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| A review determined that surveillance 9434.02 had,not been performed in Mode 1 prior to December 6, 1989. | | A review determined that surveillance 9434.02 had,not been performed in Mode 1 prior to December 6, 1989. |
| Additionally, although surveillance 9434.01, "ATWS Reactor Vessel Water Level B21-N400A (B,E,F) Channel Calibration" has never contained a requirement to place the test switch on the front of the ATWS panel in j the " TEST" position, it been revised to specify that the surveillance shall not be performed in Mode 1. | | Additionally, although surveillance 9434.01, "ATWS Reactor Vessel Water Level B21-N400A (B,E,F) Channel Calibration" has never contained a requirement to place the test switch on the front of the ATWS panel in j the " TEST" position, it been revised to specify that the surveillance shall not be performed in Mode 1. |
| l | | l The Licensing and Safety Department is evaluating changing Technical Specification 3.3.4.1 to allow one trip system, versus one trip channel, to be placed in an inoperable status for a limited time to perform |
| ;
| |
| The Licensing and Safety Department is evaluating changing Technical Specification 3.3.4.1 to allow one trip system, versus one trip channel, to be placed in an inoperable status for a limited time to perform | |
| -surveillance testing. This evaluation is expected to be completed by April 4, 1990. | | -surveillance testing. This evaluation is expected to be completed by April 4, 1990. |
| ANALYSIS OF EVENT The requirements of Technical Specification 3.3.4.1 were not met from 1710 to 1925 hours on December 6, 1989, and from 2018 to 2204 hours on December 7, 1989. Therefore, this event is reportable under the ! | | ANALYSIS OF EVENT The requirements of Technical Specification 3.3.4.1 were not met from 1710 to 1925 hours on December 6, 1989, and from 2018 to 2204 hours on December 7, 1989. Therefore, this event is reportable under the ! |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029A6421991-02-20020 February 1991 LER 91-001-00:on 910121,automatic Closure of Inboard MSIV 1B21-F022 A,B,C & D & Inboard Main Steam Drain Line Isolation Valve 1B21-F016 Occurred.Caused by Personnel Error.Maint Work Request Mwr D09786 revised.W/910220 Ltr ML20043H9231990-06-18018 June 1990 LER 90-012-00:on 900517,feedwater Sys Flow Channel Failed & Caused Sensed Low Feedwater Flow.Caused by Normal end-of- Life Failure for Converter.Power Converter Replaced & Preventive Maint Tasks established.W/900618 Ltr ML20043G1151990-06-14014 June 1990 LER 90-011-00:on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags replaced.W/900614 Ltr ML20043E4911990-06-0505 June 1990 LER 90-010-00:on 900508,Divs I & II Emergency Diesel Generators Declared Inoperable Due to Expansion Joints Not Having Required tie-rods Installed to Prevent Expansion. Caused by Const/Installation error.W/900605 Ltr ML20043C0211990-05-23023 May 1990 LER 89-038-01:on 891212,discovered That Only Two of Four Conductors of Cable to Div II Nuclear Sys Protection Sys Inverter Connected.Caused by Design Error.Design Drawings reviewed.W/900523 Ltr ML20043B5741990-05-21021 May 1990 LER 90-009-00:on 900427,discovered That Moving Filter Paper in Leak Detection Sys Drywell Air Particulate Sample Panel Not Collecting on take-up Reel.Caused by Loose Set Screw on Gear Train.Set Screw tightened.W/900521 Ltr ML20043A2351990-05-11011 May 1990 LER 90-008-00:on 900408,attempt Made for 14 Control Rod Withdrawals While Main Turbine Bypass Valves Were Open & Reactor Power Was Greater than Low Power Setpoint.Caused by Personnel Error.Reactor Shut down.W/900511 Ltr ML20042F4111990-04-30030 April 1990 LER 90-007-00:on 900331,inadequate Determination of Equipment Status Resulted in de-energization of Nuclear Sys Protection Sys.Caused by Personnel Error.Fact Sheet on Operation Issued & Personnel retrained.W/900430 Ltr ML20042E6781990-04-23023 April 1990 LER 90-005-00:on 900322,containment Penetration Identified to Have motor-operated Valve W/Inadequate Actuator on Inboard Isolation Valve.Caused by Failure to Consider Design Capabilities of Actuators.Actuators reworked.W/900423 Ltr ML20042E6791990-04-23023 April 1990 LER 90-006-00:on 900321,process Radiation Monitor Placed in Svc W/O Required Filter Due to Inadequately Specified Job Steps for Plant Mod.Caused by Personnel Error.Procedure 1502.01 to Be revised.W/900423 Ltr ML20042E1581990-04-0909 April 1990 LER 90-003-00:on 900212,determined That 13 safety-related Transmitters Inoperable Due to Housing Covers Found W/Torque Values Less than Required to Meet Environ Qualification. Corrective Actions Program enhanced.W/900409 Ltr ML20042E1551990-04-0606 April 1990 LER 90-004-00:on 900307,review of NRC Info Notice 88-024 Re Failures of air-operated Valves Determined Pressure Differential of 73 solenoid-operated Valves Less than Max Instrument Air Sys Pressure.Valves replaced.W/900406 Ltr ML20012C5831990-03-13013 March 1990 LER 90-001-00:on 900212,drywell Purge Sys Containment Penetration Failed Local Leak Rate Test.Caused by Failure to Remove Cosmolene from Surface of Valve Prior to Initial Installation.Valves replaced.W/900313 Ltr ML19354E1031990-01-18018 January 1990 LER 89-042-00:on 891219,false RCIC Div I Steam Line Differential Pressure High Signal Caused RCIC Turbine Steam Supply Isolation Valve to Shut & RCIC Sys to Trip.Caused by Sensor Design Error.Field Alteration begun.W/900118 Ltr ML19354D9161990-01-17017 January 1990 LER 89-041-00:on 891122,unit Entered Tech Spec 3.0.3 When RCIC & HPCS Sys Inoperable Simultaneously for 37 Minutes. Chiller Condensing Unit Tripped Due to Low Refrigerant Pressure.Refrigerant in Chiller recharged.W/900117 Ltr ML20005G3211990-01-11011 January 1990 LER 89-038-00:on 891212,discovered That Only 2 of 4 Cable Conductors for Div II Nuclear Sys Protection Sys Power Supply Connected.Caused by Design Drawing Deficiency.Power Supply Configurations reviewed.W/900111 Ltr ML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr ML20005G2951990-01-0808 January 1990 LER 89-039-00:on 891212,operations Shift Supervisor Notified That Three HPCS Suction Valves Not Tested within Max Surveillance Time Interval.Caused by Personnel Error. Surveillance Procedure revised.W/900108 Ltr ML20042D3011989-12-29029 December 1989 LER 89-037-00:on 891129,inboard Drywell post-LOCA Vacuum Relief Valve Failed to Indicate Fully Open During Valve Stroke Testing.Caused by Worn O-rings Allowing Air to Leak Around Solenoid piston.O-rings Replaced.W/Undated Ltr ML19354D6621989-12-21021 December 1989 LER 89-035-00:on 891129,during Channel Functional Test of ECCS Drywell Pressure Channel,Operator Selected Wrong Channel for Testing,Causing Isolation of Instrument Air Sys. Caused by Personnel Error.Briefing conducted.W/891221 Ltr ML19332F8981989-12-13013 December 1989 LER 89-036-00:on 891113,incorrect Connection of Source to Terminals Directly Below Correct Terminals Caused Div 1 Isolation of RCIC Sys.Caused by Personnel Error.Personnel Briefed on Need to Use ladders/stools.W/891213 Ltr ML19325E5841989-11-0101 November 1989 LER 89-034-00:on 891004,discovered That Inservice Station HVAC Exhaust Stack Process Radiation Monitor Had Not Been Verified as Operable,Contrary to Tech Spec 3.3.7.12.Caused by Lack of Training & Inadequate communication.W/891101 Ltr 1991-02-20
[Table view] Category:RO)
MONTHYEARML20029A6421991-02-20020 February 1991 LER 91-001-00:on 910121,automatic Closure of Inboard MSIV 1B21-F022 A,B,C & D & Inboard Main Steam Drain Line Isolation Valve 1B21-F016 Occurred.Caused by Personnel Error.Maint Work Request Mwr D09786 revised.W/910220 Ltr ML20043H9231990-06-18018 June 1990 LER 90-012-00:on 900517,feedwater Sys Flow Channel Failed & Caused Sensed Low Feedwater Flow.Caused by Normal end-of- Life Failure for Converter.Power Converter Replaced & Preventive Maint Tasks established.W/900618 Ltr ML20043G1151990-06-14014 June 1990 LER 90-011-00:on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags replaced.W/900614 Ltr ML20043E4911990-06-0505 June 1990 LER 90-010-00:on 900508,Divs I & II Emergency Diesel Generators Declared Inoperable Due to Expansion Joints Not Having Required tie-rods Installed to Prevent Expansion. Caused by Const/Installation error.W/900605 Ltr ML20043C0211990-05-23023 May 1990 LER 89-038-01:on 891212,discovered That Only Two of Four Conductors of Cable to Div II Nuclear Sys Protection Sys Inverter Connected.Caused by Design Error.Design Drawings reviewed.W/900523 Ltr ML20043B5741990-05-21021 May 1990 LER 90-009-00:on 900427,discovered That Moving Filter Paper in Leak Detection Sys Drywell Air Particulate Sample Panel Not Collecting on take-up Reel.Caused by Loose Set Screw on Gear Train.Set Screw tightened.W/900521 Ltr ML20043A2351990-05-11011 May 1990 LER 90-008-00:on 900408,attempt Made for 14 Control Rod Withdrawals While Main Turbine Bypass Valves Were Open & Reactor Power Was Greater than Low Power Setpoint.Caused by Personnel Error.Reactor Shut down.W/900511 Ltr ML20042F4111990-04-30030 April 1990 LER 90-007-00:on 900331,inadequate Determination of Equipment Status Resulted in de-energization of Nuclear Sys Protection Sys.Caused by Personnel Error.Fact Sheet on Operation Issued & Personnel retrained.W/900430 Ltr ML20042E6781990-04-23023 April 1990 LER 90-005-00:on 900322,containment Penetration Identified to Have motor-operated Valve W/Inadequate Actuator on Inboard Isolation Valve.Caused by Failure to Consider Design Capabilities of Actuators.Actuators reworked.W/900423 Ltr ML20042E6791990-04-23023 April 1990 LER 90-006-00:on 900321,process Radiation Monitor Placed in Svc W/O Required Filter Due to Inadequately Specified Job Steps for Plant Mod.Caused by Personnel Error.Procedure 1502.01 to Be revised.W/900423 Ltr ML20042E1581990-04-0909 April 1990 LER 90-003-00:on 900212,determined That 13 safety-related Transmitters Inoperable Due to Housing Covers Found W/Torque Values Less than Required to Meet Environ Qualification. Corrective Actions Program enhanced.W/900409 Ltr ML20042E1551990-04-0606 April 1990 LER 90-004-00:on 900307,review of NRC Info Notice 88-024 Re Failures of air-operated Valves Determined Pressure Differential of 73 solenoid-operated Valves Less than Max Instrument Air Sys Pressure.Valves replaced.W/900406 Ltr ML20012C5831990-03-13013 March 1990 LER 90-001-00:on 900212,drywell Purge Sys Containment Penetration Failed Local Leak Rate Test.Caused by Failure to Remove Cosmolene from Surface of Valve Prior to Initial Installation.Valves replaced.W/900313 Ltr ML19354E1031990-01-18018 January 1990 LER 89-042-00:on 891219,false RCIC Div I Steam Line Differential Pressure High Signal Caused RCIC Turbine Steam Supply Isolation Valve to Shut & RCIC Sys to Trip.Caused by Sensor Design Error.Field Alteration begun.W/900118 Ltr ML19354D9161990-01-17017 January 1990 LER 89-041-00:on 891122,unit Entered Tech Spec 3.0.3 When RCIC & HPCS Sys Inoperable Simultaneously for 37 Minutes. Chiller Condensing Unit Tripped Due to Low Refrigerant Pressure.Refrigerant in Chiller recharged.W/900117 Ltr ML20005G3211990-01-11011 January 1990 LER 89-038-00:on 891212,discovered That Only 2 of 4 Cable Conductors for Div II Nuclear Sys Protection Sys Power Supply Connected.Caused by Design Drawing Deficiency.Power Supply Configurations reviewed.W/900111 Ltr ML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr ML20005G2951990-01-0808 January 1990 LER 89-039-00:on 891212,operations Shift Supervisor Notified That Three HPCS Suction Valves Not Tested within Max Surveillance Time Interval.Caused by Personnel Error. Surveillance Procedure revised.W/900108 Ltr ML20042D3011989-12-29029 December 1989 LER 89-037-00:on 891129,inboard Drywell post-LOCA Vacuum Relief Valve Failed to Indicate Fully Open During Valve Stroke Testing.Caused by Worn O-rings Allowing Air to Leak Around Solenoid piston.O-rings Replaced.W/Undated Ltr ML19354D6621989-12-21021 December 1989 LER 89-035-00:on 891129,during Channel Functional Test of ECCS Drywell Pressure Channel,Operator Selected Wrong Channel for Testing,Causing Isolation of Instrument Air Sys. Caused by Personnel Error.Briefing conducted.W/891221 Ltr ML19332F8981989-12-13013 December 1989 LER 89-036-00:on 891113,incorrect Connection of Source to Terminals Directly Below Correct Terminals Caused Div 1 Isolation of RCIC Sys.Caused by Personnel Error.Personnel Briefed on Need to Use ladders/stools.W/891213 Ltr ML19325E5841989-11-0101 November 1989 LER 89-034-00:on 891004,discovered That Inservice Station HVAC Exhaust Stack Process Radiation Monitor Had Not Been Verified as Operable,Contrary to Tech Spec 3.3.7.12.Caused by Lack of Training & Inadequate communication.W/891101 Ltr 1991-02-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARU-603277, Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers U-603267, Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With U-603245, Monthly Operating Rept for Jul 1999 for CPS Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for Jul 1999 for CPS Unit 1.With ML20211C9621999-07-26026 July 1999 ISI Summary Rept U-603232, Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted1999-07-0909 July 1999 Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted U-603233, Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With U-603222, Monthly Operating Rept for May 1999 for Clinton Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Clinton Power Station.With ML20210K8391999-05-11011 May 1999 British Energy Annual Rept & Accounts 1998-99 ML20206H1231999-05-0505 May 1999 Illinois Power Co CPS Main CR Simulator Certification Rept U-603210, Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With U-603204, Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR211999-04-30030 April 1999 Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR21 U-603192, Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With U-603182, Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue1999-03-12012 March 1999 Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue U-603176, Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With ML20207F2031999-02-10010 February 1999 Rev 1 to CPS COLR for Reload 6 Cycle 7 ML20202J0181999-02-0303 February 1999 SER Accepting Changes in Quality Assurance Program,Which Continues to Meet Requirements of App B to 10CFR50 U-603144, Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With U-603223, Illinova Corp 1998 Annual Rept. with1998-12-31031 December 1998 Illinova Corp 1998 Annual Rept. with U-603115, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components1998-12-0404 December 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components U-603124, Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With U-603114, Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor1998-11-25025 November 1998 Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor U-603103, Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With U-603101, Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site1998-10-28028 October 1998 Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves U-603091, Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With ML20153F9871998-09-17017 September 1998 Safety Evaluation Accepting 980225 Proposed Rev 26 to Illinois Power Nuclear Program Qam ML20151U1391998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Clinton Power Station,Unit 1 ML20237E3991998-08-27027 August 1998 SER Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode, for Clinton Power Station ML20237A1521998-08-0707 August 1998 SER Re Mgt Services Agreement at Clinton Power Station. Approval Under 10CFR50.80 Not Required ML20151Y6591998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Clinton Power Station,Unit 1 U-603033, Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals1998-07-20020 July 1998 Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals U-603041, Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 ML20151U1501998-06-30030 June 1998 Revised Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 U-603023, Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 1 U-603014, Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed1998-05-28028 May 1998 Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed ML20236E7991998-05-26026 May 1998 Final Part 21 Rept Re W Dhp Circuit Breaker Auxillary Switch Operating Assembly Anomalies.Caused by Loss of Breaker Safety Function.Dhp Circuit Will Be Inspected ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted U-603004, Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable1998-05-15015 May 1998 Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable ML20216A9601998-05-0808 May 1998 Part 21 Rept Re Failure of 12 Volt DC Inverter Power Supply. Caused by Inadequately Sized Output Transistor Pair Combined W/Degraded Capacitors.Licensee Plans to Replace All Output Transistors & Degraded Capacitors U-602995, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts1998-05-0505 May 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts U-603006, Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 1 U-602994, Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable1998-04-29029 April 1998 Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable ML20216B1351998-04-21021 April 1998 Rev 0 to Illinois Power Co Clinton Power Station SVC Design Rept U-602979, Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable1998-04-0707 April 1998 Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable U-602976, Monthly Operating Rept for Mar 1998 for Clinton Power Station1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Clinton Power Station ML20217H5771998-03-27027 March 1998 Safety Evaluation Concluding That No Significant Safety Hazards Introduced at CPS for Net 32% Ampacity Derating Factor for 1 H & 3 H Conduit Fire Barrier Sys & 1 H Cable Tray Fire Barrier Sys.Requests Response Addressing Issue U-602968, Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue1998-03-24024 March 1998 Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue U-602960, Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 9804111998-03-12012 March 1998 Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 980411 U-602954, Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 9805131998-03-0909 March 1998 Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 980513 1999-09-30
[Table view] |
Text
1
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' - 20.220 ILLIN018 POWER 00MPANY CLINTON POWill $1 AllON, P.O. BOX 678, CLINTON, ILLINOIS 61727
-January 8, 1990 10CFR50.73 Docket No. 50-461 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Subj ect: Clinton Power Station -: Unit 1 Licensee Event Report No. 89-040-00
Dear Sir:
Please find enclosed-Licensee Event Report No.89-040 00:
Omission of Mode Limitations From Surveillance Procedure Results in Inonerable Anticinated Transient Without Scram Recirculation Pumn Trio System Instrumentation. This report is being submitted in accordance-with the requirements of 10CFR50.73.
Sincerely yours, 3/ A D. L. Holtzscher Acting' Manager -
Licensing and Safety TSA/krm Enclosure cc: NRC Resident Office NRC Region III, Regional Administrator INPO Records Center Illinois Department of Nuclear Safety NRC Clinton Licensing Project- Manager I
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/ ~
9001180383 900108 DR ADOCKOSOOg,gi
}-
e RC Feem 386 U.$. NUCLEAN L.E1ULATORY COMMIS$40N
- APPROVED OM9 NO. 3100-0104 LICENSEE EVENT REPORT (LER) * *" 5 5 8""
F ACiLITY NAME (1) DOCKET NUMBER (2) PAGE(3s Clinton Power Station 0 l5 l o l0 l 0141611 1 lOFl014 j
" idi Omission of Mode Limitations From Surveillance Procedure Results in Inoperable I Anticipated Transient Without Scram Recirculation Pump Trip System Instrumentation !
EVENT DATE (S) LER NUusER 461 REPORT DATE (M OTHER F ACILITIES INVOLVED (8) i ON DAY I YEAR YEAR 88,0 ( ff[,$ MONTH DAY YEAn t ACsLitv h AMes DOCKE T NUMSERISI None 0l5l0l0l0l l l
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1l2 0l 6 8 9 8l 9 0l4l0 0l0 0l1 0l 8 9l 0 0 1 6:0l0,0 i l l TM48 REPORT is $UeMITTED PUR$1.lANT TO THE Rh0VIREMENTS OF 10 CFR 5: IChece one or more of ,ae followeaFi (1H OPE R ATING MODE W 1 20 402M 20 406tel to.73tel(2 Heel 73.71M 20.406te H1HG 60.38(eH11 50.73(eH28M 73.714el ta 061 15 20 40iHoHum 30xen2i son.H2Hai _ guEgsggg<e I .. 20 406hIllite4u X 60nien2Ho son iunsiHA) assAs g _
20 400teH1Havl E0.73(eH2HIH t%73tel(2Hvis1 HOI j 20 406telt1 Het 60.73telGIIHH $0.73(el'2Hal LICENSEE CONTACT FOR TH48 LER O2l NAME TELEPHONE NUMBER ARE A CODE S. E. Rasor, Director-Plant Maintenance, extension 3204 211 l 7 913151-l8I8I811 COMPLETE ONE LINE FOR E ACM COMPONENT F AILURE DESCRISED IN THis REPORT H3)
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COMPONENT g hpR C aust SYST EM COMPONENT l I I l l l l 1 I I I f I I i 1 l ! I i I I l l I I 1 SUPPLEMENTAL REPORT EXPECTE01141 MONTM DAY l YEAR g
l $U6 Me$5 TON DATE1151 YES II' ve,. comosere IXPECTED SUOMisstON DA tti NO l l l t T a ACT mm.. ux ,,.<,.. , . . e-.. ,.+ ,*, Mu. ,v,.-n.
l l On December 6 and 7, 1989, the plant was in Mode 1 (POWER OPERATION).
Surveillance testing was performed on Anticipated Transient Without Scram (ATWS) Recirculation Pump Trip /RPT) system instrumentation in accordance with surveillance 9434.02. During the surveillance, a test switch on the l ATWS panel was placed in the " TEST" position, bypassing all four channels l in the trip system. Technical Specification (TS) 3.3.4.1 requires that i
two reactor pressure high 1cvel and two reactor vessel water level low channels per trip system be operable in Mode 1. However, one channel may be placed in an inoperable status for up to two hours for required surveillances provided the redundant trip system is operable and monitoring that parameter. While performing surveillance 9434.02, all four channels in a trip system are bypassed, placing them in an inoperable status. On December 9, 1989, the Shift Supervisor identified that on December 6 and 7, 1989, the requirements of TS 3.3.4.1 were not met. The cause of this event is attributed to an inadequate procedure.
Surveillance 9434.02 did not identify that to comply with TS 3.3.4.1 the surveillance must be performed in operational conditions other than Mode
- 1. Corrective actions include revising ATWS-RPT system instrumentation surveillances and evaluating a chat.ge to TS 3.3.4.1.
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- U.S. NUCLE AR A50VLAt0AY Conau,0ssoN LICENSEE EVENT REPORT (LER) TFXT CONTINUATION ***aovio oue nomso oio4 I EXPIAES: 8/31/N 9ACILITY esasiet H6 Docuti NUAAS$ A (21 ggg gygggg gg; pagg (33 vtan S8 g Q A4 Clinton Power Station o l5 l0 l0 lo l4 l6 l1 8l9 --
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0l0 0l2 OF 0l4 vart era =,. . w. , O.,w mac s asiaw nn DESCRIPTION OF EVENT on December 9,1989, the Shift Supervisor identified that on December 6 and 7, 1989, during the performance of surveillance testing, Technical Specification 3.3.4.1 requirements for the Anticipated Transient Without Scram (ATWS) Recirculatic Pump Trip (RPT) system instrumentation were ,
not met.
On December 6, Ifl9, the plant was in Mode 1 (POWER OPERATION) and the reactor (RCT] was at sixty-five percent power. At 1710 hours0.0198 days <br />0.475 hours <br />0.00283 weeks <br />6.50655e-4 months <br />, in accordance with surveillance 9434.02, "ATWS Reactor Pressure High-Level B21 N401A (B.E F) Channel Calibration", Control and Instrumentation (C&I) technicians began surveillance testing on reactor pressure high level channel 1B21-N401B. In accordance with the surveillance procedure, the
- C&I technicians placed the test switch on the front of ATWS panel [PL) 1RR04JB in the " TEST" position. The C&I technicians then proceeded with the channel calibration. By 1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br />, the C&I technicians had completed the surveillance with satisfactory results and had restored the system.
On December 7, 1989, at 2018 hours0.0234 days <br />0.561 hours <br />0.00334 weeks <br />7.67849e-4 months <br />, in accordance with surveillance 1 9434.02, C&I technicians began surveillance testing on reactor pressure high 1cvel channel 1B21-N401F. The test switch on the front of ATWS panel 1RR04JB was again placed in the " TEST" position. By 2204 hours0.0255 days <br />0.612 hours <br />0.00364 weeks <br />8.38622e-4 months <br />, the C&I technicians had completed the surveillance with satisfactory results and had restored the system.
On December 9, 1989, a C&I foreman requested permission from the~ Shift Supervisor to perform surveillance 9434.02 on reactor pressure high level channel 1B21-N401E. During discussion of the surveillance it was brought to the Shift Supervisor's attention that placing the test switch on the front of the ATWS panel in the " TEST" position bypasses the trip function of all four channels (two reactor pressure high level and two reactor water level low channels) in that trip system. After reviewing the applicable Technical Specifications, the Shift Supervisor identified that Technical Specification 3.3.4.1 requirements were'not met during the performance of survnillance 9434.02 on either December 6 or 7, 1989.
Technical Specification 3.3.4.1 requires that two reactor pressure high level and two reactor vessel water level low channels per trip system be i operable in Mode 1. If any one of the four channels in a trip system l becomes inoperable it must be restored to an operable status within i forty-eight hours or the plant must be placed in at least Mode 2 (STARTUP) within the next six hours. However, in accordance with the l Technical Specification, one channel may be placed in an inoperable '
status for up to two hours for required surveillances provided the redundant trip system is operable and monitoring that parameter. Placing the test switch on the front of the ATUS panel in the " TEST" position l
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0 l0 0l3lOF 0l4 vint w A w eme r ama nn bypassed four channels, placing them in an inoperable status. Therefore, the requirements of Technical Specification 3.3.4.1 were not met.
No automatic or manually initiated safety system responses were necessary i to place the plant in a safe and stable condition. No equipment or !
components were inoperable at the start of this event such that their -
inoperable condition contributed to this event.
]
CAUSE OF EVENT The cause of this event is attributed to an inadequate procedure.
Surveillance 9434.02 did not identify that to comply'with Technical Specification 3.3.4.1, surveillance 9434.02 must be performed in operational conditions other than Mode 1.
CORRECTIVE ACTIONS Surveillance 9434.02 has been revised to specify that the surveillance shall not be performed in Mode 1.
A review determined that surveillance 9434.02 had,not been performed in Mode 1 prior to December 6, 1989.
Additionally, although surveillance 9434.01, "ATWS Reactor Vessel Water Level B21-N400A (B,E,F) Channel Calibration" has never contained a requirement to place the test switch on the front of the ATWS panel in j the " TEST" position, it been revised to specify that the surveillance shall not be performed in Mode 1.
l The Licensing and Safety Department is evaluating changing Technical Specification 3.3.4.1 to allow one trip system, versus one trip channel, to be placed in an inoperable status for a limited time to perform
-surveillance testing. This evaluation is expected to be completed by April 4, 1990.
ANALYSIS OF EVENT The requirements of Technical Specification 3.3.4.1 were not met from 1710 to 1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br /> on December 6, 1989, and from 2018 to 2204 hours0.0255 days <br />0.612 hours <br />0.00364 weeks <br />8.38622e-4 months <br /> on December 7, 1989. Therefore, this event is reportable under the !
provisions of 10CFR50.73(a)(2)(1)(B) . ,
Assessment of the nuclear safety consequences and implications of this event indicates that this event is not nuclear safety significant.
During the limited time that one ATWS RPT system was inoperable the.
redundant trip system was available to limit the consequences of the unlikely occurrence of the failure to scram during an anticipated ,
transient.
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0 l0 0 l4 0F 0 l4 rtxt --- . -anc w w.nm ADDITIONAL INFORMATION No components failed during this event.
LER 89 026-00 discusses the missed verification of trip setpoints for the Average Power Range Monitors. A deficient procedure, possibly resulting-from confusion of Technical Specification requirements, resulted in the missed verification.
For further information regarding this event, contact S. E. Rasor, Director - Plant Maintenance, at (217) 935-8881, extension 3204, e
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