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{{#Wiki_filter:ENCLOSURE 1 PROPOSED TECHNICAL SPECIFICATIONS REVISIONS BROVNS FERRY NUCLEAR PLANT UNIT 2 (TVA BFN TS 250)8808120238 880803 PDR ADQCK 05000260 PDC 3.2 t BASES (Cont'd)~steam line isolation valve closure, fission product release is limited so that 10 CFR 100 guidelines are not exceeded for this accident.Reference Section 14.6.2 FSAR.An alarm with a nominal setpoint of 1.5 x normal full-power background is provided also.I Pressure instrumentation is provided to close the main steam.isolation valves in RUN Mode when the main steam line pressure drops below 825 psig.The HPCI high flow and temperature instrumentation are provided to detect a break in the HPCI steam piping.Tripping of, this instrumentation results in actuation of HPCI isolation valves.'ripping logic for the high flow is a 1-out-of-2 logic, and all sensors are required to be OPERABLE.High temperature in the vicinity of the HPCX equipment is sensed by four sets of four bimetallic temperature switches.The 16 temperature switches are arranged in two trip systems with eight temperature switches in each trip system.The HPCI trip settings of 90 psi for high flow and 200 F for high temperature are, such that core uncovery is prevented and fission product release is within limits.The RCIC high flow and temperature instrumentation are arranged the same as that for the HPCI.The trip setting of 450" H20 for high flow and 200'F for temperature are based on the same criteria as the HPCI.High temperature at the Reactor Mater Cleanup (RWCU)System floor drain in the space near the RWCU System or in the space near the pipe trench containing RWCU piping could indicate a break in the cleanup system.When high temperature occurs, the cleanup system is isolated.The instrumentation which initiates CSCS action is arranged in a dual bus system.As for other vital instrumentation arranged in this fashion, the specification preserves the effectiveness of the system even during periods when maintenance or testing is being performed.
{{#Wiki_filter:ENCLOSURE 1 PROPOSED TECHNICAL SPECIFICATIONS REVISIONS BROVNS FERRY NUCLEAR PLANT UNIT 2 (TVA BFN TS 250) 8808120238 880803 PDR ADQCK 05000260 PDC
An exception to this is when logic functional testing is being performed.
 
*$ll w\The control rod block functions are provided to prevent excessive control rod withdrawal so that MCPR does not decrease'to 1.07.The trip logic for this function is 1-out-of-n:
3.2   BASES steam (Cont'd)
'e.g., any trip on one of six APRMs, eight IRMs, or four SRMs will result in a rod block.The minimum instrument channel requirements assure sufficient
                                ~                                 t line isolation valve closure, fission product release is limited so that 10 CFR 100 guidelines are not exceeded for this accident. Reference Section 14.6.2   FSAR. An alarm with a nominal setpoint of 1.5 x normal full-power background is provided also.
.instrumentation,to assure.the.sing1e.failure criteria is met.The minimum instrument channel requirements for the RBM may be reduced by one for maintenance, testing, or calibration.
I Pressure instrumentation is provided to close the main steam. isolation valves in RUN Mode when the main steam line pressure drops below 825 psig.
This does not significantly increase the risk of an inadvertent control rod withdrawal, as the other channel is available, and the RBM is a backup system to the written sequence for withdrawal of control rods.BFN Unit 2 3.2/4.2-67 Hinimum No.Instrument Channels Operable Per Tri Ss 1 ll TABLE 3.2.A (Continued)
The HPCI high flow and temperature     instrumentation are provided to detect a break in the HPCI steam piping.     Tripping of,this instrumentation results in actuation of HPCI isolation valves. 'ripping logic for the high flow is a 1-out-of-2 logic, and all sensors are required to be OPERABLE.
PRIHARY CONTAINHENT AND REACTOR BUILDING ISOLATION INSTRUHENTATION Fn in R mark 2(3)2(12)2(14)Instrument Channel-High Radiation Hain Steam Li>>e Tunnel (6)Instrument Channel-Low Pressure Hain Steam Line (PIS-1-72>
High temperature   in the vicinity of the HPCX equipment is sensed by four sets of four bimetallic temperature switches. The 16 temperature switches are arranged in two trip systems with eight temperature switches in each trip system.
76 82, 86)Instrument Channel-High Flow Hain Steam Line (PUIS 1 13A Dy 25A D~36A-D, 50A-D)Instrument Channel-Hain Steam Line Tunnel Hi'gh Temperature Instrument Channel-Reactor Water Cleanup System Floor Drain High Temperature
The HPCI   trip settings of 90 psi for high flow   and 200 F   for high temperature are, such that core uncovery     is prevented and fission product release is within limits.
<3 times normal rated full power background
The RCIC high flow and temperature instrumentation are arranged the same as that for the HPCI. The trip setting of 450" H20 for high flow and 200'F for temperature are based on the same criteria as the HPCI.
>825 psig (4)<140/of rated steam flow<200'F 160-1800F C l.Above trip setting initiates Hain Steam Line Isolation l.Below trip setting initiates Hain Steam Line Isolation 1.Above trip setting initiates Hain Steam Line Isolation 1.Above trip setting initiates Hain Steam Line Isolation.
High temperature at the Reactor Mater Cleanup (RWCU) System floor drain in the space near the RWCU System or in the space near the pipe trench containing RWCU piping could indicate a break in the cleanup system.
l.Above trip setting initiates Isolation of Reactor Water Cleanup Line from Reactor and Reactor Water Return Line.Instrument Channel-Reactor Water Cleanup System Space High Temperature Instrument Channel-Reactor Water Cleanup System Pipe Trench Instrument Channel-Reactor Building Ventilation High Radiation-Reactor Zone 160-1800 F<150'<100 mr/hr or downscale 1.Same as above 1.Same as above 1.1 upscale or 2 downscale will a.Initiate SGTS b.Isolate reactor zone and re f uel in g fl oo r.c.Close atmosphere control system.BFN-Unit 2 TABLE 4.2.A (Cont'd)SURVEILLANCE REQUIREMENTS FOR PRIMARY CONTAINMENT AND REACTOR BUILDING ISOLATION INSTRUMENTATION
When high temperature occurs, the cleanup system is isolated.
~Func ion Group 6 Logic Group 8 (Initiating)
The instrumentation which initiates CSCS action is arranged in a dual bus system. As for other vital instrumentation arranged in this fashion, the specification preserves the effectiveness of the system even during periods when maintenance or testing is being performed. An exception to this is   when logic functional testing is being performed.
Logic Reactor Building Isolation (refueling floor)Logic Reactor Building Isolation (reactor zone)Logic SGTS Train A Logic SGTS Train B Logic SGTS Train C Logic Instrument Channel-Reactor Cleanup System Floor Drain High Temperature Instrument Channel-Reactor Cleanup System Space High Temperature Instrument Channel-Reactor Water Cleanup System Pipe Trench High Temperature Fun ional Test Once/operating cycle (18)Checked during channel functional test.No further test required.Once/6 months (18)Once/6 months (18)Once/6 months (19)Once/6 months (19)Once/6 months (19)Calibra ion Fr u nc N/A N/A (6)(6)N/A N/A N/A Once/operating cycle Once/operating cycle Once/operating cycle In rmn h k N/A N/A N/A N/A N/A N/A N/A N/A N/A N/A BFN-Unit 2 ENCLOSURE 2'ESCRIPTION AND JUSTIFICATION BROWNS FERRY NUCLEAR PLANT UNIT 2 Descri tion of Chan e This proposed technical specification change package will revise the Browns Ferry Nuclear Plant, Unit 2, Technical Specifications Table 3.2.A,"Primary Containment and Reactor-Building Isolation Instrumentation," Table 4.2.A,"Surveillance Requirements for Primary Containment and Reactor Building Isolation Instrumentation," and Section 3.2 Bases.Table 3.2'.A contains the operability requirements and trip level settings for instrumentation that initiates primary containment and reactor building isolation.
The control rod block functions are provided to prevent excessive control rod withdrawal so that MCPR does not decrease'to 1.07. The trip logic for this function is 1-out-of-n: 'e.g.,     any trip on one of six APRMs, eight IRMs, or four SRMs will result in     a rod block.
Table 4.2.A contains the complementary surveillance requirements.
The minimum instrument channel requirements     assure sufficient
The technical specification change will add surveillance requirements and trip level settings for new temperature switches being added near a pipe trench containing Reactor Mater Cleanup (RWCU)System piping.The added instrumentation is used to indicate leaks or pipe breaks and to automatically isolate the RWCU System.Section 3.2 is being changed to indicate that RWCU System pipe break detection instrumentation is available for the pipe trench containing the RWCU System piping.Refer to the attached technical specificatiens, pages 3.2/4.2-8,-43, and-67, for detailed changes.Reason for Chan e The technical specifications for the RWCU System are being revised because additional temperature switches are being added to that system for primary containment isolation purposes.The addition of four temperature switches and associated wiring provides leak detection and automatic RWCU System isolation for an RWCU pipe break in the pipe trench above the drywell equipment hatch and near the ceiling of the reactor building elevation 565.This technical specification change adds the function of these temperature switches to table 3.2.A.The minimum operability requirements and the trip level setting range is specified.
* $ ll w  \ . instrumentation,to assure. the.sing1e.failure criteria is met.         The minimum   instrument channel requirements for the RBM may be reduced by one for maintenance, testing, or calibration. This does not significantly increase the risk of an inadvertent control rod withdrawal, as the other channel is available, and the RBM is a backup system to the written sequence for withdrawal of control rods.
Also the action required for a condition with less than the minimum operability requirements being met is specified and a description of the automatic actions which occur when the trip level settings are surpassed is included.Table 4.2.A specifies the required surveillance frequencies for the new devices.Section 3.2 Bases is being changed on page 3.2/4.2-67 to correctly describe the plant, configuration after the temperature switches are added.Justification for Chan e The RWCU System does not have a safety function.It maintains high reactor-water purity to limit chemical and corrosive action, thereby limiting fouling and disposition on heat transfer surfaces.The RWCU System removes corrosion products to limit impurities available for activation by neutron flux and resultant radiation from deposition of irradiated corrosion products.The system also provides a means for removal of reactor water during heatup (reference UFSAR Section 4.9.1).The RMCU System provides Justification for Chan e (Cont'd)continuous purification of a portion of the recirculation flow.The system is normally in service.The RWCU System does contain primary containment isolation valves, which have a safety function of closing upon receipt of a low reactor pressure vessel (RPV)water level or detection of hi'gh temperatures in RWCU System spaces.The intent is to isolate the vessel incase of a RWCU line break outside primary containment or to prevent the release of radioactive material in the event of fueI damage following some other line break either inside or outside primary containment.
BFN                                         3.2/4.2-67 Unit  2
A review performed as part of the 10 CFR 50.49 Environmental Qualification program identified a length of RWCU piping which constituted a high energy line but did not have a high space temperature detection capability.
 
A postulated break in that pipe length could only be isolated due to low RPV water level or manual action.The resultant environmental conditions were considered too severe.A physical modification was recommended to lower the environmental consequences of the postulated line break.Four temperature switches are being added near the pipe trench containing the nonmonitored portion of the RWCU piping.The switches are to be wired in series with existing reactor water cleanup (RWCU)leak detection temperature switches.Including these devices in the technical specifications for the plant ensures that they are periodically tested in accordance with the plant surveillance program.The minimum number of instrument channels required to be operable per trip system will be the same as for the existing instrumentation and the action statement will be the same as for the existing instrumentation A trip level setting of less than or equal to 150'was established for the new temperature switches for equipment environmental qualification purposes..The added instrumentation will help protect safety-related equipment in the reactor building from damage caused by high temperatures resulting from a postulated RWCU System pipe break in the pipe trench.A setpoint of 150'was established from the analysis of the temperature transient that occurs in the reactor building following a break in the 4-inch RWCU system return line in the pipe trench.It has been concluded that if the setpoint were set at gl50 F, the environmental conditions in the areas affected by the pipe break would be within the environmental conditions to which safety-related equipment contained in that area have been qualified, UFSAR Section 7.3.4.7.14 requires that the high temperature" isolation setting be selected far enough above the anticipated normal area temperature to avoid spurious operation, but low enough to provide timely detection of a RWCU..System,.line break..The.maximum.normal.operational limit for the vicinity of the RWCU System pipetrench is 90'and the maximum abnormal temperature is 100'.A setpoint of less than or equal to 150'lies within the safety limits for the variable being monitored and will satisfy the applicable UFSAR requirements.
TABLE 3.2.A (Continued)
The field setpoint will be set high enough to avoid spurious isolations of the RWCU System but below the 150'limit being added to the technical specifications by this amendment.
PRIHARY CONTAINHENT AND REACTOR BUILDING ISOLATION INSTRUHENTATION Hinimum No.
4 ENCLOSURE 3 DETERMINATION OF NO SIGNIFICANT HAZARDS CONSIDERATION BROWNS FERRY NUCLEAR PLANT UNIT 2 Descri tion of Amendme t Re uest This proposed technical specification change package will revise the Browns Ferry Nuclear Plant, Unit 2, Technical Specifications, Table 3.2.A,"Primary Containment and Reactor Building Isolation Instrumentation," and Section 3.2'ases.Table 3.2.A contains the operability requirements and trip level settings for instrumentation that initiates primary containment and reactor building isolation.
Instrument Channels Operable Per Tri Ss 1    ll            Fn   in                                                                       R mark Instrument Channel           < 3  times normal rated                      l. Above  trip setting High Radiation Hain Steam     full  power background                            initiates    Hain Steam Line Li>>e Tunnel (6)                                                                   Isolation Instrument Channel-           > 825  psig (4)                              l. Below  trip setting Low Pressure Hain Steam                                                          initiates    Hain Steam Line                                                                             Line Isolation (PIS-1-72> 76   82, 86) 2(3)        Instrument Channel           <  140/ of rated steam flow                    1. Above  trip setting High Flow Hain Steam Line                                                         initiates Hain Steam (PUIS 1 13A Dy 25A D ~                                                           Line Isolation 36A-D, 50A-D) 2(12)      Instrument Channel           <  200'F                                      1. Above  trip setting Hain Steam Line Tunnel                                                           initiates    Hain Steam Hi'gh Temperature                                                                 Line Isolation.
Table 4.2.A contains the surveillance requirements for instrumentation of table 3.2.A.The technical specification change will add operability requirements and trip level settings for new temperature switches being added near the pipe trench containing Reactor Water Cleanup (RWCU)system piping.the added instrumentation is used to indicate leaks or pipe breaks and to automatically isolate the RWCU System.Section 3.2 is being changed to indicate that RWCU System pipe break detection instrumentation is available for the pipe trench containing the RWCU System piping.Refer to the attached technical specifications, pages 3.2/4.2-8,-43, and-67, for detailed changes.'as s or Pro osed No Si nificant Hazards Consideration Determinatio NRC has provided standards for determining whether a significant hazards consideration exists as stated in 10 CFR 50.92(c).A proposed amendment to an operating license involves no significant hazards considerations if operation of the facility in accordance with the proposed amendment would not (1)involve a significant increase in the probability or consequences of an accident previously evaluated, (2)create the possibility of a new or different kind of accident from an accident previously evaluated, or (3)involve a significant reduction in a margin of safety.~h The proposed amendment does not involve a significant increase in the probability or consequences of an accident previously evaluated because the amendment only adds operability surveillance requirements and trip level settings for new temperature detectors.
2(14)      Instrument Channel-           160 -  1800F                    C          l. Above  trip setting Reactor Water Cleanup                                                             initiates Isolation System Floor Drain                                                               of Reactor Water High Temperature                                                                 Cleanup Line from Reactor and Reactor Water Return Line.
The Final.Safety Analysis Report specifies that the trip level setting be high enough to avoid spurious operation but low enough to prevent exce'ssive loss of reactor coolant.Establishing the trip level setting range of 130'to 150'satisfies that requirement.
Instrument Channel-            160  1800 F                                 1. Same  as above Reactor Water Cleanup System Space High Temperature Instrument Channel            < 150'                                        1. Same  as above Reactor Water Cleanup System Pipe Trench Instrument Channel-           < 100   mr/hr or downscale                   1. 1 upscale or   2 downscale will Reactor Building                                                                  a. Initiate SGTS Ventilation High                                                                  b. Isolate reactor zone   and Radiation - Reactor Zone                                                              re fuel in g floo r.
Establishing the same operability.requirements ov..the new temperature switches.as are on the presently installed instrumentation prevents a significant increase in the probability or consequences of an accident previously evaluated.
: c. Close atmosphere control system.
The system isolates for several accident conditions and since it serves no safety function, increasing the number of devices with could cause system isolation will not affect safe operation of the plant.2.The proposed amendment does not create the possibility of a new or different kind of accident from an accident previously evaluated.
BFN-Unit 2
The new temperature switches are performing a similar function as other Bases for Pro osed No Si nificant azards Consideration Determination (Cont'd)instrumentation presently installed, and setting their operability and surveillance requirements the same as presently installed temperature switches prevents the creation of a new or different kind of accident.The increased monitoring and automatic isolation for the RWCU System will help prevent damage by high temperature to equipment required for safe'hutdown.The addition of operability and setpoint requirements for the new temperature switches ensures that the system's primary containment isolation safety function will be performed adequately.
 
The change does not affect safety functions of any equipment in ways not previously evaluated.
TABLE 4.2.A (Cont'd)
3.The proposed amendment does not involve a significant reduction in a margin of safety because the temperature switches being added are being specified to meet the same requirements as other RWCU System temperature switches which perform the same function and are'lready included in the technical specifications.
SURVEILLANCE REQUIREMENTS FOR PRIMARY CONTAINMENT AND REACTOR BUILDING ISOLATION INSTRUMENTATION
This ensures that the new temperature switches will not degrade existing features included in the technical ,specifications.
          ~Func ion                         Fun  ional Test              Calibra ion Fr  u nc          In  rmn h k Group 6 Logic                               Once/operating cycle          N/A                            N/A (18)
Also, the new temperature switches are being added to ensure that safety-related equipment'that is addressed in the technical specifications and that is required to mitigate a RWCU System pipe break will not be degraded by the environmental conditions which could result from a RWCU System pipe break in the pipe trench.Determination of Basis or Pro osed No Si nificant Hazards The primary containment isolation safety function is intended to provide timely protection against the onset and consequences of accidents involving the gross release of radioactive materials from the fuel and nuclear system process barrier and ensure automatic isolation of pipelines which penetrate the primary containment whenever monitored variables exceed preselected operational limits.The addition of operability and setpoint requirements for new temperature switches will ensure the safety function of the system will still be met.The increased automatic isolation will help ensure that the maximum environmental conditions for equipment required for safe shutdown are not exceeded.Since the application for amendment involves a proposed change that is encompassed by the criteria for which no significant hazards consideration exists, TVA has made a proposed determination that th'e application involves no significant hazards consideration.}}
Group 8 (Initiating)   Logic                Checked  during channel      N/A                            N/A functional test. No further test required.
Reactor Building Isolation                   Once/6 months (18)            (6)                            N/A (refueling floor) Logic Reactor Building Isolation                   Once/6 months (18)            (6)                            N/A (reactor zone) Logic SGTS Train A Logic                       Once/6 months (19)            N/A                            N/A SGTS Train B Logic                       Once/6 months (19)            N/A                            N/A SGTS  Train C Logic                       Once/6 months (19)            N/A                            N/A Instrument Channel-                                                       Once/operating cycle          N/A Reactor Cleanup System Floor Drain High Temperature Instrument Channel                                                       Once/operating cycle          N/A Reactor Cleanup System Space High Temperature Instrument Channel-                                                       Once/operating cycle          N/A Reactor Water Cleanup System Pipe Trench High Temperature BFN-Unit 2
 
ENCLOSURE AND JUSTIFICATION 2'ESCRIPTION BROWNS FERRY NUCLEAR PLANT UNIT 2 Descri tion of  Chan e This proposed technical specification change package will revise the Browns Ferry Nuclear Plant, Unit 2, Technical Specifications Table 3.2.A, "Primary Containment and Reactor-Building Isolation Instrumentation," Table 4.2.A, "Surveillance Requirements for Primary Containment and Reactor Building Isolation Instrumentation," and Section 3.2 Bases. Table 3.2'.A contains the operability requirements and trip level settings for instrumentation that initiates primary containment and reactor building isolation. Table 4.2.A contains the complementary surveillance requirements. The technical specification change will add surveillance requirements and trip level settings for new temperature switches being added near a pipe trench containing Reactor Mater Cleanup (RWCU) System piping. The added instrumentation is used to indicate leaks or pipe breaks and to automatically isolate the RWCU System. Section 3.2 is being changed to indicate that RWCU System pipe break detection instrumentation is available for the pipe trench containing the RWCU System piping. Refer to the attached technical specificatiens, pages 3.2/4.2-8, -43, and -67, for detailed changes.
Reason  for Chan e The  technical specifications for the RWCU System are being revised because additional temperature switches are being added to that system for primary containment isolation purposes. The addition of four temperature switches and associated wiring provides leak detection and automatic RWCU System isolation for an RWCU pipe break in the pipe trench above the drywell equipment hatch and near the ceiling of the reactor building elevation 565. This technical specification change adds the function of these temperature switches to table 3.2.A. The minimum operability requirements and the trip level setting range is specified. Also the action required for a condition with less than the minimum operability requirements being met is specified and a description of the automatic actions which occur when the trip level settings are surpassed is included. Table 4.2.A specifies the required surveillance frequencies for the new devices.
Section 3.2 Bases is being changed on page 3.2/4.2-67 to correctly describe the plant, configuration after the temperature switches are added.
Justification for Chan e The RWCU System does not have a safety function.          It maintains high reactor-water purity to limit chemical and corrosive action, thereby limiting fouling and disposition on heat transfer surfaces. The RWCU System removes corrosion products to limit impurities available for activation by neutron flux and resultant radiation from deposition of irradiated corrosion products. The system also provides a means for removal of reactor water during heatup (reference UFSAR Section 4.9.1). The RMCU System provides
 
Justification for   Chan e (Cont'd) continuous purification of a portion of the recirculation flow. The system is normally in service. The RWCU System does contain primary containment isolation valves, which have a safety function of closing upon receipt of a low reactor pressure vessel (RPV) water level or detection of hi'gh temperatures in RWCU System spaces. The intent is to isolate the vessel incase of a RWCU line break outside primary containment or to prevent the release of radioactive material in the event of fueI damage following some other line break either inside or outside primary containment.
A  review performed as part of the  10 CFR 50.49  Environmental Qualification program  identified  a length of RWCU piping  which  constituted a high energy line but did not have a high space temperature detection capability. A postulated break in that pipe length could only be isolated due to low RPV water level or manual action. The resultant environmental conditions were considered too severe. A physical modification was recommended to lower the environmental consequences of the postulated line break.
Four temperature switches are being added near the pipe trench containing the nonmonitored portion of the RWCU piping. The switches are to be wired in series with existing reactor water cleanup (RWCU) leak detection temperature switches. Including these devices in the technical specifications for the plant ensures that they are periodically tested in accordance with the plant surveillance program. The minimum number of instrument channels required to be operable per trip system will be the same as for the existing instrumentation and the action statement will be the same as for the existing instrumentation A  trip  level setting of less than or equal to 150' was established for the new temperature switches for equipment environmental qualification purposes.
. The added instrumentation    will help protect safety-related equipment in the reactor building from damage caused by high temperatures resulting from a postulated RWCU System pipe break in the pipe trench. A setpoint of 150' was  established from the analysis of the temperature transient that occurs in the reactor building following a break in the 4-inch RWCU system return line in the pipe trench. It has been concluded that       if the setpoint were set at gl50 F, the environmental conditions in the areas affected by the pipe break would be within the environmental conditions to which safety-related equipment contained in that area have been qualified, UFSAR Section 7.3.4.7.14 requires that the high temperature" isolation setting be selected far enough above the anticipated normal area temperature to avoid spurious operation, but low enough to provide timely detection of a RWCU
..System,.line break. .The. maximum. normal .operational limit for the vicinity of the RWCU System pipetrench is 90'      and the maximum abnormal temperature is 100'. A setpoint of less than or equal to 150' lies within the safety limits for the variable being monitored and will satisfy the applicable UFSAR requirements. The field setpoint will be set high enough to avoid spurious isolations of the RWCU System but below the 150' limit being added to the technical specifications by this amendment.
 
4 ENCLOSURE 3 DETERMINATION OF NO SIGNIFICANT HAZARDS CONSIDERATION BROWNS FERRY NUCLEAR PLANT UNIT 2 Descri tion of    Amendme  t Re  uest This proposed technical specification change package will revise the Browns Ferry Nuclear Plant, Unit 2, Technical Specifications, Table 3.2.A, "Primary Containment and Reactor Building Isolation Instrumentation," and Section 3.2 Table 3.2.A contains the operability requirements and trip level          'ases.
settings for instrumentation that initiates primary containment and reactor building isolation. Table 4.2.A contains the surveillance requirements for instrumentation of table 3.2.A. The technical specification change will add operability requirements and trip level settings for new temperature switches being added near the pipe trench containing Reactor Water Cleanup (RWCU) system piping. the added instrumentation is used to indicate leaks or pipe breaks and to automatically isolate the RWCU System. Section 3.2 is being changed to indicate that RWCU System pipe break detection instrumentation is available for the pipe trench containing the RWCU System piping. Refer to the attached technical specifications, pages 3.2/4.2-8, -43, and -67, for detailed changes.
nificant
                  'as s  or Pro osed No  Si          Hazards Consideration Determinatio NRC  has provided standards for determining whether a significant hazards consideration exists as stated in 10 CFR 50.92(c). A proposed amendment to an operating license involves no significant hazards considerations        if  operation of the facility in accordance with the proposed amendment would not (1) involve a significant increase in the probability or consequences of an accident previously evaluated, (2) create the possibility of a new or different kind of accident from an accident previously evaluated, or (3) involve a significant reduction in a margin of safety.
The proposed amendment does not involve a significant increase in the probability or consequences of an accident previously evaluated because the amendment only adds operability surveillance requirements and trip level settings for new temperature detectors. The Final. Safety Analysis Report specifies that the trip level setting be high enough to avoid spurious operation but low enough to prevent exce'ssive loss of reactor coolant. Establishing the   trip level setting  range  of 130' to 150' satisfies that requirement. Establishing the same  operability
  ~ h      .requirements ov..the new temperature switches .as are on the presently installed instrumentation prevents a significant increase in the probability or consequences of an accident previously evaluated. The system isolates for several accident conditions and since      it serves no safety function, increasing the number of devices with could cause system isolation will not affect safe operation of the plant.
: 2. The proposed amendment   does not create the  possibility of  a new  or different kind of accident    from an accident previously evaluated. The new temperature switches are performing    a similar function as other
 
Bases  for Pro osed No Si  nificant  azards Consideration Determination (Cont'd) instrumentation presently installed, and setting their operability and surveillance requirements the same as presently installed temperature switches prevents the creation of a new or different kind of accident.
The increased monitoring and automatic isolation for the RWCU System will help prevent damage by high temperature to equipment required for safe The addition of operability and setpoint requirements for the'hutdown.
new temperature switches ensures that the system's primary containment isolation safety function will be performed adequately. The change does not affect safety functions of any equipment in ways not previously evaluated.
: 3. The proposed amendment   does not involve a significant reduction in a margin of safety because the temperature switches being added are being specified to meet the same requirements as other RWCU System temperature switches which perform the same function and are'lready included in the technical specifications. This ensures that the new temperature switches will not degrade existing features included in the technical
    ,specifications. Also, the new temperature switches are being added to ensure that safety-related equipment'that is addressed in the technical specifications and that is required to mitigate a RWCU System pipe break will not be degraded by the environmental conditions which could result from a RWCU System pipe break in the pipe trench.
Determination of Basis    or Pro osed  No Si nificant Hazards The  primary containment isolation safety function is intended to provide timely protection against the onset and consequences of accidents involving the gross release of radioactive materials from the fuel and nuclear system process barrier and ensure automatic isolation of pipelines which penetrate the primary containment whenever monitored variables exceed preselected operational limits. The addition of operability and setpoint requirements for new temperature switches will ensure the safety function of the system will still be met. The increased automatic isolation will help ensure that the maximum environmental conditions for equipment required for safe shutdown are not exceeded.
Since the application for amendment involves a proposed change that is encompassed by the criteria for which no significant hazards consideration exists, TVA has made a proposed determination that th'e application involves no significant hazards consideration.}}

Latest revision as of 00:55, 22 October 2019

Proposed Tech Specs Re Surveillance Requirements for Primary Containment/Reactor Bldg Isolation Instrumentation
ML18033A306
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 08/03/1988
From:
TENNESSEE VALLEY AUTHORITY
To:
Shared Package
ML18033A305 List:
References
TAC-R00439, TAC-R439, NUDOCS 8808120238
Download: ML18033A306 (8)


Text

ENCLOSURE 1 PROPOSED TECHNICAL SPECIFICATIONS REVISIONS BROVNS FERRY NUCLEAR PLANT UNIT 2 (TVA BFN TS 250) 8808120238 880803 PDR ADQCK 05000260 PDC

3.2 BASES steam (Cont'd)

~ t line isolation valve closure, fission product release is limited so that 10 CFR 100 guidelines are not exceeded for this accident. Reference Section 14.6.2 FSAR. An alarm with a nominal setpoint of 1.5 x normal full-power background is provided also.

I Pressure instrumentation is provided to close the main steam. isolation valves in RUN Mode when the main steam line pressure drops below 825 psig.

The HPCI high flow and temperature instrumentation are provided to detect a break in the HPCI steam piping. Tripping of,this instrumentation results in actuation of HPCI isolation valves. 'ripping logic for the high flow is a 1-out-of-2 logic, and all sensors are required to be OPERABLE.

High temperature in the vicinity of the HPCX equipment is sensed by four sets of four bimetallic temperature switches. The 16 temperature switches are arranged in two trip systems with eight temperature switches in each trip system.

The HPCI trip settings of 90 psi for high flow and 200 F for high temperature are, such that core uncovery is prevented and fission product release is within limits.

The RCIC high flow and temperature instrumentation are arranged the same as that for the HPCI. The trip setting of 450" H20 for high flow and 200'F for temperature are based on the same criteria as the HPCI.

High temperature at the Reactor Mater Cleanup (RWCU) System floor drain in the space near the RWCU System or in the space near the pipe trench containing RWCU piping could indicate a break in the cleanup system.

When high temperature occurs, the cleanup system is isolated.

The instrumentation which initiates CSCS action is arranged in a dual bus system. As for other vital instrumentation arranged in this fashion, the specification preserves the effectiveness of the system even during periods when maintenance or testing is being performed. An exception to this is when logic functional testing is being performed.

The control rod block functions are provided to prevent excessive control rod withdrawal so that MCPR does not decrease'to 1.07. The trip logic for this function is 1-out-of-n: 'e.g., any trip on one of six APRMs, eight IRMs, or four SRMs will result in a rod block.

The minimum instrument channel requirements assure sufficient

  • $ ll w \ . instrumentation,to assure. the.sing1e.failure criteria is met. The minimum instrument channel requirements for the RBM may be reduced by one for maintenance, testing, or calibration. This does not significantly increase the risk of an inadvertent control rod withdrawal, as the other channel is available, and the RBM is a backup system to the written sequence for withdrawal of control rods.

BFN 3.2/4.2-67 Unit 2

TABLE 3.2.A (Continued)

PRIHARY CONTAINHENT AND REACTOR BUILDING ISOLATION INSTRUHENTATION Hinimum No.

Instrument Channels Operable Per Tri Ss 1 ll Fn in R mark Instrument Channel < 3 times normal rated l. Above trip setting High Radiation Hain Steam full power background initiates Hain Steam Line Li>>e Tunnel (6) Isolation Instrument Channel- > 825 psig (4) l. Below trip setting Low Pressure Hain Steam initiates Hain Steam Line Line Isolation (PIS-1-72> 76 82, 86) 2(3) Instrument Channel < 140/ of rated steam flow 1. Above trip setting High Flow Hain Steam Line initiates Hain Steam (PUIS 1 13A Dy 25A D ~ Line Isolation 36A-D, 50A-D) 2(12) Instrument Channel < 200'F 1. Above trip setting Hain Steam Line Tunnel initiates Hain Steam Hi'gh Temperature Line Isolation.

2(14) Instrument Channel- 160 - 1800F C l. Above trip setting Reactor Water Cleanup initiates Isolation System Floor Drain of Reactor Water High Temperature Cleanup Line from Reactor and Reactor Water Return Line.

Instrument Channel- 160 1800 F 1. Same as above Reactor Water Cleanup System Space High Temperature Instrument Channel < 150' 1. Same as above Reactor Water Cleanup System Pipe Trench Instrument Channel- < 100 mr/hr or downscale 1. 1 upscale or 2 downscale will Reactor Building a. Initiate SGTS Ventilation High b. Isolate reactor zone and Radiation - Reactor Zone re fuel in g floo r.

c. Close atmosphere control system.

BFN-Unit 2

TABLE 4.2.A (Cont'd)

SURVEILLANCE REQUIREMENTS FOR PRIMARY CONTAINMENT AND REACTOR BUILDING ISOLATION INSTRUMENTATION

~Func ion Fun ional Test Calibra ion Fr u nc In rmn h k Group 6 Logic Once/operating cycle N/A N/A (18)

Group 8 (Initiating) Logic Checked during channel N/A N/A functional test. No further test required.

Reactor Building Isolation Once/6 months (18) (6) N/A (refueling floor) Logic Reactor Building Isolation Once/6 months (18) (6) N/A (reactor zone) Logic SGTS Train A Logic Once/6 months (19) N/A N/A SGTS Train B Logic Once/6 months (19) N/A N/A SGTS Train C Logic Once/6 months (19) N/A N/A Instrument Channel- Once/operating cycle N/A Reactor Cleanup System Floor Drain High Temperature Instrument Channel Once/operating cycle N/A Reactor Cleanup System Space High Temperature Instrument Channel- Once/operating cycle N/A Reactor Water Cleanup System Pipe Trench High Temperature BFN-Unit 2

ENCLOSURE AND JUSTIFICATION 2'ESCRIPTION BROWNS FERRY NUCLEAR PLANT UNIT 2 Descri tion of Chan e This proposed technical specification change package will revise the Browns Ferry Nuclear Plant, Unit 2, Technical Specifications Table 3.2.A, "Primary Containment and Reactor-Building Isolation Instrumentation," Table 4.2.A, "Surveillance Requirements for Primary Containment and Reactor Building Isolation Instrumentation," and Section 3.2 Bases. Table 3.2'.A contains the operability requirements and trip level settings for instrumentation that initiates primary containment and reactor building isolation. Table 4.2.A contains the complementary surveillance requirements. The technical specification change will add surveillance requirements and trip level settings for new temperature switches being added near a pipe trench containing Reactor Mater Cleanup (RWCU) System piping. The added instrumentation is used to indicate leaks or pipe breaks and to automatically isolate the RWCU System. Section 3.2 is being changed to indicate that RWCU System pipe break detection instrumentation is available for the pipe trench containing the RWCU System piping. Refer to the attached technical specificatiens, pages 3.2/4.2-8, -43, and -67, for detailed changes.

Reason for Chan e The technical specifications for the RWCU System are being revised because additional temperature switches are being added to that system for primary containment isolation purposes. The addition of four temperature switches and associated wiring provides leak detection and automatic RWCU System isolation for an RWCU pipe break in the pipe trench above the drywell equipment hatch and near the ceiling of the reactor building elevation 565. This technical specification change adds the function of these temperature switches to table 3.2.A. The minimum operability requirements and the trip level setting range is specified. Also the action required for a condition with less than the minimum operability requirements being met is specified and a description of the automatic actions which occur when the trip level settings are surpassed is included. Table 4.2.A specifies the required surveillance frequencies for the new devices.

Section 3.2 Bases is being changed on page 3.2/4.2-67 to correctly describe the plant, configuration after the temperature switches are added.

Justification for Chan e The RWCU System does not have a safety function. It maintains high reactor-water purity to limit chemical and corrosive action, thereby limiting fouling and disposition on heat transfer surfaces. The RWCU System removes corrosion products to limit impurities available for activation by neutron flux and resultant radiation from deposition of irradiated corrosion products. The system also provides a means for removal of reactor water during heatup (reference UFSAR Section 4.9.1). The RMCU System provides

Justification for Chan e (Cont'd) continuous purification of a portion of the recirculation flow. The system is normally in service. The RWCU System does contain primary containment isolation valves, which have a safety function of closing upon receipt of a low reactor pressure vessel (RPV) water level or detection of hi'gh temperatures in RWCU System spaces. The intent is to isolate the vessel incase of a RWCU line break outside primary containment or to prevent the release of radioactive material in the event of fueI damage following some other line break either inside or outside primary containment.

A review performed as part of the 10 CFR 50.49 Environmental Qualification program identified a length of RWCU piping which constituted a high energy line but did not have a high space temperature detection capability. A postulated break in that pipe length could only be isolated due to low RPV water level or manual action. The resultant environmental conditions were considered too severe. A physical modification was recommended to lower the environmental consequences of the postulated line break.

Four temperature switches are being added near the pipe trench containing the nonmonitored portion of the RWCU piping. The switches are to be wired in series with existing reactor water cleanup (RWCU) leak detection temperature switches. Including these devices in the technical specifications for the plant ensures that they are periodically tested in accordance with the plant surveillance program. The minimum number of instrument channels required to be operable per trip system will be the same as for the existing instrumentation and the action statement will be the same as for the existing instrumentation A trip level setting of less than or equal to 150' was established for the new temperature switches for equipment environmental qualification purposes.

. The added instrumentation will help protect safety-related equipment in the reactor building from damage caused by high temperatures resulting from a postulated RWCU System pipe break in the pipe trench. A setpoint of 150' was established from the analysis of the temperature transient that occurs in the reactor building following a break in the 4-inch RWCU system return line in the pipe trench. It has been concluded that if the setpoint were set at gl50 F, the environmental conditions in the areas affected by the pipe break would be within the environmental conditions to which safety-related equipment contained in that area have been qualified, UFSAR Section 7.3.4.7.14 requires that the high temperature" isolation setting be selected far enough above the anticipated normal area temperature to avoid spurious operation, but low enough to provide timely detection of a RWCU

..System,.line break. .The. maximum. normal .operational limit for the vicinity of the RWCU System pipetrench is 90' and the maximum abnormal temperature is 100'. A setpoint of less than or equal to 150' lies within the safety limits for the variable being monitored and will satisfy the applicable UFSAR requirements. The field setpoint will be set high enough to avoid spurious isolations of the RWCU System but below the 150' limit being added to the technical specifications by this amendment.

4 ENCLOSURE 3 DETERMINATION OF NO SIGNIFICANT HAZARDS CONSIDERATION BROWNS FERRY NUCLEAR PLANT UNIT 2 Descri tion of Amendme t Re uest This proposed technical specification change package will revise the Browns Ferry Nuclear Plant, Unit 2, Technical Specifications, Table 3.2.A, "Primary Containment and Reactor Building Isolation Instrumentation," and Section 3.2 Table 3.2.A contains the operability requirements and trip level 'ases.

settings for instrumentation that initiates primary containment and reactor building isolation. Table 4.2.A contains the surveillance requirements for instrumentation of table 3.2.A. The technical specification change will add operability requirements and trip level settings for new temperature switches being added near the pipe trench containing Reactor Water Cleanup (RWCU) system piping. the added instrumentation is used to indicate leaks or pipe breaks and to automatically isolate the RWCU System. Section 3.2 is being changed to indicate that RWCU System pipe break detection instrumentation is available for the pipe trench containing the RWCU System piping. Refer to the attached technical specifications, pages 3.2/4.2-8, -43, and -67, for detailed changes.

nificant

'as s or Pro osed No Si Hazards Consideration Determinatio NRC has provided standards for determining whether a significant hazards consideration exists as stated in 10 CFR 50.92(c). A proposed amendment to an operating license involves no significant hazards considerations if operation of the facility in accordance with the proposed amendment would not (1) involve a significant increase in the probability or consequences of an accident previously evaluated, (2) create the possibility of a new or different kind of accident from an accident previously evaluated, or (3) involve a significant reduction in a margin of safety.

The proposed amendment does not involve a significant increase in the probability or consequences of an accident previously evaluated because the amendment only adds operability surveillance requirements and trip level settings for new temperature detectors. The Final. Safety Analysis Report specifies that the trip level setting be high enough to avoid spurious operation but low enough to prevent exce'ssive loss of reactor coolant. Establishing the trip level setting range of 130' to 150' satisfies that requirement. Establishing the same operability

~ h .requirements ov..the new temperature switches .as are on the presently installed instrumentation prevents a significant increase in the probability or consequences of an accident previously evaluated. The system isolates for several accident conditions and since it serves no safety function, increasing the number of devices with could cause system isolation will not affect safe operation of the plant.

2. The proposed amendment does not create the possibility of a new or different kind of accident from an accident previously evaluated. The new temperature switches are performing a similar function as other

Bases for Pro osed No Si nificant azards Consideration Determination (Cont'd) instrumentation presently installed, and setting their operability and surveillance requirements the same as presently installed temperature switches prevents the creation of a new or different kind of accident.

The increased monitoring and automatic isolation for the RWCU System will help prevent damage by high temperature to equipment required for safe The addition of operability and setpoint requirements for the'hutdown.

new temperature switches ensures that the system's primary containment isolation safety function will be performed adequately. The change does not affect safety functions of any equipment in ways not previously evaluated.

3. The proposed amendment does not involve a significant reduction in a margin of safety because the temperature switches being added are being specified to meet the same requirements as other RWCU System temperature switches which perform the same function and are'lready included in the technical specifications. This ensures that the new temperature switches will not degrade existing features included in the technical

,specifications. Also, the new temperature switches are being added to ensure that safety-related equipment'that is addressed in the technical specifications and that is required to mitigate a RWCU System pipe break will not be degraded by the environmental conditions which could result from a RWCU System pipe break in the pipe trench.

Determination of Basis or Pro osed No Si nificant Hazards The primary containment isolation safety function is intended to provide timely protection against the onset and consequences of accidents involving the gross release of radioactive materials from the fuel and nuclear system process barrier and ensure automatic isolation of pipelines which penetrate the primary containment whenever monitored variables exceed preselected operational limits. The addition of operability and setpoint requirements for new temperature switches will ensure the safety function of the system will still be met. The increased automatic isolation will help ensure that the maximum environmental conditions for equipment required for safe shutdown are not exceeded.

Since the application for amendment involves a proposed change that is encompassed by the criteria for which no significant hazards consideration exists, TVA has made a proposed determination that th'e application involves no significant hazards consideration.