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| {{Adams | | {{Adams |
| | number = ML090360191 | | | number = ML090120688 |
| | issue date = 02/02/2009 | | | issue date = 01/09/2009 |
| | title = Vogtle - Units 1 & 2, Additional Information Regarding NRC Supplemental Inspection Report 05000424-08-009 and 05000425-08-009 | | | title = IR 05000425-08-009 and 05000424-08-009; on 08/20/2008 - 12/11/2008; Vogtle Electric Generating Plant, Units 1 and 2; Supplemental Inspection IP 95001 for a Reported White Mitigating Systems Performance Index, Cooling Water System Performanc |
| | author name = Ajluni M J | | | author name = Shaeffer S |
| | author affiliation = Southern Nuclear Operating Co, Inc | | | author affiliation = NRC/RGN-II/DRP/RPB2 |
| | addressee name = Shaeffer S | | | addressee name = Tynan T |
| | addressee affiliation = NRC/NRR, NRC/RGN-II | | | addressee affiliation = Southern Nuclear Operating Co, Inc |
| | docket = 05000424, 05000425 | | | docket = 05000424, 05000425 |
| | license number = | | | license number = NPF-068, NPF-081 |
| | contact person = | | | contact person = |
| | case reference number = IR-08-009, NL-09-0124 | | | document report number = IR-08-009 |
| | document type = Letter, Licensee Response to Notice of Violation | | | document type = Inspection Report, Letter |
| | page count = 27 | | | page count = 11 |
| }} | | }} |
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| =Text= | | =Text= |
| {{#Wiki_filter:Southern Nuclear Operating Company,lnc. | | {{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION |
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| 40 Inverness Center Parkway Post Office Box 1295 Birmingham, Alabama 35201-1295 Tel 205.9925000 February 2, 2009 SOUTHERN A. COMPANY Energy to Serve YtJUr WorldS!' Docket Nos.: 50-424 50-425 NL-09-0124 Mr. Scott Shaeffer U. S. NRC Region II Sam Nunn Atlanta Federal Center, 23 T85 61 Forsyth Street, SW Atlanta, GA 30303-8931 Vogtle Electric Generating Plant -Units 1 and 2 Additional Information Regarding NRC Supplemental Inspection Report 05000424/2008009 and 05000425/2008009
| | ==REGION II== |
| | ary 9, 2009 |
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| ==Dear S Go t-t On December 11,== | | ==SUBJECT:== |
| 2008, the U.S. Nuclear Regulatory Commission (NRC) completed a supplemental inspection in accordance with Inspection Procedure 95001. The inspection results were transmitted to Southern Nuclear Company (SNC) on January 9, 2009. As documented in the referenced inspection results, the inspector opened unresolved item (URI) 05000424/2008009-01, Technical Specification Operability of the NSCW System with the Cooling Tower Return Valves in Manual Control. In order to clarify the licensing basis for the NSCW, SNC has made changes to section 9.2.1.2.3 of VEGP Updated Final Safety Analysis Report (UFSAR) in accordance with the requirements of 10 CFR 50.59 and changes to Technical Specification Bases 3.7.9 in accordance with the requirements of the Technical Specification (TS) Bases Control Program as documented in Licensing Document Change Request (LDCR) 2008039. In addition, SNC developed a position paper regarding the operability of the NSCW system with the cooling tower return valves in manual control. LDCR 2008039 and NSCW Spray Valve Operability Position Paper are provided for your information as Enclosures 1 and 2, respectively.
| | VOGTLE ELECTRIC GENERATING PLANT - NRC SUPPLEMENTAL INSPECTION REPORT 05000424/2008009 AND 05000425/2008009 |
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| This letter contains no NRC commitments.
| | ==Dear Mr. Tynan:== |
| | On December 11, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed a supplemental inspection in accordance with Inspection Procedure 95001, Inspection for One or Two White Inputs in a Strategic Performance Area, at your Vogtle Electric Generating Plant, Units 1 and 2. The purpose of the inspection was to examine the circumstances surrounding the White performance indicators reported during the fourth quarter of 2007 for the Unit 1 and Unit 2 Cooling Water Mitigating Systems Performance Index. The enclosed inspection report documents the inspection results, which were discussed on December 11, 2008, with Mr. Todd Youngblood and other members of your staff. |
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| If you have any questions, please advise.
| | The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license. |
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| Sincerely,M. J. Ajluni Manager, Nuclear Licensing U. S. Nuclear Regulatory Commission NL-09-0124 Page 2 MJAIT AH/daj
| | The inspector reviewed selected procedures and records and interviewed personnel. Based on the results of this inspection, no findings of significance were identified. |
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| ===Enclosures:===
| | In accordance with the Code of Federal Regulations 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosures, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). |
| 1. LDCR # 2008039 2. NSCW Spray Valve Operability Position Paper Southern Nuclear Operating Company Mr. J. T. Gasser, Executive Vice President Mr. T. E. Tynan. Vice President
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| -Vogtle Mr. D. H. Jones, Vice President
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| -Engineering RType: CVC7000 U. S. Nuclear Regulatorv Commission Mr. L. A. Reyes, Regional Administrator Mr. R. E. Martin, NRR Project Manager -Vogtle Mr. E. D. Morris, Acting Senior Resident Inspector
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| -Vogtle Document Control Desk Vogtle Electric Generating Plant -Units 1 and Additional Information Regarding NRC Supplemental Inspection 05000424/2008009 and Enclosure 1 LDCR # 2008039 Southern Nuclear Operating Company ..........
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| A Nuclear L1censfng Document Change . COMMN'I Management Request Page 1 of2 ......Procedure Plant: FarlevD Hatch 0 VogUe !81 Unit No. 1 ] 20 Shared IZI ActiVity/Document NIA LDCR No.: 2008039 (AotJDoc.
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| InitiatInG the Change) Version No.: 1.0 Activity/Document Version No.: NlA Title: NSCW Tower Return Valve Operatlo......---...... , ft Preparer:
| | Sincerely, |
| Mark Hickox '-.L\ 1 .IJ..
| | /RA/ |
| -Print Reviewer: | | Scott M. Shaeffer, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos.: 50-424, 50-425 License Nos.: NPF-68 and NPF-81 |
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| LDO:
| | ===Enclosure:=== |
| ... 0010, '3/1 B loe nt 1 Reviewer: /. 1\JfA. Date: tJ/A (As Needed) Print (:'
| | Inspection Report 05000424/2008009 and 05000425/2008009 w/Attachment: Supplemental Information |
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| Site Reviewer:
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| _ Date: 81'sl DB Prinl SlgnalUre Impacted Licensing Documents:
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| VEGP FSAR, Revision 15-updated 7/31/08, section 9.2.1 and VEGP Technical Specification Bases (JUly 14, 2008) section 3.7.9. Change: Added a paragraph describing the acceptability of manual operation of the NSCW Tower Return valves when administratively controlled to FSAR paragraph 9.2.1.2.3 and Technical Specification Bases 3.7.9. Justification:
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| FSAR Table 9.2.1-2, Failure Modes and Effects Analysis describes manual operator action to position the tower return valves as a credited safety function.
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| Since, manual operator action to position these valves is credited in the FSAR and analysis has shown that there is sufficient time available for the operator to recognize and position the valves to the desired alignment under administrative control, clarifying paragraphs outlining this eapabHlly were added to FSAR section 9.2.1 and TS Bases 3.7.9. Yes 181 No 0 PRB Review Required (An LDCR that Is limited In scope to that descrlbed Question 8 (FSAR only) of the Applicability Detennlnatlon Checklist does not reqUire PRB review) If No: AI/A-/ AI/A-Date: A//"f-Print Licensing Mgr. Signatunl If Yes: If'/-Date: 8)/5'/08 .-f PRB Meeting No. VP*Plant Approval:
| | REGION II== |
| '/tll1 -r Y,., I/Ir tV I 6m Date:
| | Docket Nos.: 50-424, 50-425 License Nos.: NPF-68, NPF-81 Report Nos.: 05000424/2008009 and 05000425/2008009 Licensee: Southern Nuclear Operating Company, Inc. |
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| 1 Prinl SignalG NMP-AD-Q09-F01. | | Facility: Vogtle Electric Generating Plant, Units 1 and 2 Location: Waynesboro, GA 30830 Dates: August 20 - December 11, 2008 Inspector: G. McCoy, Senior Resident Inspector Approved by: Scott M. Shaeffer, Chief Reactor Projects Branch 2 Division of Reactor Projects Enclosure |
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| Version 3.0 NMP-AD-009 Southern Nuclear Operating Company SOU1IIIIINA .......Nuclear Management Procedure Licensing Document Change Request Page 2 of2 Ves 0 No Implementation Pending-5ee Comments (e.g. NRC prior approval required, ,i rl DCP/MDC/RER completion required)
| | =SUMMARY OF FINDINGS= |
| Comments:
| | IR 05000424/2008-009, 05000425/2008-009; August 20, 2008 - December 11, 2008; Vogtle |
| _ 'I I I I i . II I fl NMP-AD-009-F01, Version NMP-AO-o09 Southern Nuclear Operating Company Nuclear Management Applicability Determination Page 1 of4Procedure Plant: Farley [ ] Hatch []
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| Unit No. H] 20 Activity/Document No.: NfA AD Version No.: 1.0 (AcUDoc. Inltl.tlna the Chlnae} Activity/Document Version No.: NfA Title: NSCW Tower Return Valve Operation Sectlon I -Activity Summary Preparer:
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| Mark HickoK Prinl_ Reviewer:
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| _ Date: '6 I l 0.1,",,0. Sin '&(S Description of Change: Added a paragraph describing the acceptability of manual operation of [he NSCW retum valves when administratively controlled 10 FSAR paragraph 9.2.1.2.3 and Technical Specification Bases 3.7.9. FSAR Table 9.2.1-2. Failure Modes and Effects Analysis describes manual operator action to position the lower return valves as a credited safety function.
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| Since. manual operalor actIon 10 position lhese valves is crediled in the FSAR and analysis has shown thallhere is sufficient lime available for the operator to recognize and position the valves to the desired alignment under administrative control. clarifying paragraphs ouUining this capability were added to FSAR section 9.2.1 and TS Bases 3.7.9. Section II -Applicable RegUlation Determination 1.0 Ves l8J Does the aetlvlty involve a change to the (Identify which): a. 0 b. 0 c. 0 d. 0 Operating License/Renewed Operating TechnIcal Environmental Protection Dry Storage Certificate of If the answerto question (1.a), (1.b), or (1.c) is yes, refer this activity to SNC Nuclear Licensing for preparalionlreview of a 10 CFR 50.92 evaluation.
| | Electric Generating Plant, Units 1 and 2; Supplemental Inspection IP 95001 for a reported White Mitigating Systems Performance Index, Cooling Water System Performance Indicator. |
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| If Ihe answer to question (1.d) Is yes, refer this activity to SNC Nuclear Ucenslng 10 request the dry storage cerl1f1cate holder to revise Ihelr certificate of ComplIance. 0 Ves No Using the guidance provided In Attachment 1 to NMP-AD*008, does the activity involve an Impact or change to the Quality Assurance Topical Report (either direct or IndIrect)?
| | This inspection was conducted by a senior resident inspector. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006. |
| If the answer to queslion (2) is yes, refer this activity to SNC Quality Assurance for preparation/review of a 10 CFR 50.54(8) evaluation.
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| NMP-AD-008*F01.
| | ===Cornerstone: Mitigating Systems=== |
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| Version NMp*AD-008 I \i -1'" I. .! :.; i "i '1 H i .j J I I *1 I B :J :il <I f <l I @ n',) " ., 1 OJ 1 j I I i i! .1 '1 i ;1 , i , J '1 I I ;i I ,!
| | The U.S Nuclear Regulatory Commission (NRC) performed this supplemental inspection in accordance with Inspection Procedure 95001 to assess the licensees evaluation associated with a White Mitigating Systems Performance Indicator, Cooling Water Systems Performance Indicator reported during the fourth quarter of 2007 and later retracted during the first quarter of 2008. The inspector determined that the decision to retract the White performance indicator was supported by the guidance of NEI 99-02, Regulatory Assessment Performance Indicator Guideline. |
| Southern Nuclear Operating Company SOUIIIIIINA.
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| ClDMNNY a.w........Nuclear Management Procedure Applicability Determination Page 2 of4 0 Ves [8J No Using the guidance provided In Attachment 2 to NMP*AD*008.
| | ===NRC-Identified and Self-Revealing Findings=== |
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| does the activity Involve an Impact or change to the Security Plan, Contingency Plan. or the Security Training and Qualification Plan (either direct or Indirect)?
| | No significance of findings were identified. |
| If the answer to question (3) is yes, refer this activity to SNC Security for preparation/review of a 10 CFR 50.54(p) evaluation.
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| 4. 0 Ves [8J No Using the guidance provided in Attachment 3 to NMP*AD-008.
| | ===Licensee-Identified Violations=== |
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| does the activity Involve an Impact or change to the Emergency Plan (either direct or Indirect)?
| | None. |
| If the answer to question (4) is yes, refer this activity to SNC Emergency Planning-for preparation/review of a 10 CFR 50.54(q) evaluation.
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| 5. 0 Ves 181 No Does the activity Involve a change to the Inservlce Inspection Program or to the Inservice Testing Program. Including relief requests?
| | =REPORT DETAILS= |
| If the answer to question (5) is yes. refer this activity to SNC Materials and Inspection Services for preparationlreview of a 10 CFR 50.55a evaluation.
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| S. 0 Ves No Using the guidance provided In Attachment 4 to NMP-AD-008. | | ==INSPECTION SCOPE== |
| | The U.S. Nuclear Regulatory Commission (NRC) performed this supplemental inspection to assess the licensees evaluation of a White Mitigating System Performance Index (MSPI), |
| | Cooling Water Systems Performance Indicator (PI) for Unit 1 and Unit 2. The White PI was reported for Unit 1 for the fourth quarter 2007 and for Unit 2 for the third quarter 2007. Both PIs were re-reported Green during the first quarter 2008. This was based on the licensee re-evaluating their NSCW unavailability which caused the PIs to initially be reported as White. This inspection reviewed this re-evaluation which lead the licensee to revise the previously reported White PIs for both units. |
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| does the j., activity Involve a change to the Fire Protection Program and/or Implementing Procedures?
| | Background On October 12, 2007, operators took manual control of the Unit 1 train A Nuclear Service Cooling Water (NSCW) tower return valves to calibrate temperature instrument 1T1668. The Shift Supervisor questioned the operability of the 1A NSCW system while the temperature instrument was being calibrated. This issue was documented in condition report (CR)2007110639. In January 2008, when the licensee was required to submit PI data for the fourth quarter 2007, the licensee conservatively determined that the train A NSCW system was inoperable without the knowledge of the operators and counted the duration the temperature instrument was being calibrated as unavailability time against the Unit 1 MSPI, Cooling Water Systems PI. The licensee reviewed the control room logs and identified that a similar condition had occurred in August 2007 on Unit 2 train B NSCW system. The licensee also counted this duration as unavailability against the Unit 2 MSPI, Cooling Water Systems PI. In conjunction with previous reported unavailability time in the NSCW system, these additional conditions caused the Unit 1 MSPI, Cooling Water Systems PI to cross the Green to White threshold in the fourth quarter of 2007. The Unit 2 MSPI, Cooling Water Systems PI was also reported as White for the fourth quarter of 2007 and retroactively for the third quarter of 2007. |
| If the answer to questIon (6) is yes, refer the activity to SNC Fire Protection for preparation/review of a fire protection evaluation in accordance with the applicable Operating License condition. 0 Ves t8I No Using the guidance provided In Attachment 5 to NMP-AD-008, does the actiVity Involve a managerial or administrative procedure change? If the answer to question (7) is yes, the change is subject to the controls of 10 CFR 50, Appendix B. Process the change in accordance wlth applicable procedures. 0 Ves 18I No Using the guidance provided In Attachment S to NMP-AD-008, does the activity Involve a change to the Updated FSARslTSAR or 10 CFR 72.212 Report (including documents Incorporated by reference)
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| that is excluded from the requirements to perform a 10 CFR 50.59 or 10 CFR 72.48 review In accordance with NEI98-07, Revision 1 or NEl98-03, Revision 1 such as (Identify which): Note: The scope of this question Is limited to the Updated FSARslTSAR and 10 CFR 72.212 Report. It does not apply to other licensing documents. Editorial Changes, Clarifications to Improve reader understanding, Correction of inconsistencies within the Updated FSARslTSAR or 10 CFR 72.212 Report which are clearly discernible (e.g., between sections), Designation of Information as historical, NMP-AD-008-F01, Version NMP-AD-008 Southern Nuclear Operating Company _A ClaMMNY 6...,____ Nuclear Management Procedure Applicability Determ Ination Page 3 of 4 Minor corrections to drawings (e.g., correcting mislabeled valves), or Similar changes that do not change the meaning or substance of Information presented (e.g., reformatting or removing detail). Incorporation of Information submitted to and approved by the NRC. If the answer to question (8) is yes, a 10CFR 50.59 screen is not required for this aspect of the activity. | |
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| If no Updated FSARslTSAR or 10 CFR 72.212 Report change is involved, this question is not applicable. D Ves 181 No Using the guidance provided In Attachment 7 to NMP-AD-008, does the activity Involve (Identify which): A temporary plant alteration to support maintenance (e.g., jumpering terminals, lifting leads, lead shielding, HVAC, scaffolding, and blocking doors) which: will be restored to the as-designed condition prior to startup if shutdown, or will be restored to the as-deslgned condition within 90 days if at power (Modes 1 and 2)? A temporary plant alteration that supports the Installation and post-modification testing of an approved plant change which: will be restored to the as-designed condition prior to startup If shutdown, or will be restored to the as-designed condition within 90 days If at power (Modes 1 and 2)1 If the answer to question (9) Is yes, refer the activity to appropriate personnel for preparation/review of an assessment of the risk associated with this temporary plant alteration and manage In accordance with 10 CFR 50.65(aX4).
| | During the first quarter of 2008, the licensee completed a detailed review of these two conditions and determined that in both cases the NSCW Ultimate Heat Sink and the Cooling Water design functions could be met during temperature instrument calibration. The licensee determined the NSCW system remained available in accordance with the guidance of NEI 99-02. Based on this determination, the licensee removed the previously reported unavailability from the PI data for both Unit 1 and Unit 2, reported the PIs as Green for the first quarter of 2008 and retroactively changed the previously reported White PIs to Green starting third quarter of 2007. The NRC has endorsed the guidance of NEI 99-02 for the determination of system availability for PI data reporting purposes. In accordance with this guideline, operator actions can be credited towards system availability if the function can be promptly restored by an operator in the control room, restoration actions are uncomplicated, contained in a written procedure, not require diagnosis or repair, and must be capable of being restored in time to satisfy Probability Risk Assessment (PRA) success criteria. The inspector determined that while the cooling tower was bypassed, plant operating procedure 1350-1, Nuclear Service Cooling Water System Operating Procedure, required the monitoring of NSCW return temperature in the control room and provided actions to be taken if NSCW return temperature limits were exceeded. |
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| 10. D Ves I8l No Does the activity Involve a change to a regulatory commitment not covered by another regulation based change process? If the answer to question (10) is yes, perfonn an evaluation consistent with NEI 99-04. 11.0 Ves 181 No Does the activity Involve a change, test, or experIment associated with the Independent Spent Fuel Storage Installation (ISFSI) or spent fuel cask design? If the answer to question (11) is yes, perform a 10 CFR 72.48 screen based on the following:
| | The operation of a single switch on the control board in main control room would return cooling to the NSCW cooling loop, even if temperature instrument 1T1668 was out of service. The inspectors determined that the NSCW system could be considered available for MSPI reporting purposes and that the licensee properly reported the PI as Green for the third and fourth quarters of 2007. The inspector noted that the licensee has modified the procedures for taking manual control of the NSCW tower return valves to make this plant condition more evident to the operators by requiring a caution tag be placed on the NSCW cooling tower return valve control switch anytime it is out of the automatic position. |
| Has the proposed actiVity been evaluated by the Certificate of Compliance (CoC) holder? D Evaluate the proposed activity against the ISFSI as described In the 10 CFR 72.212 Report. D Evaluate the proposed actiVity against the ISFSI as described in the applicable dry storage FSARITSAR and the 10 CFR 72.212 Report. NMP-AD-008-F01, Version 3.0 Southern Nuclear Operating Company ........A COMMNY....,..Nuclear Management Procedure Applicability Determination Page 40f4 12. Ves 0 No Using the guIdance provIded in Attachment 8 to NMP-AD-008, does the activity Involve a change addressed by other plant specific programs which are different from those already Identified above and are excluded from the scope of 10 CFR 50.59 and 10 CFR 72.48, and are controlled by (Identify which): o Another regulation (e.g** 10 CFRs 20, 26, 50.12, 50.46, and 72.7), (If marked Identify):, _ o Operating Llcense/Renewed Operating License condition (e.g., maximum power level), or Technical Specifications or Environmental Protection Plan (e.g., the ODCM, Technical Specifications Bases Control Program, COLR, etc.)? If the answer to question (12) is yes, perform the activity in accordance with the applicable requirement.
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| 13. Using the guidance provided in Attachment 9 to NMP-AD-008, does the activity involve a matter which could result In adverse environmental Impact (either direct or Indirect)?
| | In addition, the inspector reviewed the associated condition reports, reviewed the cause determinations performed, and reviewed the operability determinations. Inspector also interviewed operations and licensing personnel to understand the basis for their decisions. |
| Check (a) or (b) a. 181 No The nature of this change is such that it will not produce conditions which could result In significant adverse environmental Impact. b. 0 Possibly (Explain
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| _ If questIon (13.b) is checked. refer this activity to SNC Environmental Affairs for preparation/review of an Environmental Evaluation.
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| 14. Ves 0 No Are there any aspects of the activity not controlled by the processes described in items 1 -13 above? If the answer to question (14) is yes, perform a 10 CFR 50.59 screen. Question (14) must be answered yes if items 1 -13 are all answered no. Question (14) must also be answered yes for all Design Change Packages (DCPs). Minor Design Changes (MDCs), and Temporary Modifications (TMs) outside the scope of question (9). Section III -NRC Approval/
| | During this inspection, the inspector questioned the licensees determination that the NSCW system was operable with the NSCW cooling tower return valves in manual control. The inspector noted that the NSCW system is a support system for the Ultimate Heat Sink, and without the proper operation of the NSCW cooling tower return valves the Ultimate Heat Sink would not be able to accomplish its design function during a design basis accident. The inspector also noted there is no provision in the technical specifications, the USFAR nor the safety evaluations written by the NRC for the NSCW system which evaluates the operation of the system with manual control of the tower return valves without declaring the NSCW system inoperable and entering the TS action Limiting Condition for Operability (LCO). This issue is identified as an unresolved item (URI) 05000424/2008009-01, Technical Specification Operability Of The NSCW System With The Cooling Tower Return Valves In Manual Control. |
| LDCR Determination 15. 0 Ves 181 No Is NRC approval reqUired prior to Implementation of this activity?
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| If the answer to question (15) is yes. forward the activity to SNC Nuclear Licensing for preparation/review of a submittal to NRC. 16.181 Ves 0 No Does this activity require a change to a licensing document{s)?
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| If the answer to question (16) is yes. process the change in accordance with NMP-AD-009.
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| LOCR Number (if applicable):
| | EVALUATION OF INSPECTION REQUIREMENTS 02.01 Problem Identification a. |
| _ NMP-AO-o08-F01, Version NMP-AO-o08 Southern Nuclear ODeratlna ComDany sountIR.A Nuclear 10 CFR 50.59 cOMNHY Management Screening/Evaluation Page 1 of7 ............
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| ..,. Procedure Plant: FarlevD Hatch [J Voatle l5<I Unit No. 10 20 Shared rg] ActivltylDocument No.: LDeR 2008039 10 CFR 50.59 Version No.: 1.0 (AcIJDoc.
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| initiating the Chanae) Activity/Document Version No.: 1.0 TItle: NSCW Tower Return Valve Operation A. Activity Summary \1 Preparer:
| | Determination of who (i.e., licensee, self-revealing, or NRC) identified the issue and under what conditions. |
| R.-: Nuclear Hazards Reviewer: (If required)
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| Mark Hickox ' Dale: -Print Signature J .J1 ,.\ / j ,I Dale: B-/&-ot!:, Print 51g11at 8 P' Nuclear Regulalory"-I \ , Reviewer:
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| Dale: (If required)
| | The potential unavailability of the NSCW system was identified by the licensee when system operability was questioned while temperature instrument 1T1668 was being calibrated. |
| (.. Print' 51 a re Reviewer/Approver:
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| tJth I tJ/A-Date: ,J!A 0 (As Needed) Print Signature PRB Approval or eL(J(JK-If'f ¢s/oK Meeting No.: Date: , rinl Signature or PRB Meeting * PRB Meeling No. (If applicable and not idenlified above): Descriplion:
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| The proposed change is a Licensee Document Change Requesl (LDCR) to clarify the operation of the NSCW lower relurn valves (HV-1668A18 and HV-1669NB) | |
| as described . in FSAR section 9.2.1 and Technical Specification Bases 3.7.9. The NSCW tower relum valves provide a f10wpath 10 direct NSCW return waler 10 the spray header where sensible heat is transferred to the oulside environmenllhrough forced draft evaporatlve cooling or directly to lhe basin to prevent icing when outside air temperatures are low. When no NSCW pumps are In Operation.
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| the lower return valves are dosed 10 keep the return header full of water 10 prevenUminimize the affects of water hammer. When a NSCW pump is In operation and the tower return valve handswitch is In "Auto", lhe posllioning of the NSCW lower return valves is conlrolled based upon NSCW return header lemperature.
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| When the relum header temperature is low <<75 degrees) the bypass valve (HV1668B1HV1669S)
| | Determination of how long the issue existed, and prior opportunities for identification. |
| is open and the spray valve (HV1668A1HV1669A)
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| Is closed. When lhe return header lemperature is high (>75 degrees) the spray valve (HV1668A1HV1669A)
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| is open and lhe bypass valve (HV1668B/HV1669B)
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| is closed. The tower relum valves can also be positioned manually using lhe control room handswitch.
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| The handswitch (HS-1668A1HS-1669A)
| | This issue existed on October 12, 2007, while temperature instrument 1T1668 was being calibrated. A previous case was identified in August 2007 when 2T1669 was being calibrated. |
| has three positions which are maintained and controls operation of both tower relum valves. The handswitch can be placed In "Auto* and the lower return valve response would be as described above. The handswitch can also be selected to the "Open Normal* position.
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| In this position.
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| the return water would be direcled (spray valve open and bypass valve closed) to the spray header and would remain in this position irrespective of relum water temperature. | | Determination of the plant-specific risk consequences (as applicable) and compliance concerns associated with the issue. |
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| Similarly.
| | Because of the compensatory actions (monitoring temperature, etc) taken during temperature instrument calibration, the licensee determined that the risk consequences was minimal. No compliance concerns were identified because the licensee properly reported the PI data. |
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| if the NMP-AD-010-F01.
| | 02.02 Root Cause and Extent of Condition Evaluation Because the NSCW system was determined to be available while the temperature instrument was being calibrated, no cause evaluation was performed by the licensee. |
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| Version 3.0 NMP-AD-010 j,1 ii :.1 :1 0'1 ., I I i ! oj *1 ,1?c -A )l j " 'I .'1 i i i ! l ! : . , 0, ! R !1 0; I i ; I , Ii t c (I :1 oj i j !! 1 1 1 I , I I I Southern Nuclear Operating Company SOUIIIIRIIA ClOMMNY ...............
| | The licensee determined that manual operation of NSCW tower return valves during temperature instrument calibration was consistent with other manual actions for this system where sufficient time and methods were provided to ensure the safety function of the system was maintained. |
| ,-.fI" Nuclear Management Procedure 10 CFR 50.59 Screening/Evaluation Page 2 of1 handswitch is selected to the "Open Bypass* position (bypass valve open and spray valve closed), the return water would be routed directly to the basin. The valves would remain in this position irrespective of return water temperature.
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| Should a loss of offsite power occur with the handswltch in *Open Normal* or *Open Bypass*. the tower return valves would close when their respective bus is loaded back onto the Emergency Diesel Generator (EDG). Once any of the NSCW pumps are sequenced back on. either the spray or bypass valve would open to some mid-position.
| | 02.03 Corrective Actions No corrective actions were required or performed by the licensee because the NSCW system was determined to be available. However, the licensee modified plant procedures for taking manual control of the NSCW tower return valves to make this plant condition more evident to the operators by requiring a tag be placed on the NSCW cooling tower return valve control switch anytime it was out of the automatic position. |
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| dependent upon the selected position of the handswitch.
| | They also modified the plant emergency procedures to verify proper operation of the tower return valves if the control switch needed to be repositioned. These actions were considered to enhance the operators ability to maintain the NSCW system available. |
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| The valve initially only opens to a mid-position as part of the slow fill design which minimizes the affects of water hammer. After a requisite time delay, a time delay relay times out, and ultimately closes a contact in the opening circuit for either the spray or bypass valve, which drives the valve to the fully open position. | | The inspector determined that the licensee properly determined that the NSCW system was available during temperature instrument 1T1668 calibration. The inspector also determined the licensee properly reported the PI as Green for the third and fourth quarters of 2007. |
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| If the handswitch had been selected to the *Open Bypass" position, either during normal operation or during accident conditions, manual operator action would be required to place the valve either in "Auto* or *Open Normal-to ensure the return water was directed to the spray header, to allow for heat removal. Analysis has shown that with adminIstrative controls in place, there is sufficient time available for the operator to place the tower return valves in the configuration required to perform their safety function.
| | MANAGEMENT MEETINGS |
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| System Operating procedure 13150-1/2, section 4.4.15 establishes administrative controls for operating the tower return valves in manual. These controls include placing a Caution Tag on the control room handswitch (HS1668A1HS1669A)
| | ===Exit Meeting Summary=== |
| and monitoring
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| 'I NSCW return temperature.
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| If NSCW return temperature reaches 85 degrees and I continues to trend upward, the procedure instructs the operator to place the NSCW 1 tower return valves in Automatic.
| | The inspector presented the results of the supplemental inspection to Mr. Todd Youngblood and other members of licensee management and staff on December 11, 2008. The inspector confirmed that no proprietary information was provided or examined during the inspection. |
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| Additionally.
| | =SUPPLEMENTAL INFORMATION= |
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| Emergency Operating Procedure (EOP) i 19000-C, in the Reactor Operator (RO) Initial Actions step 5.b, has the operator verify I that the NSCW tower return valve handswitches are In Automatic control. The term J "verify.*
| | ==KEY POINTS OF CONTACT== |
| as used in Operations department procedures.
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| means to observe the equipment to ensure it is in the position required by the procedure step. If it is not in the position required by the procedure step. the implied meaning is to put it in the position required by the procedure step. For the cases when maintenance is performed on the temperature loops (T-1668/1669), which could render the Automatic control of the tower return valves non functional (valves may not reposition based upon NSCW return water temperature), the Caution tag on the control room handswltch would alert the operator to the off normal condition, and based upon the operator's knOWledge and training, would trigger the operator to place the handswitch in the configuration required.
| | ===Licensee Personnel=== |
| | : [[contact::M. Hickox]], Licensing Engineer |
| | : [[contact::J. Stringfellow]], Licensing Manager |
| | : [[contact::D. Vineyard]], Operations Manager |
| | : [[contact::T. Youngblood]], Engineering Manager |
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| The proposed change clarifies FSAR section 9.2.1 and TS Bases 3.7.9 on the acceptability of manually positioning the NSCW tower return valves under administrative control. References:
| | ==LIST OF ITEMS== |
| 1. VEGP FSAR, (Revision 15-7/31/08), Section(9.2.1.
| | OPENED AND CLOSED |
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| 9.2.5 and 15.0) 2. VEGP Technical Specifications, (Amendment 151/132).
| | ===Opened and Closed=== |
| | : 05000424, 425/2008009-01 URI Technical Specification Operability Of The NSCW System With The Cooling Tower Return Valves In Manual Control. (Section 01) |
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| Sections(3.7.8 and 3.7.9) 3. VEGP Environmental Protection Plan, (Amendment 97175) 4. 19000-C, E-O Reactor Trip or Safety Injection, Version 32 5. 13150-1/2.
| | ==LIST OF DOCUMENTS REVIEWED== |
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| Nuclear Cooling Water System, Version 46.1/38 NMP-AD-010-F01, Version 3.0 NMP-AD-010 Southern Nuclear Operating Company SOUftIIIINA COMPANY ....,......Nuclear Management Procedure 10 CFR 50.59 Screening/Evaluation Page 3 of7 8. 10 CFR 50.59 Screening Identify the Updated FSAR design function which applies to this activity, if applicable:
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| FSAR 9.2.1.1.1.G-The NSCW system Is designed to perform its cooling function following a loss of coolant accident (LOCA), automatically and without operator action. assuming a single failure coincident with a loss of offsite power. Does the activity to which this screening applies, represent: 0 Yes l8I No A modification.
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| addition to, or removal of a structure.
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| system, or component (SSC) such that a design function as described in the Updated FSAR is adversely affected?
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| Basis for The proposed change is an LDCR that clarifies the operation of the NSCW tower return valves as described in FSAR sections 9.2.1 and TS Bases 3.7.9. The proposed change does not involve a physical change to any plant equipment.
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| Therefore the proposed change does not involve the addition to or removal of a SSC. such that a design function as described in the Updated FSAR is adversely affected. IZI Yes 0 No A change to procedures that adversely affects the performance or method of control of a design function as described in the Updated FSAR? Basis for FSAR paragraph 9.2.1.1.1.
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| G states that -The NSCW system is designed to perform its cooling function following a loss of coolant accident (LOCA), automatically and without operator action, assuming a single failure coincident with a loss of offsite power." Since the proposed change relies upon manual operator action to align the tower spray valves under certain circumstances, the proposed change does involve a change to procedures that could affect the performance or method of control of a design function as described in the Updated FSAR. 0 Yes IZJ No An adverse change to a method of evaluation or use of an alternate method of evaluation from that described in the Updated FSAR that is used in establishing design bases or in the safety analysis?
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| Basis for The proposed change is a clarification conceming the operation of the NSCW tower return valves. All of the parameters (e.g. NSCW flow, pressure, temperature, etc.) and analytical methods used to establish the design bases and safety analysis for the NSCW system remain bounding and unaffected by the proposed change. Therefore the proposed change does not involve an adverse change to a method of evaluation or use of an alternate method of evaluation from that described in the Updated FSAR that is used in establishing design bases or in the safety analysis. 0 Yes 181 No A test or experiment not described in the Updated FSAR which is outside the reference bounds of the design basis as described in the Updated , i Ii'I 11 I'J j NMP-AD-010-F01, Version NMP-AD-010 Southern Nuclear Operating Company IOU_A COMMNY ......,..Nuclear Management Procedure 10 CFR 50.59 Screening/Evaluation Page 4 of1 FSAR or is inconsistent with the analyses or descriptions described in the updated FSAR? Basis for The proposed change is a clarification to the FSAR and TS Bases on the operation of the NSCW return valves. The proposed change does not place the NSCW system in a configuration outside the reference bounds of the design basis as described in FSAR Table 9.2.1-2 (Items 67-70) nor does it place the system in a configuration for which it was not analyzed.
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| Therefore the proposed change does not involve a test or experiment not described in the Updated FSAR which Is outside the referenced bounds of the design basis as described in the Updated FSAR or is inconsistent with the analyses or descriptions described in the Updated FSAR. 0 Yes IZI No A change to the Technical Specifications and/or Environmental Protection Plan incorporated in the operating license? Basis for The proposed change is an LDCR that clarifies the operation of the NSCW tower return valves as described in FSAR section 9.2.1 and TS Bases 3.7.9. The proposed change does not affect the Limiting conditions of Operation or the surveillance requirements associated with any component in the NSCW system or as part of the Ultimate Heat Sink as described in Technical Specifications 3.7.8 and 3.7.9. Therefore the proposed change does not involve a change to the Technical Specifications.
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| The Environmental Protection Plan incorporated in the Operating license remains unaffected as a result of this change. IF the answer to all of the questions in section B is "NO", do not complete sections C and D. Sections C and D should also be deleted from the form. IF the answer to any of questions 1, 2, or 4 in section B is "YES*, then only complete the answers to questions 1-7 in section C and complete the summary in Section D. !E only the answer to question 3 in section B is "YES", then only complete the answer to question 8 in section C and complete the summary in section D. IF question 5 is answered *YES", a license amendment is involved which requires NRC approval.
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| Do not complete sections C and D if all aspects of the activity will be addressed in the license amendment request. C. 10 CFR 50.59 Evaluation 1. 0 Yes IZI No Does the proposed activity result in more than a minimal increase in the frequency of occurrence of an accident previously evaluated in the Updated FSAR? Basis for Answer: Neither the NSCW system nor the Ultimate Heat Sink as described in FSAR sections 9.2.1 and 9.2.5 respectIvely, are accident initiators, based upon the description of accidents analyzed in FSAR section 15.01.1, 15.0.1.2, 15.0.1.3 and 15.0.1.4.
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| Therefore, the proposed change, which clarifies the operation of the NSCW tower return valves, cannot result in more than a minimal increase in the frequency of occurrence of an accident previously evaluated in the Updated FSAR since the affected system is not a credible accident initiator.
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| NMP-AD-01 O-F01. Version NMP-AD-D10 I Southern Nuclear Operatina Company ........A COMMNY......_....Nuclear Management 10 CFR 50.59 Screening/Evaluation Page 5 of7 fl ..'.*'1 2. 0 Yes 181 No Does the proposed activity result in more than a minimal increase in il likelihood of occurrence of a malfunction of a structure, system, or (SSC) important to safety previously evaluated in Updated j Basis for Answer: The NSCW system provides cooling to a number of safety :i 0 Yes No ON/A Basis for Answer: components as delineated In FSAR Table 9.2.1-1. All of the heat exchanged j to the NSCW system is rejected to the outside environment via the Ultimate J Heat Sink. All of these safety related components are credited in the FSAR Chapter 15 accident analyses with minimizing/mitigating the consequences of an accident.
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| In order for the NSCW system and Ultimate Heat Sink to perform its safety function, the NSCW tower return valves ultimately have to be al!gned to direct NSCW retum flow to the spray header. Normally, the NSCW tower return valves are in Automatic control. However, under certain circumstances (e.g. facilitate maintenance)
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| the valves may be placed in manual control, and aligned so that NSCW flow is returned directly to the tower basin or to the spray header. Analysis (DOEJ-06-19000 C V29-001, Version 2 attached to LDCR 2008039) has shown that under admInistrative control, there is sufficient time for the operator to recognize and place the tower return valves In the desired configuration and maintain NSCW temperature within analyzed limits. Manual control of the NSCW tower return valves is a credited safety function, as described in the FSAR Failure Modes and Effects Ta ble 9.2.1-2, Items 67-70. Since NSCW temperature would remain within analyzed limits and thus would not have an adverse affect on any important to safety SSC, the proposed change, which clarifies the operation of the tower return valves in FSAR section 9.2.1 and TS Bases 3.7.9. would not result in more than a minimal increase in the likelihood of occurrence of a malfunction of a SSC important to safety previously evaluated in the Updated FSAR. Does the proposed activity result in more than a minimal increase in the consequences of an accident previously evaluated in the Updated FSAR? The proposed change to clarify the manual operation of the NSCW return valves in FSAR section 9.2.1 and TS Bases 3.7.9 is consistent with the safety function of the NSCW tower return valves as described in FSAR Table 2. Items 67-70. Analysis has shown. that under administrative control, there is sufficient time for the operator to recognize and place the tower return valves in the desired configuration under worst case accident conditions.
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| Since manual operation of the NSCW tower return valves is a credited safety function as described in the FSAR and analysis has shown that the operator has sufficient time available to recognize and place the tower return valves in the desired alignment.
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| the NSCW temperature would remain within analyzed limits as described in FSAR section 9.2.5. Therefore, all equipment cooled by NSCW which is used to mitigate the consequences of an accident, would not be adversely affected, as a result of the proposed change. Consequently, the proposed change would not result in more than a minimal increase in the consequences of an accident previously evaluated in the Updated FSAR. NMP-AD-010-F01, Version NMP-AD-010 Southern Nuclear Operating Company IOVIIIIRNA COMMNY E......,.................
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| Nuclear Management Procedure 10 CFR 50.59 Screening/Evaluation Page 6 of7 4. 0 Yes 181 No Does the proposed activity result in more than a minimal increase in the o N/A consequences of a malfunction of an sse important to safety previously evaluated in the Updated FSAR? Basis for Answer: As previously stated, the proposed change would not result in the NSeW system being placed outside of analysis limIts used in establishing the design bases. Therefore all equipment cooled by NSeW would be unaffected by the proposed change. Thus, the proposed change would not result in more than a minimal increase in the consequences of a malfunction of an sse important to safety previously evaluated in the Updated FSAR. 5. 0 Yes 181 No Does_the proposed activity create the possibility for an accident of a different o N/A type than any preViously evaluated in the Updated FSAR? Basis for Answer: The proposed change would not result in the NSeW system being placed outside of analysis limits used in establishing the design bases. As such, all of the assumptions and analysis used in establishing the accident analysis would remain valid and bounding.
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| Therefore the proposed change does not create the possibility for an accident of a different type than any previously evaluated in the FSAR. 6. 0 Yes I:8l No Does the proposed activity create the possibility for a malfunction of an sse o N/A important to safety with a different result than any previously evaluated in the Updated FSAR? Basis for Answer: The proposed change is an LDeR that clarifies the manual operation of the NSeW tower return valves as described in FSAR section 9.2.1 and TS Bases 3.7.9. Manual operation of the NSeW tower return valves is a credited safety function as described in FSAR Failure Modes and Effects Table 9.2.1-2, Items 67-70. Additionally, analysis has shown that under administrative controls there is sufficient time for the operator to recognize and manually position the tower return valves to the desired configuration prior to NSCW exceeding any of its design limits. Therefore, the proposed change would not create the possibility for a malfunction of an sse important to safety with a different result than any previously evaluated in the Updated FSAR. 7.a 0 Yes I:8l No Does the proposed activity have any impact on the integrity of the fuel o N/A cladding, reactor coolant pressure boundary, or containment? Answer Question 7b only if the answer to Question 7a is Basis for Answer: As previously evaluated, the proposed change does not result in the NSeW system being placed outside of any analysis limit used in establishing the design bases. As such, all analysis and assumption used in the accident analyses remain valid and bounding.
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| Therefore the proposed change would not have any impact on the integrity of the fuel cladding, reactor coolant pressure boundary, or containment.
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| 7.b 0 Yes 0 No Does the proposed activity result in a design basis limit for a fission product IZI N/A barrier as described in the Updated FSAR being exceeded or altered? Basis for Answer: NMP-AD-01 O-F01, Version 3.0 NMP-AD-010 Southern Nuclear Operatlna Company JOU'IIIIaA CllIMMIIIYNuclear Management Procedure 10 CFR 50.59 Screening/Evaluation Page 7of7 8. 0 Yes 0 No Does the proposed activity result in a departure from a method of evaluation 181 N/A described in the Updated FSAR used in establishing the design bases or in the safety analyses?
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| Basis for Answer: Provide a summary of the 10 CFR 50.59 evaluation in Section D. IF the answer to any of the questions in section C (excluding Question 7a) is "YES", a license amendment must be obtained from the NRC before the activity may be implemented.
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| Do not complete section 0 if all aspects of the activity will be addressed in the license amendment request. D. 10 CFR 50.59 Evaluation Summary The 10 CFR 50.59 evaluation summary should include a brief description of the change and a concise summary of the responses to the evaluation questions provided in Section C. Summary: The proposed change which is an LDCR that clarifies the manual operation of the NSCW tower return valves as described in FSAR section 9.2.1 and TS Bases 3.7.9 was evaluated and it was determined that the proposed change would not result in more than a minimal increase in the consequences of an accident, would not create any new accident nor would it result in an increase in the frequency of any accident previously evaluated in the Updated FSAR. [8J Check this box indicating a copy of the completed 10 CFR 50.59 screen/evaluation will be forwarded to Nuclear Licensing.
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| NMP-AO-010-F01, Version NMP-AD-010
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| '2. 0 Vl2(2.Sl0..J i..Cl F"t.", I 'z.. VEGP-FSAR-9 C ;;l,.j'jI.V.... P of-P.'\ Q.J\, 6, to, J q. 2. *t . '1., cooling tower spray headers and return the water directly to the cooling tower basin whenever the return water temperature is below 65°F. When necessary due to low ambient temperatures, freezing of an idle NSCW train or tower basin will be prevented by operating both NSCW trains and/or both NSCW transfer pumps. and by periodically operating all three NSCW pumps In each train. Idle piping, stagnant lines, and instrument sensing lines will be protected from freezing by either Insulation.
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| electric heat tracing, space heaters, or other means. The heat tracing is controlled by ambient sensors located outdoors in a location not exposed to sun or other heat sources so as to accurately measure the ambient temperature.
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| The sensors are NEMA 4 rated for outdoor locations and are set to actuate at 38+5°F. A drain hole is provided in each of the four 12-in. supply headers to the tower spray nozzles to promote self-draining.
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| Those portions of the spray header supply piping which will not self-drain are protected from if freezing.
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| During freezing rain. enougn heat is present from the basin water to prevent a heavy ice I/. buildup. The tower return valves (HV1668A1B and HV1669A1B)
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| are normally maintained in automatic control. However, to facilitate maintenance, the valves may be aligned to return the water directly to the basin or to the spray header irrespective of return water temperature.
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| When the tower return valves are aligned to return the water directly to the basin or to the spray header, they are administratively controlled and analysis has shown that there Is sufficient time for the operator to place the valves in the configuration required, should an accident occur. Makeup or each er orm proVl ed by onn Ion . tti plan a eup water wells. The backUp source of makeup water is the Savannah River. NSCW tower basin water is the source of supply to the NSCW system and does not perform any other function.
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| The makeup supply to the tower basins and provisions to ensure adequate net positive suction head (NPSH) for the NSCW pumps are discussed in paragraph 2.4.11.5.
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| I The impact of long-term corrosion on the NSCW piping is compensated for by appropriate J corrosion allowances and addition of a corrosion inhibitor.
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| }, Each NSCW cooling tower Is provided with chemical treatment that employs biocide to prevent biological fouling, and a corrosion inhibitor.
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| Chemical treatment is added to each tower basin as required.
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| A portion of the system coolant is blown down, when makeup water is available, to prevent the accumulation of fouling agents. The blowdown rate may be controlled by conductivity or manually.
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| Upon a safety injection signal or loss of external makeup, the tower blowdown is terminated and the concentration of total dissolved solids is allowed to increase.
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| However, during the postulated 30-day design accident case (subsection 9.2.5), the solids buildup will not prevent acceptable operation of the cooling tower or associated NSCW equipment.
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| Air-operated valves CV-9446 and CV-9447 modulate NSCW tower blowdown to limit the buildup of total dissolved solids in the NSCW system. The valves close automatically upon receipt of a safety injection signal and are designed to fail closed upon a loss of offsite power. Thus, the valves will close automatically whenever required to conserve NSCW tower basin inventory.
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| The valves also close whenever the respective NSCW train is not in service as part of the keep-full system. Failure of a tower blowdown valve to close when required will be indicated by valve position lights on the main control board and by a high flow alarm in the keep-full intertie.
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| Additionally, this condition will be identified by basin level verification required by the Technical Specifications or. in a post-accident situation, by the valve status verification reqUired by the emergency instructions.
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| Isolation of the blowdown line can be effected by closing manual 9.2-5 REV 15 4/09 UHS B 3.7.9 *l.DDBO-S£}
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| 1.. Or z.. I f;'!l 'i B 3.7 PLANT SYSTEMS B 3.7.9 Ultimate Heat Sink (UHS) J 1 I BASES The UHS provides a heat sink for processing and operating heat from safety related components during a transient or accident.
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| as well as during normal operation.
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| This is done by utilizing the Nuclear Service Cooling Water (NSCW) System and the Component Cooling Water (CCW) System. The UHS consists of the NSCW System mechanical draft towers. Two 100% capacity redundant NSCW towers are provided for each unit. One tower is associated with each train of the NSCW System. Each NSCW tower consists of a basin that contains the ultimate heat sink water supply and an upper structure that contains four individual fan spray cells where the heat loads are transferred to the atmosphere.
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| Each spray cell contains one safety-related temperature controlled fan. Instrumentation is provided for monitoring basin level and water temperature.
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| The tower basins each contain a safety-related transfer pump to permit the use of the combined storage capacity of the basins. The combined storage capacity of two tower basins provides greater than a 30 day cooling water supply assuming the worst combination of meteorological conditions and accident heat loads which maximize the tower heat load, basin temperature, and . /' A 0-;0,/ evaporative losses. ....__-'" .--_ / ,/J..--, J ........_./ ..........,...-
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| ....,....-The tower return valves (HV1668A1B and HV1669A1B)
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| are normally maintained in automatic control. However, to facilitate maintenance, the valves may be aligned to return the water directly to the basin or to the spray header, irrespective of return water temperature.
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| When the tower return valves are aligned to return the water directly to the basin or to the spray header, they are administratively controlled and analysis has shown that there is sufficient time for the operator to place the valves in the configuration required, should an accident occur. _....-
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| Additional information on the design and operation of the system. along with a list of components served, can be found in FSAR, Subsection 9.2.5 (Ref. 1). APPLICABLE The UHS is the sink for heat removed from the reactor core SAFETY ANALYSES following all accidents and anticipated operational occurrences in which the unit Is cooled down and placed on residual heat removal (RHR) operation.
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| Its maximum post accident heat load occurs 20 minutes after a design basis loss of coolant accident (LOCA). Near this time, the unit switches from injection to (continued)
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| Vogt/e Units 1 and 2 B 3.7.9-1 Revision No. 0 t-r l .4<.' lol-"-1 efJr I TO Lt.?'.. -(2.. l <::'0",-;'0 PAC'le.* I L(-] Documentation of Engineering DOEJ*06-19000 C NSCW SPRAY RESTORATION HARD BYPASS Version Record ij n il ;: " 1.0 'I 1 1 I 1 I i I 11 ;. 'I' j I I I I *1 Version OrlglnatorlDate ReviewerlDate No. Description Signature Signature 1 Original Issue (pp 1-2) seeOrtsjnaJ SeeOriginl.ll J A WehrenbArll 1-6006 JMMofson HI-06 2 Update for MUR (revise pp 1 * 2) J M Morson 8-13-08 SOUTHERNCOMPANY Enerrv to Sertle YOur World-Procedu.. ENG-003 Document8llon 01 Engineering Judgment.
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| Ver. 2. 12I06I05 ATi'A" lei f-tt:\0( To Lor.. {L-"2. ::;"0/:)0 l (1 Pl,*C.£ 'l. -.:(-3 DOEJ*06*19000 C V29-601 Southern Nuclear Company A Purpose: This evaluation provides a justification for the NSCW heat up times in PAF-19000-C-V29-0ATT (Ref. 1). Destan Inputs: 1. PAP-19000-C-V29"()ATI, dated June 11,2004 2. lX2D05EOOl,RI5 3. lX4DB149-2.
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| RS 4. IX4DB149-4, RS_ 5. Crane Technical Paper 410 6. X4C1202V54, Rl and MC-V-97-0083 yl 1. FSAR. Version 13. 11130105 Evaluation:
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| From reference 2, the tower diameter is 88 ft and the depth is 80.25 ft. Then the volume of the tower is 1t (8812)2 X 80.25 tt3 x 7.4805 gall ft3 = 3.65 X 10 6 gallons. From references 3 and 4, the NSCW post-LOCA flow is 16388 gpm. Then for no mixing in the basin (i.e., plug flow) the time for the hot return water to reach the pump suction would be 3.65 x 10 6 gall [16388 gpmx 60 minlhr] 3.7 hours. If the LOCA heat load is uniformly mixed in the tower basin (and evaporation and heat transfer are neglected), the water inventory will heat up from the initially assumed 90 "F to the 9S "F design limit relatively quicldy. From reference 5, the heat content of the basin water is interpolated to be 90"F ::::> 58.0 Btullb 95 of:=) 63.0 Btullb 98 "F:=) 66.0 Btullb. From 6 (page 17), for a single train of NSCW, the maximum heat load during the first half hour after the LOCA is about 3.13 x L0 8 Btulhr. and the time to reach 95 OF is , v [3.65 x l(f gal x 8.341blgal "It (63 -58) Btullb] 13.13 x lOS Btulhr = 0.49 hr. The FSAR (Ref. 7, §9.2.5.2.4)
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| indicates a slightly higher temperature for a limited time is acceptable:
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| i, In addition, the peak basin 1elIlp!:rature durin,g three-fan coo1down operation wiU exceed ,I;1 the nominal desIgn maximum of 95°F. reaching approximately 97°F for Unit 1 and 98 Q F for Unit 26 to 8 b after RHR initiation, and remaamng above 95°F for a total of 20 h for Unit I and 35 h for Unit 2 during cooldown.
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| The NSCW tower transfer pump may be used 1 H:\OaIaWEGP\CALCS\Hard BYJl888 OOEJ V2.doc Procedure ENG.(I03 Documentallon 01 Engil'l88ringJudgnent.
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| Vet. 2, 12J06r'05 l ArT!.:\.( i.1tv1c)\jC I l 0 cit. "l. -:;; 0.".;. 0 ') W\ 6C. 1, **:f-S DOEJ-06-19000 C V29-001 Southern Nuclear Company A to transfer cooler water from the idle basin which would help keep the NSCW temperature down. Even if the peak basin tem\lefature exceeds 95°F, the excess is less than 3°P and exists for a relatively short period 10 terms of total plant life and in terms of total RHR system operation over the plant life. Because of these considerations, and because fan cooldown has a very low probability of occurrence, it is concJuded that there are no operational problems associated with tl1is mode of operation.
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| To reach 98 OF takes [3.65 x 10 6 gal x 8.341b/gal x (66 -58) Btullb]l3.13 x 10 8 Btu/hr =0.79 hr. As soon 88 the spray is returned to service, the return water temperature will reduce significantly, and the basin temperature will start decreasing.
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| Since the basis inventory will tum over about every 4 hours, the water temperature would be expected to return to the as-analyzed temperature profile within the 35 hours currently discussed in the FSAR. MUS power uprate will increase the full power leyel by 1,7%, This wjl! jngea$e the cgre decay beat (but Pot system operating temperah1J'es)
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| by a similar amount. Assuming AU accident beat sources an; increased by 1.7%, the time to teach 98 OF wopld decrease 0,79 hr t 1,017 =0.77 Conclusion:
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| Greater than Y2 hour is available to return the spray to service; and once tower spray is returned to service the basin temperature will quickly return to the as-analyzed temperature profile. 2 j J 'I j j J H:\DataWEGP\CALCSlHald Bypus OOEJ V2.cIoc ProcedIn ENG.Q03 Docunentation of Engineering Judgment.
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| Ver. 2, ,2I06f05 Vogtle Electric Generating Plant -Units 1 and Additional Information Regarding NRC Supplemental Inspection 0500042412008009 and Enclosure NSCW Spray Valve Operability Position Paper NSCW Spray Valve Operability Position The tower return valves (HV1668A1B)
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| have a control room handswitch that controls their operation.
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|
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| The handswitch (HS-1668A)
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| has three positions which are maintained.
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|
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| Note that this handswitch controls the operation of both the spray and bypass valves. The handswitch can be placed in "Open Bypass", "Open Normal", or "Auto". Assuming a train of NSCW is inservice, when you place the handswitch in Open Bypass, the bypass valve (HV1668B)
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| opens and the spray valve (HV1668A)
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| closes. In this configuration, all NSCW return flow is directed to the tower basin, bypassing the spray. The valves will remain in this position as long as any NSCW pump in that train is operating irrespective of NSCW return water temperature.
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|
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| Similarly, if the handswitch is placed in Open Normal, the spray valve will open and the bypass valve will close. In this configuration, all NSCW return flow is directed to the tower spray. The valves will remain in that position as long as a NSCW pump in that train is operating, irrespective of NSCW return water temperature.
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|
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| If the handswitch is placed in Auto, the spray valve will open and bypass valve will close when return water temperature is greater than 75 degrees, and if return water temperature drops below 65 degrees, the bypass valve will open and the spray valve will close. When a train of NSCW is shutdown, as the last pump is stopped and its breaker opens, an interlock is satisfied that closes both the spray and bypass valve. This ensures the system stays full and minimizes the effects of water hammer on subsequent pump start. When a train of NSCW is started up, as soon as the first NSCW pump is started, an interlock is satisfied that partially opens either the spray or bypass valve. If the handswitch for the tower return valves was in Auto, the valve that partially opened would be dependent upon the temperature in the return header (Le. if return temperature was high the spray valve would partially open, if return temperature was low the bypass valve would partially open). If the handswitch was in Open Normal, the spray valve would partially open. Similarly, if the handswitch was in Open Bypass, the Bypass valve would partially open. Once an Agastat time delay relay timed out, either the spray or bypass valve would then fully open dependent upon the position of the return valve handswitch.
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|
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| During a LOSP, the operation of the tower return valves would be the same as described above, although there would be some time delays involved as a result of when the loads were sequenced back on. It should be noted that the tower return valves do not receive an actuation (SI) signal. It should also be noted that the spray valve is interlocked with one of the NSCW tower fans such that whenever the spray valve is open, one NSCW fan starts and when the spray valve is closed the fan stops. All of the other fans are started automatically on return water temperature.
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|
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| The temperature loop that controls the return valves is independent of the temperature loops that control the fans.
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|
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| Position NSCW is operable with return valves in manual control. Technical Specification Requirements Technical Specification 3.7.9 provides the Limiting Condition of Operations (LCO's) and surveillance requirements (SR's) for the Ultimate Heat Sink (UHS). For the UHS to be operable:
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| (1) the basin level has to be greater than or equal to the specified level (SR 3.7.9.1) (2) the basin water temperature is maintained less than or equal to 90 degrees (SR 3.7.9.2) (3) the required number of fans/spray cells are operable which is verified by operating each of the fans for at least 15 minutes every 31 days (SR 3.7.9.3) and (4) a NSCW transfer pump has to be operable (SR 3.7.9.4).
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|
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| During the time the return valves are being manually controlled, the system operating procedure requires a caution tag to be placed on the return valves handswitch, the basin water temperature to be maintained less than 90 degrees and return water temperature to be monitored by the Operators on the plant computer.
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|
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| In the event, return water temperature exceeds 85 degrees and continues to trend up, the procedure instructs the operator to place the tower return valve handswitch back in Auto. For cases where the temperature loop that controls the return valves is taken out of service, for maintenance, the caution tag would remind the operator of this condition, and based upon training and experience, the operator would place the valve in Open Normal. Once the return valve handswitch was placed in Open Normal, the return valve would open, one of the tower fans would start, and the bypass valve would close. Similarly, if an accident were to occur, during the time the tower return valves are being manually controlled, the Emergency Operating Procedure, in the initial operator actions, contains a step that instructs the operator to place the tower return valves handswitch in Automatic.
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|
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| If the temperature loop had been removed from service for maintenance, the caution tag on the handswitch would remind the operator of this condition, and based upon training and experience the operator would place the handswitch in Open Normal. Once the return valve handsitch was placed in Open Normal, the return valve would open, one of the tower fans would start, and the bypass valve would close. The capability to open or close the tower return valves either manually or automatically from the control room is required to ensure UHS operability.
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|
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| If a valve was incapable of being stroked, the UHS would be rendered inoperable.
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|
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| All of the UHS surveillance requirements would have continued to be met in this configuration.
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|
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| Technical Specification 3.7.8 provides the LCO's and surveillance requirements for the NSCW system. For a train of NSCW to be considered operable (1) each manual, power operated and automatic valve in the 'nowpath servicing safety related equipment that is not locked, sealed or otherwise secured in position, is in the correct position (SR 3.7.8.1) (2) each automatic valve in the f10wpath that is not locked sealed or otherwise secured in position actuates to the correct position on an actual or simulated actuation signal (SR 3.7.8.2) and (3) each NSCW system pump starts automatically on an actual or simulated actuation signal (SR 3.7.8.3).
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|
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| During the time the tower return valves are in manual control (either Open Normal or Open Bypass), the position of the valves would not have any affect on a NSCW pump start (Le. there is no permissive between return valve position and NSCW pump start). Therefore, surveillance requirement SR 3.7.8.3 would be unaffected by the manual control of the tower return valves. Additionally, these valves do not receive a SI actuation signal. They are either automatically controlled by return water temperature or manually controlled by the operator.
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|
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| Therefore surveillance requirement SR 3.7.8.2 is not applicable to these valves. Lastly, the "correct position" for the tower return valves as it relates to SR 3.7.8.1 is relative.
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|
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| As long as either one of the tower return valves are open, when a train of NSCW is in operation, a f10wpath is established.
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|
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| Ultimately, for a design bases LOCA, the spray valve would have to be open to reject heat to the atmosphere.
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|
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| However, to satisfy the requirements of SR 3.7.8.1, the return valves can be open/closed dependent upon return temperature, whether or not the train is operating, or handswitch position.
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|
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| Summarizing the Technical Specification requirements, in accordance with Technical Specification 3.7.9, the ultimate heat sink must be able to perform its safety function and be operable per the requirements.
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|
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| The tower spray valve has to be capable of opening and bypass valve has to be capable of closing. The bases state the tower return valves are normally maintained in automatic control. However, to facilitate maintenance, the valves may be aligned to return the water directly to the basin or the spray header, irrespective of return water temperature.
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|
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| When the tower return valves are aligned to return the water directly to the basin or to the spray header, they are administratively controlled and analysis has shown that there is sufficient time (Le., more than half an hour) for the operator to place the valves in the configuration required, should an accident occur. Therefore, the NSCW tower return valves can perform its safety function (Le., open on high NSCW return temperature to admit water to NSCW tower spray header for cooling; also, can be opened by remote manual control from either the control room or the shutdown panel). The spray valve is capable of performing its safety function in automatic or by manually positioning the valve. Basis of Position A review of the Safety Evaluation Report (SER) for VEGP dated June 1985 contains the following information as it relates to NSCW and the UHS: 2.4.11.2 The water is returned to the cooling tower spray manifolds or in the event of low return temperature from the NSCW system, the spray manifolds are bypassed, and the water is returned directly to the basin. 7.3.2.9 On receipt of an SI or loss of offsite power signal, all preferred pumps receive an automatic start signal. If one of the preferred pumps does not start, the standby pump in the same train receives a subsequent start signal. An SI signal also isolates the cooling tower blowdown lines. Manual initiation is also provided from the control room or from the remote shutdown panels. 9.2.1 In order to further preclude waterhammer in an idle train or on pump restart following a loss of offsite power, the NSCW system includes:
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| (1) interlocks and pressure switches to close both tower valves (spray header and cold weather bypass valves) whenever the NSCW pumps in that train are not operating and to allow normal operation when the pumps are in service. 9.2.5 To guard against icing or freezing in the return line to the cooling tower, two valves function to bypass the cooling tower spray headers and return the water directly to the basin. Based upon the descriptions contained in the SER, no credit is cited for "Automatic" operation of the NSCW tower return valves, and as noted from paragraph 7.3.2.9 cited above, manual action is recognized by the NRC as part of the licensing basis of NSCW and the UHS. In fact, section 9.2.1 of the SER as quoted above uses the phrase "normal operation" when describing the operation of the tower return valves when the pumps are in service. FSAR paragraph 9.2.1.1.G states: "The NSCW system is designed to perform its cooling function following a loss of coolant accident (LOCA) automatically and without operator action, assuming a single failure coincident with a loss of offsite power." This statement does accurately state the design of the NSCW system. When all components in the NSCW system are in their standard alignment, the NSCW system would perform its design function automatically and without operator intervention.
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|
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| However, as described above, the spray valve can be manually opened from the control room handswitch and conservative analysis has shown that there is more than 0.5 hours available for the operator to return the spray valve to service prior to exceeding the FSAR temperature limits. This analysis conservatively assumes that the initial basin temperature was at the maximum Technical Specification temperature of 90 degrees at the start of the accident neglects evaporation, heat transfer to NSCW structures, and limits the water temperature to 3 degrees below the maximum analyzed transient temperature of 98°F. As discussed in section 9.2.5.2.4 of the FSAR, a short-term excursion to 98°F over a span of 20 to 30 hours is acceptable.
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|
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| This is consistent with the safety function of the tower return valves as described in FSAR Table 9.2.1-2 which states that the safety function of the spray valve is to "Open on high NSCW return temperature to admit water to NSCW tower spray header for cooling; also, can be opened by remote manual control from either the control room or the shutdown paneL" Normal makeup is from the well water pumps and this is an automatic function.
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|
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| However since well water is not safety related it can not be relied upon during an accident.
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|
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| The same is true for river water which is the backup water supply. However, to meet the 30 day mission time, per FSAR section 9.2.5.3.B, after one day of operation, one train of NSCW has to be shutdown.
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|
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| Inventory from that basin is then transferred from the shutdown basin to the operating basin using a transfer pump. Stopping the train after the first day and transferring the basin contents is all under operator manual control. Also, TS 3.7.9 allows for a transfer pump to be out of operation for up to 30 days. However, after 8 days, an alternate method for basin transfer has to be in place. This is somewhat unique in that the alternate method does not have to use safety related components and any alternate method would be highly dependent upon manual operator actions. Conclusion Manual operation of NSCW and the UHS components is required and has been shown to be an acceptable mode of operation.
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|
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| It is also consistent with other manual actions for this system where sufficient time and methods are provided that the function of the system is maintained.
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|
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| Therefore based upon a review of the FSAR, SER, plant operating procedure and Technical Specifications, it can be concluded that manual operation of the tower return valves is consistent with the licensing bases for VEGP.
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| }} | | }} |
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Category:Inspection Report
MONTHYEARIR 05000424/20243012024-11-19019 November 2024 Operator Licensing Examination Approval 05000424/2024301 and 05000425/2024301 ML24313A0632024-11-14014 November 2024 Integrated Inspection Report and Assessment Follow-Up Letter 05200025/2024003 and 05200026/2024003 IR 05000424/20240032024-10-30030 October 2024 – Integrated Inspection Report 05000424/2024003 and 05000425/2024003 IR 05000424/20240052024-08-26026 August 2024 Updated Inspection Plan for Vogtle Electric Generating Plant, Units 1 and 2 - Report 05000424/2024005 and 05000425/2024005 IR 05000424/20244012024-08-15015 August 2024 4 - Security Baseline Inspection Report 05000424-2024401, 05000425-2024401, 05200025-2024402, and 05200026-2024403 - Cover Letter ML24212A1442024-08-0101 August 2024 Integrated Inspection Report 05200025/2024002 and 05200026/2024002 IR 05000424/20240022024-07-29029 July 2024 Integrated Inspection Report 05000424/2024002 and 05000425/2024002 IR 05000424/20244042024-07-26026 July 2024 Material Control and Accounting Program Inspection Report 05000424/2024404 and 05000425/2024404 (Cover Letter) ML24194A0342024-07-12012 July 2024 Review of the Refueling Outage 1R24 Steam Generator Tube Inspection Report ML24191A3792024-07-10010 July 2024 – Initial Test Program and Operational Programs Inspection Report 05200026/2024011 ML24130A2412024-05-13013 May 2024 Integrated Inspection Report 05200025/2024001 and 05200026/2024001 ML24127A2372024-05-0909 May 2024 Initial Test Program and Operational Programs Inspection Report 05200026/2024010 IR 05000424/20240012024-04-23023 April 2024 –Integrated Inspection Report 05000424/2024001 and 05000425/2024001 IR 05000424/20230062024-02-28028 February 2024 Annual Assessment Letter for Vogtle Electric Generating Plant Units 1 and 2 - NRC Inspection Report 05000424-2023006 and 05000425-2023006 IR 05000424/20240102024-02-14014 February 2024 – Fire Protection Team Inspection Report 0500424/2024010 and 05000425/2024010 IR 05000202/20300042024-02-13013 February 2024 Integrated Inspection Report 052000250/2023004 and 05200026/2023004 IR 05000424/20230042024-02-0505 February 2024 Integrated Inspection Report 05000424-2023004 and 05000425-2023004 ML24032A0252024-02-0505 February 2024 NRC Initial Test Program and Operational Programs Integrated Inspection Report 05200026-2023009 ML24031A6102024-01-31031 January 2024 Cyber Security Inspection Report 05200026/2024401 - Public IR 05000424/20244032024-01-26026 January 2024 Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection 05000424/2024403; 05000425/2024403 ML23312A3502023-11-14014 November 2023 – Integrated Inspection Report 05200026/2023003 ML23318A4582023-11-14014 November 2023 Integrated Inspection Report 05200025/2023003 IR 05000424/20234022023-11-0606 November 2023 – Security Baseline Inspection Report 05000424/2023402 and 05000425/2023402 IR 05000424/20230032023-10-27027 October 2023 Integrated Inspection Report 05000424/2023003 and 05000425/2023003 ML23254A2032023-09-13013 September 2023 – Initial Test Program and Operational Programs Inspection Report 05200025/2023013 IR 05000424/20230912023-09-0505 September 2023 Plan Units 1 and 2 - NRC Investigation Report 2-2022-006 and Notice of Violation - NRC Inspection Report 05000424/2023091 and 05000425/2023091 ML23234A3002023-09-0101 September 2023 NRC Integrated Inspection Report 05200026/2023003 IR 05000424/20230052023-08-29029 August 2023 Updated Inspection Plan for Vogtle Electric Generating Plant, Units 1 & 2 - Report 05000424/2023005 and 05000425/2023005 ML23223A0022023-08-14014 August 2023 Integrated Inspection Report 05200025/2023002 IR 05000424/20230112023-08-11011 August 2023 Biennial Problem Identification and Resolution Inspection Report 05000424/2023011 and 05000425/2023011 ML23215A0822023-08-0404 August 2023 (Vego), Unit 3 – Initial Test Program and Operational Programs Integrated 05200025/2023011 Inspection Report IR 05000424/20234012023-07-31031 July 2023 Security Baseline Inspection Report 05000424/2023401 and 05000425/2023401 (Cover Letter) ML23212B0612023-07-31031 July 2023 Security Baseline Inspection Report 05200025/2023401 ML23216A0962023-07-26026 July 2023 Document Request for Vogtle 1 & 2 RP Inspection, Report No. 05000424/2023003 and 05000425/2023003 IR 05000424/20230022023-07-24024 July 2023 Integrated Inspection Report 05000424/2023002 and 05000425/2023002 ML23198A3802023-07-19019 July 2023 NRC Integrated Inspection Report 05200026/2023002 ML23199A0892023-07-18018 July 2023 Initial Test Program and Operational Programs Integrated Inspection Report 05200026/2023007 IR 05000424/20233012023-06-30030 June 2023 – NRC Operator License Examination Report 05000424/2023301 and 05000425/2023301 ML23128A2932023-05-11011 May 2023 NRC Integrated Inspection Report 05200026/2023001 ML23129A0222023-05-10010 May 2023 Integrated Report 05200025/2023001 ML23128A3492023-05-0909 May 2023 – Initial Test Program and Operational Programs Integrated Inspection Report 05200026/2023006 ML23121A3202023-05-0404 May 2023 NRC Initial Test Program and Operational Programs Integrated Inspection Report 05200025/2023010 IR 05000424/20040252023-04-28028 April 2023 Public Meeting Summary - Vogtle Electric Generating Plant, Units 1, 2, 3, & 4 Docket No. 5000424, 5000425, 5200025, 5200026, Meeting Number 20230375 IR 05000424/20230012023-04-26026 April 2023 Integrated Inspection Report 05000424/2023001 and 05000425/2023001 IR 05000424/20230902023-03-30030 March 2023 NRC Inspection Report 05000424/2023090 and 05000425/2023090, and Investigation Report 2-2022-006; and Apparent Violation ML23083B3702023-03-24024 March 2023 Security Baseline Inspection Report 05200026/2023401 IR 05000424/20220062023-03-0101 March 2023 Annual Assessment Letter for Vogtle Electric Generating Plant Units 1 and 2, NRC Inspection Reports 05000424/2022006 and 05000425/2022006 ML23044A3902023-02-14014 February 2023 Integrated Inspection Report05200025 2022007 ML23040A0422023-02-0909 February 2023 NRC Initial Test Program and Operational Programs Integrated Inspection Report 05200025/2022008 ML23040A3612023-02-0909 February 2023 – NRC Initial Test Program and Operational Programs Integrated Inspection Report 05200026/2022008 2024-08-26
[Table view] Category:Letter
MONTHYEARIR 05000424/20243012024-11-19019 November 2024 Operator Licensing Examination Approval 05000424/2024301 and 05000425/2024301 ML24313A0632024-11-14014 November 2024 Integrated Inspection Report and Assessment Follow-Up Letter 05200025/2024003 and 05200026/2024003 ML24305A1662024-11-0606 November 2024 Vogle Electric Generating Plant, Unit 3 - Summary of Conference Call Regarding the Fall 2024 Steam Generator Tube Inspections NL-24-0217, License Amendment Request: Source Range Neutron Flux Doubling Function Applicability2024-11-0101 November 2024 License Amendment Request: Source Range Neutron Flux Doubling Function Applicability NL-24-0385, Request for Action Matrix Deviation Due to Recent Events Impacting the Unplanned Scram with Complications Performance Indicator2024-10-31031 October 2024 Request for Action Matrix Deviation Due to Recent Events Impacting the Unplanned Scram with Complications Performance Indicator IR 05000424/20240032024-10-30030 October 2024 – Integrated Inspection Report 05000424/2024003 and 05000425/2024003 NL-24-0386, License Amendment Request: Changes to Technical Specification 3.7.6, Main Control Room Emergency Habitability System (Ves) Air Storage Tanks Response to Request for Additional Information2024-10-28028 October 2024 License Amendment Request: Changes to Technical Specification 3.7.6, Main Control Room Emergency Habitability System (Ves) Air Storage Tanks Response to Request for Additional Information NL-24-0392, Response to Requests for Additional Information Related to Proposed Alternative GEN-ISI-AL T-2024-0022024-10-28028 October 2024 Response to Requests for Additional Information Related to Proposed Alternative GEN-ISI-AL T-2024-002 NL-24-0366, Core Operating Limits Report, Cycle 26, Version 12024-10-25025 October 2024 Core Operating Limits Report, Cycle 26, Version 1 ML24297A6482024-10-23023 October 2024 5 to the Updated Final Safety Analysis Report, Technical Specification Bases Changes, Technical Requirements Manual Changes, Summary Report and Revised NRC Commitments Report ML24269A2502024-09-26026 September 2024 Acknowledgement of the Withdrawal of the Requested Exemption and License Amendment Request to Remove Tier 1 and Tier 2* Requirements NL-24-0369, Withdrawal of License Amendment Request and Exemption Request: Remove Tier 1 and Tier 2 Requirements2024-09-25025 September 2024 Withdrawal of License Amendment Request and Exemption Request: Remove Tier 1 and Tier 2 Requirements NL-24-0350, Core Operating Limits Report, Cycle 24, Version 22024-09-25025 September 2024 Core Operating Limits Report, Cycle 24, Version 2 ML24243A0072024-09-10010 September 2024 – Correction of Amendment Nos. 223 and 206 Regarding Revision to Technical Specifications to Adopt TSTF-339-A, Relocate Technical Specification Parameters to the COLR Consistent with WCAP-14483 NL-24-0337, Interim 10 CFR 21.21(a)(2) Report Regarding Operation Technology, Inc., ETAP Software Error in Transient Stability Program2024-09-0909 September 2024 Interim 10 CFR 21.21(a)(2) Report Regarding Operation Technology, Inc., ETAP Software Error in Transient Stability Program ML24102A2642024-09-0909 September 2024 – Exemption Request Regarding Final Safety Analysis Report Update Schedule (EPID L-2024-LLE-0013) - Letter ML24249A2942024-09-0606 September 2024 Correction of Amendment Nos. 218 and 201 Regarding Revision to Technical Specifications to Use Online Monitoring Methodology 05200025/LER-2024-002, Manual Reactor Protection System and Automatic Safeguards Actuation Due to an Unexpected Change in Position of a Main Feedwater Pump Minimum Flow Control Valve2024-09-0505 September 2024 Manual Reactor Protection System and Automatic Safeguards Actuation Due to an Unexpected Change in Position of a Main Feedwater Pump Minimum Flow Control Valve IR 05000424/20240052024-08-26026 August 2024 Updated Inspection Plan for Vogtle Electric Generating Plant, Units 1 and 2 - Report 05000424/2024005 and 05000425/2024005 ML24235A1952024-08-22022 August 2024 Updated Inspection Plan for Vogtle Electric Generating Plant, Units 3 and 4 - Report 05200025/2024005 and 05200026/2024005 IR 05000424/20244012024-08-15015 August 2024 4 - Security Baseline Inspection Report 05000424-2024401, 05000425-2024401, 05200025-2024402, and 05200026-2024403 - Cover Letter NL-24-0299, Exemption Request: Final Safety Analysis Report Update Schedule, Response to Request for Additional Information2024-08-14014 August 2024 Exemption Request: Final Safety Analysis Report Update Schedule, Response to Request for Additional Information 05000425/LER-2024-001, Manual Actuation of the Reactor Protection System Due to a Rod Control Fuse Opening Causing a Misaligned Shutdown Rod2024-08-0909 August 2024 Manual Actuation of the Reactor Protection System Due to a Rod Control Fuse Opening Causing a Misaligned Shutdown Rod ML24218A1842024-08-0707 August 2024 Examination Report and Cover Letter 05200026/LER-2024-001, Manual Reactor Protection System Actuation Due to Procedure Not Optimally Sequenced to Reset the Rapid Power Reduction Signal2024-08-0606 August 2024 Manual Reactor Protection System Actuation Due to Procedure Not Optimally Sequenced to Reset the Rapid Power Reduction Signal ML24212A1442024-08-0101 August 2024 Integrated Inspection Report 05200025/2024002 and 05200026/2024002 IR 05000424/20240022024-07-29029 July 2024 Integrated Inspection Report 05000424/2024002 and 05000425/2024002 IR 05000424/20244042024-07-26026 July 2024 Material Control and Accounting Program Inspection Report 05000424/2024404 and 05000425/2024404 (Cover Letter) NL-24-0126, – Units 3 and 4, License Amendment Request: Changes to Technical Specification 3.7.6, Main Control Room Emergency Habitability System (Ves) Action a and SR 3.7.6.62024-07-25025 July 2024 – Units 3 and 4, License Amendment Request: Changes to Technical Specification 3.7.6, Main Control Room Emergency Habitability System (Ves) Action a and SR 3.7.6.6 NL-24-0282, License Amendment Request and Exemption Request: Remove Tier 1 and Tier 2* Requirements2024-07-25025 July 2024 License Amendment Request and Exemption Request: Remove Tier 1 and Tier 2* Requirements ML24204A0722024-07-23023 July 2024 Issuance of Amendment No. 225, Regarding LAR to Revise TS 3.7.9 for a one-time Change to Support Nuclear Service Cooling Water Transfer Pump Repairs - Emergency Circumstances NL-24-0286, Emergency Request to Revise Technical Specification 3.7.9 for a One-Time Change to Support a Unit 1 Nuclear Service Cooling Water Transfer Pump Repair2024-07-20020 July 2024 Emergency Request to Revise Technical Specification 3.7.9 for a One-Time Change to Support a Unit 1 Nuclear Service Cooling Water Transfer Pump Repair NL-24-0261, 10 CFR 50.46 ECCS Evaluation Model Annual Report for 20232024-07-19019 July 2024 10 CFR 50.46 ECCS Evaluation Model Annual Report for 2023 ML24191A4562024-07-19019 July 2024 Request for Relief and Alternative Requirements for Squib (Explosively Actuated) Valves First Test Interval ML24194A0342024-07-12012 July 2024 Review of the Refueling Outage 1R24 Steam Generator Tube Inspection Report ML24191A3792024-07-10010 July 2024 – Initial Test Program and Operational Programs Inspection Report 05200026/2024011 NL-24-0227, Proposed Inservice Inspection Alternative GEN-ISI-AL T-2024-03 for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1)2024-07-0303 July 2024 Proposed Inservice Inspection Alternative GEN-ISI-AL T-2024-03 for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1) NL-24-0234, Application to Revise Technical Specifications to Adopt TSTF-589, Eliminate Automatic Diesel Generator Start During Shutdown2024-06-28028 June 2024 Application to Revise Technical Specifications to Adopt TSTF-589, Eliminate Automatic Diesel Generator Start During Shutdown NL-24-0143, Proposed Alternative to Use ASME Code Case N-752, Risk-Informed Categorization and Treatment for Repair/ Replacement Activities in2024-06-27027 June 2024 Proposed Alternative to Use ASME Code Case N-752, Risk-Informed Categorization and Treatment for Repair/ Replacement Activities in NL-24-0087, License Amendment Request: Changes to Technical Specification 3.7.6, Main Control Room Emergency Habitability System (Ves) Air Storage Tanks2024-06-21021 June 2024 License Amendment Request: Changes to Technical Specification 3.7.6, Main Control Room Emergency Habitability System (Ves) Air Storage Tanks NL-24-0201, Proposed Inservice Inspection Alternative GEN-ISI-ALT-2024-002 for Steam Generator Welds in Accordance with 10 CFR 50.55a(z)(1)2024-06-18018 June 2024 Proposed Inservice Inspection Alternative GEN-ISI-ALT-2024-002 for Steam Generator Welds in Accordance with 10 CFR 50.55a(z)(1) NL-24-0243, Registration of Spent Fuel Cask Use2024-06-18018 June 2024 Registration of Spent Fuel Cask Use ML24163A0632024-06-12012 June 2024 2024 Licensed Operator Re-qualification Inspection Notification Letter Vogtle, Units 3 & 4 ML24155A1772024-06-0505 June 2024 Regulatory Audit in Support of Review of the LAR to Revise Emergency Diesel Generator Frequency and Voltage Ranges for Technical Specification 3.8.1, Surveillance Requirements NL-24-0202, SNC Response to Regulatory Issue Summary 2024-01: Preparation and Scheduling of Operator Licensing Examinations2024-05-24024 May 2024 SNC Response to Regulatory Issue Summary 2024-01: Preparation and Scheduling of Operator Licensing Examinations ML24141A0482024-05-17017 May 2024 EN 56958_1 Ametek Solidstate Controls, Inc ML24094A1402024-05-16016 May 2024 Staff Response to Request for Revision to NRC Staff Assessment of Updated Seismic Hazard Information and Latest Understanding of Seismic Hazards at the Vogtle Plant Site Following the NRC Process for the Ongoing Assessment of Natural Hazard ML24120A1812024-05-13013 May 2024 Request for Withholding Information from Public Disclosure Responses to NRC Request for Additional Information for Refueling Outage IR24 Steam Generator Tube Inspection Report – Enclosure 2 ML24130A2412024-05-13013 May 2024 Integrated Inspection Report 05200025/2024001 and 05200026/2024001 ML24101A2112024-05-11011 May 2024 Expedited Issuance of Amendment No. 198 Change to Technical Specification 5.5.13, Ventilation Filter Testing Program (VFTP) 2024-09-09
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Inspection Report - Vogtle - 2008009 |
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UNITED STATES NUCLEAR REGULATORY COMMISSION
REGION II
ary 9, 2009
SUBJECT:
VOGTLE ELECTRIC GENERATING PLANT - NRC SUPPLEMENTAL INSPECTION REPORT 05000424/2008009 AND 05000425/2008009
Dear Mr. Tynan:
On December 11, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed a supplemental inspection in accordance with Inspection Procedure 95001, Inspection for One or Two White Inputs in a Strategic Performance Area, at your Vogtle Electric Generating Plant, Units 1 and 2. The purpose of the inspection was to examine the circumstances surrounding the White performance indicators reported during the fourth quarter of 2007 for the Unit 1 and Unit 2 Cooling Water Mitigating Systems Performance Index. The enclosed inspection report documents the inspection results, which were discussed on December 11, 2008, with Mr. Todd Youngblood and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspector reviewed selected procedures and records and interviewed personnel. Based on the results of this inspection, no findings of significance were identified.
In accordance with the Code of Federal Regulations 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosures, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Scott M. Shaeffer, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos.: 50-424, 50-425 License Nos.: NPF-68 and NPF-81
Enclosure:
Inspection Report 05000424/2008009 and 05000425/2008009 w/Attachment: Supplemental Information
REGION II==
Docket Nos.: 50-424, 50-425 License Nos.: NPF-68, NPF-81 Report Nos.: 05000424/2008009 and 05000425/2008009 Licensee: Southern Nuclear Operating Company, Inc.
Facility: Vogtle Electric Generating Plant, Units 1 and 2 Location: Waynesboro, GA 30830 Dates: August 20 - December 11, 2008 Inspector: G. McCoy, Senior Resident Inspector Approved by: Scott M. Shaeffer, Chief Reactor Projects Branch 2 Division of Reactor Projects Enclosure
SUMMARY OF FINDINGS
IR 05000424/2008-009, 05000425/2008-009; August 20, 2008 - December 11, 2008; Vogtle
Electric Generating Plant, Units 1 and 2; Supplemental Inspection IP 95001 for a reported White Mitigating Systems Performance Index, Cooling Water System Performance Indicator.
This inspection was conducted by a senior resident inspector. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
Cornerstone: Mitigating Systems
The U.S Nuclear Regulatory Commission (NRC) performed this supplemental inspection in accordance with Inspection Procedure 95001 to assess the licensees evaluation associated with a White Mitigating Systems Performance Indicator, Cooling Water Systems Performance Indicator reported during the fourth quarter of 2007 and later retracted during the first quarter of 2008. The inspector determined that the decision to retract the White performance indicator was supported by the guidance of NEI 99-02, Regulatory Assessment Performance Indicator Guideline.
NRC-Identified and Self-Revealing Findings
No significance of findings were identified.
Licensee-Identified Violations
None.
REPORT DETAILS
INSPECTION SCOPE
The U.S. Nuclear Regulatory Commission (NRC) performed this supplemental inspection to assess the licensees evaluation of a White Mitigating System Performance Index (MSPI),
Cooling Water Systems Performance Indicator (PI) for Unit 1 and Unit 2. The White PI was reported for Unit 1 for the fourth quarter 2007 and for Unit 2 for the third quarter 2007. Both PIs were re-reported Green during the first quarter 2008. This was based on the licensee re-evaluating their NSCW unavailability which caused the PIs to initially be reported as White. This inspection reviewed this re-evaluation which lead the licensee to revise the previously reported White PIs for both units.
Background On October 12, 2007, operators took manual control of the Unit 1 train A Nuclear Service Cooling Water (NSCW) tower return valves to calibrate temperature instrument 1T1668. The Shift Supervisor questioned the operability of the 1A NSCW system while the temperature instrument was being calibrated. This issue was documented in condition report (CR)2007110639. In January 2008, when the licensee was required to submit PI data for the fourth quarter 2007, the licensee conservatively determined that the train A NSCW system was inoperable without the knowledge of the operators and counted the duration the temperature instrument was being calibrated as unavailability time against the Unit 1 MSPI, Cooling Water Systems PI. The licensee reviewed the control room logs and identified that a similar condition had occurred in August 2007 on Unit 2 train B NSCW system. The licensee also counted this duration as unavailability against the Unit 2 MSPI, Cooling Water Systems PI. In conjunction with previous reported unavailability time in the NSCW system, these additional conditions caused the Unit 1 MSPI, Cooling Water Systems PI to cross the Green to White threshold in the fourth quarter of 2007. The Unit 2 MSPI, Cooling Water Systems PI was also reported as White for the fourth quarter of 2007 and retroactively for the third quarter of 2007.
During the first quarter of 2008, the licensee completed a detailed review of these two conditions and determined that in both cases the NSCW Ultimate Heat Sink and the Cooling Water design functions could be met during temperature instrument calibration. The licensee determined the NSCW system remained available in accordance with the guidance of NEI 99-02. Based on this determination, the licensee removed the previously reported unavailability from the PI data for both Unit 1 and Unit 2, reported the PIs as Green for the first quarter of 2008 and retroactively changed the previously reported White PIs to Green starting third quarter of 2007. The NRC has endorsed the guidance of NEI 99-02 for the determination of system availability for PI data reporting purposes. In accordance with this guideline, operator actions can be credited towards system availability if the function can be promptly restored by an operator in the control room, restoration actions are uncomplicated, contained in a written procedure, not require diagnosis or repair, and must be capable of being restored in time to satisfy Probability Risk Assessment (PRA) success criteria. The inspector determined that while the cooling tower was bypassed, plant operating procedure 1350-1, Nuclear Service Cooling Water System Operating Procedure, required the monitoring of NSCW return temperature in the control room and provided actions to be taken if NSCW return temperature limits were exceeded.
The operation of a single switch on the control board in main control room would return cooling to the NSCW cooling loop, even if temperature instrument 1T1668 was out of service. The inspectors determined that the NSCW system could be considered available for MSPI reporting purposes and that the licensee properly reported the PI as Green for the third and fourth quarters of 2007. The inspector noted that the licensee has modified the procedures for taking manual control of the NSCW tower return valves to make this plant condition more evident to the operators by requiring a caution tag be placed on the NSCW cooling tower return valve control switch anytime it is out of the automatic position.
In addition, the inspector reviewed the associated condition reports, reviewed the cause determinations performed, and reviewed the operability determinations. Inspector also interviewed operations and licensing personnel to understand the basis for their decisions.
During this inspection, the inspector questioned the licensees determination that the NSCW system was operable with the NSCW cooling tower return valves in manual control. The inspector noted that the NSCW system is a support system for the Ultimate Heat Sink, and without the proper operation of the NSCW cooling tower return valves the Ultimate Heat Sink would not be able to accomplish its design function during a design basis accident. The inspector also noted there is no provision in the technical specifications, the USFAR nor the safety evaluations written by the NRC for the NSCW system which evaluates the operation of the system with manual control of the tower return valves without declaring the NSCW system inoperable and entering the TS action Limiting Condition for Operability (LCO). This issue is identified as an unresolved item (URI)05000424/2008009-01, Technical Specification Operability Of The NSCW System With The Cooling Tower Return Valves In Manual Control.
EVALUATION OF INSPECTION REQUIREMENTS 02.01 Problem Identification a.
Determination of who (i.e., licensee, self-revealing, or NRC) identified the issue and under what conditions.
The potential unavailability of the NSCW system was identified by the licensee when system operability was questioned while temperature instrument 1T1668 was being calibrated.
b.
Determination of how long the issue existed, and prior opportunities for identification.
This issue existed on October 12, 2007, while temperature instrument 1T1668 was being calibrated. A previous case was identified in August 2007 when 2T1669 was being calibrated.
c.
Determination of the plant-specific risk consequences (as applicable) and compliance concerns associated with the issue.
Because of the compensatory actions (monitoring temperature, etc) taken during temperature instrument calibration, the licensee determined that the risk consequences was minimal. No compliance concerns were identified because the licensee properly reported the PI data.
02.02 Root Cause and Extent of Condition Evaluation Because the NSCW system was determined to be available while the temperature instrument was being calibrated, no cause evaluation was performed by the licensee.
The licensee determined that manual operation of NSCW tower return valves during temperature instrument calibration was consistent with other manual actions for this system where sufficient time and methods were provided to ensure the safety function of the system was maintained.
02.03 Corrective Actions No corrective actions were required or performed by the licensee because the NSCW system was determined to be available. However, the licensee modified plant procedures for taking manual control of the NSCW tower return valves to make this plant condition more evident to the operators by requiring a tag be placed on the NSCW cooling tower return valve control switch anytime it was out of the automatic position.
They also modified the plant emergency procedures to verify proper operation of the tower return valves if the control switch needed to be repositioned. These actions were considered to enhance the operators ability to maintain the NSCW system available.
The inspector determined that the licensee properly determined that the NSCW system was available during temperature instrument 1T1668 calibration. The inspector also determined the licensee properly reported the PI as Green for the third and fourth quarters of 2007.
MANAGEMENT MEETINGS
Exit Meeting Summary
The inspector presented the results of the supplemental inspection to Mr. Todd Youngblood and other members of licensee management and staff on December 11, 2008. The inspector confirmed that no proprietary information was provided or examined during the inspection.
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- M. Hickox, Licensing Engineer
- J. Stringfellow, Licensing Manager
- D. Vineyard, Operations Manager
- T. Youngblood, Engineering Manager
LIST OF ITEMS
OPENED AND CLOSED
Opened and Closed
- 05000424, 425/2008009-01 URI Technical Specification Operability Of The NSCW System With The Cooling Tower Return Valves In Manual Control. (Section 01)
LIST OF DOCUMENTS REVIEWED