per Plant Operating Procedure 0POP02-CV-004, "Chemical and Volume Control System Subsystem." The large letdown orifice was in service when the procedure was performed. Step 9.4 of the procedure required that the operator adjust Pressure Control Valve PCV-0135 to obtain a letdown pressure of approximately 200 psig. During the performance of the activity, the reactor operator believed he had adjusted pressure appropriately but, according to information received from the plant computer following the event, pressure had only been adjusted to 285 psig. With pressure higher than required by procedure, there was not sufficient margin to allow PCV-0135 to be opened enough to compensate for the ensuing letdown pressure increase which occurred after opening the small letdown orifice isolation valve.

Operators failed to manipulate the letdown orifice isolation valve in a manner that properly controlled pressure in the chemical and volume control system. As a result, the letdown line relief valve opened, diverting reactor coolant system (RCS) inventory to the primary relief tank. This event created the possibility of the relief valve sticking open and causing a small-break loss of coolant condition until the break could be isolated. The licensee entered this performance deficiency into their Corrective Action Program for resolution.

Analysis.

The licensee's failure to adhere to a procedure that resulted in a letdownpressure relief valve opening during a letdown orifice swap was a performance deficiency. This finding was greater than minor because it had the actual impact of lifting a relief valve and, therefore, was associated with an increase in the likelihood ofan initiating event. As the finding was associated with the cornerstone attribute of Initiating Events and affected the associated cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during power operations, it surpassed the screening criteria of Inspection Manual Chapter 0612, Appendix B. Using the Significance Determination Process of Inspection Manual Chapter 0609, Appendix A, under the initiating events cornerstone, the answer to the Phase 1 screening question of

?Assuming worst case degradation, would the findingresult in exceeding the Tech Spec limit for identified RCS leakage?" was determined to be "No" because there was no degradation of the chemical and volume control system letdown line relief valve or system that could have either decreased the probability of the relief valve to reseat nor prevent the system isolation valves from functioning, thereby precluding a draindown from the RCS to the primary relief tank. Therefore, the finding was determined to be of very low safety significance. As the root cause of the performance deficiency involved failure to follow procedure, this finding involved crosscutting aspects in the area of human performance related to personnel andattention to detail.Enforcement. Technical Specification 6.8.1.a requires that procedures be established,implemented, and maintained covering the applicable procedures in Appendix A of Regulatory Guide 1.33. Appendix A, Item 3.n, requires procedures be maintained for the chemical and volume control system. Plant Operating Procedure 0POP02-CV-004, "Chemical and Volume Control System Subsystem," Revision 41, was not properly implemented in that failure to follow procedure resulted in the lifting of a letdown relief valve. The opening of the letdown relief valve increased the risk of an initiating event of an interfacing system small loss of coolant accident and degraded the reactor coolant system barrier integrity. Because this finding was entered into the licensee's Corrective Action Program as CR 05-12063 and is of very low safety significance, this finding is being treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000499/2005005-01, Inadvertent Letdown Relief Valve Opening..2Improper Fuel HandlingIntroduction. A Green self-revealing noncited violation of Technical Specification 6.8.1.aand Regulatory Guide 1.33, Appendix A, was identified for failure to adhere to a procedure during fuel movement.Description. On October 12, 2005, while off-loading the reactor core in Unit 2, fuelmovers challenged the interlocks in the fuel transfer system. Specifically, a fuel mover attempted to lower a fuel assembly in the upender while the upender was still rising.

The interlock prevented the upender from making contact with the fuel assembly. There was an apparent miscommunication in that the refuel machine operator understood that the upender was fully raised when in fact it was still moving. Step 7.10 of Plant Operating Procedure 0POP08-FH-0003, "Fuel Transfer System," required that fuel movers visually verify that the upender is in the vertical position prior to moving a fuel assembly using the fuel handling machine.

Analysis.

The inspectors determined that this finding was a performance deficiency, inthat the fuel movers failed to follow procedure. This issue was determined to be more than minor, because it involved the potential damage to fuel assemblies. Because this issue involves fuel assembly handling it is not suitable for evaluation under the NRC Significance Determination Process. Therefore, this finding was reviewed by NRC management and determined to be of very low safety significance (Green) because the event did not result in damage to a fuel assembly. As the root cause of the performance deficiency involved failure to follow procedure, this finding involved crosscutting aspectsin the area of human performance related to personnel and attention to detail.Enforcement. Technical Specification 6.8.1.a requires that procedures be established,implemented, and maintained covering the applicable procedures in Appendix A of Regulatory Guide 1.33. Appendix A, Item 2.k. requires procedures be implemented for preparation for refueling and refueling equipment operation . Plant Operating Procedure 0POP08-FH-0003, "Fuel Transfer System," Revision 26, was not properly implemented in that failure to follow procedure resulted in challenged interlocks in the fuel transfer system. The failure to follow procedure increased the risk of potential damage to fuel assemblies. Because this finding was entered into the licensee's Corrective Action Program as CR 05-12885 and is of very low safety significance, this finding is being treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000499/2005005-02, Improper Fuel Handling.

1R22 Surveillance Testing

(71111.22)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, procedurerequirements, and Technical Specifications to ensure that the two below listed surveillance activities demonstrated that the SSC's tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the following significant surveillance test attributes were adequate:

(1) preconditioning;
(2) evaluation of testing impact on the plant;
(3) acceptance criteria;
(4) test equipment;
(5) procedures;
(6) jumper/lifted lead controls;
(7) test data;
(8) testing frequency and method demonstrated Technical Specification operability;
(9) test equipment removal;
(10) restoration of plant systems;
(11) fulfillment of ASME Code requirements;
(12) updating of performance indicator data;
(13) engineering evaluations, root causes, and bases for returning tested SSC's not meeting the test acceptance criteria were correct;
(14) reference setting data; and
(15) annunciators and alarms setpoints. The inspectors also verified that the licensee identified and implemented any needed corrective actions associated with the surveillance testing.
  • (Unit 2) Plant Surveillance Procedure 0PSP03-RC-0006, "Reactor CoolantInventory," Revision 15, September 28, 2005*(Unit 1) Plant Surveillance Procedure 0PSP03-CS-0003, "Containment SprayPump 1C(2C) Inservice Test," Revision 12, December 6, 2005 The inspectors completed two samples.

b. Findings

No findings of significance were identified.

===Cornerstone: Emergency Preparedness1EP2Alert Notification System Testing (71114.02)

a. Inspection Scope

The inspectors discussed with licensee staff the status of offsite siren and tone alertradio systems to determine the adequacy of licensee methods for testing the alert and===

notification system in accordance with 10 CFR Part 50, Appendix E. The licensee's alert and notification system testing program was compared with criteria in NUREG-0654, "Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants," Revision 1, Federal Emergency Management Agency (FEMA) Report REP-10, "Guide for the Evaluation of Alert and Notification Systems for Nuclear Power Plants," and the licensee's current FEMA-approved alert and notification system design report. The inspectors also reviewed Plant General Procedure 0PGP05-ZV-0006, "Emergency Notification and Response System," Revision 3, and Desktop Guide ZV-0013, "Alert Radio Maintenance and Distribution," Revision 0. The inspectors completed one sample during this inspection.

b. Findings

No findings of significance were identified.1EP3Emergency Response Organization Augmentation Testing (71114.03)

a. Inspection Scope

The inspectors reviewed Plant General Procedure 0PGP05-ZV-0014, "EmergencyResponse Activities," Revisions 2, 3, and 5, Form 19, "ENRS Test (Autodialer Test),"

and the results of three call-in and drive-in drills to determine the licensee's ability to staff emergency response facilities in accordance with the licensee emergency plan and the requirements of 10 CFR Part 50 Appendix E. The inspectors also interviewed licensee staff responsible for maintaining the licensee's Emergency Notification and Response System. The inspectors completed one sample during this inspection.

b. Findings

No findings of significance were identified.1EP5Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)

a. Inspection Scope

The inspectors reviewed the following documents related to the licensee's correctiveaction program to determine the licensee's ability to identify and correct problems in accordance with 10 CFR 50.47(b)(14) and 10 CFR Part 50 Appendix E.0PGP03-ZX-0002, "Condition Reporting Process," Revision 30 0ERP01-ZV-RE02, Form 2, "Emergency Event Documentation Worksheet," EventNumber 1C0301, Unusual Event, July 15, 20030ERP01-ZV-RE02, Form 2, "Emergency Event Documentation Worksheet," EventNumber 1C0401, Unusual Event, April 6, 2004Drill reports for 10 combined functional and stand-alone station emergencypreparedness drills and exercisesNine Quality Assurance Audits and Monitoring Reports Summaries of all corrective actions assigned to the emergency preparednessdepartment between June 2003 and September 2005Details of 17 selected condition reports The inspector completed one sample during this inspection.

b. Findings

No findings of significance were identified.4.OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed licensee submittals for the performance indicators listed belowfor the period July 1, 2004, through September 30, 2005. The definitions and guidance of NEI 99-02, "Regulatory Assessment Indicator Guideline," Revisions 2 and 3, were used to verify the licensee's basis for reporting each data element in order to verify the accuracy of performance indicator data reported during the assessment period. Thelicensee's performance indicator data were also reviewed against the requirements of Plant General Procedure 0PGP05-ZV-0013, "Performance Indicator Tracking Guide,"

Revision 1.Emergency Preparedness Cornerstone

  • Drill and Exercise Performance *Emergency Response Organization Participation
  • Alert and Notification System ReliabilityThe inspectors reviewed a 100 percent sampling of drill and exercise scenarios,licensed operator simulator training sessions, notification forms, and attendance and critique records associated with training sessions, drills, and exercises conducted during the verification period. The inspectors reviewed 23 selected emergency responder qualification and training records, and a 100 percent sample of quarterly drill participation records. The inspectors reviewed a 100 percent sample of siren test and maintenance records and procedures. The inspectors also interviewed licensee personnel that were accountable for collecting and evaluating the PI data. The inspectors completed three samples during this inspection.

b. Findings

No findings of significance were identified.4OA2Identification and Resolution of Problems (71152).1Daily CR Review

a. Inspection Scope

As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"and in order to help identify repetitive equipment failures or specific human performance issues for followup, the inspectors performed a daily screening of items entered into the licensee's corrective action program. This review was accomplished by reviewing hard copy or electronic summaries of each CR, attending various daily screening meetings, and accessing the licensee's computerized corrective action program database.

b. Findings and Observations

No findings of significance were identified.

.2 Semiannual Sample Review

a. Inspection Scope

On December 23, 2005, the inspectors completed a semiannual review of licenseeinternal documents, reports, and performance indicators to identify trends that might indicate the existence of more significant safety issues. The inspector's review nominally considered the 6-month period of July through December 2005, although some examples expanded beyond those dates when the scope of the trend warranted.

Corrective actions associated with a sample of the issues identified in the licensee's trend reports were reviewed for adequacy. The inspectors evaluated the licensee's implementation of the corrective action program as specified in licensee Plant General Procedure 0PGP03-ZX-0002, "Condition Reporting Process," and 10 CFR Part 50, Appendix B. Documents reviewed by the inspectors included:

  • Condition Record Daily Monitor* System Performance Indicators
  • System Health Reports
  • Systems Engineering Quick Hitter List
  • Quality Assurance Audit Reports
  • Selected Work Orders from the 3rd and 4th Quarters of 2005
  • South Texas Project Internal Performance Summary Reports

b. Findings and Observations

No findings of significance were identified. However, the inspectors did make thefollowing observations which were shared with licensee management.* The equipment reliability of the essential chillers continue to remain problematicand the number of unplanned entries into Technical Specification required Limiting Conditions for Operation appear to be trending in a negative manner* In the fourth quarter of the year, vital inverter issues became more visiblefollowing the inverter replacements which took place during the most recent refueling outages in each unit* Reactivity management issues regarding control rod drive mechanism andcontrol board valve mis-position errors appear to represent a negative trend in site performance

4OA3 Event Followup

(Closed) LER 05000499/20050004-00 and LER 05000499/20050004-01, Inoperability ofEssential Cooling Water 2A and 2B Trains

a. Inspection Scope

The inspectors reviewed LER 05000499/20050004 and the subsequent event reportSupplement 1, to verify that the cause of the essential cooling water (ECW) Train 2B inoperability for more than the Technical Specification allowed outage time was identified and that corrective actions were reasonable. The inoperability was declared due to cavitation pitting, circumferential cracking, secondary axial cracking and pipe end to flange weld separations discovered in the aluminum bronze pipe inside a slip-on flange immediately downstream of the Component Cooling Water Heat Exchanger 2B ECW return throttle valve. The structural integrity of the pipe could not be verified using the requirements of NRC Generic Letter 90-05, "Guidance for Performing Temporary Repair of ASME Code Class 1, 2, and 3 Piping," so the train was declared inoperable due to non-compliance with ASME Code requirements.

b. Findings

Introduction.

A Green self-revealing NCV was identified for the failure to perform therequired actions specified in Technical Specification 3.7.4 with less than three independent ECW loops operable.Description. In May 2005, cavitation damage was discovered in the slip-on flangeassembly immediately downstream of the component cooling water (CCW) Heat Exchanger 1B ECW Return Throttle Valve 1-EW-0064. Work requests were initiated to inspect the CCW heat exchanger return throttle valves in all trains of both units. Cavitation pitting, circumferential pipe cracking, secondary axial pipe cracking, and pipeend to flange weld separation were also discovered in the aluminum bronze pipe inside a slip-on flange immediately downstream of the CCW Heat Exchanger 2A ECW return throttle valve, 2-EW-0027. Structural integrity of the pipe could not be verified using the requirements of NRC Generic Letter 90-05, "Guidance for Performing Temporary Repair of ASME Code Class 1, 2, and 3 Piping." Because structural integrity could not be demonstrated, ECW Train 2A was declared noncompliant with ASME Code requirements and inoperable per Technical Specification requirements. The licensee determined, based on metallurgical analysis of the failed parts, that ECW Train 2A was inoperable for an undetermined period of time. The condition logically existed for a period longer than the Technical Specification 3

.7.4 allowed outage time although the

length of time is not known. On August 15, 2005 an inspection of the corresponding Train 2B throttle valve, 2-EW-0064, discovered a similar condition and it was also declared inoperable.

Initial root cause analysis and engineering evaluation results for the condition (APTECHcalculation AES-C-5862-1, CR 05-8601-25) concluded that the discovered condition on ECW Train 2A justifies the acceptance criteria for both the upset and faulted conditions per the 2004 edition of the ASME Section XI pipe flaw acceptance criteria. The licensee is committed to the 1989 version of the ASME code and used those limits to determine the initial operability impact . Since ECW Train 2A was acceptable per the 2004 version of the code and since ECW Train 2C was also considered operable, the safety function for the ECW system was met and the safety consequences were low. The condition discovered on ECW Train 2B was susceptible only to a seismic event which has a very low frequency of occurrence at the South Texas Project site. It was noted in the licensee's root cause analysis that several missed opportunities toprevent the condition had occurred:*A hydraulic transients analysis completed in May 1984 by the constructionarchitect/engineer identified the cavitation potential of the ECW throttle valves.

The analysis recommended valve manufacturer's data should be reviewed in light of the low-back pressure, high-head-drop conditions. *In December 1985, an ECW design verification review identified that the systemthrottle valves could experience flashing or cavitation conditions. The review recommended that restricting orifices should be added as needed. However, the licensee's response erroneously dismissed the cavitation item because pressure at the discharge of the valve is much greater than the vapor pressure.*A May 1986 observation and evaluation of the ECW system preoperationaltesting noted that the CCW discharge butterfly valve was noisy, identified a potential solution, and recommended further hydraulic transient testing.

Documented results of the hydraulic transient testing in July 1986 report concluded the noise at the CCW heat exchanger throttle valves was due to cavitation potential but did not warrant reorientation of the valves. It was recommended that the valves should be specifically included in the "Plant Vibration Monitoring Program" and further actions be based on results from that program.*In 1990, the licensee completed its response to NRC Generic Letter 89-13,"Service Water System Problems Affecting Safety-Related Equipment."

Although the focus of the generic letter was bio-fouling and heat transfer degradation, Recommended Action 3 was to "Ensure by establishing a routine inspection and maintenance program for open-cycle service water system piping and components that corrosion, erosion, protective coating failure, silting and bio-fouling cannot degrade the performance of the safety-related systems supplied by service water." The licensee's response to this recommendation was that the preventive maintenance program meets the requirements of this recommended action. The preventive maintenance program, however, is based on components and does not normally address maintenance of piping.

  • In 1991, inspections were performed on Train 1B and 1C CCW heat exchangerECW return throttle valves. These inspections were performed in response to concerns about bio-fouling. When the valves were inspected, damage was noted to the valve body and portions of the valves' seat rings were missing. In response to the observed damage to the seating surfaces, the licensee committed to never use these valves as maintenance boundary isolation valves. No actions were taken, however, to initiate preventive maintenance activities tomonitor erosion of the valves.*Early in 1999 (CR 99-550), erosion of ECW piping in high flow velocity areas wasidentified as a potential system-wide issue. During routine system maintenance, erosion wear had been identified at aluminum bronze tubesheets, in piping elbows, and in other fittings at areas of relatively high flow velocity. Because of the problems experienced with high flow noise and cavitation sounds, the piping downstream of the CCW heat exchanger ECW return throttle valves was identified as one of the main areas of concern. Some initial pipe wall thickness readings were obtained with ultrasonic testing. Because of the carbon steel slip-on flange, these readings were taken in the aluminum bronze piping just downstream of the flange. The readings showed wall loss of up to about 0.050 inches in some areas. While this amount of wall thinning was significant, it was still well above the minimum wall thickness. Based on these sample readings, ECW piping erosion was considered a long term "life of the plant"issue. Action to develop a wall thickness monitoring plan was therefore extended.*In July 2003, CR 03-10566 was written by the ECW system engineer to performan inspection of the gear operator and the internals of the Train 1B CCW heat exchanger ECW return throttle valve. This inspection was in response to a previous failure of a gear operator on one of the self-cleaning strainer backwash throttle valves, the failure of a circulating water system motor operated butterfly valve, and industry operating experience with butterfly valve stem to disc separation. A CCW heat exchanger ECW return throttle valve was selected because it is subject to flow-induced high vibrations. Train 1B was selected because it was scheduled for an extended allowed outage time maintenance window in October 2003. Removal of the valve from the system was requested to also allow internal visual inspection of the downstream piping to aid in selecting appropriate measuring locations for the proposed ECW erosion monitoring program. Although planning for the work order was completed in August 2003, the work order was not worked during the October 2003 extended allowed outage time and was then not implemented until May 2005.The licensee entered this performance deficiency into their Corrective Action Programfor resolution.
Analysis.

The performance deficiency associated with this event is a failure to complywith the required actions specified in Technical Specification 3.7.4. This finding isgreater than minor because it affected the availability, reliability and capability objectives of the mitigating systems reactor safety cornerstone. Engineering analysis subsequent to finding degraded ECW Train 2B piping determined that if a seismic event had occurred, Train 2B of ECW could have been rendered non-functional. The finding was only of very low safety significance because of the low frequency of occurrences of seismic events and because the minimum required two trains of ECW for accident mitigation would have been available. Additionally, the finding did not involve the total loss of any safety function, identified by a licensee PRA, IPEEE, or similar analysis, that contributed to the external event initiated core damage accident sequences. As there were several missed opportunities to prevent the performance deficiency, this issue involved crosscutting aspects in the area of problem identification and resolution.Enforcement. Technical Specification 3.7.4 requires in part, that with only two of threerequired ECW loops operable, three loops be restored to operable within seven days or be in at least Hot Standby within six hours. Contrary to the above, an analysis of cavitation induced pipe cracking discovered by inspection had rendered ECW Train 2B inoperable for an indeterminate time greater than 7 days while Unit 2 continued to operate at 100 percent power. Because this failure to perform the Technical Specification requirement is of very low safety significance and has been entered into the licensee Corrective Action Program (CR 05-8601), this violation is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000499/2005005-03, Inoperability of Essential Cooling Water Trains 2A and 2B.4OA5Other.1(Closed) Unresolved Item (URI) 05000498;499/2005004-01: Potential for Submerged Cables. In Condition Report (CR) 03-18389, it was documented that the grade had been raisedaround some manholes in the yard that contained safety-related cables so that there was a potential for water to drain into the cable vaults below. In NRC Inspection Report 05000498;499/2005004, this Unresolved Item was opened in order to gather more information about the issue, including allowing the licensee to complete inspections of the cable vaults.On December 21, 2005, regional inspectors conducted telephonic interviews withlicensee personnel, and reviewed new information from CR 03-18389. The inspectors determined that the corrective actions for the 2003 CR had not been prompt, which is a violation of Title 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action." The licensee had inspected all of the cable vaults that contain safety-related cables and, although water was found, no cables were submerged. In addition, the cable vaults with the highest water level contained cables that were going to be replaced in July 2006 so that the condition would have been discovered before the cables would have become submerged. Therefore, this issue is minor because it would not have become a moresignificant safety concern if left uncorrected. Although this issue should be corrected, it constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section IV of the Enforcement Policy..2Temporary Instruction 2515/160: Pressurizer Penetration Nozzles and Steam SpacePiping Connections in U.S. Pressurized Reactors

a. Inspection Scope

Implementation of this technical instruction was required for facilities that includeAlloy 600 base metal materials or Alloy 82/182 weld metal materials in the design of their pressurizer penetration nozzles, heater sleeves, or steam space piping components. The inspectors observed and reviewed the inspection of 13 such welds and independently inspected five of the such welds. The inspectors reviewed the certification for the nondestructive examination inspectors performing the work and determined them to be current and correct.

b. Findings

No findings of significance were identified.4OA6 Meetings, Including ExitThe results of the Licensed Operator Requalification inspection were presented to Mr. G. Parkey, Vice President, Generation, and other members of his staff on September 1, 2005.The results of the preliminary inspection were presented to Mr. T. Jordan, VicePresident, Engineering and Technical, and other members of the licensee staff at the conclusion of the Heat Sink Performance biennial inspection on October 05, 2005, during a telephonic exit. The results of the inservice and Temporary Instruction 2515/160 inspection werepresented to Mr. J. Sheppard, President and Chief Executive Officer, and other members of licensee management on October 13, 2005.The results of the emergency preparedness inspection were presented toMr. J. Sheppard and other members of his staff on November 30, 2005. The results of the review of Unresolved Item 2005004-01 were presented toMs. R. Savage, Senior Staff Specialist, and Mr. M. Ruvalcaba, Systems Engineering Supervisor, on December 21, 2005, during a telephonic exit.The results of the resident inspection were presented to Mr. G. Parkey and othermembers of licensee management on January 12, 2006.

During each exit meeting, the inspectors asked the licensee representatives whetherany materials examined during the inspection should be considered proprietary. No proprietary information was identified. Licensee management acknowledged the inspection findings. Other MeetingsMr. Claude Johnson, Branch Chief, Division of Reactor Safety, visited the site andtoured selected areas of the facility on October 13, 2005. Mr. Bruce Mallett, Regional Administrator, visited the site and toured selected areas ofthe facility on December 19, 2005. 40A7Licensee-Identified ViolationsThe following violations of very low significance (Green) were identified by the licenseeand are violations of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.* Technical Specification 3.3.2 Action 30 states, in part, that with irradiated fuel inthe spent fuel pool and with the number of operable engineered safety feature actuation channels less than the minimum channels operable requirement, fuel movement within the spent fuel pool or crane operation with loads over the spent fuel pool may proceed provided the fuel handling building exhaust air filtration system is in operation and discharging through at least one train of HEPA filters and charcoal absorbers (emergency mode). On October 22, 2005, during an outage work review, the licensee identified that Technical Specification 3.3.2, Action 30 was not performed as required. On October 19, 2005, during fuel movement, Train C fuel handling building HVAC engineered safety feature actuation relays became inoperable due to Electrical Bus E2C11 being de-energized for planned maintenance and the fuel handling building exhaust air filtration system was not placed in emergency mode. These relays require direct current power to automatically place the Fuel Handling building HVAC in the emergency mode and would not have actuated with Bus E2C11 de-energized.

The bus was de-energized for approximately three hours. This item was documented in the licensee's Corrective Action Program as Condition Report 05-13732. This finding is of very low safety significance due to the short duration of the condition and that the ability to manually align to the emergency mode was not compromised.* 10 CFR 50.54(q) requires a licensee maintain and follow an approvedemergency plan. Contrary to this, the licensee did not follow their emergency plan by removing ARM-8095, which was required by their emergency action level scheme. This was identified in the licensee's corrective action system asCondition Report 04-10494. This finding is of very low safety significance because it involved one of several indicators for a single emergency action level at the Notification of Unusual Event level.ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Bowman, Manager, Operations
W. Bullard, Manager, Health Physics
J. Conly, Licensing Engineer
T. Frawley, Manager, Performance Improvement
R. Gangluff, Manager, Chemistry
S. Head, Manager, Licensing
J. Heil, System Engineering
T. Jordan, Vice President, Engineering and Technical
J. Lovejoy, Manager, Instrumentation and Control Maintenance
N. Mayer, Supervisor, Outage and Projects
M. McBurnett, Manager, Quality and Licensing
A. McGallird, Supervisor, Nuclear Steam Supply System Engineering
A. Mikus, Supervisor, Communication and Public Affairs
W. Mookhoek, Senior Engineer, Quality and Licensing
J. Morris, Engineer, Licensing Staff
G. Parkey, Vice President, Generation
T. Powell, Manager, Systems Engineering
D. Rencurrel, Manager, Plant Engineering
R. Savage, Senior Staff Specialist
J. Sheppard, President and CEO
M. Smith, Supervisor, Quality
L. Spiess, Nondestructive Evaluation Technician, Level III
J. Stauber, Inservice Inspection Program Engineer
D. Stillwell, Supervisor, Configuration Control and Analysis
T. Walker, Manager, Quality
C. Younger, Inservice Inspection Engineer

AttachmentA-2

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and

Closed

05000499/2005005-01NCVInadvertent Letdown Relief Valve Opening(Section 1R20.1)05000499/2005005-02NCV Improper Fuel Handling (Section 1R20.2)

05000499/2005005-03 NCVInoperability of Essential Cooling Water 2Aand 2B Trains(Section 4OA3)

Closed

0500499/2005-004-00LERInoperability of Essential Cooling Water 2Aand 2B Trains (Section 4OA3)0500499/2005-004-01LERInoperability of Essential Cooling Water 2Aand 2B Trains (Section 4OA3)05000498;499/2005004-01 URIPotential for Submerged Cables(Section 4OA5.1)

AttachmentA-3

LIST OF DOCUMENTS REVIEWED

In addition to the documents identified in the inspection report, the following documents wereselected and reviewed by the inspectors to accomplish the objectives and scope of the