ML17252B552: Difference between revisions
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| issue date = 06/05/1980 | | issue date = 06/05/1980 | ||
| title = LER 80-017/03L-0 for Dresden, Unit 2 Re Double Valve Indication Was Observed on the HPCI Inboard Isolation Valve. Upon Trying to Cycle the Valve, the Valve Failed to Close | | title = LER 80-017/03L-0 for Dresden, Unit 2 Re Double Valve Indication Was Observed on the HPCI Inboard Isolation Valve. Upon Trying to Cycle the Valve, the Valve Failed to Close | ||
| author name = Stephenson | | author name = Stephenson B | ||
| author affiliation = Commonwealth Edison Co | | author affiliation = Commonwealth Edison Co | ||
| addressee name = Keppler J | | addressee name = Keppler J | ||
| addressee affiliation = NRC/RGN-III | | addressee affiliation = NRC/RGN-III | ||
| docket = 05000237 | | docket = 05000237 | ||
Line 14: | Line 14: | ||
| document type = Letter, Licensee Event Report (LER) | | document type = Letter, Licensee Event Report (LER) | ||
| page count = 2 | | page count = 2 | ||
}} | }} | ||
=Text= | |||
{{#Wiki_filter:*** | |||
e Commonwec9 Edison Dresden Nuclear Power Station R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 June 5, 1980 BBS Ltr. /180-476 James G. Keppler, Regional Director Directorate of Regulatory Operations - Region. III U.S. Nuclear Regulatory Commission* | |||
799 Roosevelt Road Glen Ellyn, IL 60137 | |||
*Reportable Occurrence Report /180-17/031-0, Docket /1050-237, is being submitted to your office in accordance with Dresden Nuclear Power Station Technical Specific*ation 6.6.B.2.(b), conditions leading to operation in a degraded mode permitted by a limiting condition for operation or plant shutdown required by a limiting condition for operation. | |||
,~~?~. | |||
B. B. Stephenson~ | |||
Station Superintendent Dresden Nuclear Power Station BBS/nh Enclosure cc/ Director of Inspection & Enforcement Director of Management Information & Program Control File/NRC | |||
LICENSEE EVENT REPORT | |||
., CONTROL BLOCK: I* | |||
1----.1....,_..1-__.....__._...._;;;._-'s\..!J I10 (PLEASE PRIN.T ORTYPAIL REQUIRED INFORMATIO~J | |||
~ I II L I D I R I s I 2 101 0 I 0 I - I 0 I 0 I 0 I 0 I 0 I - I 0 I 0 IQ)I 4 11 I 1 11 I 1 1G)I I I.@ | |||
~ 9 LICENSEE. CODE . 14 15 | |||
* LlCENSE NUMBER 25 26. LICENSE TYPE. JO 57 CAT 58 . | |||
CON'T | |||
~ :;~~~; ~©I o I s 1o I o I o I 2 13 11 101 o1 s 1 1 12 I a 1o I© 1 o I 6. 1 o I s I a I o 1G) | |||
~ 60 61 DOCKET NUMBER 68 69 . EVENT DATE 74 75 REPORT DATE ao EVENT DESCRIPTION A":'D PROBABLE_CONSEQUENCES@ | |||
}o I 2 I I *Following a uni"t scram, double* valve indication was observed on the HPCI-inboard j 0 13 I: isolation valve *. Upon trying to cycle. the valve, the valve failed to close (T.S.3.7.D.l). The health and safety of the public was not endangered because the l0 14 I | |||
) 0 I sJ I HPCI steam line was isolable _ via the outboard isolation valve and other ECCS systems | |||
- 0 Is I* were operable. 'J'his - is the first occurrence of* this type. | |||
I l a ,,7 r 1Cr'Tal". L,___;_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,__,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_-,---,-..,_-,-..,_..,_...:.._..,_..,_..,_..,_..,_..,_..,_..,_~ | |||
~ 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE COiJE SUBCOOE COMPONENT.CODE SUB CODE SUBCOOE ISIFI@ L!J@ w@ lvlAILlvlolPI@ L!J@) | |||
9 . 10 11 12 13 18 19 w@ | |||
20 SEQUENTIAL OCCURRENCE AEPOP.T REVISION. | |||
~ LEA/AO CV ENT YEAR. REPORT NO. CODE TYPE NO. | |||
~ .REPORT NUMBER I 8 I.0 I* I l I 0 I l I 7I I ........ , I 0 I 31 LEJ 1=J ~ | |||
_ 21 22 23 24 . 26 27 28 29 JO 31 ACTION FUTURE EFFECT SHUTDOWN ~ ATTACHMENT NPR0-4 PRIME COMP. COMPONENT TAKEN ACT.ION' ON PLANT METHOD . . HOURS' ''_SUBMITTED FORM :;us. SUPPLIER. MANUFACTURER - ---**-* | |||
. 33~@~@* . 34 ' . 35 L:J@. L.:J@ | |||
35* . | |||
I J-7 0 | |||
I 0 I 0 I 40.I L!:J@ 41 . . | |||
l:J<§ 42 | |||
-~. I L I 2 I 0 I 0 I@ . | |||
44 . . .. 47 - -~- | |||
43 | |||
.CAUSE DESCRIPTION AND CORRECTIVE ACTIONS@ . | |||
, , I0 I r The failure was due to a packing leak on the valve' causing water to enter the valve | |||
) 1 11 t .I _motor operator. The mo.tor dr:!,ed out and the valve was rep~cked and. cycled 1-successfully. N_o further action deemed necessary. | |||
) 1 I2 I | |||
::IJJ]*'L,_;._;_-.,--.,--.,--.,-_;__-.,--.,--.,--.,--.,--.,--.,--.,--.,--.,--.,--.,--.,-~-.,--.,-~-.,--.,--.,--.,--.,------.,-~~~~~ | |||
~8-9~..............._,......._._..................,_...;.................-.--.--.--.--.---'-.-..--.--.--.--.--.--..,..-.--,---,---,---,---,---,---,---,---,---,---.,..-,---,--..--,---.--.-....... _ | |||
~ 80* | |||
FACILITY 13Q\ METHOD OF (:;':;\ | |||
re uu@ *1 I 0* | |||
STATUS 9 | |||
ACTIVITY 10 0 | |||
CONTENT | |||
% POWER o_ | |||
12 n OTHER STATUS I 0 l@).._I..;,;,.N:..:.IA=--------~ | |||
~ | |||
(.;;;'\ | |||
DISCOVERY 45 46 DISCOVERY OESCRIPTlON ~ _ | |||
ll.JQ2)~1.........~O~p~e~r~a~t~or-=-O~b~s~e~rv;;;...;..;a~t~1~*o~n-=-...............................................................___.*I 80 RELEASED OF RELEASE. AMOUNT OF ACTIVITY ~ LOCATION OF RELEA~E@ | |||
7161.. LU@ W(§ 1. . ._..;N~/-=A_ __,___ __.,....l N/A | |||
~ 9 10 11 44 45. 80 | |||
?ERSONNEL EXPOSURES * . *-Q_ | |||
: m. ro 8 9 NUMBER 1 o 1o 11 A | |||
'l2J@~ | |||
TYPE 12 | |||
. OESCRIPTlON 13 | |||
...:..;N..:...;/A:.:...._ _.....;__ _ _ _._,.;.___ _ _ _ _ _ _ _ _ _ _ _ _- - - - ' | |||
so PERSONNEL INJURIES* * (,;"";\ | |||
:CW* 8 9 NUMBER I0 I 0 I0 11 I@~--- | |||
OESCRIPTION6 12. | |||
__* -*_N..;,._/A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __,___, | |||
* 00 LOSS OF OR DAMAGE TO FACl.LJTY f'43\ | |||
TYPE DESCRIPTION* ".:::::) | |||
3TI: LU@ | |||
8- 9 10 | |||
. ~/A 80. | |||
PUBLICITY (';;;\ | |||
NR.C USE ONLY ISSUED/,;";;\ DESCRIPTION~ | |||
:IT£J;. l.::J'6 N /A 1111111111111~ | |||
: 8. 9 IQ. 68 69 80*; | |||
K. Zirwas X-529 0 a. | |||
N A,'/i E CF PP. E P.t\ RE A 1,....,_,_,....':;miiimi--t"-"llAilliiiii_ii!l__.,.limiilll. .r'"*W;iiill'll}} |
Latest revision as of 10:44, 4 February 2020
ML17252B552 | |
Person / Time | |
---|---|
Site: | Dresden |
Issue date: | 06/05/1980 |
From: | Stephenson B Commonwealth Edison Co |
To: | James Keppler NRC/RGN-III |
References | |
BBS LTR 80-476 LER 80-017/03L-0 | |
Download: ML17252B552 (2) | |
Text
e Commonwec9 Edison Dresden Nuclear Power Station R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 June 5, 1980 BBS Ltr. /180-476 James G. Keppler, Regional Director Directorate of Regulatory Operations - Region. III U.S. Nuclear Regulatory Commission*
799 Roosevelt Road Glen Ellyn, IL 60137
- Reportable Occurrence Report /180-17/031-0, Docket /1050-237, is being submitted to your office in accordance with Dresden Nuclear Power Station Technical Specific*ation 6.6.B.2.(b), conditions leading to operation in a degraded mode permitted by a limiting condition for operation or plant shutdown required by a limiting condition for operation.
,~~?~.
B. B. Stephenson~
Station Superintendent Dresden Nuclear Power Station BBS/nh Enclosure cc/ Director of Inspection & Enforcement Director of Management Information & Program Control File/NRC
LICENSEE EVENT REPORT
., CONTROL BLOCK: I*
1----.1....,_..1-__.....__._...._;;;._-'s\..!J I10 (PLEASE PRIN.T ORTYPAIL REQUIRED INFORMATIO~J
~ I II L I D I R I s I 2 101 0 I 0 I - I 0 I 0 I 0 I 0 I 0 I - I 0 I 0 IQ)I 4 11 I 1 11 I 1 1G)I I I.@
~ 9 LICENSEE. CODE . 14 15
- LlCENSE NUMBER 25 26. LICENSE TYPE. JO 57 CAT 58 .
CON'T
~ :;~~~; ~©I o I s 1o I o I o I 2 13 11 101 o1 s 1 1 12 I a 1o I© 1 o I 6. 1 o I s I a I o 1G)
~ 60 61 DOCKET NUMBER 68 69 . EVENT DATE 74 75 REPORT DATE ao EVENT DESCRIPTION A":'D PROBABLE_CONSEQUENCES@
}o I 2 I I *Following a uni"t scram, double* valve indication was observed on the HPCI-inboard j 0 13 I: isolation valve *. Upon trying to cycle. the valve, the valve failed to close (T.S.3.7.D.l). The health and safety of the public was not endangered because the l0 14 I
) 0 I sJ I HPCI steam line was isolable _ via the outboard isolation valve and other ECCS systems
- 0 Is I* were operable. 'J'his - is the first occurrence of* this type.
I l a ,,7 r 1Cr'Tal". L,___;_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,__,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_..,_-,---,-..,_-,-..,_..,_...:.._..,_..,_..,_..,_..,_..,_..,_..,_~
~ 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE COiJE SUBCOOE COMPONENT.CODE SUB CODE SUBCOOE ISIFI@ L!J@ w@ lvlAILlvlolPI@ L!J@)
9 . 10 11 12 13 18 19 w@
20 SEQUENTIAL OCCURRENCE AEPOP.T REVISION.
~ LEA/AO CV ENT YEAR. REPORT NO. CODE TYPE NO.
~ .REPORT NUMBER I 8 I.0 I* I l I 0 I l I 7I I ........ , I 0 I 31 LEJ 1=J ~
_ 21 22 23 24 . 26 27 28 29 JO 31 ACTION FUTURE EFFECT SHUTDOWN ~ ATTACHMENT NPR0-4 PRIME COMP. COMPONENT TAKEN ACT.ION' ON PLANT METHOD . . HOURS' _SUBMITTED FORM :;us. SUPPLIER. MANUFACTURER - ---**-*
. 33~@~@* . 34 ' . 35 L:J@. L.:J@
35* .
I J-7 0
I 0 I 0 I 40.I L!:J@ 41 . .
l:J<§ 42
-~. I L I 2 I 0 I 0 I@ .
44 . . .. 47 - -~-
43
.CAUSE DESCRIPTION AND CORRECTIVE ACTIONS@ .
, , I0 I r The failure was due to a packing leak on the valve' causing water to enter the valve
) 1 11 t .I _motor operator. The mo.tor dr:!,ed out and the valve was rep~cked and. cycled 1-successfully. N_o further action deemed necessary.
) 1 I2 I
- IJJ]*'L,_;._;_-.,--.,--.,--.,-_;__-.,--.,--.,--.,--.,--.,--.,--.,--.,--.,--.,--.,--.,-~-.,--.,-~-.,--.,--.,--.,--.,------.,-~~~~~
~8-9~..............._,......._._..................,_...;.................-.--.--.--.--.---'-.-..--.--.--.--.--.--..,..-.--,---,---,---,---,---,---,---,---,---,---.,..-,---,--..--,---.--.-....... _
~ 80*
FACILITY 13Q\ METHOD OF (:;':;\
re uu@ *1 I 0*
STATUS 9
ACTIVITY 10 0
CONTENT
% POWER o_
12 n OTHER STATUS I 0 l@).._I..;,;,.N:..:.IA=--------~
~
(.;;;'\
DISCOVERY 45 46 DISCOVERY OESCRIPTlON ~ _
ll.JQ2)~1.........~O~p~e~r~a~t~or-=-O~b~s~e~rv;;;...;..;a~t~1~*o~n-=-...............................................................___.*I 80 RELEASED OF RELEASE. AMOUNT OF ACTIVITY ~ LOCATION OF RELEA~E@
7161.. LU@ W(§ 1. . ._..;N~/-=A_ __,___ __.,....l N/A
~ 9 10 11 44 45. 80
?ERSONNEL EXPOSURES * . *-Q_
- m. ro 8 9 NUMBER 1 o 1o 11 A
'l2J@~
TYPE 12
. OESCRIPTlON 13
...:..;N..:...;/A:.:...._ _.....;__ _ _ _._,.;.___ _ _ _ _ _ _ _ _ _ _ _ _- - - - '
so PERSONNEL INJURIES* * (,;"";\
- CW* 8 9 NUMBER I0 I 0 I0 11 I@~---
OESCRIPTION6 12.
__* -*_N..;,._/A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __,___,
- 00 LOSS OF OR DAMAGE TO FACl.LJTY f'43\
TYPE DESCRIPTION* ".:::::)
3TI: LU@
8- 9 10
. ~/A 80.
PUBLICITY (';;;\
NR.C USE ONLY ISSUED/,;";;\ DESCRIPTION~
- IT£J;. l.::J'6 N /A 1111111111111~
- 8. 9 IQ. 68 69 80*;
K. Zirwas X-529 0 a.
N A,'/i E CF PP. E P.t\ RE A 1,....,_,_,....':;miiimi--t"-"llAilliiiii_ii!l__.,.limiilll. .r'"*W;iiill'll