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{{#Wiki_filter:;y                                                                                                  -
i ;,        f Of-                      .-                          NIHOINIA ELECTIllC AND POWT lt COMPANY Ricitwoxo,VinotutA enent
        ,                                                                                                                                i February 14,1991 o
i LU.S. N'uclear Regulatory Commission                                        Serial No.:      91 057
                              ' Attention: Document Control Desk                                          NL&P/RMN Washington, D.C. 20555 '                                                  Docket Nos.: 50 338 q
50 339 License Nos.: NPF 4 N PF          ,      ,
Gentlemen:
1^            '
VIRGINIA- ELECTRIC' ANu POWER COMPANY NORTH ANNA' POWER STATION UNITS 1 AND 2                                                                '
                                = PROPOSED- TECHNICAL SPECIFICATION CHANGES AUXILIARY FEEDWATER PUMP TESTING Pursuant 10:10 CFRl 50.90, the Virginla= Electric and Power Company requests Lamen.dments, in the form?of changes to the Technical Specifications, to Operating
                                ' License Numbers NPF-4 and NPF-7 for North Anna Power Station Units 1 and 2, respectively,'                                                                                        j 1The' proposed changes to the North Anna Units 1 and 2 Technical Specifice,tions will allow improvements to.the monthly auxiliary feedwater pump tests. These changes-are !ntended to replace our December 28,1989 request (letter serial nusbar 89-833).
                                ;NRC Bulletin 88-04 " Safety Related Pump Loss" identified uncerns with hydraulic instability in pumps operating near their shut off heads, in our August 8,1988 reply to
                              - that bulletin we committed to disassembling and inspecting the auxiliary feedwater                      '
  ,                            . pumps and to mir,!mize operation at low flow. The inspections indicated that some -                      ,
idegradation had occurred which was not revealed by the high pressure-low flow 4                    testing. The pumps have since been overhauled and our. quarterly ASME Section XI
                                ' testing procedures have been revised to allow full flow tests. . A new full flow recirculation line was added during the latest Unit 2 refueling outage and is being                    ,
installed during the current Unit 1 outage to permit full flow testing e' power without affecting the steam' generators or normal feedwater regulation. Ou, quarterly Section                    4 Xl testing is now done at flow conditions near the pump's best efficiency point. This lost p,ovides early warning of degradation and is similar to conditions when the pump p                              Lis perfc rming its safety function. If the monthly test could be done under similar p                                conditions, safety we. Id be enhanced because there would be less pump wear and more effective testing.
G l                                                                                                                                    od
"                      '9102210237 910214                  '
                        . DR              ADoCK 0500    8                                                                      ggy
    .          .      .          m      .                    .      _.        ._._ _ _          . . . .-          _ . _ .          fh
 
    . . _Li_ ~ y n                    '
: h 1. ;                              3 s                        '
This does not affect our MERITS submittal, tharefore a MERITS change is not attached.
LThe proposed; changes are provided in Attachments 1 and 2. A discussion of the
                    . L proposed changes:with the technical justification and safety evaluation of the
                            . proposed changes is provided in Attachment 3.-
Th!s requestihas been.' reviewed by the Station Nuclear Safety and Operating
                          -Committee;and the Management Safety Review Committee. It has been determined that this request does not involve an unreviewed safety question as defined in 10 CFR
              <          " 50.59 o_r a significant hazards consideration as defined in 10 CFR 50.92. The basis for jour determinglon that no significant hazards consideration is involved is presented in
                            ' Attachment 4.
Because of the need .to revise procedures, please allow us 60 days to implement
:these changes from the' dates of issuance. Should you have any questions or require                              l
                            ' additional information, please contact us at your earliest convenience.
                          > Very truly ud2;rs,
                                    .)
                                    -f r/
W.' L. Ste
                                              / rt .@
7                                                                                        ;
Senior Vich President - Nuclear
                                .                                                                                                          l
                          ? Attachments 4                                  1. . Proposed Technical Specification Change for North Anna Unit 1 i2. Proposed Technical Specification Change for. North Anna Unit 2 rt                  >
: 3. Discussion of Proposed Changes:                                                                        ,
14.110 CFR 50.92 Evaluation cc:'      LU.S.~ Nuclear _ Regulatory Corrmiss on
        <                              ; Region il
    ,            s
                                        - 101 Madetta Street, N.W. :
Suite 2900-LAtlanta, GA- 30323 Mr. M. S. Lesser
,.                                      -NRC Senior. Resident inspector 1 North Anna Power Stdion 3
Commissioner.
                                        -Department of Health j
Room 400 109 Governor Street
,g                                        Richmond, Virginia .23219 I
r
                +            -            lA~              - - -                    , , , -      , , . . < , - - . .
                                                                                                              .      - -w ,, , , ,, w e    ,
 
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s E                          COMMONWEALTH OF VIRGINIA )
  #                                                              )
                      . COUNTYOFHENRICO                          )
                        , Ths . foregoing.. document was -.. acknowledged _ before me, in -and. for the-County and; Commonwealth aforesaid, today by. E. W. Harrell, who is Vice
-                            President - 1 Nuclear -- Operations, for W. L. Stewart, who is Senior Vice' c
                          . President.- Nuclear, of xVirginia Electric and Power Company. He is duly        j authorized, to executeLand file the foregoing document in behalf of that c
Company,' .andLthe. statements in the document are true to the best of his k.nowledge and belief.
                                    ' Acknowledged : before me' this. ./  day of t.  //IAaat      , 19_f_/
ii..y Commission ; Expires .
                                                                    /~ f//n 3/        , 19 W .
d                                  ;
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Latest revision as of 09:16, 21 December 2020

Application for Amends to Licenses NPF-4 & NPF-7,changing Tech Specs to Allow Improvements to Monthly Auxiliary Feedwater Pump Tests,Per NRC Concerns Noted in Response to NRC Bulletin 88-004 Re Hydraulic Pump Instability
ML20066H670
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 02/14/1991
From: Stewart W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20066H678 List:
References
91-057, 91-57, IEB-88-004, IEB-88-4, NUDOCS 9102210237
Download: ML20066H670 (3)


Text

y -

i ;, f Of- .- NIHOINIA ELECTIllC AND POWT lt COMPANY Ricitwoxo,VinotutA enent

, i February 14,1991 o

i LU.S. N'uclear Regulatory Commission Serial No.: 91 057

' Attention: Document Control Desk NL&P/RMN Washington, D.C. 20555 ' Docket Nos.: 50 338 q

50 339 License Nos.: NPF 4 N PF , ,

Gentlemen:

1^ '

VIRGINIA- ELECTRIC' ANu POWER COMPANY NORTH ANNA' POWER STATION UNITS 1 AND 2 '

= PROPOSED- TECHNICAL SPECIFICATION CHANGES AUXILIARY FEEDWATER PUMP TESTING Pursuant 10:10 CFRl 50.90, the Virginla= Electric and Power Company requests Lamen.dments, in the form?of changes to the Technical Specifications, to Operating

' License Numbers NPF-4 and NPF-7 for North Anna Power Station Units 1 and 2, respectively,' j 1The' proposed changes to the North Anna Units 1 and 2 Technical Specifice,tions will allow improvements to.the monthly auxiliary feedwater pump tests. These changes-are !ntended to replace our December 28,1989 request (letter serial nusbar 89-833).

NRC Bulletin 88-04 " Safety Related Pump Loss" identified uncerns with hydraulic instability in pumps operating near their shut off heads, in our August 8,1988 reply to

- that bulletin we committed to disassembling and inspecting the auxiliary feedwater '

, . pumps and to mir,!mize operation at low flow. The inspections indicated that some - ,

idegradation had occurred which was not revealed by the high pressure-low flow 4 testing. The pumps have since been overhauled and our. quarterly ASME Section XI

' testing procedures have been revised to allow full flow tests. . A new full flow recirculation line was added during the latest Unit 2 refueling outage and is being ,

installed during the current Unit 1 outage to permit full flow testing e' power without affecting the steam' generators or normal feedwater regulation. Ou, quarterly Section 4 Xl testing is now done at flow conditions near the pump's best efficiency point. This lost p,ovides early warning of degradation and is similar to conditions when the pump p Lis perfc rming its safety function. If the monthly test could be done under similar p conditions, safety we. Id be enhanced because there would be less pump wear and more effective testing.

G l od

" '9102210237 910214 '

. DR ADoCK 0500 8 ggy

. . . m . . _. ._._ _ _ . . . .- _ . _ . fh

. . _Li_ ~ y n '

h 1. ; 3 s '

This does not affect our MERITS submittal, tharefore a MERITS change is not attached.

LThe proposed; changes are provided in Attachments 1 and 2. A discussion of the

. L proposed changes:with the technical justification and safety evaluation of the

. proposed changes is provided in Attachment 3.-

Th!s requestihas been.' reviewed by the Station Nuclear Safety and Operating

-Committee;and the Management Safety Review Committee. It has been determined that this request does not involve an unreviewed safety question as defined in 10 CFR

< " 50.59 o_r a significant hazards consideration as defined in 10 CFR 50.92. The basis for jour determinglon that no significant hazards consideration is involved is presented in

' Attachment 4.

Because of the need .to revise procedures, please allow us 60 days to implement

these changes from the' dates of issuance. Should you have any questions or require l

' additional information, please contact us at your earliest convenience.

> Very truly ud2;rs,

.)

-f r/

W.' L. Ste

/ rt .@

7  ;

Senior Vich President - Nuclear

. l

? Attachments 4 1. . Proposed Technical Specification Change for North Anna Unit 1 i2. Proposed Technical Specification Change for. North Anna Unit 2 rt >

3. Discussion of Proposed Changes: ,

14.110 CFR 50.92 Evaluation cc:' LU.S.~ Nuclear _ Regulatory Corrmiss on

<  ; Region il

, s

- 101 Madetta Street, N.W. :

Suite 2900-LAtlanta, GA- 30323 Mr. M. S. Lesser

,. -NRC Senior. Resident inspector 1 North Anna Power Stdion 3

Commissioner.

-Department of Health j

Room 400 109 Governor Street

,g Richmond, Virginia .23219 I

r

+ - lA~ - - - , , , - , , . . < , - - . .

. - -w ,, , , ,, w e ,

i' q . .

s E COMMONWEALTH OF VIRGINIA )

  1. )

. COUNTYOFHENRICO )

, Ths . foregoing.. document was -.. acknowledged _ before me, in -and. for the-County and; Commonwealth aforesaid, today by. E. W. Harrell, who is Vice

- President - 1 Nuclear -- Operations, for W. L. Stewart, who is Senior Vice' c

. President.- Nuclear, of xVirginia Electric and Power Company. He is duly j authorized, to executeLand file the foregoing document in behalf of that c

Company,' .andLthe. statements in the document are true to the best of his k.nowledge and belief.

' Acknowledged : before me' this. ./ day of t. //IAaat , 19_f_/

ii..y Commission ; Expires .

/~ f//n 3/ , 19 W .

d  ;

i~

d

_ 1[ ,h/iff_ ~

Notary Public l

1

, u I

1, i=

). ,

s (SEAL) l

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