IR 05000269/2005004: Difference between revisions

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{{Adams
{{Adams
| number = ML060600417
| number = ML053050479
| issue date = 02/15/2006
| issue date = 10/28/2005
| title = Integrated Inspection Report 05000269/2005004, 05000270/2005004, 05000287/2005004, Unresolved Items 2005004-10 and 2005004-08
| title = IR 05000269-05-004, IR 05000270-05-004, IR 05000287-05-004, 07/01/2005 - 09/30/2005; Oconee Nuclear Station, Units 1, 2, and 3; Maintenance Risk Assessments and Emergent Work Control, Surveillance Testing, Identification and Resolution of P
| author name = Hamilton B
| author name = Ernstes M
| author affiliation = Duke Power Co
| author affiliation = NRC/RGN-II/DRP/RPB1
| addressee name =  
| addressee name = Jones R
| addressee affiliation = NRC/Document Control Desk, NRC/RGN-II
| addressee affiliation = Duke Energy Corp
| docket = 05000269, 05000270, 05000287
| docket = 05000269, 05000270, 05000287
| license number = DPR-038, DPR-047, DPR-055
| license number = DPR-038, DPR-047, DPR-055
| contact person =  
| contact person =  
| case reference number = IR-05-004
| document report number = IR-05-004
| document type = Letter, Licensee Response to Notice of Violation
| document type = Inspection Report, Letter
| page count = 40
| page count = 47
}}
}}


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=Text=
=Text=
{{#Wiki_filter:BRUCE H HAMILTON_ Duke! Vice Pres dent f-Oftwer( Oconee Nuclear Station Duke Povwer ONO1 VP.' 7800 Rocherster Highway February 15, 2006 Seneca, $C 29672 864 885 3487 864 885 4208 fax U.S. Nuclear Regulatory Commission Washington, DC 20555-0001 ATTENTION:
{{#Wiki_filter:October 28, 2005
Document Control Desk SUBJECT: Duke Energy Corporation Oconee Nuclear Station Units 1, 2 and 3 Docket Nos: 50-269, 270 and 287 Integrated Inspection Report 05000269/2005004, 05000270/2005004, 05000287/2005004, Unresolved Items 2005004-10 and 2005004-08 The subject Inspection Report issued on October 28, 2005, identified a number of Non-Cited Violations (NCVs) and.opened six new Unresolved Items (URIs) .Duke is not contesting any of the NCVs, but does wish to present additional information for the NRC staff's consideration prior to final disposition of URI 2005004-10 and 2005004-08. Both of these URIs are directly related to the Oconee High Energy Line Break (HELB) mitigation strateg URI 2005004-10 relates to the maintenance of containment electrical penetration enclosure URI 2005004-08 relates to compliance with the reportability requirements of 10 CFR 50.73 for the east penetration room blow out panel deficiency.


The information contained in Attachment 1 supports the following conclusions for URI 2005004-10:
==SUBJECT:==
* There are no environmental qualification (EQ)requirements that the electrical penetration enclosures in the penetration room be designed, installed or maintained to meet a NEMA 4 classification.
OCONEE NUCLEAR STATION - INTEGRATED INSPECTION REPORT 05000269/2005004, 05000270/2005004, 05000287/2005004


* The parameters for the EQ of the penetration enclosures in the penetration rooms following a pipe rupture outside containment are pressure, temperature and 100% relative humidity.: ,G C)www. dukepowe com U. S. Nuclear Regulatory Commission February 15, 2006 Page 2* The effects of missing enclosure covers has resulted in contamination of terminal boards. Assuming that this contamination could have an adverse affect on plant operation during a HELB, evaluation of various failures at the component level has concluded that this condition would not prevent safe shutdown from a HELB event.* The lack of maintenance on these penetration enclosures had no impact on safety.The information contained in Attachment 2 supports the following conclusions for URI 2005004-08:
==Dear Mr. Jones:==
* Intermediate break sizes are not required to be postulated as part of the Oconee Nuclear Station (ONS) licensing basis for analyzing the effects from postulated piping breaks outside containment.
On September 30, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Oconee Nuclear Station. The enclosed report documents the inspection findings which were discussed on October 4, 2005, with Mr. Bruce Hamilton and other members of your staff.


* No operator actions are required to mitigate flooding consequences for the licensing basis feedwater line break in the east penetration room. The Reactor Protection System trips the reactor on high reactor coolant pressur The Automatic Feedwater Isolation System isolates main feedwater to the affected main feedwater line. These systems will perform their associated actions regardless of the Integrated Control System.* There is at least 10 minutes available for operator action to terminate flooding from "critical cracks" in the! main feedwater piping.* Electrical penetrations in the east penetration room will not be subjected to submergence following the postulated main feedwater line break or a "critical crack" in the main feedwater piping. Therefore, instrumentation inside the reactor building will remain available to the operators.
The inspection examined activities conducted under your licenses as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your licenses. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.


* This issue does not meet the reportabilty requirements set forth in 10 CFR 50.7 U. S. Nuclear Regulatory Commission February 15, 2006 Page 3 Additionally, in a letter from Duke to the NRC, dated January 31, 2006, Duke provided the NRC staff with the proposed scope and schedule for actions necessary to address licensing basis issues associated with HELB events outside of containmen The actions described in the Janua:ry 31, 2006 letter will address concerns associated with the b:Low out panel deficiency and jet impingement resulting from line breaks and critical cracks in the east penetration room.If you have any questions or comments regarding these issues, please contact Noel Clarkson of the Oconee Nuclear Site Regulatory Compliance Group at 864-885-3077.
This report documents two self-revealing and four NRC-identified findings of very low safety significance (Green); five of which were determined to be violations of NRC requirements.


Very truly yours, Bruce H. Hamilton, Vice President Oconee Nuclear Site Enclosure U. S. Nuclear Regulatory Commission February 15, 2006 Page 4 cc: Mr. L. N. Olshan, Project Manager Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Mail Stop 0-14 H25 Washington, D.C. 20555 Dr. W. D. Travers, Regional Administrator U.S. Nuclear Regulatory Commission-Region II Atlanta Federal Center 61 Forsyth St., SW, Suite 23T85 Atlanta, Georgia 30303 Mr. M. E. Ernstes, Chief Branch 1 DRP U.S. Nuclear Regulatory Commission-Region II Atlanta Federal Center 61 Forsyth St., SW, Suite 23T85 Atlanta, Georgia 30303 Mr. M. C. Shannon Senior Resident Inspector Oconee Nuclear Station Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
However, because of their very low safety significance and because the issues were entered into your corrective action program, the NRC is treating these five findings as non-cited violations (NCVs) consistent with Section VI.A of the NRC Enforcement Policy. If you contest any of the findings in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the United States Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Oconee facility.
Background:
As identified in the NRC Inspection Report, dated October 26, 2005, Unresolved Item (URI) 05D00269, 270, 287/2005004-10 exists due to failure of ONS to identify a condition adverse tc quality by not maintaining the electrical penetration enclosures in the east and west penetration rooms as "spray-proof"/NEMA 4 enclosure The NRC stated (per discussion with NRR) that the Oconee Nuclear Site (ONS) High Energy Line Break (HELB)licensing basis for electrical penetration should consider both spray and direct jet impingement.


The Inspection Report, dated October 25, 2005, states that inspectors identified that covers for a significant number of electrical penetrations were missing or improperly attached.Due to missing enclosure hardware and resulting potential terminal block contamination, it was postulated that safety-related electrical systems would be significantly affected due to grounds and shorts following a HELB and mitigation equipment would thus be unavailable.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's


Discussion:
DEC
The electrical penetrations originally installed at Oconee were manufactured by Viking Industries Inc and Westinghouse (used only for 6900V reactor coolant pump (RCP) motor power).Subsequently, additional penetrations manufactured by D. G.O'Brien and Conax were installed.


Calculation OSC-8505 (Oconee HELB EQ Analysis for Penetration Rooms) has been revised to qualify the various manufactured penetration assemblies for the new main steam (MS) and main feedwater (MFDW) temperature and pressure profile The qualification for the MS temperature profile is based on. the short duration of the temperature spike and the inability to transfer heat to the terminal blocks in that short time frame.The new MS and MFDW profiles have been documented in revisions to the Environmental Qualification Criteria Manual (EQCN).These revisions to the EQCM for the new MS and MFDW profiles maintained the environment as a 100% relative humidity environmen Chemical spray and submergence elevation are considered not applicable and direct steam impingement is not include Regarding the qualification of the assemblies for moisture intrusion, the qualification conclusions are manufacturer dependent and are summarized as follows: 1 Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
* Per the Conax qualification test report (OM 363-023), both the inside and outside containment portions of the electrical penetration have the same design materials and potent:Lal paths for moisture intrusio Additionally, a design basis test was performed on the Kulka series terminal blocks used within Conax electrical penetrations which included a chemical spray simulation.


* Per the D.G. O'Brien qualification test report (OM 337-0089), the outside containment portion of the electrical penetration has been tested under a series of HELB-event conditions which included 100% relative humidity at elevated temperature, and this testing included evaluations on the Weidmueller and Allen Bradley terminal block connection Most of the D.G. O'Brien assemblies are installed in the west penetration room, and thus would not needto be qualified for moisture intrusion resulting from a HELB occurring in the East Penetration Room.The only D.G. O'Brien assemblies installed in the Eas: Penetration Room are 2EA09 aLnd 3EA12. Neither of these is credited for a HELB.* Per the Viking qualification test report (OM 337-0080), the LOCA qualification for the electrical penetrations was performed without the installation of the junction box covers and also included 100% relative humidity at elevated temperatur Tab 6 of the Viking qualification test report references the Duke Power Test Report TR-028 (MCM-1393.02-0004) for evaluating the applications of Buchanan terminal blocks within a condensing steam environmen This test included 100% relative humidity due to a water spray being applied to the steam entrance of the test chamber at elevated temperature and pressure conditions.
Sincerely,
/RA/
Michael E. Ernstes, Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos.: 50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55


Based on these test results, there is no concern with potential moisture intrusion for these electrical penetrations used within applications located inside the electrical penetration room areas. This qualification does not depend on the penetration enclosure boxes being sealed. In fact, the applicable EQMM sections state "The cables entering electrical penetration assemble junction boxes do not require environmental seLling.The junction boxes are vented." The original Viking enclosures were modified by NSM-970 (Replace Grating with Solid Cover Plate on Types B thru K Electrical Penetrations)
===Enclosure:===
in the 1977-1982 timefram The modification replaced the original metal grating that served as the front 2 Attachment 1 Duke Energy Response to UnresoLved Item 2005004-10 (Failure to Maintain Containment ElectricaL Penetration Enclosures)
NRC Integrated Inspection Report 05000269/2005004,05000270/2005004, 05000287/2005004 w/Attachment: Supplemental Information
covers for both the inside and outside containment enclosures.


As stated in the Safety Evalua:ion, the modification
REGION II==
... replaces existing grate covers on the penetration room and reactor building ends of electrical penetrations type B thru J.This revision will increase equipment reliability and personnel safety by eliminating paths through which foreign debris can enter through the electrical connection areas." For the penetration room side, the modification installed a large solid sheet metal cover and two smaller covers; one on the enclosure front to provide visual access to the pressure gauge and test fittings and another on the enclosure top to cover a pressure test valve knob. The reactor building side has one solid sheet metal cover.No documents associated with the modification mention these enclosures as now meeting NEMA 4 requirement The National Electrical Manufacturers Association defines a NEMA 4 enclosure as: "Enclosures constructed for either indoor or outdoor use to provide a degree of protection to personnel against incidental contact with the enclosed equipment; to provide degree of protection against falling dirt, rain, sleet, snow, windblown dust, splashing water, and hose-directed water; and will be undamaged by the external formation of ice on the enclosure.
Docket Nos:
50-269, 50-270, 50-287 License Nos:
DPR-38, DPR-47, DPR-55 Report No:
50-269/2005004, 50-270/2005004, 50-287/2005004 Licensee:
Duke Energy Corporation Facility:
Oconee Nuclear Station, Units 1, 2, and 3 Location:
7800 Rochester Highway Seneca, SC 29672 Dates:
July 1, 2005 - September 30, 2005 Inspectors:
M. Shannon, Senior Resident Inspector A. Hutto, Resident Inspector E. Riggs, Resident Inspector R. Aiello, Senior Operations Engineer (Section 1R11)
S. Rose, Senior Operations Engineer (Section 1R11)
M. Chitty, Operations Engineer (Section 1R11)
Approved by:
Michael E. Ernstes, Chief Reactor Projects Branch 1 Division of Reactor Projects


While this modification provided an additional measure of protection from potential wetting, no testing was done to determine if the enclosures did indeed qualify as NEMA 4 enclosure The NSM revised two vendor drawings to indicate the new cover design; no changes were made to EQ-related documents to take credit for the replacement of the original metal grating covers.The misconception that NEMA 4 applies to terminal blocks used in containment penetrations may have been taken from CGD-3007.02-04-0001 (Commercial Grade Item Evaluation for States Terminal Blocks, Test Switches and Accessories).
=SUMMARY OF FINDINGS=
IR 05000269/2005004, IR 05000270/2005004, IR 05000287/2005004, 07/01/2005 -


Section 2.2.3 of the CDG states: "These terminal blocks and test switches must be installed inside an enclosure (NEMA 4 or equivalent in areas where direct steam or spray impingement is postulated during 3 Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
09/30/2005; Oconee Nuclear Station, Units 1, 2, and 3; Maintenance Risk Assessments and Emergent Work Control, Surveillance Testing, Identification and Resolution of Problems, and Event Followup.
accident scenarios)." None of the penetrations use States terminal blocks, therefore this CGD is not applicable.


An engineering walkdown was performed on all penetrations in the east penetration rooms. The purpose of the inspection was to ascertain the extent of penetration terminal boards with observed contaminatio An initial conservative assumption was that if any indication of terminal board contamination was found, all circuits in that penetration were assumed to be affecte If required, an additional evaluation of the individual terminal boards was performe The following eighteen penetrations were found that had evidence of terminal board contamination:
The report covered a three-month period of inspection by the onsite resident inspectors and three operations engineers. Six Green findings, five of which were non-cited violations (NCVs), were identified. The significance of most findings is indicated by their color (Green, White,
Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.


Attachment 1 Item 2005004-10 (Failure to Maintain Containment Duke Energy Response to Unresolved Electrical Penetration Enclosures)
===NRC Identified and Self-Revealing Findings===
Unit Penetration Penetration Number Number Manufacturer Potentially Affected Components 1 EA 09 Viking R. C. Pump 1A2 Seal Leakage Flow 1RC MIOOO R. C. Pump 1AI Seal Leakage Flow IRC MI0001 R. C. Pump IAI Seal Lower Cavity Transmitter 1RC PT0219 Pressurizer Temperature LRC RD0043C Quench Tank Pressure Transmitter ICS PT0042 lWD3-PT Quench Tank Level Transmitter ICS LT0045P lWDl-LT HPI Nozzle Warming Line Al Flow lHPIFT 0185 HPI Nozzle Warming Line A2 Flow lHPIFT0186 C/D Waste Disposal System Quench Tank Temp. lCS RD0048 Reactor Vessel Level Loop A lRC LT0005A 1 1 EB 09 Viking CCTV Camera 4 Signal Process Amp._ I. V Lamera 2 Signai Process Amp.1 1 EC 08 Viking R. C. Pump lAl Term Box R. C. Pump lAl Oil Lift Pump Motor (AC)R. C. Pump lAl Oil Lift Pump Motor (DC)R. C. Pump lAl Motor Heater 1 1 EC 12 Viking R. C. Pump Mtr. lAl Inlet Valve lLPSW7 (Power & Control)R. C. Pump Mtr. lAl Outlet Valve lLPSW8 (Power & Control)R. B. Cooling Unit Fan LA Damper Position Indication R. C. Pump Mtr. 1A2 Inlet Valve lLPSW13 Computer Points R. C. Pump Mtr. IA1 Inlet Valve lLPSW7 Computer Points R. B. Pen Room Vent Sample Valve IPR59 (Control)R. C. Pump Mtr. lAl Inlet Valve lLPSW7 Computer Points R. B. Pen Room Vent Sample Valve IPR59 (Control)R C. D>iimr. 1t 1.r Al Ouitlet Ja1vte 1T PQWR C(nmniitpr Peints R. B. Pen Room Vent Sample Valve IPR59 (Control)R. C. Pump Mtr. lAl Outlet Valve lLPSW8 Computer Points R. B. Pen Room Vent Sample Valve IPR59 (Control)I R. C. Pump Mtr. 1A2 Outlet Valve 1LPSW14 Computer Points 5 Duke Energy Response to Unresolved Electrical Penetration Enclosures)
===Cornerstone: Initiating Events===
Attachment 1 Item 2005004-10 (Failure to Maintain Containment Unit Penetration Penetration Number Number Manufacturer Potentially Affected Components R. B. Pen Room Vent Sample Valve IPR60 (Control)R. C. Pump Mtr. 1A2 Outlet Valve lLPSWI4 Computer Points R. B. Pen Room Vent Sample Valve lPR60 (Control)R. B. Cooling Unit Fan IA Damper Position Indication Computer Points R. B. Pen Room Vent Sample Valve IPR60 (Control)R. B. Cooling Unit Fan LA Damper Position Indication Computer Points R. B. Pen Room Vent Sample Valve lPR60 (Control)R. C. Pump Mtr. 1A2 Outlet Valve lLPSW14 (Power & Control)R. C. Pump Mtr. 1A2 Inlet Valve lLPSW13 (Power & Control)R. C. Pump Mtr. lAl Inlet Valve lLPSW7 Heater R. C. Pump Mtr. 1A2 Inlet Valve lLPSWI3 Heater R. B. Pen Room Vent Sample Valve iPR60 (Power)R. B. Pen Room Vent Sample Valve 1PR59 (Power)I 1 ED 13 Viking R. C. Pump lAl Oil Tank Level Alarm R. C. Pump 1A2 Oil Tank Level Alarm Fuel Handling System Loose Parts Monitor Channels 1, 2, 3, and 4 Loose Parts Monitor Channel 21 Loose Parts Monitor Channel 7 Loose Parts Monitor Channel 21 Loose Parts Monitor Channel 7 Loose Parts Monitor Channel 8 Loose Parts Monitor Channel 22 Loose Parts Monitor Channel 18 Tnnqe Parts Mnnitor Chnnnel 1.Loose Parts Monitor Channel 8 Loose Parts Monitor Channel 22 Loose Parts Monitor Channel 18 Loose Parts Monitor Channel 12 6 Attachment 1 Item 2005004-10 (Failure to Maintain Containment Duke Energy Response to Unresolved Electrical Penetration Enclosures)
*
Unit Penetration Penetration Number Number Manufacturer Potentially Affected Components Loose Parts Monitor Channel 11 Loose Parts Monitor Channel 9 Loose Parts Monitor Channel 17 Loose Parts Monitor Channel 10 Loose Parts Monitor Channel 11 Loose Parts Monitor Channel 9 Loose Parts Monitor Channel 17 Loose Parts Monitor Channel 10 Fuel Handling System Main Fuel Handling Bridge Console Light/Recept.
: '''Green.'''
A self-revealing finding was identified for inadequate maintenance and oversight of repair efforts on the actuator of 3DW-18 (the Unit 3 Upper Surge Tank (UST) Makeup Valve). Specifically, while attempting to repair an air leak on the actuator of 3DW-18, maintenance technicians removed the valves bonnet and were ready to remove the valves diaphragm with no hydraulic isolations made between the valve and the main condenser. Had the diaphragm been removed from 3DW-18, it is likely that Unit 3 would have tripped due to a loss of main condenser vacuum, as the top of the UST dome is vented to the main condenser.


Receptacle for TCA-1000 Position Instrument
This event was considered to be a performance deficiency, as the licensee failed to provide adequate maintenance and oversight of the efforts to repair an air leak on the 3DW-18 actuator; thereby, increasing the likelihood of a unit trip with a loss of normal heat sink. This issue was considered to be more than minor because it affected the Initiating Events cornerstone objective of limiting the likelihood of events that upset plant stability. The finding is associated with the configuration control attribute, in that the inadequate maintenance and oversight of the repairs to the actuator of 3DW-18 increased the likelihood of a reactor trip with a loss of normal heat sink due to inadequate configuration control of a secondary plant system. The consequences of the finding were assessed through Phase 2 of the SDP, and although the likelihood of a unit trip was increased and would have resulted in a loss of the normal heat sink, the exposure time for this condition was less than 3 days and all other mitigation capabilities described on the Phase 2, SDP worksheet for transient (reactor trip)core damage sequences were maintained. Consequently, the finding was determined to be of very low safety significance. This finding involved the cross-cutting aspect of human performance. (Section 1R13)
- I-TT_.--rue- nalluillig aystuill P A System CRD Service Structure Fan Monitor Panel I I 1 EE 04 Viking Incore Detector Assy 48 Loc. 0-12 Incore Detector Assy 49 Loc. M-14 Incore Detector Assy 48 Loc. 0-12 Incore Detector Assy 49 Loc. M-14 Incore Detector Assy 18 Loc. L-1 1 Incore Detector Assy 21 Loc. H-13 Incore Detector Assy 20 Loc. K-12 Incore Detector Assy 18 Loc. L-1 1 Incore Detector Assy 21 Loc. H-13 Incore Detector ASRY 20 inc. K-1 2 Incore Detector Assy 18 Loc. L-1 1 Incore Detector Assy 20 Loc. K-12 Incore Detector Assy 18 Loc. L-11 Incore Detector Assy 18 Loc. L-11 7 Attachment 1 Item 2005004-10 (Failure to Maintain Containment Duke Energy Response to Unresolved Electrical Penetration Enclosures)
*
Unit Penetration Penetration Number Number Manufacturer Potentially Affected Components Incore Detector Assy 21 Loc. H-13 Incore Detector Assy 18 Loc. L-1 1 Incore Detector Assy 48 Loc. 0-12 Incore Detector Assy 49 Loc. M-14 Incore Detector Assy 50 Loc. L-13 Incore Detector Assy 20 Loc. K-12 Incore Detector Assy 21 Loc. H-13 Incore Detector Assy 48 Loc. 0-12 Incore Detector Assy 50 Loc. L-13 Incore Detector Assy 49 Loc. M-14 1 1 EF 11 Viking Pressurizer Heater Group G (Power)Pressunzer Heater Groupi J (Power)2 2 EB 09 Viking TVCAMERA#7 TV CAMERA # 5 TVCAMERA#7 TV CAMERA #5 TV CAMERA #5 2 2 ED 10 Viking 2FDW-105 STM. GEN. '2A' ISOLATION VLV.2HP-228 2A1 RCP SEAL RETURN STOP VLV.2HP-226 2A2 RCP SEAL RETURN STOP VLV.RB AUX. VENT FAN '2A' VIBRATION SW.RB AUX. VENT FAN '2B' VIBRATION SW.RB AUX. VENT FAN '2A' VIBRATION SW.PRR ATTY V_-NTPAN '?R VIRRATTON5SW 2HP-228 2A1 RCP SEAL RETURN STOP VLV. (OAC)2HP-226 2A2 RCP SEAL RETURN STOP VLV. (OAC)H2 SAMPLE VLV. 2SV211 H2 SAMPLE VLV. 2SV212 8 Attachment 1 Item 2005004-10 (Failure to Maintain Containment Duke Energy Response to Unresolved Electrical Penetration Enclosures)
: '''Green.'''
Unit Penetration Penetration Number Number Manufacturer Potentially Affected Components RBCU '2A' VIBRATION SW.RBCU '2B' VIBRATION SW.RBCU '2A' VIBRATION SW.RBCU '2B' VIBRATION SW.2CC-5 RCP '2A1' COOLER OULTET VLV. (OAC)H2 SAMPLE VLV. 2SV213 H2 SAMPLE VLV. 2SV214 2CC-5 RCP '2A1' COOLER OULTET VLV.H2 SAMPLE VLV. 2SV-210 2GWD-12 WASTE DISPOSAL SYS. QUENCH TANK VENT VLV.2HP-228 '2A1' RCP SEAL RETURN STOP VLV. (MOTOR PWR.)2HP-226 '2A2' RCP SEAL RETURN STOP 'VLV. (MOTROR PWR.)RBCU '2B' MOTOR HEATER 2GWD-12 (SEE TERM. BLK. 10 ABOVE)RBCU '2A' MOTOR HEATER 2 2 EF 06 Viking RCP '2A1' TACHOMETER RCP '2A1' ZERO SPEED SWITCH NO. 1 RCP '2A1' STATOR TEMP. RTD RCP '2A1' MANIFOLD OIL PRESS. SW. 2PS 103 RCP '2A1' MANIFOLD OIL PRESS. SW. 2PS 109 RCP'2A1' MANIFOLD OIL PRESS. SW. 2PS110 RCP '2A1' WATER LEAKAGE PROBE (L2AI)RCP '2A1' DC OIL PUMP PRESS. SW. 2SP107 RCP '2A1' UPPER OIL POT LEVEL SENSOR 2RCLT0135 R PIA 1I TTPPPFR OJT. POT T.VFJ..SFN.SOR 2RCLTO1 35 RCP '2A1' LOWER OIL POT LEVEL SENSOR 2RCLT0136 RCP '2A1' VIBRATION DETECTOR RCP '2A1' ZERO SPEED SWITCH NO. 2_ _ _RCP '2A1' STATOR TEMP. RTD 9 Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
A NRC-identified non-cited violation of 10 CFR 50 Appendix B, Criterion X, Inspection, was identified for the failure to develop and implement an inspection program for monitoring the main steam line in the Unit 1, 2 and 3 East Penetration Rooms. The finding was considered to be a performance deficiency in that the licensee had committed to perform inspections of the steam lines to support the acceptability of Dukes design and analysis for the main steam lines, but the inspections were not being performed.
Unit Penetration Penetration Number Number Manufacturer Potentially Affected Components RCP '2A1 AC OIL PUMP PRESS. SWITCH RCP '2A1' ZERO SPEED SWITCH NO. 3 RCP '2A1' LOWER OIL POT LEVEL SENSOR 2RCLT0136 2 2 EF 09 Viking PZR. HEATER GROUP 2E___ _PZR. HEATER GROUP 2H 3 3 EB 08 Viking RB TELEPHONE SYS TERMINAL CAB MAIN FUEL HANDLING BRIDGE TB 2234 RC PUMP DRAIN OIL STAND PIPE PS424 RB PA SYSTEM SPEAKER RC PUMP DRAIN OIL STAND PIPE 3SV233 RC PUMP DRAIN OiL STAND PHIPE PS425 RC PUMP DRAIN OIL STAND PIPE 3SV234 MAIN FUEL HANDLING BRIDGE TB 2234 SOUND POWERED TELEPHONE MAIN FUEL HANDLING BRIDGE TB 2234 3 3 EC 04 Viking POWER RANGE NUCLEAR CHANNEL NI-5 RC WIDE RANGE PRESSURE (3PT21P)RC NARROW RANGE PRESSURE (3PT17P)RC OUTLET TEMP (3RD1A)RC FLOW LOOP A (3FT14B)RC FLOW LOOP B (3FTI5B)Note: Subsequent walkdown has determined that terminal block area 3 3 ED 08 Viking RB AUX VENT FAN 3B (PWR)RB AUX VENT FAN 3A (PWR)10 Attachment 1 Item 2005004-10 (Failure to Maintain Containment Duke Energy Response to Unresolved Electrical Penetration Enclosures)
Unit Penetration Penetration Number Number Manufacturer Potentially Affected Components RB ELEVATOR (PWR)EMERGENCY LIGHTING RC PUMP 3A1 CT 3 3 ED 10 Viking STM GEN 3A SAMPLE ISOL VALVE 3FDWVA0105 HYDROGEN SAMPLE SV214 (OEE-331-23)
RC PUMP 3A1 SEAL RETURN HPI VALVE 3HP-V43B RC PUMP 3A2 SEAL RETURN HPI VALVE 3HP-V43D RB AUX VENT FAN 3A VIB SW COMPUTER & RESET RB AUX VENT FAN 3A VIB SW COMPUTER & RESET SHIELD FOR RB AUX VENT FAN 3A VIB SW RB AUX VENT FAN 3B VIB SW COMPUTER & RESET RB AUAX V~1ii FAN 3B ViB SW COW1V1U'1 R & RESET SHIELD FOR RB AUX VENT FAN 3B VIB SW RC PUMP 3A1 SEAL RETURN HPI VALVE 3HP-V43B COMPUTER RC PUMP 3A2 SEAL RETURN HPI VALVE 3HP-V43D COMPUTER STM GEN 3A VENT VALVE 3RCVA0156 AND LS0156 STM GEN 3A VENT VALVE 3RCVA0155 AND LS0155 RB COOLING UNIT FANS 3A & 3B VIEB SWS HYDROGEN SAMPLE SV210 HYDROGEN SAMPLE SV211 HYDROGEN SAMPLE SV212 HYDROGEN SAMPLE SV213 RC PUMP 3A1 COOLER OUTLET VALVE 3CCVA2 STM GEN 3A VENT VALVE 3RCVA0156 AND LS0156 OTTFNCT4 TANK V.NT VAT .VF. 3WV1 HYDROGEN SAMPLE SV214 RC PUMP 3A1 SEAL RETURN HPI VALVE 3HP-V43B (PWR)RC PUMP 3A2 SEAL RETURN HPI VALVE 3HP-V43D (PWR)RB COOLING UNIT FAN 3B MOTOR HEATER 11 Duke Energy Response to Unresolved Electrical Penetration Enclosures)
Attachment 1 Item 2005004-10 (Failure to Maintain Containment Unit Penetration Penetration Number Number Manufacturer Potentially Affected Components STM GEN 3A SAMPLE ISOL VALVE 3FDWVA0105 HEATER QUENCH TANK VENT VALVE 3WDV1 HEATER RB COOLING UNIT FAN 3A MOTOR HEATER Note: Subsequent walkdown has determined that terminal block area where 3RC-155 and 3RC-156 are landed is not contaminated.


3 3 ED 11 Viking HPI & PURIFICATION LETDOWN COOLER 3A OUTLET VALVE 3HP4 RC PUMP 3A2 COOLER OUTLET VALVE 3CC-6 RB PURGE OUTLET VALVE 3PR-1 RC PUMP 3A2 COOLER OUTLET VALVE 3CC-6 COMPUTER RB COOLING UNIT FAN 3C VIB1 SW RB SAMPLING LINE OUTLET VALVE 3PR-9 RB SAMPLING LINE INLET VALVE 3PR-7 RB PURGE OUTLET VALVE 3PR-1 (PWR)RB COOLING UNIT FAN 3C MOTOR HEATER (PWR)3 3 ED 13 Viking RC PUMP 3A1 OIL TANK LEVEL ALARM RC PUMP 3A2 OIL TANK LEVEL ALARM FUEL HANDLING TRANSFER SYS 3B INCORE TANK LIGHT RELAY LOOSE PARTS MONITOR CHAN 1 (INCORE TUBE 1)LOOSE PARTS MONITOR CHAN 3 (INCORE TUBE 41)LOOSE PARTS MONITOR CHAN 2 (INCORE TUBE 34)LOOSE PARTS MONITOR CHAN 4 (INCORE TUBE 52)T QOSE' PARTR MC)N1TOP CT-TAN T1 (MAIN PDW T TNPv Al FLOW SENSOR HEAD 3B VALVE 3LP104 LOOSE PARTS MONITOR CHAN 7 (CF LINE A)LOOSE PARTS MONITOR CHAN 8 (CF LINE B)LOOSE PARTS MONITOR CHAN 22 (MAIN FDW LINE B)12 Attachment 1 Item 2005004-10 (Failure to Maintain Containment Duke Energy Response to Unresolved Electrical Penetration Enclosures)
The finding was considered to be more than minor because it impacted the Reactor Safety Initiating Events Cornerstone in that failure to perform the inspections could lead to failure to identify degrading main steam line conditions, which would cause an increase in the likelihood of an initiating event. The finding was screened as having very low safety significance under the Initiating Events Cornerstone, in that it did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available. This finding involved the cross-cutting aspect of Problem Identification and Resolution. (Section 1R22.3)
Unit Penetration Penetration Number Number Manufacturer Potentially Affected Components LOOSE PARTS MONITOR CHAN 18 (SG A VENT LINE)LOOSE PARTS MONITOR CHAN 12 (RC PUMP A2 DISCHARGE)
LOOSE PARTS MONITOR CHAN 11 (RC PUMP A2 SUCTION)LOOSE PARTS MONITOR CHAN 9 (RC PUMP Al SUCTION)LOOSE PARTS MONITOR CHAN 17 (SG A HANDHOLE)LOOSE PARTS MONITOR CHAN 10 (RC PUMP Al DISCHARGE)
PA SYSTEM TB PAJ18 (PWR)FLOW SENSOR HEAD 3B VALVE 3LP104 FUEL HANDLING TRANSFER SYS 3A HEATER MAIN FUEL HANDLING BRIDGE CONSOLE LIGHT/RECPT TB2234 1~ r~f' '~~ f'~A I (r%^^ ~ lF't~ T ThT('TTTTh~
X5"Tn'~ T T~RCri FOR TCA-lu000POS1l.1ON INSTIR-UNM1,4vic JD I23J FUEL HANDLING TRANSFER SYS 3B HEATER FUEL HANDLING TRANSFER SYS 3A FUEL HANDLING TRANSFER SYS 3A (PWR)FUEL HANDLING TRANSFER SYS 3B (PWR)ANN FOR CRD SERVICE STRUCTURE FAN MONITOR PNL #1 3 3 EF 10 Viking PRESS HEATER GROUP D (PWR)PRESS HEATER GROUP A (PWR)PRESS HEATER GROUP 3K (PWR)13 Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment ElectricaL Penetration Enclosures)
The electrical penetrations with evidence of terminal board contamination have been evaluated as follows: I. Unit 1 A. Affected Penetrations Oconee Nuclear Station (ONS) Reactor and Engineering Systems (RES) engineering has identified a number of electrical penetrations inside the east penetration room with contamination on the terminal strips. The affected electrical penetrations include:* Electrical Penetration lEA9* Electrical Penetration 1EB9* Electrical Penetration 1EC8* Electrical Penetration 1EC12* Electrical Penetration 1ED13* Electrical Penetration 1EF11* Electrical Penetration 1EE4 The following equipment is served by the above electrical penetrations and would therefore be vulnerable to failure following a main steam line break (MSLB) or feedwater line break(FWLB)
inside the East Penetration Rooms: Component Penetration Drawin g lAl & 1A2 RCP Seal Leakage lEA9 0-767-A42 lAl RCP Lower Seal Cavity Pressure 1EA9 0-767-A42 Quench Tank Level, Pressure and Temperature 1EA9 0-767-A42 lAl & 1A2 HPI Nozzle Warming Flow lEA9 0-767-A42 Pressurizer Temperature (IRC RD0043C) lEA9 0-767-A42 RV Level LT-5A lEA9 0-767-A42 Cameras inside the RB IEB9 0-767-A35 lAl RCP Term Box, AC & DC Oil Lift Pumps, Mtr Htr 1EC8 0-767-A6 lAl RCP Motor LPSW Inlet & Outlet Valves IEC12 0-767-A8 1A2 RCP Motor LPSW Inlet & Outlet Valves lEC12 0-767-A8 IPR-59 and IPR-60 IEC12 0-767-,8 1A RBCU Damper Position Indication IEC12 0-767-A8 lAl & 1A2 RCP Oil Tank Alarms IED13 0-767-A13 Loose Parts Monitoring System IED13 0-767-A13 Fuel Handling Systems lED13 0-767-A13 CRD Service Structure Monitoring Panel 1 IED13 0-767-A13 Pressurizer Heater Groups G & J lEFL 1 0-767-Al Incore Detector Assemblies 1EE4 -767-A58 14 Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
B. Effects on Environmentally Qualified Components A review of the ONS Equipment Database (EDB) was performed to identify which equipment was required to be environmentally qualifie Only the pressurizer temperature instrument (l:RC RD0043C) was listed as EQ.However, this instrument does not perform any safety functio Failure of this instrument does not affect the RG 1.97 pressurizer level indication in that density compensation is provided by lRC RD0043A and lRC RD0043B.C. Effects on Non-EQ Components All of the remaining components that could be affected by the contaminated penetrations are not environmentally qualified and are therefore not expected to functicn following MSLBs or FWLBs inside the East Penetraticn Room.With that being said, the effects of possible alarming conditions that may affect the operators, were evaluated as follows: Various alarms related to the operation of the lAl and 1A2 reactor coolant pump (RCP) may be received in the control room. Computer alarms may be generated for high RCP seal leakage. Statalarm 1SA-6, A-5 (RC Pump Al Seal Cavity Pressure Hi/Low) may actuate. Statalarms lSA-16, A-6 (RC Pump MotorlAl Oil Pot Low Level) and D-2 (RC Pump Motor 1A2 Oil Pot Low Level) may actuate. These statalarm response guides direct the operators to monitor the affecte RCP parameters and to refer to AP/1/A/1700/16, Abnormal Reactor Coolant Pump Operatio Operators may elect to secure the lAl and 1A2 RCPs based on these failed instruments.


Continued operation of these reactor coolant pumps is not required for accident mitigation or bringing the unit to a safe shutdown condition.
===Cornerstone: Mitigating Systems===
*
: '''Green.'''
A NRC-identified non-cited violation of 10 CFR 50.74 was identified for failure to make a notification of a change in operator or senior operator status regarding information for one licensed operator concerning his medical qualification. Specifically, the operator failed to meet the American Nuclear Standards Institute /American Nuclear Society (ANSI/ANS-3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, 1983 Standard for a blood pressure (BP) limitation. This impacted the NRCs ability to perform its regulatory function, in that the NRC was not able to make a licensing decision with regards to a potential restriction to ensure compliance with ANSI/ANS-3.4. Consequently, an operator stood several watches in a Technical Specification license position with his BP greater than the ANSI/ANS limits.


The lAl and 1A2 RCP Motor low pressure service water (LPSW)inlet & outlet valves are normally open. Contamination of the terminals may prevent closure of the affected valves.These valves are closed by the operator to isolate the applicable RCP motor and bearing coolers for maintenance.
This finding is of very low safety significance because there was no evidence that the operator endangered plant operations as a result of hypertension while performing licensed duties since the original issuance of his license. However, the regulatory significance was important because pertinent information was not provided to the NRC when the operator knowingly discontinued taking his medication. Subsequently, this impacted a licensing decision for the individual.


These valves may also be closed to isolate possible leaks in the applicable RCP motor stator or bearing coolers (ref.OSS-0254.00-00-1039).
(Section 1R11.2)
*
: '''Green.'''
A NRC-identified non-cited violation of 10 CFR 50 Appendix B, Criterion X, Inspection, was identified for the failure to develop and implement an inspection program for inspection and cleaning of the containment electrical penetrations located in the East and West Penetration Rooms of Units 1, 2, and 3.


However, cooler leakage is rot postulated to occur during a MSLB or FWLB inside tie east 15 Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
The finding was considered to be a performance deficiency in that the licensee had failed to develop an inspection program for their containment electrical penetrations to ensure cleanliness of the electrical connections. The inspectors concluded that if left uncorrected (no inspection) debris and rust accumulation could lead to failure of the electrical circuits during a high energy line break as a result of grounds and shorts. Therefore, failure to perform cleanliness inspections was considered to be more than minor because it could impact the Reactor Safety Mitigating Systems Cornerstone objective for reliability of a mitigating system/train (i.e., circuits needed to mitigate a high energy line break.
penetration room. Therefore, loss of function for these valves does not adversely affect the operator's ability to mitigate the consequences of a MSLB or FWLB.Loss of the quench tank level, pressure and temperature instruments do not affect the operator's ability to place the unit in a safe shutdown conditio Although these instruments are listed as Reg Guide (RG) 1.97 instruments, they have been classified as Category 3. Category 3 instruments are not required to be environmentally qualified in that they do not play a key role in the management of an accident (ref. Updated Final Safety Analysis Report (UFSAR) 7.5.2.35 -7.5.2.37).


Statalarms 1SA-6 A-7 (CS Quench Tank Level High/Low), 1SA-6 B-7 (CS Quench Tank Pressure High), and 1SA-6 C-7 (CS Quench Tank Temperature High) may actuate. Operators are directed to determine the cause of the alarm. A low level alarm would cause the quench tank pump and the component drain pump to trip. These pumps are not required to mitigate the consequences of an accident.Failure of the lAl & 1A2 high pressure injection (HPI)nozzle warming flow transmitters may generate computer alarms. There is no computer alarm response information availabl However, these instruments are not required for any safe shutdown functio These instruments do not play any role in the control of HPI flow following an accident.No actions are expected to be taken by the operator during emergency operations, should these instruments fail.Several components are not normally in service, with their power removed. These include the reactor building (RB)cameras, RV Level LT-5A, RB Fuel Handling Systems, PR-59 and PR-60. Therefore, no alarms are expected for these components.
The finding was screened as very low safety significance in the Phase 1 review under the Mitigating Systems Cornerstone, in that failure to perform an electrical penetration inspection was not considered to be a design deficiency, was not considered to represent a loss of safety system function, was not considered to represent an actual loss of safety function of a single train, and did not involve seismic, flooding or severe weather. This finding involved the cross-cutting aspect of Problem Identification and Resolution. (Section 1R22.2)
*
: '''Green.'''
A NRC-identified non-cited violation of 10 CFR 50 Appendix B, Section XVI, Corrective Action, for inadequate corrective actions related to the lack of timeliness of repairs to a Unit 2 East Penetration Room floor seal.


The 1A Reactor Building Cooling Unit (RBCU) damper position indication may fail. However, this indication is not required to verify proper operation of the RBCU. The damper is part of the non-QA ductwork and is not safety related (ref. OSS-0254.00-00-1026).
The failure to promptly repair the damaged floor seal was considered to be a performance deficiency. The finding was considered to be more than minor because if left uncorrected, additional seal area could fail and it would affect the Mitigating System Cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events, in that the high pressure injection (HPI) pumps could be flooded following a high energy line break in the East Penetration Room. However, in the seals current level of degradation, the inspectors concluded that the deficiency would not by itself result in the loss of function of the HPI pumps, because flooding would be limited by the size of the degraded/failed seal. Consequently, the finding was determined to be of very low safety significance, as it was screened out under the Mitigating Systems Cornerstone in the SDP Phase 1 Screening Worksheet with the determination that there was no loss of safety function. This finding involved the cross-cutting aspect of Problem Identification and Resolution. (Section 4OA2.6)


No operator action is expected from a failure oE the position indication.
===Cornerstone: Barrier Integrity===
*
: '''Green.'''
A self revealing, non-cited violation (NCV) of 10 CFR 50 Appendix B,
Criterion X, Inspection, was identified for an inadequate quality control (QC)inspection associated with the installation of the thermal overloads on the Unit 1 and 2 Control Room Outside Air Booster Fan (CROABF) Train B.


Numerous channels in the Loose Parts Monitoring System may be affecte The only operator action would be to 16 Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
The finding was considered to be a performance deficiency because the licensee failed to conduct an adequate QC inspection of the installation of the S4.4 overload relay heater elements on the safety-related B CROABF. The licensees failure to correctly install the thermal overloads on the Unit 1 and 2, B Train,
determine if the alarms generated were valid. Operator response to the failed channels would be to notify maintenance for repairs (ref. OP/l/A/1105/011).
CROABF was considered to be more than minor because it affected the Barrier Integrity Cornerstone attribute of maintaining control room habitability. Similar to NCV 05000269/2005002-02, this finding represented a similar degradation of the barrier function of the control room against smoke and/or a toxic atmosphere; thereby, requiring a Phase 3 evaluation be performed. However, since the exposure time associated with this CROABF finding is shorter than that used in the Phase 3 evaluation of NCV 05000269/2005002-02, it too is considered to be of very low safety significance. This finding involved the cross-cutting aspect of human performance. (Section 4OA3.3)


The control rod drive (CRD) service structure monitoring panel may be affecte Statalarms 1SA-2 D-6 (CRD Even Cooling Fan Fail) or 1SA-2 E-6 (CRD Odd Cooling Fan Fail)may actuate. Operators would be directed to monitcr the area temperature The CRD Service Structure Cooling Fans do not provide any accident mitigation functio Failure of any or all of the fans following a MSLB or FWLB inside the east penetration room will not result in any additional actions by the operator.Numerous incore detector assemblies may be affecte The incore detectors are not required post acciden With the reactor tripped, the neutron flux is monitored using NI-1 through NI-4, which are the RG 1.97 instruments (ref. UFSAR 7.5.2.12).
===Licensee-Identified Violations===
None


Effects on Pressurizer Heater Groups G and J do not add any additional consequences to the MSLB and FWLB inside the East Penetration Room. Statalarm 1SA-6 E-8 (Pressurizer Heaters Ground Fault) would be actuated due to failures of motor control centers (MCCs) 1XH, 1XI, 1XJ, and 1XK:. These MCCs are located inside the east penetration room and are expected to be lost due to environmental conditions resulting from a MSLB or FWLB inside the east penetration room. Pressurizer heaters with power routed through the SSF would remain available.
=REPORT DETAILS=


Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
Summary of Plant Status:
II. Unit 2 A. Affected Penetrations RES has identified a number of electrical penetrations inside the east penetration room with contamination on the terminal strips. The affected electrical penetrations include:* Electrical Penetration 2EB9* Electrical Penetration 2ED10* Electrical Penetration 2EF6* Electrical Penetration 2EF9 The following equipment is served by the above electrical penetrations and would therefore be vulnerable to failure following MSLB and FWLB inside the East Penetration Rooms: Component Penetration Drawing Reactor Building Cameras 2EB9 0-1767-A35 2A SG Sample Isolation (2FDW-105)
Unit 1 entered the report period at 100 percent rated thermal power (RTP). The unit was reduced to approximately 88 percent RTP on August 6, 2005, to perform turbine valve movement testing. The unit was returned to 100 percent RTP on the same day. The unit operated at or near 100 percent RTP for the remainder of the inspection period.
2EDIO 0-1767-AIO 2A1 RCP Seal Return Valve (2HP-228)
2EDLO 0-1767-AlO 2A1 RCP Cooler Outlet Valve (2CC-5) 2ED1O 0-1767-AIO 2A2 RCP Seal Return Valve (2HP-226)
2ED10 0-1767-A10 Quench Tank Vent Valve (2GWD-12)
2ED10 0-1767-A10 RB Hydrogen Sample Valves (SV210 -SV214) 2ED1O 0-1767-A10 2A & 2B RB Aux Fan Vibration Switches 2EDO 0-1767-AlO 2A & 2B RBCU Fan Vibration Switches 2ED1O 0-1767-l10 2A & 2B RBCU Motor Heaters 2ED10 0-1767-A10 2A1 RCP Instrumentation 2EF6 0-1767-AI39 Pressurizer Heater Groups 2E and 2H 2EF9 0-1767-Al B. Effects on Environmentally Qualified Components A review of the EDB was performed to identify which equipment was required to be environmentally qualified.


The 2A steam generator (SG) sample isolation valve (2FDW-105), the Quench Tank Vent Valve (2GWD-12), and the! RB Hydrogen Sample Valves (SV210 -SV214) are the only components listed as environmentally qualified.
Unit 2 entered the report period at 100 percent RTP. The unit was reduced to approximately 88 percent RTP on July 9, 2005, to perform turbine valve movement testing. The unit was returned to 100 percent RTP on the same day. On September 26, 2005, the unit commenced a power coastdown in advance of the End-of-Cycle 21 (2EOC21) refueling outage, and the unit completed the inspection period at approximately 93 percent RTP. The unit operated at or near 100 percent RTP for the remainder of the inspection period.


2FDW-105 is normally closed. The valve is opened periodically to sample the 2A SG. The valve receives an 18 Attachment 1 Duke Energy Response to UnresoLved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
Unit 3 entered the report period at 100 percent RTP. The unit automatically tripped on August 31, 2005, due to the complete loss of power to the newly installed digital control rod drive (CRD) system while performing CRD testing. A design deficiency resulted in an excessive cooldown of the reactor coolant system (RCS), resulting in an engineered safeguards actuation on low RCS pressure at 1600 psig. The unit entered a forced outage to identify the cause of the trip and overcooling event and to conduct repairs. Following repairs, the unit was taken critical on September 6, 2005, and returned to 100 percent RTP on September 8, 2005. The unit operated at or near 100 percent RTP for the remainder of the inspection period.
automatic closure signal from engineered safeguards (ES)Channel 1, but it does not perform any event mitigation functio The valve is not required to close for containment isolation (reE. OSS-0254.00-00-1036).


Therefore, failure of the valve to operate following a MSLB or FWLB inside the east penetration room has no adverse consequence.
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
{{a|1R01}}


The Quench Tank Vent Valve (2GWD-12)
==1R01 Adverse Weather Protection Tornado Watch (Remnants of Huricane Katrina)
is normally closed.The valve may be opened periodically to vent the quench tank to the gaseous waste disposal system. If opened, the valve automatically closes following an engineering safeguards signal to isolate containmen This automatic closure function is credited for large break loss of coolant accident (LOCA), rod ejection accident, and. small break LOCA (ref. OSS-0254.00-00-1032).


The automatic closure function is not required for MSLB or FWLB inside the east penetration room.The RB Hydrogen Sample Valves are normally closed with the power removed. The loss of the hydrogen sample valves (SV210 through SV214) would result in the loss of cne hydrogen analyzer channel. The hydrogen analyzers are no longer required to mitigate design basis accident The hydrogen analyzers have been reclassified as RG 1.97 Category 3 instruments (ref. Selected Licensee Commitment 16.7.4 Bases). As such the analyzers are no longer required to be environmentally qualified.
====a. Inspection Scope====
==
The inspectors verified that the licensee responded appropriately to a tornado watch issued for Oconee County, SC on August 29, 2005. The inspectors verified that operations personnel entered abnormal procedure AP/0/A/1700/006, Natural Disaster, and that there were no ongoing maintenance activities on systems that required restoration by the procedure. The inspectors also verified that control room personnel had completed Enclosure 5.4, Severe Weather, as required by the AP.


C. Effects on Non-EQ components All of the remaining components that could be affected by the contaminated penetrations are not environmentally qualified and are therefore not expected to function following MSLBs or FWLBs inside the East Penetration Room.With that being said, the effects of possible alarming conditions that may affect the operators, were evaluated as follows: The RB cameras are not normally in service with the! power removed. Therefore, no alarms are expected for these components.
====b. Findings====
No findings of significance were identified. {{a|1R04}}


The 2A1 RCP Seal Return Valve (2HP-228)
==1R04 Equipment Alignment
and 2A2 RCEF Seal Return Valve (2HP-226)
are normally open. The valves are 19 Attachment 1 Duke Energy Response to UnresoLved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
not required to operate to mitigate any design basis accident However, the valves are designed to automatically close when the seal inlet flow to the applicable RC Pump is low coupled with low component cooling flow. In addition, these valves provide input to another interlock to automatically close 2HP-21 when all four RCP seal return valves are closed. Neither of these non-safety automatic closure circuits are required to function for accident mitigatio It should be noted that should an ES Channel 2 signal actuate due to the accident, 2HP-21 will automatically close to isolate all RCP seal return (ref. OSS-0254.00-00-1001).


The 2A1 RCP Cooler Outlet Valve (2CC-5) is normally open.The valve is not required to close to mitigate any design basis accident However, operators may close the valve following a defective cooling coil on the 2A1 RCP to isolate reactor coolant system (RCS) leakage into the CC system (ref. OSS-0254.00-1022).
====a. Inspection Scope====
==
The inspectors conducted partial equipment alignment walkdowns to evaluate the operability of selected redundant trains or backup systems while the other train or system was inoperable or out of service. The walkdowns included, as appropriate, reviews of plant procedures and other documents to determine correct system lineups, and verification of critical components to identify any discrepancies which could affect operability of the redundant train or backup system. The following three systems were included in this review:
* The high pressure service water (HPSW) system with the B HPSW pump out of service (OOS) for the replacement of the pumps rotating element
* Keowee Hydro Unit (KHU) -1 and the underground power path with KHU-2 OOS following an emergency lockout while attempting to generate to the grid (Problem Investigation Process report (PIP) O-05-5118)
* Primary instrument air system with a backup instrument air compressor OOS for maintenance


This is not required to be postulated with a MSLB or FWLB inside the east penetration room.Failure of the 2A & 2B RB Aux Fan Vibration Switches may cause computer alarms for high vibration on the affected fans (ref. OSS-0254.00-00-1030).
====b. Findings====
No findings of significance were identified. {{a|1R05}}


No operator acticn is expected to occur other than notifying Engineering to evaluate the alarms.Failure of the 2A & 2B RBCU Fan Vibration Switches may cause computer alarms for high vibration on the affected fans. The RBCUs are actuated by an engineering safeguards signal on high reactor building pressur Should these alarms occur during normal operation, the operators may secure both the 2A and 2B RBCUs, if running. MSLB and FWLB outside containment will not actuate engineering safeguards on high reactor building pressur Therefore, the RBCUs should not be operating in the emergency cooling mcde of operatio The operator may secure the affected RECUs, if it is concluded that they are not needed to mitigate the event. Regardless if the RBCUs are left operating or tripped by the operator, t:he RBCUs are not required to mitigate a MSLB or FWLB inside the east penetration room (ref. OSS-0254.00-00-1026).
==1R05 Fire Protection


Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
====a. Inspection Scope====
Failure of the 2A & 2B RBCU Motor Heaters are not expected to result in any additional alarms in the control room.The affected 2A1 RCP instrumentation includes the following:
==
* Tachometer
The inspectors conducted tours in eighteen areas of the plant to verify that combustibles and ignition sources were properly controlled, and that fire detection and suppression capabilities were intact. The inspectors selected the areas based on a review of the licensees safe shutdown analysis and the probabilistic risk assessment based sensitivity studies for fire-related core damage sequences. Inspections of the following areas were conducted during this inspection period:
* Zero Speed Switches No. 1, 2, and 3* Stator Temperature RTD* Oil Pressure Switches 2PS103, 2PS109, 2P110* Water Leakage Probe* DC Oil Pump Pressure Switch 2PS107* AC Oil Pump Pressure Switch* Upper Oil Pot Sensor LT135* Lower Oil Pot Sensor LT136* Vibration Detector Failure of the 2A1 RCP instrumentation may result in various alarms related to the operation of the pump.Statalarms 2SA-1 E-8 (RC Pump 2A1 Oil Tank Level High), 2SA-9 E-2 (RC Pump Vibration Emergency High), 2SA-16, D-1 (RC Pump Motor 2A1 Oil Pot Low Level) and 2SA-16 E-1 (RCP 2A1 Oil Lift Pump Pressure Low) may actuate. These!statalarm response guides direct the operators to monitor the affected RCP parameters and to refer to AP/2/A/1700/16, Abnormal Reactor Coolant Pump Operatio Operators may elect to secure the 2A1 RCP based on these failed instrument Continued operation of this reactor coolant pump is not required for accident mitigation or bringing the unit to a safe shutdown condition.
* Unit 1, 2, and 3 Turbine Building Basement Level (3)
* Unit 1, 2, and 3 Equipment Rooms (3)
* Unit 1 and 2 East and West Penetration Rooms (4)
* Unit 1, 2, and 3 Auxiliary Shutdown Panels (2)
* Unit 1, 2, and 3 Turbine Building Ground Level (3)
* Unit 1, 2, and 3 Turbine Building Operating Level (3)


The effects on Pressurizer Heater Groups 2E and 2H do not add any additional consequences to the MSLB and FWLB inside the East Penetration Room. Statalarm 2SA-6 E-8 (Pressurizer Heaters Ground Fault) would be actuated due to failures of MCC 2XH, 2XI, 2XJ, and 2XK. These MCCs are located inside the east penetration room and are expected to be lost due to environmental conditions resulting from a MSLB or FWLB inside the east penetration room. Pressurizer heaters with power routed through the SSF would remain available.
====b. Findings====
No findings of significance were identified. {{a|1R11}}


AtteLchment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
==1R11 Licensed Operator Requalification
III. Unit 3 A. Affected Penetrations RES has identified a number of electrical penetrations inside the east penetration room with contamination on the terminal strips. The affected electrical penetrations include:* Electrical Penetration 3EB8* Electrical Penetration 3EC4* Electrical Penetration 3ED8* Electrical Penetration 3ED10* Electrical Penetration 3EDl1* Electrical Penetration 3ED13* Electrical Penetration 3EF10 The following equipment is served by the above electrical penetrations and would therefore be vulnerable to failure following MSLB and FWLB inside the East Penetratio Rooms: Component Penetration Drawing RB Telephone System 3EB8 0-2767-A36 RB Fuel Handling System 3EB8 0-2767-A36 RC Pump Oil Drain Standpipe Press Switches 3EB8 0-2767-A36 Power Range Detector NI-5 3EC4 0-2767-A21 RC Wide Range Pressure (3PT-21P)
3EC4 0-2767-A21 RC Narrow Range Pressure (3PT-17P)
3EC4 0-2767-A21 RC Outlet Temperature (3RD-lA) 31EC4 0-2767-A21 RC Loop A Flow (3FT-14B)
3EC4 0-2767-A21 RC Loop B Flow (3FT-15B)
3EC4 0-2767-A21 3A & 3B RB Aux Fans 3ED8 0-2767-A6 RB Elevator 3ED8 0-2767-A6 RB Emergency Lighting 3ED8 0-2767-A6 3A1 RCP Current Transformer 3ED8 0-2767-A6 3A Steam Generator Sample (3FDW-105)
3ED1O 0-2767-A10 3A1 RCP Seal Return Valve 3ED10 0-2767-A10 3A2 RCP Seal Return Valve 3ED10 0-2767-A10 3A & 3B RB Aux Fans Vib Switches 3ED1O 0-2767-AlO 3A & 3B RBCU Fans Vib Switches 3ED10 0-2767-A10 3A & 3B RBCU Fan Motor Heaters 3ED1O 0-2767-A10 RC Loop A High Point Vents (3RC-155 & 3RC-156) 3ED10 0-2767-A10 RB Hydrogen Sample Valves (SV210 -SV214) 3ED10 0-2767-A1O 3A1 RCP Cooler Outlet Valve (3CC-5) 3ED10 0-2767-AlO


Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
==
Quench Tank Vent Valve (3GWD-12)
===.1 Simulator Training===
3ED10 0-2767-A10 3B Letdown Cooler Outlet (3HP-4) 3EDl 1 0-2767-A11 3A2 RCP Cooler Outlet Valve (3CC-6) 3ED1 1 0-2767-A11 RB Purge Outlet Valve (3PR-1) 3ED1l 0-2767-A11 3C RBCU Fan Vib Switch 3ED11 0-2767-A11 3C RBCU Fan Motor Heater 3ED11 0-2767-All RB Sampling Inlet & Outlet Valves (3PR-7 & 3PR-9) 3EDl1 0-2767-All 3A1 & 3A2 RCP Oil Tank Level Alarms 3ED13 0-2767-A13 RB Fuel Handling Transfer System 3ED13 0-2767-A 13 Incore Tank Light Relay 3ED13 0-2767-A13 Loose Parts Monitoring System 3ED13 0-2767-A 13 3LP-104 Flow Sensor 3ED13 0-2767-A13 RB PA System 3ED13 0-2767-A13 CRD Service Structure Fan Monitor Panel 1 3ED13 0-2767-A 13 Pressurizer Heater Groups A, D, & K 3EF10 0-2767-Al B. Effects on Environmentally Qualified Components A review of the Equipment Database was performed to identify which equipment was required to be environmentally qualifie The following EQ related components include:* RC Wide Range Pressure (3PT-21P)* RC Narrow Range Pressure (3PT-17P)* 3A SG Sample Isolation (3FDW-105)
====a. Inspection Scope====
* RC Loop A High Point Vent Valves (3RC-155 & 3RC-156)* Quench Tank Vent Valve (3GWD-12)* RB Hydrogen Sample Valves (SV210 -SV214)* 3B Letdown Cooler Outlet (3HP-4)* RB Sampling Inlet & Outlet Valves (3PR-7 & 3PR-9)The RC Wide Range Pressure (3PT-21P)
The inspectors observed licensed operator simulator training on September 21, 2005.
provides input. to ES Analog Channel A (ref. OSS-0254.00-00-2003).


This transmitter also provides input to Statalarm 3SA-2 D-4 (RC Press Emergency Low). Additional inspections were performed on the affected terminal strip. No contamination was detected on the terminals used by this component.
The scenario involved a main steam line break outside of containment. The simulated event was complicated by a failure of valves needed to isolate the faulted steam generator. The inspectors observed crew performance in order to assess licensed operator performance and the evaluators critique, focusing on: communications; ability to take timely and proper actions; prioritizing, interpreting, and verifying alarms; correct use and implementation of procedures, including the abnormal procedures; timely control board operation and manipulation, including immediate operator actions; and oversight and direction provided by the shift supervisor and shift technical advisor. The inspectors did not observe any problems during the scenario.


Therefore, this component will not be affected by M[SLB or FWLB inside the east penetration room.The RC Narrow Range Pressure (3PT-17P)
====b. Findings====
and RC Outle!t Temperature (3RD 1A) provide input to RPS Channel AI.Additional inspections were performed on the affect~ed terminal strip. The limited amount of contamination would 23 Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
No findings of significance were identified.
not impact the function of the component Therefcre, these components will not be affected by MSLB or FWLB inside the east penetration room.3FDW-105 is normally closed. The valve is opened periodically to sample the 3A SG. The valve receives an automatic closure signal from ES Channel 1, but it does not perform any event mitigation functio The valve is not required to close for containment isolation (ref. CiSS-0254.00-00-1036).


Therefore, failure of the valve to operate following a MSLB or FWLB inside the east penetration room has no adverse consequence.
===.2 Requalification Program===
====a. Inspection Scope====
The inspectors reviewed the facility operating history and associated documents in preparation for this inspection. During the weeks of March 21 - 25 (in office) and March 28 - April 1 (on site), 2005, the inspectors reviewed documentation, interviewed licensee personnel, and observed the administration of simulator operating tests and Job performance Measures (JPMs) associated with the licensees operator requalification program. Each of the activities performed by the inspectors was done to assess the effectiveness of the licensee in implementing requalification requirements identified in 10 CFR 55, Operators Licenses. The evaluations were also performed to determine if the licensee effectively implemented operator requalification guidelines established in NUREG-1021, Operator Licensing Examination Standards for Power Reactors, and Inspection Procedure 71111.11, Licensed Operator Requalification Program. The inspectors also reviewed and evaluated the licensees simulation facility for adequacy for use in operator licensing examinations. The inspectors observed two operator crews during the performance of the operating tests. Documentation reviewed included written examinations, JPMs, simulator scenarios, licensee procedures, on-shift records, simulator modification request records and performance test records, the feedback process, licensed operator qualification records, remediation plans, watchstanding, and medical records. The records were inspected against the criteria listed in Inspection Procedure 71111.11. Documents reviewed during the inspection are listed in the to this report.


The RC Loop A High Point Vent Valves (3RC-155 & 3RC-156)are normally closed with the power removed. However, these valves are required to be capable of being opened to vent non-condensable gases and/or steam from the RCS that might inhibit natural circulatio These valves are also required to be capable of being opened to provide a. letdown path to aid in maintaining pressurizer level (ref. OSS-0254.00-00-1033).
====b. Findings====
=====Introduction:=====
A Green NRC-identified non-cited violation (NCV) of 10 CFR 50.74(c),
Notification of change in operator or senior operator status, was identified for failure to notify the NRC of a change in a licensed operators medical status.


Additional inspections were performed on the affected terminal strip. No contamination was detected on the terminals used by these valves. Therefore, these valves will not be affected by MSLB or FWLB inside the east penetration room.The Quench Tank Vent Valve (3GWD-12)
=====Description:=====
is normally closed.The valve may be opened periodically to vent the cqench tank to the gaseous waste disposal system. If oper.ed, the valve automatically closes following an engineering safeguards signal to isolate containmen This automatic closure function is credited for large break LOCA, rod ejection accident, and small break LOCA (ref. OSS-0254.00-00-1032).
The NRC identified that, during the period between December 20, 2004 and January 24, 2005, an operator stood several watches in a TS license position with blood pressure (BP) greater than ANSI/ANS-3.4-1983, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, limits. When the facility became aware of the operators failure to meet these limits, they failed to notify the NRC.


The automatic closure function is not required for MSLB or FWLB inside the east penetration room.The RB hydrogen sample valves are normally closed with the power removed. The loss of the hydrogen sample valves (SV210 through SV214) would result in the loss of one hydrogen analyzer channel. The hydrogen analyzers are no longer required to mitigate design basis accident The hydrogen analyzers have been reclassified as RG 1..C7 Category 3 instruments (ref. SLC 16.7.4 Bases). As such the analyzers are no longer required to be environmentally qualified.
A NRC licensed operators medical record indicated that he had BP in excess of the ANSI/ANS-3.4-1983 limits. On February 12, 2004, the facility licensee sent a letter to the NRC identifying that this operator was on medication for controlling high BP. The NRC doctor stated that a medical condition was not necessary to be placed on his license since he was on medication and it was being controlled. In a medical examination on December 20, 2004, the facility determined that the operator took it upon himself to try to reduce his BP with diet but was unsuccessful. This medical examination also determined that the operators non-medicated BP was outside of the ANSI/ANS-3.4-1983 limits. In the meantime, the operator conducted licensed activities with his BP greater than the ANSI/ANS-3.4-1983 limits during the period stated above.


Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment ElectricaL Penetration Enclosures)
=====Analysis:=====
The 3B Letdown Cooler Outlet (3HP-4) will not be adversely affecte The cabling connected the affected terminals provide position indication only. The valve power and control cabling are routed through the west penetration room.The RB sampling inlet and outlet valves (3PR-7 & 3PR-9) are normally open to provide a flow path to monitor radiation levels inside the Reactor Buildin The valves are required to close following actuation of ES Channel 1 to provide containment isolation (ref. OSS-0254.00-00-4001).
The facility licensees failure to report that one of their licensed operators did not meet the requirements of ANSI/ANS-3.4-1983 as required by 10 CFR 50.74 was a performance deficiency. This was reasonably within the licensees ability to foresee and prevent. Because this issue affected the NRCs ability to perform its regulatory function, it was evaluated using the traditional enforcement process. The regulatory significance was important because pertinent information was not provided to the NRC when the operator knowingly discontinued taking his medication. Subsequently, this impacted a licensing decision for the individual. This finding is of very low safety significance (Green) because there was no evidence that the operator endangered plant operations as a result of hypertension while performing licensed duties since the original issuance of his license.


This automatic closure function is credited for large break LOCA, rod ejection accident, and small break LOCA. The automatic closure function is not required for MSLE or FWLB inside the east penetration room.C. Effects on Non-EQ Components All of the remaining components that could be affected by the contaminated penetrations are not environmentally qualified and are therefore not expected to functicn following MSLBs or FWLBs inside the East Penetraticn Room.With that being said, the effects of possible alarming conditions that may affect the operators, were evaluated as follows: Numerous components are not normally in service with the power isolated or do not have alarming capability.
=====Enforcement:=====
10 CFR 50.74 states, in part, that each licensee shall notify the NRC within 30 days of identifying a permanent disability or illness as described in 10 CFR 55.25 of this chapter. 10 CFR 55.25 states, in part, that If, during the term of the license, the licensee develops a permanent physical or mental condition that causes the licensee to fail to meet the requirements of § 55.21 of this part, the facility licensee shall notify the Commission, within 30 days of learning of the diagnosis, in accordance with § 50.74(c). For conditions for which a conditional license (as described in § 55.33(b) of this part) is requested, the facility licensee shall provide medical certification on Form NRC 396 to the Commission (as described in § 55.23 of this part).


Therefore, no alarms are expected for these components.
The facility licensee must also certify which industry standard (i.e., the 1983 or 1996 version of ANSI/ANS-3.4, or other NRC-approved method) was used in making the fitness determination. 10CFR 55.57(b)(1) states, in part, the medical condition and general health of the licensee continue to be such as not to cause operational errors that endanger public health and safety. It is incumbent upon the facility licensee to ensure that individual licensed operators are medically qualified to operate the plant or perform licensed duties. The facilitys physician must determine whether the operator meets the requirements of section 55.57(b)(1), (i.e., the operators medical condition and general health will not adversely affect the performance of assigned operator duties or cause operational errors that endanger public health and safety.) Furthermore, the facility must notify the NRC on NRC Form 396 regarding his medical status and potential medical issues that may require a license condition.


These components include:* RB telephone system* RB Fuel Handling and Transfer Systems* RB Elevator* RB Emergency Lighting* Incore Tank light relay* RB PA System A number of other reactor protective system (RPS) Channel A parameters may be affecte These include NI-5, 3FT-14B, and 3FT-15B. Should the failure mode result in a non-conservative instrument output, RPS Channel A may not be able to actuate on high flux, or flux-flow imbalanc The affected RPS trip functions are not credited for MSLB or 25 Attachment 1 Duke Energy Response to UnresoLved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
Contrary to the above, the licensee failed to notify the NRC after becoming aware of a potential disqualifying medical condition. The failure to report noncompliance with the ANSI/ANS-3.4-1983 medical requirements, as implied by 10 CFR 50.74, is of low safety significance. Additionally, this issue has been entered into the facilitys corrective action program (PIP O-05-02152). Therefore, this violation is being treated as an NCV, consistent with section VI.A of the NRC Enforcement Policy: NCV 05000269,270,287/
FWLB. Therefore the RPS channel is not considered to be adversely affected and will continue to perform its associated safety function for MSLB or FWLB inside the east penetration room. (ref. OSS-0254.00-00-2002).
2005004-01, Performing Licensed Duties While Medically Unqualified.
{{a|1R12}}


Failure of the RCP drain oil standpipe pressure switches and solenoids (3PS-424, 3PS-425, 3SV-233, 3SV-234) may result in computer alarms associated with 3A1 and 3A2 RCP Motor Oil Standpipes (see OEE-350-18).
==1R12 Maintenance Effectiveness


The associated computer points for these alarms are D2235 and D2236.However, there is no alarm response information available for these alarms. Review of the RCP normal operating procedure (OP/1103/006)
====a. Inspection Scope====
and the RCP abnormal operating procedure (AP/1700/16)
==
did not reveal any additional information that would provide insight into operator respons Therefore, it may be concluded that the operators would contact Engineering prior to taking any action to respond to these alarms.Failure of the 3A and 3B RB aux fans and vibration switches may cause computer alarms for high vibration on the affected fans (ref. OSS-0254.00-00-1030).
The inspectors reviewed the licensees effectiveness in performing routine maintenance activities. This review included an assessment of the licensees practices pertaining to the identification, scoping, and handling of degraded equipment conditions, as well as common cause failure evaluations. For each item selected, the inspectors performed a detailed review of the problem history and surrounding circumstances, evaluated the extent of condition reviews as required, and reviewed the generic implications of the equipment and/or work practice problem. For those systems, structures, and components (SSCs) scoped in the maintenance rule per 10 CFR 50.65, the inspectors verified that reliability and unavailability were properly monitored and that 10 CFR 50.65 (a)(1) and (a)(2) classifications were justified in light of the reviewed degraded equipment condition. The inspectors reviewed the following items:
* KHU-2, which included the following PIPs: O-05-5118, KHU-2 Emergency Lockout While Attempting to Generate to the Grid; and O-05-5365, KHU-2 Emergency Lockout While Performing PT/0/A/0620/016, Keowee Hydro Emergency Start Test
* 1RIA-40 (Unit 1, Condenser Air Ejector Offgas Radiation Indicating Alarm),which included the following: PIP O-05-5009,1RIA-40 count rate indication has been increasing over time and varies significantly when compared to 2RIA-40 and 3RIA-40; and IP/0/B/0360/037, 1RIA-40, Sorrento Gas Monitor


No operator action is expected to occur other than notifying Engineering to evaluate the alarms.The 3A1 RCP current transformer may be affecte This may result in a loss of amperage indication for the affected RCP. The loss of indication for motor current is acceptable.
====b. Findings====
No findings of significance were identified. {{a|1R13}}


The 3A1 & 3A2 RCP seal return valves (3HP-228 and 3HP-226)are normally open. The valves are not required to operate to mitigate any design basis accident However, the valves are designed to automatically close when the seal inlet flow to the applicable RC Pump is low coupled with low component cooling flow. In addition, these valves provide input to another interlock to automatically close 3HP-21 when all four RCP seal return valves are closed.Neither of these non-safety automatic closure circuits is required to function for accident mitigatio It should be noted that should an ES Channel 2 signal actuate due to the accident, 3HP-21 will automatically close to isolate all RCP seal return (ref. OSS-0254.00-00-1001).
==1R13 Maintenance Risk Assessment and Emergent Work Evaluations


Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
====a. Inspection Scope====
Failure of the 3A, 3B, and 3C RBCU vibration switches may cause computer alarms for high vibration on the affected fans. The RBCUs are actuated by an engineering safeguards signal on high reactor building pressur Should these alarms occur during normal operation, the operators may secure all of the RBCUs, if running. MSLB and FWLE outside containment will not actuate engineering safeguards on high reactor building pressur Therefore, the RBCUs should not be operating in the emergency cooling mode of operation.
==
The inspectors evaluated the following attributes for the eight selected SSCs and activities listed below:
: (1) the effectiveness of the risk assessments performed before maintenance activities were conducted;
: (2) the management of risk;
: (3) that, upon identification of an unforseen situation, necessary steps were taken to plan and control the resulting emergent work activities; and
: (4) that maintenance risk assessments and emergent work problems were adequately identified and resolved.
* Relay replacement on standby bus to main feeder bus supply breakers B1T-6 and B1T-7 with the A Lee Combustion Turbine OOS
* B HPSW pump with the 1X6 Motor Control Center OOS for relay replacement
* B HPSW pump with the Primary Instrument Air Compressor OOS
* PIP O-05-4724, Near Miss During Scheduled Work to 3DW-18
* PIP O-05-5376, Orange Risk Condition During Severe Thunderstorm Warning with KHU-2 and the Overhead Power Path OOS
* PIP O-05-5551, Tornado Watch (Remnants of Hurricane Katrina) Combine With Yellow Risk Significant Maintenance Items to Cause Orange Risk Condition
* PIP O-05-5938, Unable to Isolate and Drain Elevated Water Storage Tank Due to Orange Risk Condition Activity With no Documented Plant Operations Review Committee Review
* PIP O-05-5987, Unit 2 Reactor Protection System Channel B Placed in Manual Bypass Due to Inoperability of 2NI-6


The operator may secure the affected RBCUs, if it is concluded that they are not needed to mitigate the event.Regardless, if the RBCUs are left operating or tripped by the operator, the RBCUs are not required to mitigate a MSLB or FWLB inside the east penetration room (ref. OSS-0254.00-00-1026).Failure of the 3A, 3B, and 3C RBCU motor heaters are not expected to result in any additional alarms in the control room.The 3A1 & 3A2 RCP cooler outlet valves (3CC-5 and 3CC-6)are normally open. The valves are not required to close to mitigate any design basis accident However, operators may close the valve(s) following a defective cooling coil on the affected RCP to isolate RCS leakage into the component cooling (CC) system (ref. OSS-0254.00-1022).
====b. Findings====
=====Introduction:=====
A Green self-revealing finding (FIN) was identified for inadequate maintenance and oversight of repair efforts on the actuator of 3DW-18 (the Unit 3 Upper Surge Tank (UST) Makeup Valve). Specifically, while attempting to repair an air leak on the actuator of 3DW-18, maintenance technicians removed the valves bonnet and were ready to remove the valves diaphragm with no hydraulic isolations made between the valve and the main condenser. Had the diaphragm been removed from 3DW-18, it is likely that Unit 3 would have tripped due to a loss of main condenser vacuum, as the top of the UST dome is vented to the main condenser.


RCP cooler ruptures are not required to be postulated with a MSLB or FWLB inside the east penetration room.Failure of the 3A1 & 3A2 :RCP oil tank level alarms may result in statalarms inside the control room. Statalarms 3SA-1 E-8 (RC Pump Motor 3A1 Oil Pot Low Level) and. 3SA-1 E-9 (RC Pump Motor 3A2 Oil Pot Low Level) may actuate.These statalarm response guides direct the operators to monitor the affected RCP ]parameters and to refer to AP/3/A/1700/16, Abnormal :Reactor Coolant Pump Operation.
=====Description:=====
At approximately 3 p.m. on July 20, 2005, with Unit 3 in Mode 1 at 100 percent RTP, the bonnet of 3DW-18 was removed to repair an air leak on the valves actuator. The maintenance crew was ready to pull the valves diaphragm, when they noticed it was under a vacuum. The work crew stopped work and questioned the condition with the Work Control Center (WCC) Senior Reactor Operator (SRO). The removal of the diaphragm would have exposed the units main condenser to a 6-inch pathway to atmosphere. PIP O-05-4724 states, The WCC SRO knew that there was no hydraulic isolation on the line and immediately stopped the crew and instructed them to return the valve to the condition they had found it in before they started work. Had the diaphragm been removed from the valve it would have most likely resulted in a unit trip on loss of vacuum. The WCC SRO was under the impression that the work order was only for repair of an air leak on the actuator and not for disassembly of the valve itself. As documented in PIP O-05-4724, a licensee investigation concluded that, Operations (OPS) personnel failed to follow their approved tagout process.


Operators may elect to secure the 3A1 and 3A2 RCPs based on these failed instrument Continued operation of these reactor coolant pumps is naot required for accident mitigation or bringing the unit to a safe shutdown condition.
Consequently, they failed to comprehend that hydraulic isolation was required for DW-18 Repair Air Leak on Actuator work. After determining that work external to the system only was being performed an inadequate tagout that led to this event was issued. The PIP also states that, The details of the work scope required to ensure proper isolation would occur was unclear to OPS personnel. Consequently, OPS personnel did not recognize that a hydraulic isolation of DW-18 was necessary.


Numerous channels in the Loose Parts Monitoring System may be affecte The only operator action would be to determine if the alarms generated were valid. Operator 27 Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
=====Analysis:=====
response to the failed channels would be to notify SPOC for repairs (ref. OP/3/A/1105/011).
This event was considered to be a performance deficiency, as the licensee failed to provide adequate maintenance and oversight of the efforts to repair an air leak on the 3DW-18 actuator; thereby, increasing the likelihood of a unit trip with a loss of normal heat sink. This issue was considered to be more than minor because it affected the Initiating Events cornerstone objective of limiting the likelihood of events that upset plant stability. The finding is associated with the configuration control attribute, in that the inadequate maintenance and oversight of the repairs to the actuator of 3DW-18 increased the likelihood of a reactor trip with a loss of normal heat sink due to inadequate configuration control of a secondary plant system. The consequences of the finding were assessed through Phase 2 of the SDP, and although the likelihood of a unit trip was increased and would have resulted in a loss of the normal heat sink, the exposure time for this condition was less than 3 days and all other mitigation capabilities described on the Phase 2, SDP worksheet for transient (reactor trip) core damage sequences were maintained. Consequently, the finding was determined to be of very low safety significance (Green). This finding involved the cross-cutting aspect of human performance.


The RB Purge Outlet Valve (3PR-1) is normally closed and must remain closed for containment isolation (ref. OSS-0254.00-00-4001).
=====Enforcement:=====
This finding was not a violation of regulatory requirements because the Unit 3 main condenser is not considered to be safety-related, and therefore not under the requirements of 10 CFR 50, Appendix B. This finding is identified as FIN 05000287/2005004-02, Inadequate Maintenance and Oversight Increased the Likelihood of a Unit 3 Reactor Trip with a Loss of Normal Heat Sink. This issue has been entered into the licensees corrective action program as PIP O-05-4724.
{{a|1R14}}


The power supply to the valve is normally isolated (ref. PI/3/A/0115/008).
==1R14 Personnel Performance During Non-routine Plant Evolutions


Therefore, no alarms are expected for this component.
====a. Inspection Scope====
==
The inspectors reviewed the operating crews performance during selected non-routine events and/or transient operations to determine if their response was appropriate to the event. As applicable, the inspectors:
: (1) reviewed operator logs, plant computer data, or strip charts to determine what occurred and how the operators responded;
: (2) deter-mined if operator responses were in accordance with the responses required by procedures and training;
: (3) evaluated the occurrence and subsequent personnel response using the SDP; and
: (4) confirmed that personnel performance deficiencies were captured in the licensees corrective action program. The non-routine evolutions reviewed during this inspection period included the following:
* PIP O-05-5118, KHU-2 Emergency Lockout While Attempting to Generate to the Grid
* PIP O-05-5365, KHU-2 Emergency Lockout While Performing PT/0/A/0620/016, Keowee Hydro Emergency Start Test
* PIP O-05-5613, Unit 3 Reactor Trip
* PIP O-05-5252, Abnormal Statalarms Following Standby Shutdown Facility (SSF) Diesel Generator (DG) Start
* PIP O-05-0122, Supply Breaker for Unit 3, SSF-Powered Pressurizer Heaters Found Out of Position


The 3LP-104 flow sensor (LPIFS0002)
====b. Findings====
provides the operator with indication that flow has been established in the primary boron dilution flow path. Flow can also be verified by monitoring the valve position indications (ref.OSS-0254.00-00-1028).
=====Introduction:=====
An Unresolved Item (URI) was identified regarding inadequate design control associated with the failure to close the Unit 3, Bank 2, Group C pressurizer heater supply breaker prior to entering Mode 3 following the 3EOC21 refueling outage (RFO). This issue resulted in the SSF auxiliary service water (ASW) system being unable to perform its intended safety function and has been designated as an URI pending a Phase 3 risk analysis.


Therefore, loss of the flow sensor would not inhibit the operators from verifying flow through the primary boron dilution flow path. If flow in the primary flow path cannot :be verified, the alternate boron dilution flow path could be aligned. However, there is no requirement to open the boron dilution flow path following a MSLB or FWLB inside the east penetration room.The CRD Service Structure Monitoring Panel 1 may be affecte Statalarms 3SA-2 D-6 (CRD Even Cooling Fan Fail)or 3SA-2 E-6 (CRD Odd Cooling Fan Fail) may actuate.Operators would be directed to monitor the area temperature The CRD service structure cooling fans do not provide any accident mitigation functio Failure of any or all of the fans following a MSLB or FWLB inside the east penetration room will not result in any additional actions by the operator.The effects on pressurizer heater groups A, D, & K do not add any add tional consequences to the MSLB and FWLB inside the East Penetration Room. Statalarm 3SA-6 E-8 (Pressurizer Heaters Ground Fault) would be actuated due to failures of MCC 3XH, 3XI, 3XJ, and 3XK. These MCCE; are located inside the east penetration room and are expected to be lost clue to environmental conditions resulting from a MSLB or FWL3 inside the east penetration room. Pressurizer heaters wit} power routed through the SSF would remain available.
=====Description:=====
On March 7, 2002, the licensee documented, in PIP O-02-1066, the lack of sufficient SSF-powered pressurizer heaters to maintain single phase, natural circulation RCS flow during an SSF-related event. On May 6, 2002, the licensee documented this issue in Licensee Event Report (LER) 50-269/2002-01, Pressurizer Heat Loss Exceeds Standby Shutdown Facility Powered Heater Capacity, and on December 30, 2003, the licensee received the low to moderate safety significant (White) violation 05000269, 270,287/2003012-01, Failure to Promptly Identify and Correct Insufficient SSF Pressurizer Heater Capacity. One of the corrective actions associated with PIP O-02-1066 was to increase the capacity of SSF-powered pressurizer heaters for each Oconee unit. On Unit 3, these modifications were performed during the 3EOC21 RFO in the Fall of 2004.


The effect of grounds and shorts on the 120 VDC and 120 VAC systems for circuits routed through penetrations with contaminated terminal blocks is expected to be minimal.28 Attachment 1 Duke Energy Response to Unresolved Item 2005004-10 (Failure to Maintain Containment Electrical Penetration Enclosures)
As documented in PIP O-05-0122, on January 4, 2005, with Unit 3 in Mode 1, the licensee discovered that supply breaker PXSF-4A for the Unit 3, Pressurizer Heater Bank 2, Group C was open. The unit was at approximately 20 percent RTP with power escalation in progress following the completion of the 3EOC21 RFO. A licensee investigation concluded that the cause of the breaker being mispositioned was the failure of operations personnel to follow management guidance for the removal and restoration process. A contributing cause to this incident was the lack of procedural guidance to ensure the breaker would be placed in the desired position, in that the startup procedure was not changed to reflect the installation and operation of this new equipment. The breaker had been mispositioned for approximately 234 hours prior to being closed by the licensee on January 4, 2005.
Short circuits (both DC and AC) would be cleared by protective devices. The DC system is normally ungrounded and in the event of DC grounds at the penetration enclosure, the battery chargers would be available to support the DC system voltage. Both the penetration enclosures and the 120 VAC panelboards are grounded through the plant grounding systems. Grounds on the 120 VAC systems at the penetration terminal boards would be cleared by protective devices.Conclusions:
1. There are no EQ requirements that the electrical penetration enclosures in the penetration room be designed, installed or maintained to meet a NEMA 4 classification.


2. The parameters for the environmental qualification of the penetration enclosures in the penetrations rooms following a pipe rupture outside containment are pressure, temperature, and 100% relative humidity.3. The affects of missing enclosure covers has resulted in contamination of terminal boards. Assuming that this contamination could have an adverse affect on plant operation during a HELB, evaluation of various failures at the Component level has concluded that this condition would not prevent safe-shutdown from a HELB evrent.4. While a HELB may affect instrumentation and controls as discussed above, instrumentation and controls necessary for successful event mitigation remain availabl Specifically, operators are trained to use RG 1.97 instrumentation Eor post-accident response.29 Attachment 2 Duke Energy Response to Unresolved Item 2005004-08 (Failure to Meet the Reportability Requirements of 10 CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency)
=====Analysis:=====
URI 05000269, 270, 287/2005004-8 is concerned with reportability of the possible loss of the High Pressure Injection (HPI) Pumps due to Auxiliary Building (AB) flooding following feedwater line breaks (FWLB) or "critical cracks" in the main feedwater piping located inside the East Penetration Room. Duke concluded that flooding of the AB following a FWLB would be precluded by the automatic trip of the reactor and subsequent isolation of the break by the Automatic Feedwater Isolation System (AFIS). Duke has also concluded that operator action would be required to terminate break flow from a postulated "critical crack" in the main feedwater piping. Using very conservative crack flow rates, calculations showed that the operators have at least 10 minutes to take action. The inspectors questioned these conclusions and provided a differing opinion on the event outcome. Secondly, the inspectors disagreed with the flow pathway to the HPI pump rooms. The bases for Duke's cornclusions are provided in the subsequent paragraphs.
The inspectors determined that the licensees failure to maintain design control of PXSF-4A following its installation was a performance deficiency because the licensee failed to update procedural guidance associated with the breakers operation. The failure to maintain adequate design control over the breaker PXSF-4A was considered to be more than minor because it affected the mitigating systems cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding is associated with the configuration control attribute, in that, the operational lineup for the Unit 3, Pressurizer Heater Bank 2, Group C supply breaker was not maintained. A Phase 1 SDP screening was performed, and it was determined that a Phase 2 analysis was required, as the finding represented an actual loss of the safety function of the SSF. This was based on the conclusion that during an SSF-related event, the insufficient SSF-powered pressurizer heaters would result in the inability to control RCS pressure via a pressurizer steam bubble. This would result in the inability to maintain single phase, natural circulation RCS flow without utilizing solid plant operations; thereby, rendering the SSF ASW system inoperable as indicated in the TS bases. The Phase 2 initiator and system dependancy table within the Oconee Risk Informed Notebook references a note to submit any findings associated with the SSF-powered, pressurizer heaters for a Phase 3 risk evaluation by a Regional Senior Reactor Analyst. This finding involved the cross-cutting aspect of human performance.


The inspectors listed their issues with Duke's analysis based on assumptions regarding how the plant would respond to the event.Duke believes that several of these assumptions are incorrect.
=====Enforcement:=====
10 CFR 50, Appendix B, Criterion III, Design Control, requires, in part, that measures be established to assure that design basis for structures, systems, and components covered by Appendix B are correctly translated into specifications, drawings, procedures and instructions. Contrary to the above, the licensee failed to maintain adequate design control of the Unit 3, Bank 2 Group C pressurizer heater breaker, in that, the licensee failed to update the startup procedure with regard to the newly installed breaker. Pending determination of the risk significance, this finding will be identified as URI 05000287/2005004-03, Failure to Maintain Design Control of the SSF Supply Power Breaker for Unit 3, Bank 2, Group C Pressurizer Heaters.
{{a|1R15}}


Each of these assumptions are addressed below: 1. The flooding evaluation was considered to be inaccurate by the inspectors in that the flooding was not limited by the floor drains. Instead, the inspectors identified that a pipe chase in the high pressure injection (HPI) Pump Rooms would allow direct flow into the room closest to the break.Response: The penetration room floor sealing is adequate to prevent gross leakage of water from the east penetration room directly down into the HPI pump rooms via the pipe chase below the east penetration room. These floor seals have been tested to show that they could withstand at least 5 feet of water without failure. This is documented in a memo to file dated 1/1.6/2003, file no. OS-292. Therefore, any water trapped inside the east penetration will not flow directly into the pipe chase below.No appreciable water level is expected to accumulate inside the east penetration room. There is a significant amount of non-reinforced wall area in each unit's east penetration room.Failure of these walls would limit the amount of water that 1 Attachment 2 Duke Energy Response to Unresolved Item 2005004-08 (Failure to Meet the Reportability Requirements of 10 CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency)
==1R15 Operability Evaluations
could accumulate on the floor of the east penetration room. The floor area of the east penetration room was calculated to be 3085 sq.ft. (ref. OSC-8265, "East Penetration Room FloodLing from Feedwater Line Breaks").
Unit 1 has a total length of approximately 79 feet of openings created by failed walls. Unit 2 has a total length of approximately 76 feet of openings created by failed walls. Unit 3 has a total length of approximately 100 feet of openings created by failed walls.These walls are not designed to withstand the resulting pressure from feedwater line breaks or cracks and are expected to fail.Based on an opening of 70 feet, the corresponding water level in the room would be limited to less than 2 inches for the postulated critical crack and less than 4 inches for the!terminal end break in the main feedwater piping. Therefore, the penetration room floor seals provide adequate protection to assure a direct flow path does not exist to the pipe chase below. In addition, no submergence of the electrical penetrations in the east penetration room is expected to occur based on the failures of the non-reinforced walls. The lowest electrical penetrations in the east penetration room are! at least 2 feet above the floor. Therefore, instrumentation served by these electrical penetrations will not be subjected to submergence and will remain available.


Failure of some non-reinforced walls in the east penetration room can provide a direct flow path to the 3 rd floor of the auxiliary buildin The pipe chase can be accessed from the 3 rd floor corridor of the auxiliary buildin However, there are 2-inch high curbs that inhibit the flow of water from the 3 rd floor corridor to the pipe chase rooms. Once the water reaches the 3 rd floor of the auxiliary building, the floodwater may take several routes. These routes include the stairwells, elevator shaft(s), various rooms on the 3 rd floor without curbing, the truck bay, floor drains, and the yard area. The multiple pathways are expected to release water from the 3 rd floor before any appreciable level is established on the 3 rd Floor Elevatio As such, no direct flow path into the pipe chase exists on the 3 rd floor.Water from the 3 rd floor of the auxiliary building can flow to the second floor via leakage under doors to the spiral stairs located at columns R64, R82, and R97. The pipe chase can also be accessed from the 2 nd floor of the auxiliary building.However, there are 2-inch high curbs that inhibit the flow of 2 Attachment 2 Duke Energy Response to Unresolved Item 2005004-08 (Failure to Meet the Reportability Requirements of 10 CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency)
====a. Inspection Scope====
water from the 2 nd floor into the pipe chase rooms. No appreciable water level is expected on the 2 nd Floor. As such, no direct flow path into the pipe chase exists on the 2`3 floor.Failure of some non-reinforced walls in the east penetration room can provide a direct flow path to the Ist floor of the auxiliary buildin In addition, some water from the 3r'l floor will drain to the 1st floor via numerous stairwell Another access point was discovered for water entry into the HPI pump rooms through the pipe chase from the decay heat cooler rooms on each unit. Although there are 2-inch curbs to inhibit water from entering the decay heat cooler rooms from the lst floor corridor of the auxiliary building, water can enter the decay heat cooler room from the trench if it overflow The trench runs below the corridor and spans nearly the entire length of the 1st floor (column 64 to column 97). The trench is approximately 614 feet in length, 2.5 feet in width, and.approximately 2 feet deep. The trench is equipped with 18 drains, 12 directed to Unit 1&2 waste system and 6 directed to Unit 3 waste system. The decay heat cooler rooms also have floor drains, but some water may enter the HPI pump rooms via the pipe chase in the decay heat cooler room. Entry of water into the decay heat cooler rooms requires the lst floor corridor to be completely filled with water. Should this occur, it is expected that each room (Unit 1, 2, and 3) will be affected equally. Therefore, there would be no preferential flow to one unit's HPI pump room. Based on the room configurations, a 2/3 to 1/3 flow split is expected between Unit 1 & 2 HPI pump room and Unit 3 HPI pump room, respectively.
==
The inspectors reviewed selected operability evaluations affecting risk significant systems, to assess, as appropriate:
: (1) the technical adequacy of the evaluations;
: (2) whether continued system operability was warranted;
: (3) whether other existing degraded conditions were considered;
: (4) if compensatory measures were involved, whether the compensatory measures were in place, would work as intended, and were appropriately controlled; and
: (5) where continued operability was considered unjustified, the impact on Technical Specification (TS) limiting condition for operations (LCOs). The inspectors reviewed the following seven operability evaluations:
* PIP O-05-4502, During the Performance of Low Pressure Injection (LPI) Valve Stroke Performance Test (PT), 3LP-7 Stroked Too Quickly
* PIP O-05-4503, SSF Reactor Coolant Makeup Unit Pump Suction Temperature Oscillating
* PIP O-05-4646, Water Discovered Inside of 230kV Switchyard DC Distribution Panelboards SY-DC1, DYA, DYB, DYC and DYD
* PIP O-05-4649, Single Failure Vulnerability of DC Panel with KHU-2 Aligned to Overhead Power Path
* PIP O-05-4720, SSF DG Engine Exhaust Fan Suction Found Partially Blocked
* PIP O-05-5086, Actual Size of Maximum [Reactor Building Emergency Sump]
Screen Opening is Larger Than Stated in the LPI Design Basis Document
* PIP O-05-5118, KHU-2 Emergency Lockout While Attempting to Generate to the Grid


Minor leakage into the HPI pump rooms could be expected from leaking penetration room floor seals down through the pipe chase. However, the holdup time for water in the penetration room is very limited due to the wall failures expected to occur following feedwater line breaks and critical cracks. The leakage consideration does not alter the conclusions reached in Oconee Nuclear Station (ONS) flooding analysis.2. The inspectors have concluded that the licensee is required to postulate the worst case break in accordance with the Giambusso Letter, which the inspectors believe to be larger than the critical crack, but smaller than the terminal end break. Breaks larger than the critical crack but smaller than the terminal end break would invalidate the flooding 3 AttELchment 2 Duke Energy Response to Unresolved Item 2005004-08 (Failure to Meet the Reportability Requirements of 10 CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency)
====b. Findings====
analysis and increase the probability of HPI failure due to flooding.Response: Contrary to the conclusions drawn by the inspectors, break sizes between the critical crack size and the terminal end line break are not required to be postulate The Giambusso letter required the following breaks to be analyzed:* Full Circumferential breaks in piping exceeding L inch (i.e, double ended breaks)* Longitudinal Breaks in piping runs exceeding 4 inches.The break area is equal to the effective cross-sectional flow area upstream of the break location The Schwencer Letter added the requirement to analyze critical cracks. The Schwencer letter defined the critical crack size as a length equal to 1/2 the pipe diameter and a width equal to 1/2 the wall thicknes This forms the licensing basis break size selectio There is no requirement imposed for the postulation of intermediate break sizes for the protection against postulated high energy line breaks outside containment.
No findings of significance were identified. {{a|1R16}}


Feedwater line breaks are postulated at the locations specified in Duke's response to the Giaimbusso letter, contained in MDS Report OS-73.2. The only break location postulated in the report is at the terminal end for each main feedwater line (at the penetration downstream of the isolation check valve).Secondly, "critical cracks" are postulated in accordance with the Schwencer letter. Crack locations were not identified in MDS Report OS-73.2. However, Duke considers crack locations upstream of the feedwater isolation check valves to provide the bounding case for AB floodin The following provides the Duke analysis for the main feedwater break and "critical crack" cases.CASE 1: AB Flooding Evaluation for Postulated Feedwater Line Breaks in the Penetration Room: Two cases were performed for the postulated feedwater line break. Case la was analyzed with the integrated control system (ICS) not providing any automatic actions, which Duke maintains as the bounding case for AB floodin Case lb was analyzed with ICS in automatic and performing all of its design functions.
==1R16 Operator Work-Arounds Risk Significant Operator Work-Arounds


The resultant pressure in the penetration room following the 4 Attachment 2 Duke Energy Response to Unresolved Item 2005004-08 (Failure to Meet the Reportability Requirements of 10 CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency)
====a. Inspection Scope====
postulated main feedwater line break was sufficient to cause the blowout panels used for flooding protection to open to release water to the outside. However, it was also discovered that portions of the east penetration room walls/doors may fail allowing water to be released to other areas of the AB. In both cases, no credit was taken for any release of water through the open blowout panels. In addition, both cases assumed that the reactor was operating at full power.Case la Results: The analysis (OSC-7726)
==
showed that the reactor tripped on high reactor coolant system (RCS) pressure at approximately 15 seconds after the feedwater line break. Subsequent to the reactor trip, the (automatic feedwater isolation system) AFIS low steam generator (SG) pressure setpoint was reached at approximately 64 seconds with the feedwater control valves fully closed at approximately 89 seconds after the feedwater line break. The flooding analysis assumed that the main feedwater control valves remained open until closed by AFIS. The total integrated mass of liquid released to the AB was calculated to be approximately 200,800 lbm or the equivalent volume of 25,091 gallons (based on 212 0 F). The critical volumes for HPI pump flooding is 41,058 gallons (for Unit 1 & 2) and 25,624 gallons (for Unit 3). Therefore, it was concluded that insufficient water would be released to the AB to create a flooding concern for the HPI pumps, regardless of the flow split assumed in the AB floor drain system. Therefore, the HPI system would not be lost following the licensing basis main feedwater line break.Case lb Results: The analysis (OSC-8884)
The inspectors reviewed the significant operator work-around listed below to determine if the functional capability of the respective system or the human reliability in responding to an initiating event were affected. The inspectors specifically evaluated the effect of the operator work-arounds on the ability to implement abnormal or emergency operating procedures. The inspectors also assessed what impact it would have on the unit if the work-around could not be properly performed.
showed that the reactor tripped on high RCS pressure at approximately
* PIP O-05-5935, 1CS-5 Failed to Close After Pumping the Quench Tank to 1A Bleed Hold Up Tank. 1CS-5 was declared inoperable, requiring 1CS-6 to be deactivated to isolate the containment penetration. In order to decrease the frequency at which the quench tank is pumped, the maximum operating level of the quench tank was increased. Additionally, OPS personnel must clear tags on 1CS-6 to unisolate the containment penetration in order to pump the quench tank.
:21 seconds after the feedwater line break. The AFIS low SG pressure trip setpoint was reached at approximately 45 seconds with the feedwater control valves fully closed at approximately 82 seconds following the line break. Safety Analysis added another 10 seconds to the valve closure for conservatis Although the trip was delayed by about 6 seconds, the feedwater control valves were closed earlier (even with the additional 10 second conservatism).


The total integrated mass of liquid released to the AB was calculated to be approximately 191,300 lbm or the equivalent volume of 23,903 gallons (based on 212 0 F). Comparison of the integrated liquid mass released from the two cases show that the liquid release was bounded by the ICS in Manual cas Attachment 2 Duke Energy Response to Unresolved Item 2005004-08 (Failure to Meet the Reportability Require:nents of 10.CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency)
====b. Findings====
Therefore, the conclusions contained in the operability evaluation remain valid.CASE 2: AB Flooding Evaluation for Postulated Critical Cracks in the Main Feedwater Line inside the Penetration Room: A "Critical crack" in the main feedwater piping will result in much lower peak pressures inside the East Penetration Room. The lower blowout panels provided for flood protection may not open due to the lower calculated peak pressure for "critical cracks".However, the upper panels will open to relieve the steam released from the "critical crack". Therefore, it was assumed that the water released from the critical crack would flow to other areas of the AB and no water would be directed to outside.The plant response following the postulated "critical crack" is different from the feedwater line break in that Operator action is required to trip the reactor and isolate feedwater to the faulted main feedwater line.Duke stated that at least 10 minutes were available for operator action. This time was based on very conservative crack flow estimates and an assumed flow split between the units waste systems based on the number of floor drains. To more accurately model crack flow, a contraction coefficient was applied to the critical crack flow to reflect the characteristics of flow through an orifice. The contraction coefficient was determined to be 0.6, based on the square root of the ratio in flow areas in the crack and the main feedwater piping and the expected velocity through the main feedwater piping. The contraction coefficient was applied to the critical flow calculation contained in OSC-8036, "Flow from feedwater (FDW) Line Crack into the Penetration Room". TVle flowrate through the critical crack was calculated to be 528.06 lbm/sec at an enthalpy of 426.1 btu/lbm. Not all of the mass released from the crack will remain in liquid form. In fact, approximately 25% of the liquid will flash to steam. The remaining 75% will remain in the liquid state and be released through the failed walls. The volumetric liquid release rate was calculated to be approximately 3000 gpm.Based on engineering judgement that approximately 69% of the water released from a crack would flow to Unit 1&2 waste system, 6 Attachment 2 Duke Energy Response to Unresolved Item 2005004-08 (Failure to Meet the Reportability Requirements of 10 CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency)
No findings of significance were identified. {{a|1R19}}
while 31% would flow to Unit 3, regardless of the unit with the crack. No detailed analysis is available to support this judgment; however, since no direct pathways exist that would allow water to flow preferentially to one unit's HPI pump rooms via the pipe chase, the judgment is considered to be reasonable.
 
==1R19 Post-Maintenance Testing (PMT)
 
====a. Inspection Scope====
==
The inspectors reviewed PMT procedures and/or test activities, as appropriate, for selected risk significant systems to assess whether:
: (1) the effect of testing on the plant had been adequately addressed by control room and/or engineering personnel;
: (2) testing was adequate for the maintenance performed;
: (3) acceptance criteria were clear and adequately demonstrated operational readiness consistent with design and licensing basis documents;
: (4) test instrumentation had current calibrations, range, and accuracy consistent with the application;
: (5) tests were performed as written with applicable prerequisites satisfied;
: (6) jumpers installed or leads lifted were properly controlled;
: (7) test equipment was removed following testing; and
: (8) equipment was returned to the status required to perform its safety function. The inspectors observed testing and/or reviewed the results of the following six tests:
* PT/2/A/0204/007, 2B Reactor Building Spray (RBS) Pump Test, following testing and inspection of the pumps motor
* PT/1/A/0251/001, Unit 1and 2 A Low Pressure Service Water Pump Test, following pump lubrication
* PT/2/A/0600/13A, 2A Motor Driven Emergency Feedwater (MDEFW) Pump Test, following pump lubrication
* PT/0/A/0400/005, SSF ASW Pump Test, following the replacement of the outboard stuffing box packing
* PT/0/A/0620/016, Keowee Hydro Emergency Start Test, following repairs associated with the second emergency lockout on KHU-2
* OP/0/A/1600/010, Operation of the SSF DG, following routine preventive maintenance
 
====b. Findings====
No findings of significance were identified. {{a|1R22}}
 
==1R22 Surveillance Testing
 
==
===.1 Routine Surveillance===
====a. Inspection Scope====
The inspectors witnessed surveillance tests and/or reviewed test data of the five risk-significant SSCs listed below, to assess, as appropriate, whether the SSCs met TS, Updated Final Safety Analysis Report (UFSAR), and licensee procedure requirements.
 
In addition, the inspectors determined if the testing effectively demonstrated that the SSCs were ready and capable of performing their intended safety functions.
 
*
*PT/3/A/0600/013, 3B MDEFW Pump Test
*
*PT/2/A/0202/011, 2C High Pressure Injection (HPI) Pump Test
* HP/0/B/1000/060 D, Procedure for Vent, Air Ejector and Reactor Building Sampling and Analysis
* AM/0/A/1300/059, Pump - Submersible - Emergency SSF Water Supply -
Installation and Removal
*
*PT/3/A/0600/012, Unit 3 Turbine Driven Emergency Feedwater Pump Test Note: (*) Indicates in-service test (IST).
 
====b. Findings====
No findings of significance were identified.
 
===.2 Inadequate Inspection of Containment Electrical Penetrations===
====a. Inspection Scope====
As part of the surveillance inspection procedure, the inspectors reviewed the activities associated with inspection and cleaning of the containment electrical penetrations following identification by the inspectors that a significant number of electrical penetration covers had been removed during previous maintenance activities.
 
====b. Findings====
=====Introduction:=====
The inspectors identified a Green non-cited violation (NCV) of 10 CFR 50 Appendix B, Criterion X, Inspection, for failure to develop and implement an inspection program for inspection and cleaning of the containment electrical penetrations located in the East and West Penetration Rooms. Discussions with the licensee disclosed that no procedures were in place to perform inspections or cleaning.
 
=====Description:=====
Information Notice (IN) 82-03, Environmental Tests of Electrical Terminal Blocks, indicated that cleanliness of terminations and terminal blocks in circuits important to safety is of concern. It stated, in part, that the cleanliness aspects are addressed in Appendix B of 10 CFR 50 and that these regulations require the licensee to establish appropriate procedures to assure that equipment is maintained in an acceptable state. It also indicated that licensees are reminded that their plant preventive maintenance program should assure that periodic inspection of those terminations and terminal blocks for cleanliness and installation integrity is performed following any maintenance activity affecting them.
 
Based on discussions with NRR, it was concluded that IN 82-03 and 10 CFR 50 Appendix B, Criterion X, required the licensee to develop and implement a program for inspection of the containment electrical penetrations. Discussions during August 2005 disclosed that the licensee did not have a program for routine inspection and cleaning of the containment electrical penetrations. The inspectors noted that many of the protective covers had been removed and some of the terminal blocks had indications of dirt and rust accumulation. Therefore, the failure to develop an inspection program for the containment electrical penetrations was considered to be a violation.
 
=====Analysis:=====
The finding was considered to be a performance deficiency in that the licensee had failed to develop an inspection program for their containment electrical penetrations to ensure cleanliness of the electrical connections. The inspectors concluded that if left uncorrected (no inspection), debris and rust accumulation could lead to failure of the electrical circuits during a high energy line break as a result of grounds and shorts.
 
Therefore, failure to perform cleanliness inspections was considered to be more than minor because it could impact the Reactor Safety Mitigating Systems Cornerstone objective for reliability of a mitigating system/train (i.e., circuits needed to mitigate a high energy line break (HELB)). The finding was screened as very low safety significance (Green) in the Phase 1 review under the Mitigating Systems Cornerstone, in that failure to perform an electrical penetration inspection was not considered to be a design deficiency, was not considered to represent a loss of safety system function, was not considered to represent an actual loss of safety function of a single train, and did not involve seismic, flooding or severe weather. This finding involved the cross-cutting aspect of Problem Identification and Resolution.
 
=====Enforcement:=====
10 CFR 50 Appendix B, Criterion X, Inspection, requires that a program for inspection of activities affecting quality shall be established and executed to verify conformance with the instructions and procedures. Contrary to the above, the licensee failed to establish an inspection program for inspection of the containment electrical penetrations to ensure proper cleanliness of the penetrations. Because this issue was of very low safety significance and has been entered into the licensees corrective action program (PIP O-05-4491), this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000269,270,287/2005004-04:
Failure to Develop and Implement a Cleanliness Inspection Program for the Containment Electrical Penetrations.
 
===.3 Inadequate Inspection of Main Steam Lines===
====a. Inspection Scope====
As part of the surveillance inspection procedure, the inspectors reviewed the inspection activities associated with licensee commitments to the 1972 Giambusso Letter (HELB).
 
====b. Findings====
=====Introduction:=====
The inspectors identified a Green NCV of 10 CFR 50 Appendix B, Criterion X, Inspection, for failure to develop and implement an inspection program for monitoring the main steam line in the East Penetration Rooms. Discussions with the licensee disclosed that the main steam line postulated break areas were not being inspected.
 
=====Description:=====
The Oconee licensing basis for high energy line breaks is contained in the December 15, 1972, letter from A. Giambusso to Duke Power Company (Giambusso letter) and the licensees response to the letter which is documented in Oconee MDS Report No. OS-73.2, Analysis of Effects Resulting from Postulated Piping Breaks Outside Containment. In response to Question 7 of the Giambusso letter, which is related to a main steam line break in the East Penetration Room, OS-73.2 Supplement 1, dated June 22, 1973, stated that Duke will increase the inservice inspection to include the metal to surface inspection of the postulated break area every 5 years to detect any surface defects. The licensee also provided drawings (OS-73.2 Supplement 1, Figure 2.1-1.b) showing the postulated break area in the East Penetration Room.
 
In August 2005 the inspectors asked for the latest inspection results for the main steam lines. The inspectors were informed that the main steam line terminal end break area was inaccessible and could not be inspected. The licensee had not informed the NRC that the terminal end break area provided on Figure 2.1-1.b was in error and that inspection of the main steam line piping in the East Penetration Rooms was not being performed. This issue was captured in PIP O-05-06354, which reflected the licensees intention to ask NRR for an exemption from the inspection requirements.
 
=====Analysis:=====
The finding was considered to be a performance deficiency in that the licensee had committed to perform inspections of the steam lines to support the acceptability of Dukes design and analysis for the main steam lines, but the inspections were not being performed. The finding was considered to be more than minor because it impacted the Reactor Safety Initiating Events Cornerstone in that failure to perform the inspections could lead to failure to identify degrading main steam line conditions, which would cause an increase in the likelihood of an initiating event. The finding was screened as being of very low safety significance (Green) under the Initiating Events Cornerstone, in that the finding did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available. This finding involved the cross-cutting aspect of Problem Identification and Resolution (PI&R).
 
=====Enforcement:=====
10 CFR 50 Appendix B, Criterion X, Inspection, requires that a program for inspection of activities affecting quality shall be established and executed to verify conformance with the instructions and procedures. Contrary to the above, the licensee failed to establish and execute the inspection program for inspection of the main steam lines committed to as part of their response to the 1972 Giambusso letter. Because the failure to perform the inspections was considered to be of very low safety significance and has been entered into the licensees corrective action program (PIP O-05-06354),this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000269,270,287/2005004-05: Failure to Implement an Inspection Program for the Main Steam Lines.
{{a|1R23}}
 
==1R23 Temporary Modifications
 
====a. Inspection Scope====
==
While performing plant status inspection activities, the inspectors reviewed the activities associated with the improper enclosure of the Unit 3 Train B low pressure injection (LPI)/reactor building spray (RBS) pump room (Room 81), described in the licensees corrective action program as PIP O-05-5564.
 
====b. Findings====
=====Introduction:=====
An URI was identified regarding the improper blocking of the ventilation paths into and out of Unit 3 Auxiliary Building Room 81 (Train B LPI/RBS pump room).
 
The natural circulation ventilation pathways (circular stairs) are required for heat removal from the room during the recirculation phase following a loss of coolant accident (LOCA)to ensure the LPI and RBS pump and motor bearings do not exceed maximum operating temperatures. The issue will be documented as an Unresolved Item pending completion of a Phase 3 analysis.
 
=====Description:=====
On August 30, 2005, the licensee generated PIP O-05-5564, which documents that a tent enclosure had been inappropriately installed in the Unit 3 portion of the Auxiliary Building and was blocking airflow from the stairway access into LPI/RBS pump room 81. The enclosure had been installed on about August 9, 2005, to allow for lead removal work in the room. The airflow pathway is credited in Oconee design calculation OSC-6667 for air movement and heat removal during design basis accidents (LOCA recirculation phase). OSC-6667 provides the various maximum room temperatures following an accident. Previous testing by the licensee found that relatively small increases in room temperature (<20 degrees F) above those calculated in OSC-6667, could render the LPI and RBS pumps inoperable. Consequently, since the air flow pathway credited in calculation OSC-6667 did not exist with the tent enclosure installed, the Unit 3 B train LPI and RBS pumps could not be considered operable during this period.
 
=====Analysis:=====
The finding was considered to be a performance deficiency because the licensee failed to maintain the plant design in accordance with their design calculation OSC-6667 for design basis accidents, in that the assumed airflow pathway for heat removal was closed off. Since the LPI and RBS pumps cannot be considered operable in this condition, this finding was considered to be more than minor because it would impact the Reactor Safety Mitigating System Cornerstone for ensuring the availability, reliability and capability of a system that responds to initiating events to prevent undesirable consequences. A Phase 1 evaluation concluded that under the Mitigating Systems Cornerstone, the finding represented an actual loss of safety function of a single train for greater than its TS allowed time; therefore, a Phase 2 evaluation was required. The Phase 2 evaluation (dominated by small break loss of coolant accident)indicated that the issue was greater than Green and that a Phase 3 evaluation would be necessary. This finding involved the cross-cutting aspect of human performance.
 
=====Enforcement:=====
10 CFR 50, Appendix B, Criterion III, Design Control, requires in part that design changes, including field changes, are approved by the organization that performed the original design. Contrary to the above, a design change was made to the airflow pathway credited in design calculation OSC-6667 prior to obtaining approval from the licensees design organization. This issue was placed in the licensees corrective action program as PIP O-05-5564. Pending determination of the risk significance, this issue will be identified as URI 05000287/2005004-06, Inadequate Design Control of Unit 3 LPI/RBS Room Ventilation Pathways.
 
===Cornerstone: Emergency Preparedness===
1E6 Drill Evaluation
 
====a. Inspection Scope====
The inspectors observed and evaluated a simulator based emergency preparedness drill held on September 22, 2005. The drill scenario involved a security related event with postulated planted explosives. The scenario progressed to a general emergency after simulated damage to plant systems from various explosions. During the scenario, the operators were required to identify entry into an unusual event, alert and general emergency. The inspectors verified that the operators properly classified the event and made the appropriate notifications to the counties, state and NRC. The inspectors also verified that the protective action recommendations were issued in accordance with the licensees emergency procedures. The inspectors reviewed the post drill critique to verify that the licensee captured any drill deficiencies or weaknesses.
 
====b. Findings====
No findings of significance were identified.
 
==OTHER ACTIVITIES==
{{a|4OA2}}
 
==4OA2 Identification and Resolution of Problems==
===.1 Daily Screening of Corrective Action Reports===
As required by Inspection Procedure (IP) 71152, "Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed daily screening of items entered into the licensees corrective action program. This review was accomplished by reviewing copies of PIPs, attending daily screening meetings, and accessing the licensees computerized database.
 
===.2 Semi-Annual Trend Review===
====a. Inspection Scope====
As required by IP 71152, "Identification and Resolution of Problems," the inspectors performed a review of the licensees Corrective Action Program (CAP) and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues; but, also considered the results of daily inspectors CAP item screenings discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six month period of March 2005 through September 2005, although some examples expanded beyond those dates when the scope of the trend warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, plant health team vulnerability lists, focus area reports, system health reports, self-assessment reports, maintenance rule reports, and Safety Review Group monthly reports. The inspectors compared and contrasted their results with the results contained in the licensees latest quarterly trend reports. Corrective actions associated with a sample of the issues identified in the licensees trend report were reviewed for adequacy.
 
b.
 
Assessment and Observations No findings of significance were identified. In general, the licensee has identified trends and has appropriately addressed the trends in the CAP. Inspection Report 05000269,270,287/2005003 documented a trend with regard to the generation of 23 PIPs for dropped flags on relays associated with various plant equipment during the previous six months. Following further inspection, this trend has been closed, as the increased documentation associated with this trend was part of the licensees effort to investigate the cause of the dropped relay flags in conjunction with the relay manufacturer. Additionally, none of the specified relays have picked up, nor has there been any negative impact on plant equipment. The licensee and relay manufacturer continue to investigate this observation.
 
===.3 Focused Review===
====a. Inspection Scope====
The inspectors performed an in-depth review of an issue entered into the licensees corrective action program. The sample was within the mitigating systems cornerstone and involved risk significant systems. The inspectors reviewed the actions taken to determine if the licensee had adequately addressed the following attributes:
*
* Evaluation and disposition of operability and reportability issues
* Consideration of previous failures, extent of condition, generic or common cause implications
* Prioritization and resolution of the issue commensurate with safety significance
* Identification of the root cause and contributing causes of the problem
* Identification and implementation of corrective actions commensurate with the safety significance of the issue.
 
The following issue and corrective actions was reviewed:
* PIP O-05-4892, Unit 3, East to West Pen. Room Security/Fire Door Stuck shut
 
====b. Findings====
No findings of significance were identified.
 
===.4 East Penetration Room Blowout Panel/HELB Issue===
====a. Inspection Scope====
The inspectors performed a Problem Identification and Resolution (IP 71152) inspection for the implementation of the East Penetration Room blowout panel corrective actions related to NCV 05000269,270,287/2002004-02, Unauthorized Design Changes to the East Penetration Room Blowout Panels.
 
====b. Findings====
=====Introduction:=====
The inspectors identified an URI for untimely corrective actions in resolving the East Penetration Room blowout panel issue. The blowout panels had been improperly modified, causing the plant to be outside the Oconee licensing basis for pressure relieving capacity for the panels and for flood mitigation panels not being assured of proper operation. This issue was previously documented as URI 05000269, 270,287/2000008-04 and NCV 05000269,270,287/2002004-02. As of September 30, 2005, the blowout panels had not been repaired to ensure flood mitigation, nor had a license amendment been requested to correct the design pressure blowout capacity.
 
This lack of corrective action was considered to be unresolved, pending completion of a Phase 3 analysis.
 
=====Description:=====
In the fall of 1999, the inspectors noted that the blowout panels listed in the HELB licensing basis document OSC -73.2 (response to Giambusso Letter) had been epoxied and bolted in place. These panels were originally designed to limit the East Penetration Room pressurization following a main feed water or main steam line break or crack. In addition, the lower blowout panels were originally designed to allow water from the break or crack to leave the room and prevent flooding of safety-related equipment. As noted above, an URI was initiated in 2000 and an NCV was issued in 2002.
 
Subsequent to the NCV documented in 2002, the licensee determined that the blowout panels would not perform their design function to prevent flooding in the East Penetration Room. This condition is outside the licensing basis as specified in design document OSC-73.2. The licensee stated that modifications are necessary to prevent flooding of the auxiliary building because the East Penetration Room doors and block walls would likely fail during a HELB and the blowout panels are not assured of opening.
 
The proposed modifications include installation of a knee wall to prevent flooding and installation of new blowout panels.
 
As of September 30, 2005, the licensee has not developed a modification or a schedule for bringing the three units back into compliance with the licensing basis. The guidance in GL 91-18, Attachment 1, Section 4.3, Current Licensing Basis and 10 CFR 50, Appendix B, states that, If the licensee does not resolve the degraded or nonconforming condition at the first available opportunity or does not appropriately justify a longer completion schedule, the staff would conclude that corrective action has not been timely and would consider taking enforcement action. This non-conforming condition was identified in 1999, but to date the licensee has not taken adequate and timely corrective action.
 
=====Analysis:=====
The finding was considered to be a performance deficiency in that the licensee failed to implement timely corrective actions to repair the previously unauthorized modification of the East Penetration Room blowout panels. Since postulated flooding following a feedwater HELB would impact the HPI and emergency feedwater (EFW)functions, this finding was considered to be more than minor because it would impact the Reactor Safety Mitigating System Cornerstone for ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The Phase 1 evaluation was performed and it was concluded that under the Mitigating Systems Cornerstone that the finding represented an actual loss of a safety function of the HPI system, which required a Phase 2 evaluation. The Phase 2 evaluation (dominated by main steam line break) indicated that the issue was greater than Green and that a Phase 3 evaluation would be required. The previous Phase 3 analysis performed for NCV 05000269,270,287/ 2002004-02 found that the risk significance was Green. However, since that analysis, new information has been identified that may impact the significance of the issue. Therefore, a new Phase 3 analysis is necessary. This finding involved the cross-cutting aspect of Problem Identification and Resolution (PI&R).
 
=====Enforcement:=====
10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, requires in part that measures be established to assure that conditions adverse to quality, such as deficiencies, deviations, and non-conformances are promptly identified and corrected.
 
Contrary to the above, Units 1, 2, and 3 have continued to be operated outside their licensing basis for meeting HELB criteria because the East Penetration Room blowout panels are not assured of opening to prevent auxiliary building flooding. In addition, the panels do not meet the design criteria for blowout capacity and corrective actions have not been taken in a timely manner to resolve the deficiency. Pending determination of the risk significance, this issue is being identified as URI 05000269,270,287/2005004-07, Untimely Corrective Actions in Correcting the East Penetration Room Blowout Panel Deficiency.
 
===.5 Failure to Report the East Penetration Room Blow Out Panel Deficiency per===
10 CFR 50.73
 
====a. Inspection Scope====
The inspectors reviewed the licensees operability evaluation and reportability evaluation related to improper modifications of the East Penetration Room blowout panels.
 
====b. Findings====
=====Introduction:=====
An URI was identified regarding the failure to report a condition that could have prevented fulfillment of a safety function of a system as required by 10 CFR 50.73.
 
The reportable condition was the improper modification of the East Penetration Room blow out panels which in their present condition would prevent the release of water following a feedwater HELB. Since the panels would not release the water outside the auxiliary building, leakage out of the room would eventually lead to flooding of the HPI pumps and this would prevent fulfillment of a safety function of a system (HPI) needed to place the plant in a cold shutdown condition. This issue is considered to be unresolved, pending determination of safety significance.
 
=====Description:=====
In the late 1980's / early 1990's, the East Penetration Room blowout panels were coated with a metal shield elastomeric flasing compound followed by a polyester reinforcing fabric and then another coating of the metal shield elastomeric flasing compound. There is no information available on the physical strength or adhesion of the compounds. In addition, bolts and screws were installed on the outside of the panels to secure the panels in place. These undocumented modifications were implemented in order for the licensee to meet penetration room ventilation requirements for being able to draw a vacuum in the room. These modifications increased the panel blowout strength to values in excess of 144 pounds per square foot, although the licensing basis strength is limited to less than 63 pounds per square foot. Based on subsequent calculations, the licensee determined that the floor level blow out panels, that were designed to limit flooding in the auxiliary building, would not blow out under all conditions and flooding of the auxiliary building would occur.
 
In June 2004, the licensee made a presentation to Region II management. The presentation noted that the panels could not be assured of blowing out and plant modifications were needed to ensure flooding of the auxiliary building would not take place. This condition appeared to be reportable, so the licensee was asked to review the condition for reportability.
 
The licensee concluded that although there may be from 44,000 to 64,000 gallons of water available to flood the auxiliary building equipment, the floor drains would equalize the inventory between the Unit 1 and 2 HPI pump room and the Unit 3 HPI pump room, and none of the HPI pumps would be affected. In addition, the licensee assumed that the SSF makeup pump would be unaffected and would be able to stabilize the plant in hot standby. Based on these conditions, the licensee concluded that there would be no loss of safety function.
 
However, the inspectors found problems with the licensees analysis.
* Following a HELB, the plants licensing basis requires the licensee to go to cold shutdown. The SSF makeup pump cannot perform this function and is also not in the licensing basis to mitigate a HELB. Therefore, the HPI pumps are the only pumps that can be credited to provide the safety function to mitigate this accident and they must remain functional.
* The licensee inappropriately assumed that the HELB flood inventory would equalize between the Unit 1, 2, and Unit 3 HPI pump rooms. However, the inspectors noted that flooding of the HPI pump rooms is not limited by the floor drains as assumed in the licensees operability evaluation. The inspectors identified that each HPI pump room has a pipe chase that will direct flow into the room closest to the break. Therefore, the inspectors concluded that the available postulated flood inventory would cause flooding of the unit specific HPI pumps and render them inoperable.
* The licensee concluded that inventory from a postulated HELB crack would be 50,000 gallons and less than 20,000 gallons from a full break. This was based on operator action for the crack at 10 minutes and automatic feedwater isolation system (AFIS) actuation for a full break (<2 minutes). The inspectors noted that the licensee did not assume breaks sized between a crack and a full break, which would also not be isolated by an AFIS signal. The inspectors noted in the licensing basis (Giambusso letter) that the licensee is required to mitigate the effects from the worst case break, which in this case would be a break greater than a crack (5,000 gpm for 10 minutes), but less than a full break (13,000 gpm assumed to be isolated by AFIS in about 2 minutes). Based on this finding, the inspectors noted that the flood inventory would be much greater than analyzed by the licensee and would increase the probability of flooding in the HPI pump rooms
* The licensee assumed that AFIS would isolate a full break in less than 2 minutes. Because main steam headers are tied together, the inspectors noted that AFIS could not actuate on low steam pressure to isolate feedwater until there was a turbine trip. A turbine trip would require a reactor trip. Oconee does not have a SG low level trip. Therefore, discussions with the licensee indicated that the reactor trip needs to be initiated from a loss of feed water pumps. The only applicable feed water pump trip would be initiated on loss of suction pressure for >90 seconds. The inspectors noted that on a feedwater line break, feedwater flow would increase; thereby creating low feed pump suction pressures. The integrated control system would attempt to recover the proper feedwater flow by reducing the feedwater regulating valve position at a rate of 20 percent per minute or 30 percent over the first 90 seconds. The inspectors noted that with the feed water regulating valves at a position equivalent to 70 percent flow, feed water pump suction pressure would likely increase enough such that the low suction pressure trips would not occur. At lower volume breaks, feedwater pump trips are even less likely. Based on this discussion, the inspectors concluded that an AFIS isolation of the break is questionable and operator action at the licensing basis time of 10 minutes should be used for any flooding analysis.
 
Based on the above, the inspectors concluded that the licensees operability evaluation was inadequate and that a single active failure (as postulated in the licensees reportability analysis) was not required to cause a loss of the HPI pumps due to flooding. Therefore, the adverse condition of the blow out panels creating a situation where the HPI pumps (which are needed to mitigate a HELB) would be lost, was considered to be reportable per 10 CFR 50.73. The issue was discussed with the licensee. However, the licensee concluded that their evaluation was satisfactory.
 
=====Analysis:=====
The issue was considered to be a performance deficiency in that the licensee failed to report a condition that could have prevented fulfillment of a safety function as required by 10 CFR 50.73. The failure to report has the potential to impact the NRCs ability to perform its regulatory function. Therefore, this issue will be processed using traditional enforcement as specified in the Enforcement Policy IV.A.3. Determination of the safety significance by the Region II Senior Reactor Analyst will be necessary to determine the severity level of the violation.
 
=====Enforcement:=====
10 CFR 50.73, Part (v), requires the reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to (A) shutdown the reactor and maintain it in a safe shutdown condition (licensing basis is cold shutdown) and (D) mitigate the consequences of an accident Contrary to the above, the licensee failed to report that improper modifications to the East Penetration Room blowout panels would prevent the fulfillment of the safety function of the HPI system to mitigate the consequences of a HELB accident (i.e., to shutdown the reactor and maintain it in a cold shutdown condition). Pending determination of the risk significance, this issue is being identified as URI 05000269,270,287/2005004-08, Failure to Meet the Reportability Requirements of 10 CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency.
 
===.6 Untimely Corrective Actions for Unit 2 East Penetration Room Floor Seal Deficiency===
====a. Inspection Scope====
:
While performing routine plant tours to identify any adverse plant conditions, the inspectors followed up on a previously noted damaged floor seal in the Unit 2 East Penetration Room.
 
====b. Findings====
=====Introduction:=====
The inspectors identified a Green NCV of 10 CFR 50 Appendix B, Section XVI, Corrective Action for inadequate corrective actions related to the lack of timeliness of repairs to a Unit 2 East Penetration Room floor seal. The inspectors concluded that the damaged floor seal, if left uncorrected could lead to flooding of safety-related equipment following a high energy line break in the Unit 2 East Penetration Room.
 
=====Description:=====
On July 14, 2004, the licensee wrote a deficiency tag and work request on a partially extruded floor seal in the Unit 2 East Penetration Room. The affected floor seal fills a gap approximately 4 inches by six feet between two sections of reinforced concrete flooring in the room. The deficiency tag on the damaged seal was over a year old yet repairs had not been initiated. Further review found that the degraded condition had not been placed into the PIP process.
 
=====Analysis:=====
The failure to promptly repair the damaged floor seal was considered to be a performance deficiency. The finding was considered to be more than minor because if left uncorrected, additional seal area could fail and it would affect the Mitigating System Cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events, in that the HPI pumps could be flooded following a HELB in the East Penetration Room. However, in the seals current level of degradation, the inspectors concluded that the deficiency would not by itself result in the loss of function of the HPI pumps, because flooding would be limited by the size of the degraded/failed seal. Consequently, the finding was determined to be of very low safety significance (Green), as it was screened out under the Mitigating Systems Cornerstone in the SDP Phase 1 Screening Worksheet with the determination that there was no loss of safety function. This finding involved the cross-cutting aspect of Problem Identification and Resolution.
 
=====Enforcement:=====
10 CFR 50 Appendix B, Section XVI, Corrective Action, requires Contrary to the above, the licensee failed to correct a partially extruded Unit 2 East Penetration Room floor seal that if left uncorrected, could degrade to the point that safety related equipment could be affected following a HELB. Because this issue was of very low safety significance and has been entered into the licensees Corrective Action Program as PIP O-05-6097, this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000270/
2005004-09, Untimely Corrective Actions for Repairs to a Unit 2 East Penetration Room Floor Seal.
 
===.7 Failure to Maintain Containment Electrical Penetration Enclosures===
====a. Inspection Scope====
While performing routine plant tours to identify adverse plant conditions, the inspectors followed up on the observation that the containment electrical penetrations were degraded, in that cover plates were either missing or attached improperly.
 
====b. Findings====
=====Introduction:=====
The inspectors identified an URI for failure to identify a condition adverse to quality in that East and West Penetration Room containment electrical penetrations enclosures had not been maintained as spray proof enclosures. Because these electrical enclosures have not been maintained, grounding and shorting of these circuits located in the East and West Penetration Rooms could lead to significant losses of safety-related electrical systems, controls and indications following a HELB. The issue will be documented as an URI pending further inspection.
 
=====Description:=====
In June 2005, the inspectors identified that covers for a significant number of electrical penetrations were missing or improperly attached. These included specific penetrations which contained electrical circuits needed to mitigate the consequences of a high energy line break in the East Penetration Room and place the plant in a cold shutdown condition. Discussions with NRR concluded that the Oconee licensing basis requires the plant to be able to reach cold shutdown following a HELB while assuming one active failure. During discussions with the licensee, the licensee stated that the covers were not necessary to maintain the environmental qualification of the unprotected electrical circuits, and therefore, the as found degraded penetrations were acceptable to meet their safety function without the covers. Discussions with NRR concluded that the electrical penetrations would not meet their as tested environmental qualification if they could be impacted by direct or indirect spray and/or became dirty or rusted.
 
The inspectors noted that roughly 70 penetrations in the East Penetration Rooms had some sort of closure problem, and likely an equal number of problems in the West Penetration Rooms. The licensee initiated PIP O-05-4491 on July 9, 2005. The licensee also initiated repairs to the open penetration enclosures, which had still not been completed by the end of the inspection period.
 
The licensee performed an operability assessment and concluded that The cables entering the electrical penetration assembly junction boxes do not require environmental sealing, and all the electrical penetrations are outside the zone of influence for the two HELB scenarios under consideration in the penetration rooms. The inspectors questioned why piping cracks would be outside the zone of influence and the engineers stated that the licensing basis for breaks or cracks did not include spray impingement, and therefore, did not have to be considered. Discussions with NRR concluded that the licensing basis for Oconee required not only spray, but direct jet impingement from postulated breaks. The breaks to be considered were cracks along the entire length of feedwater and steam line piping. The inspectors concluded that a postulated 13,000 gpm leak from a feedwater line break or 6,600 gpm leak from a feedwater line crack would affect the open penetrations and that the penetrations were required to be protected from the effects (i.e., direct or indirect spray) from a crack or break.
 
The inspectors observed debris and dust on the electrical terminal blocks inside the electrical penetration panels, rust on the terminal blocks and inside other components in the electrical penetration panels, and debris on top of the electrical penetration panels that would likely be washed into the panel during a postulated HELB. The inspectors also noted that with the covers missing/improperly installed, the terminal blocks could be sprayed down during a HELB. Based on an e-mail from NRR, Electrical Engineering Section, dated July 27, 2005, NRR concluded that terminal blocks are qualified for a harsh environment when not subjected to direct spray; where direct spray is anticipated, the terminal blocks are installed in enclosures. Oconees commercial dedication for the safety-related terminal blocks required the terminal blocks to be installed in NEMA 4 enclosures (i.e., spray protected). NRR went on to state that cleanliness of the terminal blocks is required because accumulation of dirt and rust introduces a conductive path for current that could distort the signals from instrumentation circuits. Since the electrical penetration panels were not maintained, it was concluded by the inspectors that the original environmental qualification no longer encompassed the as found condition.
 
The inspectors concluded that multiple grounds and shorts would cause erratic actuation of alarm circuits and potentially cause unwarranted actuation/operation of emergency core cooling system and other plant equipment. These conditions would further hinder the ability of the operations staff to mitigate the HELB. The inspectors also concluded that the low voltage electrical systems were not designed to operate with multiple grounds and shorts and the likely affect would be to cause distortion of the instrumentation signals even on circuits that were not directly impacted by the HELB.
 
The inspectors noted that in the original licensing basis requirements, contained in the 1972 Giambusso letter, the licensee was required to verify that the rupture of a pipe carrying high energy fluid will not directly or indirectly result in loss of redundancy in any portion of the protection system, class 1E electrical system, engineered safety feature equipment, cable penetrations, or their interconnecting cables required to mitigate the consequences of the break and place the plant in cold shutdown. The licensee did not take exception to this requirement. The inspectors noted that many of the electrical penetrations needed to place the plant in hot standby were not being maintained. The inspectors concluded that the licensee was presently operating outside their licensing basis because a HELB in the East Penetration Rooms could cause a loss of redundancy of the circuitry needed to place the plant in hot standby. The listing of which penetrations would be needed to place the plant in cold shutdown are not known at this time because the licensee contends that they only have to ensure ability to go to hot standby and therefore do not have to meet the requirement for loss of redundancy in placing the plant in cold shutdown.
 
=====Analysis:=====
The finding was considered to be a performance deficiency in that the licensee failed to maintain the containment electrical penetration covers as NEMA 4 enclosures.
 
This finding was considered to be more than minor because direct and/or indirect spray from a HELB could affect multiple electrical circuits; thereby, increasing the likelihood of a reactor trip and that mitigation equipment would not be available. This would impact the Initiating Events Cornerstone objective to limit the likely hood of those events that upset plant stability, as well as the Mitigating Systems Cornerstone objective for ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
 
For the Phase 1 review, the inspectors concluded that the HELB could affect the unprotected reactor protection circuits and cause a reactor trip and affect circuits such as pressurizer level and steam generator pressure, which are used to mitigate the consequences of a HELB. Therefore, based on the Initiating Events Cornerstone for transient initiators, the inspectors concluded that the finding contributed to both the likelihood of a reactor trip and that mitigation equipment would not be available. These conditions required that a Phase 2 evaluation be performed.
 
Because the instrumentation circuits in the control room could be erratic due to the grounds and shorts resulting in degradation of the vital 120 vac and 120 vdc systems, and the inability to perform the various mitigation procedures due to erratic indications, it was assumed for the Phase 2 analysis that mitigation systems controlled from the control room were lost. Further inspection activities are being planned to support the analysis. This finding involved the cross-cutting aspect of Problem Identification and Resolution (PI&R).
 
=====Enforcement:=====
10 CFR 50 Appendix B, Criterion XVI, Corrective Action, requires that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected. Contrary to the above, the license failed to identify and correct penetration covers that had been removed or misadjusted over a number of years of maintenance activities, which created conditions adverse to quality where dust, dirt, rust, and spray could impact circuits needed to mitigate the consequences of a HELB and cause erratic operation of the 120 vac and 120 vdc vital electrical systems. Pending further inspection and analysis, this issue is being identified as an Unresolved Item, URI 05000269,270,287/2005004-10, Failure to Maintain Containment Electrical Penetration s.
 
===.8 Failure to Properly Identify Main Feedwater Line Terminal Ends===
====a. Inspection Scope====
The inspectors performed a Problem Identification and Resolution inspection for the main feedwater system piping and supports located in the East Penetration Rooms. This inspection was chosen as part of the annual sample required by IP 71152. This issue is unresolved pending determination of risk determination.
 
====b. Findings====
=====Introduction:=====
An URI was identified regarding the failure to identify a condition adverse to quality, in that feedwater terminal ends had not been identified and therefore actions to mitigate the affects from a terminal end line break had not been implemented.
 
=====Description:=====
The Oconee licensing basis for high energy line breaks is contained in the 1972 Giambusso letter, which implemented GDC-4, and contained in the licensees response to the Giambusso letter which is documented in Oconee MDS report No. OS-73.2, Analysis of Effects Resulting from Postulated Piping Breaks Outside Containment.
 
The 1972 Giambusso Letter required the licensees to postulate breaks on ASME Class 1, 2 and 3 piping at the terminal ends. It required that The plant should be designed so that the reactor can be shutdown and maintained in a safe shutdown condition in the event of a postulated rupture outside containment of a pipe containing a high energy fluid, including the double ended rupture of the largest piping in the main steam and feedwater systems. Plant structures, systems and components important to safety should be designed and located in the facility to accommodate the effects of such a postulated pipe failure to the extent necessary to assure that a safe shutdown condition of the reactor can be accomplished and maintained.
 
An attachment to the letter defined terminal ends as extremities of piping that connect to structures, components or pipe anchors that act as rigid constraints to piping motion and thermal expansion. Rigid restraints that are welded to piping systems are considered to be terminal ends. The feedwater lines are restrained at the containment penetration by using a collar that is welded to the feedwater pipe with a structural anchor that is welded to the collar and attached to the containment structure. Since the collar weld acts as a rigid constraint to piping motion and thermal expansion, each welded location is considered to be a feedwater terminal end. However, the licensee only assumed a break upstream of the collar. The feedwater line has a whip restraint at this location to protect equipment in the East Penetration Room from the affects of this break. Since the licensee did not assume a break downstream of the collar, there is no equipment protection from a break at that location.
 
A feedwater line break downstream of the collar would result in a non-postulated/
unprotected feedwater line break in the East Penetration Room. The East Penetration Rooms are not designed for an unprotected feedwater line break and would be over pressurized. In addition, jet impingement and spray from the break would affect the electrical penetrations and other piping systems in the area of the break.
 
Discussions were held with the licensee concerning this issue. The licensee concluded that it is acceptable to assume that the terminal end line break can be taken at a location of the feedwater piping in the middle of the collar. This position was discussed with an NRR expert, but the licensees position was not supported because the postulated terminal end break is required to be taken at the point of restriction. The inspectors concluded that the area in the middle of the collar could actually be an area with the lowest stress and likely would not see the full affects of thermal expansion and applied stress.
 
=====Analysis:=====
The finding is considered to be a performance deficiency in that although it is a design deficiency, the licensee failed to identify the problem during the six years of HELB design reconstitution. An unprotected terminal end line break would cause overpressurization of the East Penetration Room, loss of circuitry needed to mitigate a HELB, flooding of the HPI pump rooms, and structural damage to the East Penetration Rooms. Structural damage, jet impingement, and spray would damage systems such as building spray, letdown, low pressure service water, low pressure injection, emergency feedwater, instrument air, etc, since for many of these systems both trains are routed through the East Penetration Rooms. Damage to these systems would impact the ability to reach cold shutdown conditions. This performance deficiency was considered to be more than minor because an unprotected terminal end line break would impact the Reactor Safety Mitigating Systems Cornerstone objective for ensuring the availability, reliability and function of systems needed to respond to a HELB. For the Phase 1 review, the inspectors concluded that an unprotected terminal end line break would result in a loss of safety function of the Auxiliary Building, the multiple mitigation safety systems listed above, and containment cooling and containment integrity from unrestrained feedwater piping thrust. This would therefore impact mitigation and containment integrity. Based on this, a Phase 2 evaluation was required. The Phase 2 sequence for main steam line break was used because the postulated break is between the feedwater check valve and the steam generator. A break at this location would be similar to a steam line break. Based on the assumptions that the Auxiliary Building would be damaged, electrical indication and control circuits would be damaged and systems located in the East Penetration Room would be damaged, the Phase 2 sheet for main steam line break indicated that the issue could be greater than Green and that a Phase 3 analysis would be required. This finding involved the cross-cutting aspect of Problem Identification and Resolution.
 
=====Enforcement:=====
10 CFR 50 Appendix B, Criterion XVI, Corrective Action, requires that measures shall be established to assure that conditions adverse to quality are promptly identified. Contrary to the above, the licensee failed to identify that unprotected feedwater line terminal ends existed that could impact the mitigation systems needed to protect the plant from a HELB. Pending determination of the risk significance, this issue is being identified as URI 05000269,270,287/2005004-11, Failure to Identify Unmitigated/Unprotected Feedwater Line Terminal Ends.
 
===.9 Summary of PI&R Cross-Cutting Findings===
A Green NCV involving the cross-cutting aspect of PI&R is documented in Section
{{a|1R22}}
 
==1R22.2. The licensee failed to develop and implement a program for the inspection and==
cleaning of the containment electrical penetrations located in each units East and West Penetration Rooms, delaying the possible identification of conditions adverse to quality.
 
A second Green NCV involving the cross-cutting aspect of human performance is documented in Section 1R22.3. Licensee personnel failed to develop and implement a program for the inspection of the main steam lines located in each units East Penetration Rooms, delaying the possible identification of conditions adverse to quality.
 
A third Green NCV involving the cross-cutting aspect of PI&R is documented in Section 4OA2.6. The licensee failed to place a deficiency observed in the Unit 2 East Penetration Room floor into the corrective action program, delaying the identification of a condition adverse to quality, as well as, its resolution.
 
A URI involving the cross-cutting aspect of PI&R is documented in Section 4OA2.4. The licensee failed to take prompt and adequate corrective action for a deficient condition within each units East Penetration Rooms, that was identified in the Fall of 1999, resulting in all three Oconee Units operating outside their licensing basis since the units East Penetration Room blowout panels were improperly modified and have not been repaired.
 
A second URI involving the cross-cutting aspect of PI&R is documented in Section 4OA2.7. The licensee failed to identify a condition adverse to quality, in that, improperly maintained electrical penetration enclosures located within each units East and West Penetration Rooms had not be identified and placed into the licensees corrective action program; thereby, delaying resolution of this deficient condition.
 
A third URI involving the cross-cutting aspect of PI&R is documented in Section 4OA2.8.
 
The licensee failed to identify a condition adverse to quality, in that, the feedwater piping terminal ends located within each units East Penetration Room have not been properly identified.
 
{{a|4OA3}}
 
==4OA3 Event Followup==
===.1 Recent Events===
====a. Inspection Scope====
The inspectors evaluated one licensee event and two degraded conditions for plant status and mitigating actions in order to provide input in determining the need for an Incident Investigation Team (IIT), Augmented Inspection Team (AIT), or Special Inspection (SI). As appropriate, the inspectors:
: (1) observed plant parameters and status, including mitigating systems/trains and fission product barriers;
: (2) determined alarms/conditions preceding or indicating the event;
: (3) evaluated performance of mitigating systems and licensee actions;
: (4) confirmed that the licensee properly classified the event in accordance with emergency action level procedures and made timely notifications to NRC and state/county governments, as required (10 CFR Parts 20, 50.9, 50.72);
: (5) communicated details regarding the event to management, risk analysts and others in the Region and Headquarters as input to their determining the need for an IIT, AIT, or SI.
* PIP O-05-5118, KHU-2 Emergency Lockout While Attempting to Generate to the Grid
* PIP O-05-5365, KHU-2 Emergency Lockout While Performing PT/0/A/0620/016, Keowee Hydro Emergency Start Test
* PIP O-05-5613, Unit 3 Reactor Trip (SI documented in Inspection Report 05000287/2005010)
 
====b. Findings====
Except as identified in SI Inspection Report 05000287/2005010, no findings of significance were identified.
 
===.2 (Closed) LER 05000269/2005-01-00, Exceeded TS: Emergency Power Path Aux Power===
Source Inoperable The inspectors reviewed the circumstances surrounding the KHU overhead power path exceeding the TS allowed outage times due to a failed contactor for the overhead main step-up transformer cooling system normal power supply. The licensee also categorized this event as an unanalyzed condition due to a potential single failure vulnerability affecting both emergency power paths. This deficiency, its associated risk significance, and the licensees corrective actions were documented in Inspection Report 05000269,270,287/2005003 as a Green NCV of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action. This LER is closed.
 
===.3 (Closed) LER 269/2004-04-01, Improper Overloads Installed on Control Room===
Ventilation Filter Train
 
====a. Inspection Scope====
The inspectors reviewed the licensees TS LCO action statement entry, causal evaluation, corrective actions and operability assessment surrounding the unexpected tripping of the Unit 1 and 2, B Train, Control Room Outside Air Booster Fan (CROABF).
 
====b. Findings====
=====Introduction:=====
A Green self-revealing NCV of 10 CFR 50 Appendix B, Criterion X, Inspection, was identified for an inadequate quality control (QC) inspection associated with the incorrect installation of the Unit 1 and 2 CROABF, B Train, motor thermal overload relays.
 
=====Description:=====
On November 17, 2004, the filters of the B Train, outside air portion of the Unit 1 and 2 Control Room Ventilation System were replaced, and the associated booster fans motor bearings were lubricated as part of a preventive maintenance task.
 
During the subsequent post-maintenance testing, the fan tripped unexpectedly after 2.5 hours of operation. As documented in PIP O-04-7937, a licensee investigation determined that the apparent cause of the tripping of the B CROABF was the use of undersized heater overloads (S4.0) on the fans motor. The fans overloads were replaced with larger S4.4 heater overloads, and a 4 hour post-maintenance test was conducted satisfactorily. The inadequate design controls associated with this issue were previously documented as NCV 05000269/2005002-02, Improper Thermal Overloads Installed in the Unit 1 and 2, B Train, CROABF.
 
At 3 p.m. on April 10, 2005, the B CROABF was found tripped. Troubleshooting efforts revealed that the B CROABF center phase overload relay had tripped. The licensees root cause evaluation concluded that the cause of the fan tripping was the off-center installation of S4.4 heater element within the thermal overload relay. This heater element was previously replaced as part of the recovery from the November 17, 2004, trip of the B CROABF. The replacement heaters were installed per IP/0/A/3011/015, Removal and Replacement of Motor Control Center, Panelboards and Remote Starter Components, which required the installer and QC inspectors to verify that the overload heaters were properly centered; however, the as-found heater position was off-center.
 
As determined by subsequent testing, an off-center heater element will cause the overload relay to trip at a lower current than a relay with the heater element properly centered. The licensee replaced the S4.4 overload relay heater elements on the A and B CROABFs with S37.5 heater overloads, which are rated at 25 amps. The A and B CROABFs were then operated satisfactorily for 12 hours.
 
=====Analysis:=====
The finding was considered to be a performance deficiency because the licensee failed to conduct an adequate QC inspection of the installation of the S4.4 overload relay heater elements on the safety-related B CROABF. The licensees failure to correctly install the thermal overloads on the Unit 1 and 2, B Train, CROABF was considered to be more than minor because it affected the Barrier Integrity Cornerstone attribute of maintaining control room habitability. The inspectors reviewed this finding in accordance with IMC 0609, Significance Determination Process. Similar to NCV 05000269/2005002-02, this finding represented a similar degradation of the barrier function of the control room against smoke and/or a toxic atmosphere; thereby, requiring a Phase 3 evaluation be performed. However, since the exposure time associated with this CROABF finding is shorter than that used in the Phase 3 evaluation of NCV 05000269/2005002-02, it too is considered to be of very low safety significance (Green).
 
This finding involved the cross-cutting aspect of human performance.
 
=====Enforcement:=====
10 CFR 50 Appendix B, Criterion X, Inspection, requires, in part, that inspection of activities affecting quality be executed in conformance with the documented instructions, procedures, and drawings. IP/0/A/3011/015 required that the overload heaters be installed correctly, centered, and inspected by QC. Contrary to the above, the licensee failed to perform adequate QC inspections of the Unit 1 and 2, B Train, CROABF, in that, the center phase thermal overload was not properly centered within the relay housing, resulting in the center phase overload tripping prematurely at a lower current than the fans operating motor current. Because this issue was of very low safety significance and was placed in the licensees corrective action program as PIP O-05-2361, this violation is being treated as an NCV in accordance with Section VI.A.1 of the Enforcement Policy: NCV 05000269,270/2005004-12, Inadequate QC Inspection Results in the Improper Installation of Thermal Overloads on the Unit 1 and 2 B Train, CROABF.
 
{{a|4OA4}}
 
==4OA4 Summary of Human Performance Cross-Cutting Findings==
A Green Finding involving the cross-cutting aspect of human performance is documented in Section 1R13. Licensee personnel failed to fully understand the scope of maintenance on a Unit 3 secondary system makeup valve, resulting in an inadequate maintenance tagout. This nearly resulted in a Unit 3 trip with a loss of normal heat sink.
 
A Green NCV involving the cross-cutting aspect of human performance is documented in Section 4OA3.3. A licensee QC inspectors failed to properly inspect the installation of a heater element within the thermal overload relay for the Unit 1 and 2, B Train CROABF, resulting in the overload relay tripping at a reduced current.
 
A URI involving the cross-cutting aspect of human performance is documented in Section1R14. Licensee personnel failed to update procedural guidance for the control of the newly installed equipment, Unit 3, SSF-powered Pressurizer Heater Bank 2, Group C, resulting in the supply breaker, PXSF-4A, not being closed prior to entering Mode 3.
 
A second URI involving the cross-cutting aspect of human performance is documented in Section 1R23. Licensee personnel improperly blocked the ventilation paths into and out of Auxiliary Building Room 81 (Train B, LPI/RBS pump room). This ventilation path is required for heat removal from the room during the recirculation phase of a LOCA to ensure that the LPI and RBS pump and motor bearings do not exceed maximum operating temperatures.
 
{{a|4OA5}}
 
==4OA5 Other Activities==
Operational Readiness of Offsite Power (Temporary Instruction (TI) 2515/163)
Completion of this TI was documented in Inspection Report 05000269,270,287/
2005003. However, after NRC headquarters review of the information provided, additional information related to the TI was requested. The inspectors collected this information from licensee discussions, site procedures, and other licensee documentation. The information was provided to the headquarters staff for further analysis.
 
{{a|4OA6}}
 
==4OA6 Management Meetings (Including Exit Meeting)==
===.1===
===Exit Meeting Summary===
The inspectors presented the inspection results to Mr. Bruce Hamilton, Station Manager, and other members of licensee management at the conclusion of the inspection on October 4, 2005. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.
 
===.2 Regulatory Performance Meeting Summary===
On September 20, 2005, NRC Region II (RII) held an Oconee regulatory performance meeting with Duke Energy to discuss the results of a supplemental inspection (IR 05000269,270,287/2005010) conducted May 31 - June 2, 2005. That inspection assessed the licensees problem identification, root cause evaluation, extent of condition determination, and corrective actions associated with two White findings in the Mitigating Systems Cornerstone, which placed the performance of Oconee Units 1, 2 and 3 in the Degraded Cornerstone Column of the NRCs Action Matrix for the third quarter 2004. The two findings involved:
: (1) pressurizer ambient heat losses in all three Oconee units exceeding the capacity of the pressurizer heaters powered from the SSF; and
: (2) procedural criteria for manning the SSF during a fire in certain areas. The meeting focused on the corrective actions associated with these White findings, as well as with the supplemental inspection, in order to arrive at a shared understanding of the performance issues, underlying causes, and planned licensee actions.
 
This meeting was opened to the public. Attendees included: Oconee site management and staff (indicated on the Attachment to this report); NRC Region II management (indicated on Attachment to this report); and the resident inspectors. The presentation material used for the discussion is available from the NRCs document system (ADAMS)as Accession Number ML052650202. ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
=SUPPLEMENTAL INFORMATION=
 
==KEY POINTS OF CONTACT==
Licensee
: [[contact::L. Azzarello]], Modification Engineering Manager
: [[contact::S. Batson]], Superintendent of Operations
: [[contact::D. Baxter]], Engineering Manager
: [[contact::R. Brown]], Emergency Preparedness Manager
: [[contact::S. Capps]], Mechanical/Civil Engineering Manager
: [[contact::N. Clarkson]], Regulatory Compliance*
: [[contact::N. Constance]], Operations Training Manager
: [[contact::C. Curry]], Maintenance Manager
: [[contact::G. Davenport]], Compliance Manager
: [[contact::C. Eflin]], Requalification Supervisor
: [[contact::T. Gillespie]], Reactor and Electrical Systems Manager
: [[contact::T. Grant]], Engineering Supervisor, Reactor & Electrical Systems
: [[contact::R. Griffith]], QA Manager
: [[contact::B. Hamilton]], Station Manager*
: [[contact::D. Hubbard]], Training Manager
: [[contact::R. Jones]], Site Vice President*
: [[contact::T. King]], Security Manager
: [[contact::L. Nicholson]], Safety Assurance Manager*
: [[contact::B. Spear]], Engineer, Reactor & Electrical Systems
: [[contact::J. Twiggs]], Manager, Radiation Protection
: [[contact::J. Weast]], Regulatory Compliance*
NRC
: [[contact::M. Ernstes]], Chief of Reactor Projects Branch 1*
: [[contact::C. Casto]], Director RII Division of Reactor Projects*
: [[contact::W. Travers]], Regional Administrator, RII
*Note: Personnel indicated with an asterisk attended the regulatory performance meeting on
September 20, 2005. (See section 4OA6.2 for further details.)
 
==ITEMS OPENED, CLOSED, AND DISCUSSED==
===Opened===
: 05000287/2005004-03
: 05000287/2005004-06
: 05000269,270,287/2005004-07
: 05000269,270,287/2005004-08
: 05000269,270,287/2005004-10
: 05000269,270,287/2005005-11 URI URI URI URI URI URI Failure to Maintain Design Control of the SSF Supply Power Breaker for Unit 3, Bank 2, Group C Pressurizer Heaters (Section 1R14)
Inadequate Design Control of Unit 3 LPI/RBS Room Ventilation Pathways (Section 1R23)
Untimely Corrective Actions in Correcting the East Penetration Room Blowout Panel Deficiency (Section 4OA2.4)
Failure to Meet the Reportability Requirements of 10 CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency (Section 4OA2.5)
Failure to Maintain Containment Electrical Penetration Enclosures (Section 4OA2.7)
Failure to Identify Unmitigated/Unprotected Feedwater Line Terminal Ends (Section 4OA2.8)
 
===Opened and Closed===
: 05000269,270,287/2005004-01
: 05000287/2005004-02
: 05000269,270,287/2005004-04
: 05000269,270,287/2005004-05 NCV FIN NCV NCV Performing Licensed Duties While Medically Unqualified (Section 1R11.2)
Inadequate Maintenance and Oversight Increased the Likelihood of a Unit 3 Reactor Trip with a Loss of Normal Heat Sink (Section 1R13)
Failure to Develop and Implement a Cleanliness Inspection Program for the Containment Electrical Penetrations (Section 1R22.2)
Failure to Implement an Inspection Program for the Main Steam Lines (Section 1R22.3)
: 05000270/2005004-09
: 05000269,270/2005004-12 NCV NCV Untimely Corrective Actions for Repairs to a Unit 2 East Penetration Room Floor Seal (Section 4OA2.6)
Inadequate QC Inspection Results in the Improper Installation of Thermal Overloads on the Unit 1 and 2, B Train, CROABF (Section 4OA3.3)
 
===Closed===
: 05000269/2005-01-00
: 05000269/2004-04-01 LER LER Exceeded Tech Spec: Emergency Power Path Aux Power Source Inoperable (Section 4OA3.2)
Improper Overloads Installed on Control Room Ventilation Filter Train (Section 4OA3.3)
Items
 
===Discussed===
2515/163 TI Operational Readiness of Offsite Power (Section 4OA5)
 
==DOCUMENTS REVIEWED==


Even if a 50/50 split were taken between the units' waste systems, there would still be at least 10 minutes available for operator action.Duke could perform more detailed analysis to support the judgment by creating flooding models for the auxiliary building to address the concern for cracks; however, Duke has previously committed to implement flood prevention features that will eliminate the flooding potential to other areas of the auxiliary building following postulated feedwater line breaks and cracks inside the east penetration room. These modifications include improving the flood outlet device in the east penetration room and improving the structural integrity of the non-reinfcorced walls in the east penetration room (ref. 11/14/2005 letter from Duke to the NRC).7
}}
}}

Latest revision as of 14:15, 15 January 2025

IR 05000269-05-004, IR 05000270-05-004, IR 05000287-05-004, 07/01/2005 - 09/30/2005; Oconee Nuclear Station, Units 1, 2, and 3; Maintenance Risk Assessments and Emergent Work Control, Surveillance Testing, Identification and Resolution of P
ML053050479
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 10/28/2005
From: Ernstes M
NRC/RGN-II/DRP/RPB1
To: Rosalyn Jones
Duke Energy Corp
References
IR-05-004
Download: ML053050479 (47)


Text

October 28, 2005

SUBJECT:

OCONEE NUCLEAR STATION - INTEGRATED INSPECTION REPORT 05000269/2005004, 05000270/2005004, 05000287/2005004

Dear Mr. Jones:

On September 30, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Oconee Nuclear Station. The enclosed report documents the inspection findings which were discussed on October 4, 2005, with Mr. Bruce Hamilton and other members of your staff.

The inspection examined activities conducted under your licenses as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your licenses. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents two self-revealing and four NRC-identified findings of very low safety significance (Green); five of which were determined to be violations of NRC requirements.

However, because of their very low safety significance and because the issues were entered into your corrective action program, the NRC is treating these five findings as non-cited violations (NCVs) consistent with Section VI.A of the NRC Enforcement Policy. If you contest any of the findings in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the United States Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Oconee facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's

DEC

document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Michael E. Ernstes, Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos.: 50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55

Enclosure:

NRC Integrated Inspection Report 05000269/2005004,05000270/2005004, 05000287/2005004 w/Attachment: Supplemental Information

REGION II==

Docket Nos:

50-269, 50-270, 50-287 License Nos:

DPR-38, DPR-47, DPR-55 Report No:

50-269/2005004, 50-270/2005004, 50-287/2005004 Licensee:

Duke Energy Corporation Facility:

Oconee Nuclear Station, Units 1, 2, and 3 Location:

7800 Rochester Highway Seneca, SC 29672 Dates:

July 1, 2005 - September 30, 2005 Inspectors:

M. Shannon, Senior Resident Inspector A. Hutto, Resident Inspector E. Riggs, Resident Inspector R. Aiello, Senior Operations Engineer (Section 1R11)

S. Rose, Senior Operations Engineer (Section 1R11)

M. Chitty, Operations Engineer (Section 1R11)

Approved by:

Michael E. Ernstes, Chief Reactor Projects Branch 1 Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000269/2005004, IR 05000270/2005004, IR 05000287/2005004, 07/01/2005 -

09/30/2005; Oconee Nuclear Station, Units 1, 2, and 3; Maintenance Risk Assessments and Emergent Work Control, Surveillance Testing, Identification and Resolution of Problems, and Event Followup.

The report covered a three-month period of inspection by the onsite resident inspectors and three operations engineers. Six Green findings, five of which were non-cited violations (NCVs), were identified. The significance of most findings is indicated by their color (Green, White,

Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

NRC Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green.

A self-revealing finding was identified for inadequate maintenance and oversight of repair efforts on the actuator of 3DW-18 (the Unit 3 Upper Surge Tank (UST) Makeup Valve). Specifically, while attempting to repair an air leak on the actuator of 3DW-18, maintenance technicians removed the valves bonnet and were ready to remove the valves diaphragm with no hydraulic isolations made between the valve and the main condenser. Had the diaphragm been removed from 3DW-18, it is likely that Unit 3 would have tripped due to a loss of main condenser vacuum, as the top of the UST dome is vented to the main condenser.

This event was considered to be a performance deficiency, as the licensee failed to provide adequate maintenance and oversight of the efforts to repair an air leak on the 3DW-18 actuator; thereby, increasing the likelihood of a unit trip with a loss of normal heat sink. This issue was considered to be more than minor because it affected the Initiating Events cornerstone objective of limiting the likelihood of events that upset plant stability. The finding is associated with the configuration control attribute, in that the inadequate maintenance and oversight of the repairs to the actuator of 3DW-18 increased the likelihood of a reactor trip with a loss of normal heat sink due to inadequate configuration control of a secondary plant system. The consequences of the finding were assessed through Phase 2 of the SDP, and although the likelihood of a unit trip was increased and would have resulted in a loss of the normal heat sink, the exposure time for this condition was less than 3 days and all other mitigation capabilities described on the Phase 2, SDP worksheet for transient (reactor trip)core damage sequences were maintained. Consequently, the finding was determined to be of very low safety significance. This finding involved the cross-cutting aspect of human performance. (Section 1R13)

Green.

A NRC-identified non-cited violation of 10 CFR 50 Appendix B, Criterion X, Inspection, was identified for the failure to develop and implement an inspection program for monitoring the main steam line in the Unit 1, 2 and 3 East Penetration Rooms. The finding was considered to be a performance deficiency in that the licensee had committed to perform inspections of the steam lines to support the acceptability of Dukes design and analysis for the main steam lines, but the inspections were not being performed.

The finding was considered to be more than minor because it impacted the Reactor Safety Initiating Events Cornerstone in that failure to perform the inspections could lead to failure to identify degrading main steam line conditions, which would cause an increase in the likelihood of an initiating event. The finding was screened as having very low safety significance under the Initiating Events Cornerstone, in that it did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available. This finding involved the cross-cutting aspect of Problem Identification and Resolution. (Section 1R22.3)

Cornerstone: Mitigating Systems

Green.

A NRC-identified non-cited violation of 10 CFR 50.74 was identified for failure to make a notification of a change in operator or senior operator status regarding information for one licensed operator concerning his medical qualification. Specifically, the operator failed to meet the American Nuclear Standards Institute /American Nuclear Society (ANSI/ANS-3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, 1983 Standard for a blood pressure (BP) limitation. This impacted the NRCs ability to perform its regulatory function, in that the NRC was not able to make a licensing decision with regards to a potential restriction to ensure compliance with ANSI/ANS-3.4. Consequently, an operator stood several watches in a Technical Specification license position with his BP greater than the ANSI/ANS limits.

This finding is of very low safety significance because there was no evidence that the operator endangered plant operations as a result of hypertension while performing licensed duties since the original issuance of his license. However, the regulatory significance was important because pertinent information was not provided to the NRC when the operator knowingly discontinued taking his medication. Subsequently, this impacted a licensing decision for the individual.

(Section 1R11.2)

Green.

A NRC-identified non-cited violation of 10 CFR 50 Appendix B, Criterion X, Inspection, was identified for the failure to develop and implement an inspection program for inspection and cleaning of the containment electrical penetrations located in the East and West Penetration Rooms of Units 1, 2, and 3.

The finding was considered to be a performance deficiency in that the licensee had failed to develop an inspection program for their containment electrical penetrations to ensure cleanliness of the electrical connections. The inspectors concluded that if left uncorrected (no inspection) debris and rust accumulation could lead to failure of the electrical circuits during a high energy line break as a result of grounds and shorts. Therefore, failure to perform cleanliness inspections was considered to be more than minor because it could impact the Reactor Safety Mitigating Systems Cornerstone objective for reliability of a mitigating system/train (i.e., circuits needed to mitigate a high energy line break.

The finding was screened as very low safety significance in the Phase 1 review under the Mitigating Systems Cornerstone, in that failure to perform an electrical penetration inspection was not considered to be a design deficiency, was not considered to represent a loss of safety system function, was not considered to represent an actual loss of safety function of a single train, and did not involve seismic, flooding or severe weather. This finding involved the cross-cutting aspect of Problem Identification and Resolution. (Section 1R22.2)

Green.

A NRC-identified non-cited violation of 10 CFR 50 Appendix B, Section XVI, Corrective Action, for inadequate corrective actions related to the lack of timeliness of repairs to a Unit 2 East Penetration Room floor seal.

The failure to promptly repair the damaged floor seal was considered to be a performance deficiency. The finding was considered to be more than minor because if left uncorrected, additional seal area could fail and it would affect the Mitigating System Cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events, in that the high pressure injection (HPI) pumps could be flooded following a high energy line break in the East Penetration Room. However, in the seals current level of degradation, the inspectors concluded that the deficiency would not by itself result in the loss of function of the HPI pumps, because flooding would be limited by the size of the degraded/failed seal. Consequently, the finding was determined to be of very low safety significance, as it was screened out under the Mitigating Systems Cornerstone in the SDP Phase 1 Screening Worksheet with the determination that there was no loss of safety function. This finding involved the cross-cutting aspect of Problem Identification and Resolution. (Section 4OA2.6)

Cornerstone: Barrier Integrity

Green.

A self revealing, non-cited violation (NCV) of 10 CFR 50 Appendix B,

Criterion X, Inspection, was identified for an inadequate quality control (QC)inspection associated with the installation of the thermal overloads on the Unit 1 and 2 Control Room Outside Air Booster Fan (CROABF) Train B.

The finding was considered to be a performance deficiency because the licensee failed to conduct an adequate QC inspection of the installation of the S4.4 overload relay heater elements on the safety-related B CROABF. The licensees failure to correctly install the thermal overloads on the Unit 1 and 2, B Train,

CROABF was considered to be more than minor because it affected the Barrier Integrity Cornerstone attribute of maintaining control room habitability. Similar to NCV 05000269/2005002-02, this finding represented a similar degradation of the barrier function of the control room against smoke and/or a toxic atmosphere; thereby, requiring a Phase 3 evaluation be performed. However, since the exposure time associated with this CROABF finding is shorter than that used in the Phase 3 evaluation of NCV 05000269/2005002-02, it too is considered to be of very low safety significance. This finding involved the cross-cutting aspect of human performance. (Section 4OA3.3)

Licensee-Identified Violations

None

REPORT DETAILS

Summary of Plant Status:

Unit 1 entered the report period at 100 percent rated thermal power (RTP). The unit was reduced to approximately 88 percent RTP on August 6, 2005, to perform turbine valve movement testing. The unit was returned to 100 percent RTP on the same day. The unit operated at or near 100 percent RTP for the remainder of the inspection period.

Unit 2 entered the report period at 100 percent RTP. The unit was reduced to approximately 88 percent RTP on July 9, 2005, to perform turbine valve movement testing. The unit was returned to 100 percent RTP on the same day. On September 26, 2005, the unit commenced a power coastdown in advance of the End-of-Cycle 21 (2EOC21) refueling outage, and the unit completed the inspection period at approximately 93 percent RTP. The unit operated at or near 100 percent RTP for the remainder of the inspection period.

Unit 3 entered the report period at 100 percent RTP. The unit automatically tripped on August 31, 2005, due to the complete loss of power to the newly installed digital control rod drive (CRD) system while performing CRD testing. A design deficiency resulted in an excessive cooldown of the reactor coolant system (RCS), resulting in an engineered safeguards actuation on low RCS pressure at 1600 psig. The unit entered a forced outage to identify the cause of the trip and overcooling event and to conduct repairs. Following repairs, the unit was taken critical on September 6, 2005, and returned to 100 percent RTP on September 8, 2005. The unit operated at or near 100 percent RTP for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

==1R01 Adverse Weather Protection Tornado Watch (Remnants of Huricane Katrina)

a. Inspection Scope

==

The inspectors verified that the licensee responded appropriately to a tornado watch issued for Oconee County, SC on August 29, 2005. The inspectors verified that operations personnel entered abnormal procedure AP/0/A/1700/006, Natural Disaster, and that there were no ongoing maintenance activities on systems that required restoration by the procedure. The inspectors also verified that control room personnel had completed Enclosure 5.4, Severe Weather, as required by the AP.

b. Findings

No findings of significance were identified.

==1R04 Equipment Alignment

a. Inspection Scope

==

The inspectors conducted partial equipment alignment walkdowns to evaluate the operability of selected redundant trains or backup systems while the other train or system was inoperable or out of service. The walkdowns included, as appropriate, reviews of plant procedures and other documents to determine correct system lineups, and verification of critical components to identify any discrepancies which could affect operability of the redundant train or backup system. The following three systems were included in this review:

  • The high pressure service water (HPSW) system with the B HPSW pump out of service (OOS) for the replacement of the pumps rotating element
  • Keowee Hydro Unit (KHU) -1 and the underground power path with KHU-2 OOS following an emergency lockout while attempting to generate to the grid (Problem Investigation Process report (PIP) O-05-5118)
  • Primary instrument air system with a backup instrument air compressor OOS for maintenance

b. Findings

No findings of significance were identified.

==1R05 Fire Protection

a. Inspection Scope

==

The inspectors conducted tours in eighteen areas of the plant to verify that combustibles and ignition sources were properly controlled, and that fire detection and suppression capabilities were intact. The inspectors selected the areas based on a review of the licensees safe shutdown analysis and the probabilistic risk assessment based sensitivity studies for fire-related core damage sequences. Inspections of the following areas were conducted during this inspection period:

  • Unit 1, 2, and 3 Turbine Building Basement Level (3)
  • Unit 1, 2, and 3 Equipment Rooms (3)
  • Unit 1, 2, and 3 Auxiliary Shutdown Panels (2)
  • Unit 1, 2, and 3 Turbine Building Ground Level (3)
  • Unit 1, 2, and 3 Turbine Building Operating Level (3)

b. Findings

No findings of significance were identified.

==1R11 Licensed Operator Requalification

==

.1 Simulator Training

a. Inspection Scope

The inspectors observed licensed operator simulator training on September 21, 2005.

The scenario involved a main steam line break outside of containment. The simulated event was complicated by a failure of valves needed to isolate the faulted steam generator. The inspectors observed crew performance in order to assess licensed operator performance and the evaluators critique, focusing on: communications; ability to take timely and proper actions; prioritizing, interpreting, and verifying alarms; correct use and implementation of procedures, including the abnormal procedures; timely control board operation and manipulation, including immediate operator actions; and oversight and direction provided by the shift supervisor and shift technical advisor. The inspectors did not observe any problems during the scenario.

b. Findings

No findings of significance were identified.

.2 Requalification Program

a. Inspection Scope

The inspectors reviewed the facility operating history and associated documents in preparation for this inspection. During the weeks of March 21 - 25 (in office) and March 28 - April 1 (on site), 2005, the inspectors reviewed documentation, interviewed licensee personnel, and observed the administration of simulator operating tests and Job performance Measures (JPMs) associated with the licensees operator requalification program. Each of the activities performed by the inspectors was done to assess the effectiveness of the licensee in implementing requalification requirements identified in 10 CFR 55, Operators Licenses. The evaluations were also performed to determine if the licensee effectively implemented operator requalification guidelines established in NUREG-1021, Operator Licensing Examination Standards for Power Reactors, and Inspection Procedure 71111.11, Licensed Operator Requalification Program. The inspectors also reviewed and evaluated the licensees simulation facility for adequacy for use in operator licensing examinations. The inspectors observed two operator crews during the performance of the operating tests. Documentation reviewed included written examinations, JPMs, simulator scenarios, licensee procedures, on-shift records, simulator modification request records and performance test records, the feedback process, licensed operator qualification records, remediation plans, watchstanding, and medical records. The records were inspected against the criteria listed in Inspection Procedure 71111.11. Documents reviewed during the inspection are listed in the to this report.

b. Findings

Introduction:

A Green NRC-identified non-cited violation (NCV) of 10 CFR 50.74(c),

Notification of change in operator or senior operator status, was identified for failure to notify the NRC of a change in a licensed operators medical status.

Description:

The NRC identified that, during the period between December 20, 2004 and January 24, 2005, an operator stood several watches in a TS license position with blood pressure (BP) greater than ANSI/ANS-3.4-1983, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, limits. When the facility became aware of the operators failure to meet these limits, they failed to notify the NRC.

A NRC licensed operators medical record indicated that he had BP in excess of the ANSI/ANS-3.4-1983 limits. On February 12, 2004, the facility licensee sent a letter to the NRC identifying that this operator was on medication for controlling high BP. The NRC doctor stated that a medical condition was not necessary to be placed on his license since he was on medication and it was being controlled. In a medical examination on December 20, 2004, the facility determined that the operator took it upon himself to try to reduce his BP with diet but was unsuccessful. This medical examination also determined that the operators non-medicated BP was outside of the ANSI/ANS-3.4-1983 limits. In the meantime, the operator conducted licensed activities with his BP greater than the ANSI/ANS-3.4-1983 limits during the period stated above.

Analysis:

The facility licensees failure to report that one of their licensed operators did not meet the requirements of ANSI/ANS-3.4-1983 as required by 10 CFR 50.74 was a performance deficiency. This was reasonably within the licensees ability to foresee and prevent. Because this issue affected the NRCs ability to perform its regulatory function, it was evaluated using the traditional enforcement process. The regulatory significance was important because pertinent information was not provided to the NRC when the operator knowingly discontinued taking his medication. Subsequently, this impacted a licensing decision for the individual. This finding is of very low safety significance (Green) because there was no evidence that the operator endangered plant operations as a result of hypertension while performing licensed duties since the original issuance of his license.

Enforcement:

10 CFR 50.74 states, in part, that each licensee shall notify the NRC within 30 days of identifying a permanent disability or illness as described in 10 CFR 55.25 of this chapter. 10 CFR 55.25 states, in part, that If, during the term of the license, the licensee develops a permanent physical or mental condition that causes the licensee to fail to meet the requirements of § 55.21 of this part, the facility licensee shall notify the Commission, within 30 days of learning of the diagnosis, in accordance with § 50.74(c). For conditions for which a conditional license (as described in § 55.33(b) of this part) is requested, the facility licensee shall provide medical certification on Form NRC 396 to the Commission (as described in § 55.23 of this part).

The facility licensee must also certify which industry standard (i.e., the 1983 or 1996 version of ANSI/ANS-3.4, or other NRC-approved method) was used in making the fitness determination. 10CFR 55.57(b)(1) states, in part, the medical condition and general health of the licensee continue to be such as not to cause operational errors that endanger public health and safety. It is incumbent upon the facility licensee to ensure that individual licensed operators are medically qualified to operate the plant or perform licensed duties. The facilitys physician must determine whether the operator meets the requirements of section 55.57(b)(1), (i.e., the operators medical condition and general health will not adversely affect the performance of assigned operator duties or cause operational errors that endanger public health and safety.) Furthermore, the facility must notify the NRC on NRC Form 396 regarding his medical status and potential medical issues that may require a license condition.

Contrary to the above, the licensee failed to notify the NRC after becoming aware of a potential disqualifying medical condition. The failure to report noncompliance with the ANSI/ANS-3.4-1983 medical requirements, as implied by 10 CFR 50.74, is of low safety significance. Additionally, this issue has been entered into the facilitys corrective action program (PIP O-05-02152). Therefore, this violation is being treated as an NCV, consistent with section VI.A of the NRC Enforcement Policy: NCV 05000269,270,287/

2005004-01, Performing Licensed Duties While Medically Unqualified.

==1R12 Maintenance Effectiveness

a. Inspection Scope

==

The inspectors reviewed the licensees effectiveness in performing routine maintenance activities. This review included an assessment of the licensees practices pertaining to the identification, scoping, and handling of degraded equipment conditions, as well as common cause failure evaluations. For each item selected, the inspectors performed a detailed review of the problem history and surrounding circumstances, evaluated the extent of condition reviews as required, and reviewed the generic implications of the equipment and/or work practice problem. For those systems, structures, and components (SSCs) scoped in the maintenance rule per 10 CFR 50.65, the inspectors verified that reliability and unavailability were properly monitored and that 10 CFR 50.65 (a)(1) and (a)(2) classifications were justified in light of the reviewed degraded equipment condition. The inspectors reviewed the following items:

  • KHU-2, which included the following PIPs: O-05-5118, KHU-2 Emergency Lockout While Attempting to Generate to the Grid; and O-05-5365, KHU-2 Emergency Lockout While Performing PT/0/A/0620/016, Keowee Hydro Emergency Start Test
  • 1RIA-40 (Unit 1, Condenser Air Ejector Offgas Radiation Indicating Alarm),which included the following: PIP O-05-5009,1RIA-40 count rate indication has been increasing over time and varies significantly when compared to 2RIA-40 and 3RIA-40; and IP/0/B/0360/037, 1RIA-40, Sorrento Gas Monitor

b. Findings

No findings of significance were identified.

==1R13 Maintenance Risk Assessment and Emergent Work Evaluations

a. Inspection Scope

==

The inspectors evaluated the following attributes for the eight selected SSCs and activities listed below:

(1) the effectiveness of the risk assessments performed before maintenance activities were conducted;
(2) the management of risk;
(3) that, upon identification of an unforseen situation, necessary steps were taken to plan and control the resulting emergent work activities; and
(4) that maintenance risk assessments and emergent work problems were adequately identified and resolved.
  • Relay replacement on standby bus to main feeder bus supply breakers B1T-6 and B1T-7 with the A Lee Combustion Turbine OOS
  • B HPSW pump with the 1X6 Motor Control Center OOS for relay replacement
  • B HPSW pump with the Primary Instrument Air Compressor OOS
  • PIP O-05-4724, Near Miss During Scheduled Work to 3DW-18
  • PIP O-05-5376, Orange Risk Condition During Severe Thunderstorm Warning with KHU-2 and the Overhead Power Path OOS
  • PIP O-05-5551, Tornado Watch (Remnants of Hurricane Katrina) Combine With Yellow Risk Significant Maintenance Items to Cause Orange Risk Condition
  • PIP O-05-5938, Unable to Isolate and Drain Elevated Water Storage Tank Due to Orange Risk Condition Activity With no Documented Plant Operations Review Committee Review

b. Findings

Introduction:

A Green self-revealing finding (FIN) was identified for inadequate maintenance and oversight of repair efforts on the actuator of 3DW-18 (the Unit 3 Upper Surge Tank (UST) Makeup Valve). Specifically, while attempting to repair an air leak on the actuator of 3DW-18, maintenance technicians removed the valves bonnet and were ready to remove the valves diaphragm with no hydraulic isolations made between the valve and the main condenser. Had the diaphragm been removed from 3DW-18, it is likely that Unit 3 would have tripped due to a loss of main condenser vacuum, as the top of the UST dome is vented to the main condenser.

Description:

At approximately 3 p.m. on July 20, 2005, with Unit 3 in Mode 1 at 100 percent RTP, the bonnet of 3DW-18 was removed to repair an air leak on the valves actuator. The maintenance crew was ready to pull the valves diaphragm, when they noticed it was under a vacuum. The work crew stopped work and questioned the condition with the Work Control Center (WCC) Senior Reactor Operator (SRO). The removal of the diaphragm would have exposed the units main condenser to a 6-inch pathway to atmosphere. PIP O-05-4724 states, The WCC SRO knew that there was no hydraulic isolation on the line and immediately stopped the crew and instructed them to return the valve to the condition they had found it in before they started work. Had the diaphragm been removed from the valve it would have most likely resulted in a unit trip on loss of vacuum. The WCC SRO was under the impression that the work order was only for repair of an air leak on the actuator and not for disassembly of the valve itself. As documented in PIP O-05-4724, a licensee investigation concluded that, Operations (OPS) personnel failed to follow their approved tagout process.

Consequently, they failed to comprehend that hydraulic isolation was required for DW-18 Repair Air Leak on Actuator work. After determining that work external to the system only was being performed an inadequate tagout that led to this event was issued. The PIP also states that, The details of the work scope required to ensure proper isolation would occur was unclear to OPS personnel. Consequently, OPS personnel did not recognize that a hydraulic isolation of DW-18 was necessary.

Analysis:

This event was considered to be a performance deficiency, as the licensee failed to provide adequate maintenance and oversight of the efforts to repair an air leak on the 3DW-18 actuator; thereby, increasing the likelihood of a unit trip with a loss of normal heat sink. This issue was considered to be more than minor because it affected the Initiating Events cornerstone objective of limiting the likelihood of events that upset plant stability. The finding is associated with the configuration control attribute, in that the inadequate maintenance and oversight of the repairs to the actuator of 3DW-18 increased the likelihood of a reactor trip with a loss of normal heat sink due to inadequate configuration control of a secondary plant system. The consequences of the finding were assessed through Phase 2 of the SDP, and although the likelihood of a unit trip was increased and would have resulted in a loss of the normal heat sink, the exposure time for this condition was less than 3 days and all other mitigation capabilities described on the Phase 2, SDP worksheet for transient (reactor trip) core damage sequences were maintained. Consequently, the finding was determined to be of very low safety significance (Green). This finding involved the cross-cutting aspect of human performance.

Enforcement:

This finding was not a violation of regulatory requirements because the Unit 3 main condenser is not considered to be safety-related, and therefore not under the requirements of 10 CFR 50, Appendix B. This finding is identified as FIN 05000287/2005004-02, Inadequate Maintenance and Oversight Increased the Likelihood of a Unit 3 Reactor Trip with a Loss of Normal Heat Sink. This issue has been entered into the licensees corrective action program as PIP O-05-4724.

==1R14 Personnel Performance During Non-routine Plant Evolutions

a. Inspection Scope

==

The inspectors reviewed the operating crews performance during selected non-routine events and/or transient operations to determine if their response was appropriate to the event. As applicable, the inspectors:

(1) reviewed operator logs, plant computer data, or strip charts to determine what occurred and how the operators responded;
(2) deter-mined if operator responses were in accordance with the responses required by procedures and training;
(3) evaluated the occurrence and subsequent personnel response using the SDP; and
(4) confirmed that personnel performance deficiencies were captured in the licensees corrective action program. The non-routine evolutions reviewed during this inspection period included the following:
  • PIP O-05-5118, KHU-2 Emergency Lockout While Attempting to Generate to the Grid
  • PIP O-05-5365, KHU-2 Emergency Lockout While Performing PT/0/A/0620/016, Keowee Hydro Emergency Start Test
  • PIP O-05-5252, Abnormal Statalarms Following Standby Shutdown Facility (SSF) Diesel Generator (DG) Start
  • PIP O-05-0122, Supply Breaker for Unit 3, SSF-Powered Pressurizer Heaters Found Out of Position

b. Findings

Introduction:

An Unresolved Item (URI) was identified regarding inadequate design control associated with the failure to close the Unit 3, Bank 2, Group C pressurizer heater supply breaker prior to entering Mode 3 following the 3EOC21 refueling outage (RFO). This issue resulted in the SSF auxiliary service water (ASW) system being unable to perform its intended safety function and has been designated as an URI pending a Phase 3 risk analysis.

Description:

On March 7, 2002, the licensee documented, in PIP O-02-1066, the lack of sufficient SSF-powered pressurizer heaters to maintain single phase, natural circulation RCS flow during an SSF-related event. On May 6, 2002, the licensee documented this issue in Licensee Event Report (LER) 50-269/2002-01, Pressurizer Heat Loss Exceeds Standby Shutdown Facility Powered Heater Capacity, and on December 30, 2003, the licensee received the low to moderate safety significant (White) violation 05000269, 270,287/2003012-01, Failure to Promptly Identify and Correct Insufficient SSF Pressurizer Heater Capacity. One of the corrective actions associated with PIP O-02-1066 was to increase the capacity of SSF-powered pressurizer heaters for each Oconee unit. On Unit 3, these modifications were performed during the 3EOC21 RFO in the Fall of 2004.

As documented in PIP O-05-0122, on January 4, 2005, with Unit 3 in Mode 1, the licensee discovered that supply breaker PXSF-4A for the Unit 3, Pressurizer Heater Bank 2, Group C was open. The unit was at approximately 20 percent RTP with power escalation in progress following the completion of the 3EOC21 RFO. A licensee investigation concluded that the cause of the breaker being mispositioned was the failure of operations personnel to follow management guidance for the removal and restoration process. A contributing cause to this incident was the lack of procedural guidance to ensure the breaker would be placed in the desired position, in that the startup procedure was not changed to reflect the installation and operation of this new equipment. The breaker had been mispositioned for approximately 234 hours0.00271 days <br />0.065 hours <br />3.869048e-4 weeks <br />8.9037e-5 months <br /> prior to being closed by the licensee on January 4, 2005.

Analysis:

The inspectors determined that the licensees failure to maintain design control of PXSF-4A following its installation was a performance deficiency because the licensee failed to update procedural guidance associated with the breakers operation. The failure to maintain adequate design control over the breaker PXSF-4A was considered to be more than minor because it affected the mitigating systems cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding is associated with the configuration control attribute, in that, the operational lineup for the Unit 3, Pressurizer Heater Bank 2, Group C supply breaker was not maintained. A Phase 1 SDP screening was performed, and it was determined that a Phase 2 analysis was required, as the finding represented an actual loss of the safety function of the SSF. This was based on the conclusion that during an SSF-related event, the insufficient SSF-powered pressurizer heaters would result in the inability to control RCS pressure via a pressurizer steam bubble. This would result in the inability to maintain single phase, natural circulation RCS flow without utilizing solid plant operations; thereby, rendering the SSF ASW system inoperable as indicated in the TS bases. The Phase 2 initiator and system dependancy table within the Oconee Risk Informed Notebook references a note to submit any findings associated with the SSF-powered, pressurizer heaters for a Phase 3 risk evaluation by a Regional Senior Reactor Analyst. This finding involved the cross-cutting aspect of human performance.

Enforcement:

10 CFR 50, Appendix B, Criterion III, Design Control, requires, in part, that measures be established to assure that design basis for structures, systems, and components covered by Appendix B are correctly translated into specifications, drawings, procedures and instructions. Contrary to the above, the licensee failed to maintain adequate design control of the Unit 3, Bank 2 Group C pressurizer heater breaker, in that, the licensee failed to update the startup procedure with regard to the newly installed breaker. Pending determination of the risk significance, this finding will be identified as URI 05000287/2005004-03, Failure to Maintain Design Control of the SSF Supply Power Breaker for Unit 3, Bank 2, Group C Pressurizer Heaters.

==1R15 Operability Evaluations

a. Inspection Scope

==

The inspectors reviewed selected operability evaluations affecting risk significant systems, to assess, as appropriate:

(1) the technical adequacy of the evaluations;
(2) whether continued system operability was warranted;
(3) whether other existing degraded conditions were considered;
(4) if compensatory measures were involved, whether the compensatory measures were in place, would work as intended, and were appropriately controlled; and
(5) where continued operability was considered unjustified, the impact on Technical Specification (TS) limiting condition for operations (LCOs). The inspectors reviewed the following seven operability evaluations:
  • PIP O-05-4502, During the Performance of Low Pressure Injection (LPI) Valve Stroke Performance Test (PT), 3LP-7 Stroked Too Quickly
  • PIP O-05-4646, Water Discovered Inside of 230kV Switchyard DC Distribution Panelboards SY-DC1, DYA, DYB, DYC and DYD
  • PIP O-05-4649, Single Failure Vulnerability of DC Panel with KHU-2 Aligned to Overhead Power Path
  • PIP O-05-4720, SSF DG Engine Exhaust Fan Suction Found Partially Blocked
  • PIP O-05-5086, Actual Size of Maximum [Reactor Building Emergency Sump]

Screen Opening is Larger Than Stated in the LPI Design Basis Document

  • PIP O-05-5118, KHU-2 Emergency Lockout While Attempting to Generate to the Grid

b. Findings

No findings of significance were identified.

==1R16 Operator Work-Arounds Risk Significant Operator Work-Arounds

a. Inspection Scope

==

The inspectors reviewed the significant operator work-around listed below to determine if the functional capability of the respective system or the human reliability in responding to an initiating event were affected. The inspectors specifically evaluated the effect of the operator work-arounds on the ability to implement abnormal or emergency operating procedures. The inspectors also assessed what impact it would have on the unit if the work-around could not be properly performed.

  • PIP O-05-5935, 1CS-5 Failed to Close After Pumping the Quench Tank to 1A Bleed Hold Up Tank. 1CS-5 was declared inoperable, requiring 1CS-6 to be deactivated to isolate the containment penetration. In order to decrease the frequency at which the quench tank is pumped, the maximum operating level of the quench tank was increased. Additionally, OPS personnel must clear tags on 1CS-6 to unisolate the containment penetration in order to pump the quench tank.

b. Findings

No findings of significance were identified.

==1R19 Post-Maintenance Testing (PMT)

a. Inspection Scope

==

The inspectors reviewed PMT procedures and/or test activities, as appropriate, for selected risk significant systems to assess whether:

(1) the effect of testing on the plant had been adequately addressed by control room and/or engineering personnel;
(2) testing was adequate for the maintenance performed;
(3) acceptance criteria were clear and adequately demonstrated operational readiness consistent with design and licensing basis documents;
(4) test instrumentation had current calibrations, range, and accuracy consistent with the application;
(5) tests were performed as written with applicable prerequisites satisfied;
(6) jumpers installed or leads lifted were properly controlled;
(7) test equipment was removed following testing; and
(8) equipment was returned to the status required to perform its safety function. The inspectors observed testing and/or reviewed the results of the following six tests:
  • PT/2/A/0204/007, 2B Reactor Building Spray (RBS) Pump Test, following testing and inspection of the pumps motor
  • PT/1/A/0251/001, Unit 1and 2 A Low Pressure Service Water Pump Test, following pump lubrication
  • PT/2/A/0600/13A, 2A Motor Driven Emergency Feedwater (MDEFW) Pump Test, following pump lubrication
  • PT/0/A/0400/005, SSF ASW Pump Test, following the replacement of the outboard stuffing box packing
  • PT/0/A/0620/016, Keowee Hydro Emergency Start Test, following repairs associated with the second emergency lockout on KHU-2
  • OP/0/A/1600/010, Operation of the SSF DG, following routine preventive maintenance

b. Findings

No findings of significance were identified.

==1R22 Surveillance Testing

==

.1 Routine Surveillance

a. Inspection Scope

The inspectors witnessed surveillance tests and/or reviewed test data of the five risk-significant SSCs listed below, to assess, as appropriate, whether the SSCs met TS, Updated Final Safety Analysis Report (UFSAR), and licensee procedure requirements.

In addition, the inspectors determined if the testing effectively demonstrated that the SSCs were ready and capable of performing their intended safety functions.

  • PT/3/A/0600/013, 3B MDEFW Pump Test
  • PT/2/A/0202/011, 2C High Pressure Injection (HPI) Pump Test
  • HP/0/B/1000/060 D, Procedure for Vent, Air Ejector and Reactor Building Sampling and Analysis
  • AM/0/A/1300/059, Pump - Submersible - Emergency SSF Water Supply -

Installation and Removal

  • PT/3/A/0600/012, Unit 3 Turbine Driven Emergency Feedwater Pump Test Note: (*) Indicates in-service test (IST).

b. Findings

No findings of significance were identified.

.2 Inadequate Inspection of Containment Electrical Penetrations

a. Inspection Scope

As part of the surveillance inspection procedure, the inspectors reviewed the activities associated with inspection and cleaning of the containment electrical penetrations following identification by the inspectors that a significant number of electrical penetration covers had been removed during previous maintenance activities.

b. Findings

Introduction:

The inspectors identified a Green non-cited violation (NCV) of 10 CFR 50 Appendix B, Criterion X, Inspection, for failure to develop and implement an inspection program for inspection and cleaning of the containment electrical penetrations located in the East and West Penetration Rooms. Discussions with the licensee disclosed that no procedures were in place to perform inspections or cleaning.

Description:

Information Notice (IN) 82-03, Environmental Tests of Electrical Terminal Blocks, indicated that cleanliness of terminations and terminal blocks in circuits important to safety is of concern. It stated, in part, that the cleanliness aspects are addressed in Appendix B of 10 CFR 50 and that these regulations require the licensee to establish appropriate procedures to assure that equipment is maintained in an acceptable state. It also indicated that licensees are reminded that their plant preventive maintenance program should assure that periodic inspection of those terminations and terminal blocks for cleanliness and installation integrity is performed following any maintenance activity affecting them.

Based on discussions with NRR, it was concluded that IN 82-03 and 10 CFR 50 Appendix B, Criterion X, required the licensee to develop and implement a program for inspection of the containment electrical penetrations. Discussions during August 2005 disclosed that the licensee did not have a program for routine inspection and cleaning of the containment electrical penetrations. The inspectors noted that many of the protective covers had been removed and some of the terminal blocks had indications of dirt and rust accumulation. Therefore, the failure to develop an inspection program for the containment electrical penetrations was considered to be a violation.

Analysis:

The finding was considered to be a performance deficiency in that the licensee had failed to develop an inspection program for their containment electrical penetrations to ensure cleanliness of the electrical connections. The inspectors concluded that if left uncorrected (no inspection), debris and rust accumulation could lead to failure of the electrical circuits during a high energy line break as a result of grounds and shorts.

Therefore, failure to perform cleanliness inspections was considered to be more than minor because it could impact the Reactor Safety Mitigating Systems Cornerstone objective for reliability of a mitigating system/train (i.e., circuits needed to mitigate a high energy line break (HELB)). The finding was screened as very low safety significance (Green) in the Phase 1 review under the Mitigating Systems Cornerstone, in that failure to perform an electrical penetration inspection was not considered to be a design deficiency, was not considered to represent a loss of safety system function, was not considered to represent an actual loss of safety function of a single train, and did not involve seismic, flooding or severe weather. This finding involved the cross-cutting aspect of Problem Identification and Resolution.

Enforcement:

10 CFR 50 Appendix B, Criterion X, Inspection, requires that a program for inspection of activities affecting quality shall be established and executed to verify conformance with the instructions and procedures. Contrary to the above, the licensee failed to establish an inspection program for inspection of the containment electrical penetrations to ensure proper cleanliness of the penetrations. Because this issue was of very low safety significance and has been entered into the licensees corrective action program (PIP O-05-4491), this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000269,270,287/2005004-04:

Failure to Develop and Implement a Cleanliness Inspection Program for the Containment Electrical Penetrations.

.3 Inadequate Inspection of Main Steam Lines

a. Inspection Scope

As part of the surveillance inspection procedure, the inspectors reviewed the inspection activities associated with licensee commitments to the 1972 Giambusso Letter (HELB).

b. Findings

Introduction:

The inspectors identified a Green NCV of 10 CFR 50 Appendix B, Criterion X, Inspection, for failure to develop and implement an inspection program for monitoring the main steam line in the East Penetration Rooms. Discussions with the licensee disclosed that the main steam line postulated break areas were not being inspected.

Description:

The Oconee licensing basis for high energy line breaks is contained in the December 15, 1972, letter from A. Giambusso to Duke Power Company (Giambusso letter) and the licensees response to the letter which is documented in Oconee MDS Report No. OS-73.2, Analysis of Effects Resulting from Postulated Piping Breaks Outside Containment. In response to Question 7 of the Giambusso letter, which is related to a main steam line break in the East Penetration Room, OS-73.2 Supplement 1, dated June 22, 1973, stated that Duke will increase the inservice inspection to include the metal to surface inspection of the postulated break area every 5 years to detect any surface defects. The licensee also provided drawings (OS-73.2 Supplement 1, Figure 2.1-1.b) showing the postulated break area in the East Penetration Room.

In August 2005 the inspectors asked for the latest inspection results for the main steam lines. The inspectors were informed that the main steam line terminal end break area was inaccessible and could not be inspected. The licensee had not informed the NRC that the terminal end break area provided on Figure 2.1-1.b was in error and that inspection of the main steam line piping in the East Penetration Rooms was not being performed. This issue was captured in PIP O-05-06354, which reflected the licensees intention to ask NRR for an exemption from the inspection requirements.

Analysis:

The finding was considered to be a performance deficiency in that the licensee had committed to perform inspections of the steam lines to support the acceptability of Dukes design and analysis for the main steam lines, but the inspections were not being performed. The finding was considered to be more than minor because it impacted the Reactor Safety Initiating Events Cornerstone in that failure to perform the inspections could lead to failure to identify degrading main steam line conditions, which would cause an increase in the likelihood of an initiating event. The finding was screened as being of very low safety significance (Green) under the Initiating Events Cornerstone, in that the finding did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available. This finding involved the cross-cutting aspect of Problem Identification and Resolution (PI&R).

Enforcement:

10 CFR 50 Appendix B, Criterion X, Inspection, requires that a program for inspection of activities affecting quality shall be established and executed to verify conformance with the instructions and procedures. Contrary to the above, the licensee failed to establish and execute the inspection program for inspection of the main steam lines committed to as part of their response to the 1972 Giambusso letter. Because the failure to perform the inspections was considered to be of very low safety significance and has been entered into the licensees corrective action program (PIP O-05-06354),this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000269,270,287/2005004-05: Failure to Implement an Inspection Program for the Main Steam Lines.

==1R23 Temporary Modifications

a. Inspection Scope

==

While performing plant status inspection activities, the inspectors reviewed the activities associated with the improper enclosure of the Unit 3 Train B low pressure injection (LPI)/reactor building spray (RBS) pump room (Room 81), described in the licensees corrective action program as PIP O-05-5564.

b. Findings

Introduction:

An URI was identified regarding the improper blocking of the ventilation paths into and out of Unit 3 Auxiliary Building Room 81 (Train B LPI/RBS pump room).

The natural circulation ventilation pathways (circular stairs) are required for heat removal from the room during the recirculation phase following a loss of coolant accident (LOCA)to ensure the LPI and RBS pump and motor bearings do not exceed maximum operating temperatures. The issue will be documented as an Unresolved Item pending completion of a Phase 3 analysis.

Description:

On August 30, 2005, the licensee generated PIP O-05-5564, which documents that a tent enclosure had been inappropriately installed in the Unit 3 portion of the Auxiliary Building and was blocking airflow from the stairway access into LPI/RBS pump room 81. The enclosure had been installed on about August 9, 2005, to allow for lead removal work in the room. The airflow pathway is credited in Oconee design calculation OSC-6667 for air movement and heat removal during design basis accidents (LOCA recirculation phase). OSC-6667 provides the various maximum room temperatures following an accident. Previous testing by the licensee found that relatively small increases in room temperature (<20 degrees F) above those calculated in OSC-6667, could render the LPI and RBS pumps inoperable. Consequently, since the air flow pathway credited in calculation OSC-6667 did not exist with the tent enclosure installed, the Unit 3 B train LPI and RBS pumps could not be considered operable during this period.

Analysis:

The finding was considered to be a performance deficiency because the licensee failed to maintain the plant design in accordance with their design calculation OSC-6667 for design basis accidents, in that the assumed airflow pathway for heat removal was closed off. Since the LPI and RBS pumps cannot be considered operable in this condition, this finding was considered to be more than minor because it would impact the Reactor Safety Mitigating System Cornerstone for ensuring the availability, reliability and capability of a system that responds to initiating events to prevent undesirable consequences. A Phase 1 evaluation concluded that under the Mitigating Systems Cornerstone, the finding represented an actual loss of safety function of a single train for greater than its TS allowed time; therefore, a Phase 2 evaluation was required. The Phase 2 evaluation (dominated by small break loss of coolant accident)indicated that the issue was greater than Green and that a Phase 3 evaluation would be necessary. This finding involved the cross-cutting aspect of human performance.

Enforcement:

10 CFR 50, Appendix B, Criterion III, Design Control, requires in part that design changes, including field changes, are approved by the organization that performed the original design. Contrary to the above, a design change was made to the airflow pathway credited in design calculation OSC-6667 prior to obtaining approval from the licensees design organization. This issue was placed in the licensees corrective action program as PIP O-05-5564. Pending determination of the risk significance, this issue will be identified as URI 05000287/2005004-06, Inadequate Design Control of Unit 3 LPI/RBS Room Ventilation Pathways.

Cornerstone: Emergency Preparedness

1E6 Drill Evaluation

a. Inspection Scope

The inspectors observed and evaluated a simulator based emergency preparedness drill held on September 22, 2005. The drill scenario involved a security related event with postulated planted explosives. The scenario progressed to a general emergency after simulated damage to plant systems from various explosions. During the scenario, the operators were required to identify entry into an unusual event, alert and general emergency. The inspectors verified that the operators properly classified the event and made the appropriate notifications to the counties, state and NRC. The inspectors also verified that the protective action recommendations were issued in accordance with the licensees emergency procedures. The inspectors reviewed the post drill critique to verify that the licensee captured any drill deficiencies or weaknesses.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

.1 Daily Screening of Corrective Action Reports

As required by Inspection Procedure (IP) 71152, "Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed daily screening of items entered into the licensees corrective action program. This review was accomplished by reviewing copies of PIPs, attending daily screening meetings, and accessing the licensees computerized database.

.2 Semi-Annual Trend Review

a. Inspection Scope

As required by IP 71152, "Identification and Resolution of Problems," the inspectors performed a review of the licensees Corrective Action Program (CAP) and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues; but, also considered the results of daily inspectors CAP item screenings discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six month period of March 2005 through September 2005, although some examples expanded beyond those dates when the scope of the trend warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, plant health team vulnerability lists, focus area reports, system health reports, self-assessment reports, maintenance rule reports, and Safety Review Group monthly reports. The inspectors compared and contrasted their results with the results contained in the licensees latest quarterly trend reports. Corrective actions associated with a sample of the issues identified in the licensees trend report were reviewed for adequacy.

b.

Assessment and Observations No findings of significance were identified. In general, the licensee has identified trends and has appropriately addressed the trends in the CAP. Inspection Report 05000269,270,287/2005003 documented a trend with regard to the generation of 23 PIPs for dropped flags on relays associated with various plant equipment during the previous six months. Following further inspection, this trend has been closed, as the increased documentation associated with this trend was part of the licensees effort to investigate the cause of the dropped relay flags in conjunction with the relay manufacturer. Additionally, none of the specified relays have picked up, nor has there been any negative impact on plant equipment. The licensee and relay manufacturer continue to investigate this observation.

.3 Focused Review

a. Inspection Scope

The inspectors performed an in-depth review of an issue entered into the licensees corrective action program. The sample was within the mitigating systems cornerstone and involved risk significant systems. The inspectors reviewed the actions taken to determine if the licensee had adequately addressed the following attributes:

  • Evaluation and disposition of operability and reportability issues
  • Consideration of previous failures, extent of condition, generic or common cause implications
  • Prioritization and resolution of the issue commensurate with safety significance
  • Identification of the root cause and contributing causes of the problem
  • Identification and implementation of corrective actions commensurate with the safety significance of the issue.

The following issue and corrective actions was reviewed:

  • PIP O-05-4892, Unit 3, East to West Pen. Room Security/Fire Door Stuck shut

b. Findings

No findings of significance were identified.

.4 East Penetration Room Blowout Panel/HELB Issue

a. Inspection Scope

The inspectors performed a Problem Identification and Resolution (IP 71152) inspection for the implementation of the East Penetration Room blowout panel corrective actions related to NCV 05000269,270,287/2002004-02, Unauthorized Design Changes to the East Penetration Room Blowout Panels.

b. Findings

Introduction:

The inspectors identified an URI for untimely corrective actions in resolving the East Penetration Room blowout panel issue. The blowout panels had been improperly modified, causing the plant to be outside the Oconee licensing basis for pressure relieving capacity for the panels and for flood mitigation panels not being assured of proper operation. This issue was previously documented as URI 05000269, 270,287/2000008-04 and NCV 05000269,270,287/2002004-02. As of September 30, 2005, the blowout panels had not been repaired to ensure flood mitigation, nor had a license amendment been requested to correct the design pressure blowout capacity.

This lack of corrective action was considered to be unresolved, pending completion of a Phase 3 analysis.

Description:

In the fall of 1999, the inspectors noted that the blowout panels listed in the HELB licensing basis document OSC -73.2 (response to Giambusso Letter) had been epoxied and bolted in place. These panels were originally designed to limit the East Penetration Room pressurization following a main feed water or main steam line break or crack. In addition, the lower blowout panels were originally designed to allow water from the break or crack to leave the room and prevent flooding of safety-related equipment. As noted above, an URI was initiated in 2000 and an NCV was issued in 2002.

Subsequent to the NCV documented in 2002, the licensee determined that the blowout panels would not perform their design function to prevent flooding in the East Penetration Room. This condition is outside the licensing basis as specified in design document OSC-73.2. The licensee stated that modifications are necessary to prevent flooding of the auxiliary building because the East Penetration Room doors and block walls would likely fail during a HELB and the blowout panels are not assured of opening.

The proposed modifications include installation of a knee wall to prevent flooding and installation of new blowout panels.

As of September 30, 2005, the licensee has not developed a modification or a schedule for bringing the three units back into compliance with the licensing basis. The guidance in GL 91-18, Attachment 1, Section 4.3, Current Licensing Basis and 10 CFR 50, Appendix B, states that, If the licensee does not resolve the degraded or nonconforming condition at the first available opportunity or does not appropriately justify a longer completion schedule, the staff would conclude that corrective action has not been timely and would consider taking enforcement action. This non-conforming condition was identified in 1999, but to date the licensee has not taken adequate and timely corrective action.

Analysis:

The finding was considered to be a performance deficiency in that the licensee failed to implement timely corrective actions to repair the previously unauthorized modification of the East Penetration Room blowout panels. Since postulated flooding following a feedwater HELB would impact the HPI and emergency feedwater (EFW)functions, this finding was considered to be more than minor because it would impact the Reactor Safety Mitigating System Cornerstone for ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The Phase 1 evaluation was performed and it was concluded that under the Mitigating Systems Cornerstone that the finding represented an actual loss of a safety function of the HPI system, which required a Phase 2 evaluation. The Phase 2 evaluation (dominated by main steam line break) indicated that the issue was greater than Green and that a Phase 3 evaluation would be required. The previous Phase 3 analysis performed for NCV 05000269,270,287/ 2002004-02 found that the risk significance was Green. However, since that analysis, new information has been identified that may impact the significance of the issue. Therefore, a new Phase 3 analysis is necessary. This finding involved the cross-cutting aspect of Problem Identification and Resolution (PI&R).

Enforcement:

10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, requires in part that measures be established to assure that conditions adverse to quality, such as deficiencies, deviations, and non-conformances are promptly identified and corrected.

Contrary to the above, Units 1, 2, and 3 have continued to be operated outside their licensing basis for meeting HELB criteria because the East Penetration Room blowout panels are not assured of opening to prevent auxiliary building flooding. In addition, the panels do not meet the design criteria for blowout capacity and corrective actions have not been taken in a timely manner to resolve the deficiency. Pending determination of the risk significance, this issue is being identified as URI 05000269,270,287/2005004-07, Untimely Corrective Actions in Correcting the East Penetration Room Blowout Panel Deficiency.

.5 Failure to Report the East Penetration Room Blow Out Panel Deficiency per

10 CFR 50.73

a. Inspection Scope

The inspectors reviewed the licensees operability evaluation and reportability evaluation related to improper modifications of the East Penetration Room blowout panels.

b. Findings

Introduction:

An URI was identified regarding the failure to report a condition that could have prevented fulfillment of a safety function of a system as required by 10 CFR 50.73.

The reportable condition was the improper modification of the East Penetration Room blow out panels which in their present condition would prevent the release of water following a feedwater HELB. Since the panels would not release the water outside the auxiliary building, leakage out of the room would eventually lead to flooding of the HPI pumps and this would prevent fulfillment of a safety function of a system (HPI) needed to place the plant in a cold shutdown condition. This issue is considered to be unresolved, pending determination of safety significance.

Description:

In the late 1980's / early 1990's, the East Penetration Room blowout panels were coated with a metal shield elastomeric flasing compound followed by a polyester reinforcing fabric and then another coating of the metal shield elastomeric flasing compound. There is no information available on the physical strength or adhesion of the compounds. In addition, bolts and screws were installed on the outside of the panels to secure the panels in place. These undocumented modifications were implemented in order for the licensee to meet penetration room ventilation requirements for being able to draw a vacuum in the room. These modifications increased the panel blowout strength to values in excess of 144 pounds per square foot, although the licensing basis strength is limited to less than 63 pounds per square foot. Based on subsequent calculations, the licensee determined that the floor level blow out panels, that were designed to limit flooding in the auxiliary building, would not blow out under all conditions and flooding of the auxiliary building would occur.

In June 2004, the licensee made a presentation to Region II management. The presentation noted that the panels could not be assured of blowing out and plant modifications were needed to ensure flooding of the auxiliary building would not take place. This condition appeared to be reportable, so the licensee was asked to review the condition for reportability.

The licensee concluded that although there may be from 44,000 to 64,000 gallons of water available to flood the auxiliary building equipment, the floor drains would equalize the inventory between the Unit 1 and 2 HPI pump room and the Unit 3 HPI pump room, and none of the HPI pumps would be affected. In addition, the licensee assumed that the SSF makeup pump would be unaffected and would be able to stabilize the plant in hot standby. Based on these conditions, the licensee concluded that there would be no loss of safety function.

However, the inspectors found problems with the licensees analysis.

  • Following a HELB, the plants licensing basis requires the licensee to go to cold shutdown. The SSF makeup pump cannot perform this function and is also not in the licensing basis to mitigate a HELB. Therefore, the HPI pumps are the only pumps that can be credited to provide the safety function to mitigate this accident and they must remain functional.
  • The licensee inappropriately assumed that the HELB flood inventory would equalize between the Unit 1, 2, and Unit 3 HPI pump rooms. However, the inspectors noted that flooding of the HPI pump rooms is not limited by the floor drains as assumed in the licensees operability evaluation. The inspectors identified that each HPI pump room has a pipe chase that will direct flow into the room closest to the break. Therefore, the inspectors concluded that the available postulated flood inventory would cause flooding of the unit specific HPI pumps and render them inoperable.
  • The licensee concluded that inventory from a postulated HELB crack would be 50,000 gallons and less than 20,000 gallons from a full break. This was based on operator action for the crack at 10 minutes and automatic feedwater isolation system (AFIS) actuation for a full break (<2 minutes). The inspectors noted that the licensee did not assume breaks sized between a crack and a full break, which would also not be isolated by an AFIS signal. The inspectors noted in the licensing basis (Giambusso letter) that the licensee is required to mitigate the effects from the worst case break, which in this case would be a break greater than a crack (5,000 gpm for 10 minutes), but less than a full break (13,000 gpm assumed to be isolated by AFIS in about 2 minutes). Based on this finding, the inspectors noted that the flood inventory would be much greater than analyzed by the licensee and would increase the probability of flooding in the HPI pump rooms
  • The licensee assumed that AFIS would isolate a full break in less than 2 minutes. Because main steam headers are tied together, the inspectors noted that AFIS could not actuate on low steam pressure to isolate feedwater until there was a turbine trip. A turbine trip would require a reactor trip. Oconee does not have a SG low level trip. Therefore, discussions with the licensee indicated that the reactor trip needs to be initiated from a loss of feed water pumps. The only applicable feed water pump trip would be initiated on loss of suction pressure for >90 seconds. The inspectors noted that on a feedwater line break, feedwater flow would increase; thereby creating low feed pump suction pressures. The integrated control system would attempt to recover the proper feedwater flow by reducing the feedwater regulating valve position at a rate of 20 percent per minute or 30 percent over the first 90 seconds. The inspectors noted that with the feed water regulating valves at a position equivalent to 70 percent flow, feed water pump suction pressure would likely increase enough such that the low suction pressure trips would not occur. At lower volume breaks, feedwater pump trips are even less likely. Based on this discussion, the inspectors concluded that an AFIS isolation of the break is questionable and operator action at the licensing basis time of 10 minutes should be used for any flooding analysis.

Based on the above, the inspectors concluded that the licensees operability evaluation was inadequate and that a single active failure (as postulated in the licensees reportability analysis) was not required to cause a loss of the HPI pumps due to flooding. Therefore, the adverse condition of the blow out panels creating a situation where the HPI pumps (which are needed to mitigate a HELB) would be lost, was considered to be reportable per 10 CFR 50.73. The issue was discussed with the licensee. However, the licensee concluded that their evaluation was satisfactory.

Analysis:

The issue was considered to be a performance deficiency in that the licensee failed to report a condition that could have prevented fulfillment of a safety function as required by 10 CFR 50.73. The failure to report has the potential to impact the NRCs ability to perform its regulatory function. Therefore, this issue will be processed using traditional enforcement as specified in the Enforcement Policy IV.A.3. Determination of the safety significance by the Region II Senior Reactor Analyst will be necessary to determine the severity level of the violation.

Enforcement:

10 CFR 50.73, Part (v), requires the reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to (A) shutdown the reactor and maintain it in a safe shutdown condition (licensing basis is cold shutdown) and (D) mitigate the consequences of an accident Contrary to the above, the licensee failed to report that improper modifications to the East Penetration Room blowout panels would prevent the fulfillment of the safety function of the HPI system to mitigate the consequences of a HELB accident (i.e., to shutdown the reactor and maintain it in a cold shutdown condition). Pending determination of the risk significance, this issue is being identified as URI 05000269,270,287/2005004-08, Failure to Meet the Reportability Requirements of 10 CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency.

.6 Untimely Corrective Actions for Unit 2 East Penetration Room Floor Seal Deficiency

a. Inspection Scope

While performing routine plant tours to identify any adverse plant conditions, the inspectors followed up on a previously noted damaged floor seal in the Unit 2 East Penetration Room.

b. Findings

Introduction:

The inspectors identified a Green NCV of 10 CFR 50 Appendix B, Section XVI, Corrective Action for inadequate corrective actions related to the lack of timeliness of repairs to a Unit 2 East Penetration Room floor seal. The inspectors concluded that the damaged floor seal, if left uncorrected could lead to flooding of safety-related equipment following a high energy line break in the Unit 2 East Penetration Room.

Description:

On July 14, 2004, the licensee wrote a deficiency tag and work request on a partially extruded floor seal in the Unit 2 East Penetration Room. The affected floor seal fills a gap approximately 4 inches by six feet between two sections of reinforced concrete flooring in the room. The deficiency tag on the damaged seal was over a year old yet repairs had not been initiated. Further review found that the degraded condition had not been placed into the PIP process.

Analysis:

The failure to promptly repair the damaged floor seal was considered to be a performance deficiency. The finding was considered to be more than minor because if left uncorrected, additional seal area could fail and it would affect the Mitigating System Cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events, in that the HPI pumps could be flooded following a HELB in the East Penetration Room. However, in the seals current level of degradation, the inspectors concluded that the deficiency would not by itself result in the loss of function of the HPI pumps, because flooding would be limited by the size of the degraded/failed seal. Consequently, the finding was determined to be of very low safety significance (Green), as it was screened out under the Mitigating Systems Cornerstone in the SDP Phase 1 Screening Worksheet with the determination that there was no loss of safety function. This finding involved the cross-cutting aspect of Problem Identification and Resolution.

Enforcement:

10 CFR 50 Appendix B, Section XVI, Corrective Action, requires Contrary to the above, the licensee failed to correct a partially extruded Unit 2 East Penetration Room floor seal that if left uncorrected, could degrade to the point that safety related equipment could be affected following a HELB. Because this issue was of very low safety significance and has been entered into the licensees Corrective Action Program as PIP O-05-6097, this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000270/

2005004-09, Untimely Corrective Actions for Repairs to a Unit 2 East Penetration Room Floor Seal.

.7 Failure to Maintain Containment Electrical Penetration Enclosures

a. Inspection Scope

While performing routine plant tours to identify adverse plant conditions, the inspectors followed up on the observation that the containment electrical penetrations were degraded, in that cover plates were either missing or attached improperly.

b. Findings

Introduction:

The inspectors identified an URI for failure to identify a condition adverse to quality in that East and West Penetration Room containment electrical penetrations enclosures had not been maintained as spray proof enclosures. Because these electrical enclosures have not been maintained, grounding and shorting of these circuits located in the East and West Penetration Rooms could lead to significant losses of safety-related electrical systems, controls and indications following a HELB. The issue will be documented as an URI pending further inspection.

Description:

In June 2005, the inspectors identified that covers for a significant number of electrical penetrations were missing or improperly attached. These included specific penetrations which contained electrical circuits needed to mitigate the consequences of a high energy line break in the East Penetration Room and place the plant in a cold shutdown condition. Discussions with NRR concluded that the Oconee licensing basis requires the plant to be able to reach cold shutdown following a HELB while assuming one active failure. During discussions with the licensee, the licensee stated that the covers were not necessary to maintain the environmental qualification of the unprotected electrical circuits, and therefore, the as found degraded penetrations were acceptable to meet their safety function without the covers. Discussions with NRR concluded that the electrical penetrations would not meet their as tested environmental qualification if they could be impacted by direct or indirect spray and/or became dirty or rusted.

The inspectors noted that roughly 70 penetrations in the East Penetration Rooms had some sort of closure problem, and likely an equal number of problems in the West Penetration Rooms. The licensee initiated PIP O-05-4491 on July 9, 2005. The licensee also initiated repairs to the open penetration enclosures, which had still not been completed by the end of the inspection period.

The licensee performed an operability assessment and concluded that The cables entering the electrical penetration assembly junction boxes do not require environmental sealing, and all the electrical penetrations are outside the zone of influence for the two HELB scenarios under consideration in the penetration rooms. The inspectors questioned why piping cracks would be outside the zone of influence and the engineers stated that the licensing basis for breaks or cracks did not include spray impingement, and therefore, did not have to be considered. Discussions with NRR concluded that the licensing basis for Oconee required not only spray, but direct jet impingement from postulated breaks. The breaks to be considered were cracks along the entire length of feedwater and steam line piping. The inspectors concluded that a postulated 13,000 gpm leak from a feedwater line break or 6,600 gpm leak from a feedwater line crack would affect the open penetrations and that the penetrations were required to be protected from the effects (i.e., direct or indirect spray) from a crack or break.

The inspectors observed debris and dust on the electrical terminal blocks inside the electrical penetration panels, rust on the terminal blocks and inside other components in the electrical penetration panels, and debris on top of the electrical penetration panels that would likely be washed into the panel during a postulated HELB. The inspectors also noted that with the covers missing/improperly installed, the terminal blocks could be sprayed down during a HELB. Based on an e-mail from NRR, Electrical Engineering Section, dated July 27, 2005, NRR concluded that terminal blocks are qualified for a harsh environment when not subjected to direct spray; where direct spray is anticipated, the terminal blocks are installed in enclosures. Oconees commercial dedication for the safety-related terminal blocks required the terminal blocks to be installed in NEMA 4 enclosures (i.e., spray protected). NRR went on to state that cleanliness of the terminal blocks is required because accumulation of dirt and rust introduces a conductive path for current that could distort the signals from instrumentation circuits. Since the electrical penetration panels were not maintained, it was concluded by the inspectors that the original environmental qualification no longer encompassed the as found condition.

The inspectors concluded that multiple grounds and shorts would cause erratic actuation of alarm circuits and potentially cause unwarranted actuation/operation of emergency core cooling system and other plant equipment. These conditions would further hinder the ability of the operations staff to mitigate the HELB. The inspectors also concluded that the low voltage electrical systems were not designed to operate with multiple grounds and shorts and the likely affect would be to cause distortion of the instrumentation signals even on circuits that were not directly impacted by the HELB.

The inspectors noted that in the original licensing basis requirements, contained in the 1972 Giambusso letter, the licensee was required to verify that the rupture of a pipe carrying high energy fluid will not directly or indirectly result in loss of redundancy in any portion of the protection system, class 1E electrical system, engineered safety feature equipment, cable penetrations, or their interconnecting cables required to mitigate the consequences of the break and place the plant in cold shutdown. The licensee did not take exception to this requirement. The inspectors noted that many of the electrical penetrations needed to place the plant in hot standby were not being maintained. The inspectors concluded that the licensee was presently operating outside their licensing basis because a HELB in the East Penetration Rooms could cause a loss of redundancy of the circuitry needed to place the plant in hot standby. The listing of which penetrations would be needed to place the plant in cold shutdown are not known at this time because the licensee contends that they only have to ensure ability to go to hot standby and therefore do not have to meet the requirement for loss of redundancy in placing the plant in cold shutdown.

Analysis:

The finding was considered to be a performance deficiency in that the licensee failed to maintain the containment electrical penetration covers as NEMA 4 enclosures.

This finding was considered to be more than minor because direct and/or indirect spray from a HELB could affect multiple electrical circuits; thereby, increasing the likelihood of a reactor trip and that mitigation equipment would not be available. This would impact the Initiating Events Cornerstone objective to limit the likely hood of those events that upset plant stability, as well as the Mitigating Systems Cornerstone objective for ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

For the Phase 1 review, the inspectors concluded that the HELB could affect the unprotected reactor protection circuits and cause a reactor trip and affect circuits such as pressurizer level and steam generator pressure, which are used to mitigate the consequences of a HELB. Therefore, based on the Initiating Events Cornerstone for transient initiators, the inspectors concluded that the finding contributed to both the likelihood of a reactor trip and that mitigation equipment would not be available. These conditions required that a Phase 2 evaluation be performed.

Because the instrumentation circuits in the control room could be erratic due to the grounds and shorts resulting in degradation of the vital 120 vac and 120 vdc systems, and the inability to perform the various mitigation procedures due to erratic indications, it was assumed for the Phase 2 analysis that mitigation systems controlled from the control room were lost. Further inspection activities are being planned to support the analysis. This finding involved the cross-cutting aspect of Problem Identification and Resolution (PI&R).

Enforcement:

10 CFR 50 Appendix B, Criterion XVI, Corrective Action, requires that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected. Contrary to the above, the license failed to identify and correct penetration covers that had been removed or misadjusted over a number of years of maintenance activities, which created conditions adverse to quality where dust, dirt, rust, and spray could impact circuits needed to mitigate the consequences of a HELB and cause erratic operation of the 120 vac and 120 vdc vital electrical systems. Pending further inspection and analysis, this issue is being identified as an Unresolved Item, URI 05000269,270,287/2005004-10, Failure to Maintain Containment Electrical Penetration s.

.8 Failure to Properly Identify Main Feedwater Line Terminal Ends

a. Inspection Scope

The inspectors performed a Problem Identification and Resolution inspection for the main feedwater system piping and supports located in the East Penetration Rooms. This inspection was chosen as part of the annual sample required by IP 71152. This issue is unresolved pending determination of risk determination.

b. Findings

Introduction:

An URI was identified regarding the failure to identify a condition adverse to quality, in that feedwater terminal ends had not been identified and therefore actions to mitigate the affects from a terminal end line break had not been implemented.

Description:

The Oconee licensing basis for high energy line breaks is contained in the 1972 Giambusso letter, which implemented GDC-4, and contained in the licensees response to the Giambusso letter which is documented in Oconee MDS report No. OS-73.2, Analysis of Effects Resulting from Postulated Piping Breaks Outside Containment.

The 1972 Giambusso Letter required the licensees to postulate breaks on ASME Class 1, 2 and 3 piping at the terminal ends. It required that The plant should be designed so that the reactor can be shutdown and maintained in a safe shutdown condition in the event of a postulated rupture outside containment of a pipe containing a high energy fluid, including the double ended rupture of the largest piping in the main steam and feedwater systems. Plant structures, systems and components important to safety should be designed and located in the facility to accommodate the effects of such a postulated pipe failure to the extent necessary to assure that a safe shutdown condition of the reactor can be accomplished and maintained.

An attachment to the letter defined terminal ends as extremities of piping that connect to structures, components or pipe anchors that act as rigid constraints to piping motion and thermal expansion. Rigid restraints that are welded to piping systems are considered to be terminal ends. The feedwater lines are restrained at the containment penetration by using a collar that is welded to the feedwater pipe with a structural anchor that is welded to the collar and attached to the containment structure. Since the collar weld acts as a rigid constraint to piping motion and thermal expansion, each welded location is considered to be a feedwater terminal end. However, the licensee only assumed a break upstream of the collar. The feedwater line has a whip restraint at this location to protect equipment in the East Penetration Room from the affects of this break. Since the licensee did not assume a break downstream of the collar, there is no equipment protection from a break at that location.

A feedwater line break downstream of the collar would result in a non-postulated/

unprotected feedwater line break in the East Penetration Room. The East Penetration Rooms are not designed for an unprotected feedwater line break and would be over pressurized. In addition, jet impingement and spray from the break would affect the electrical penetrations and other piping systems in the area of the break.

Discussions were held with the licensee concerning this issue. The licensee concluded that it is acceptable to assume that the terminal end line break can be taken at a location of the feedwater piping in the middle of the collar. This position was discussed with an NRR expert, but the licensees position was not supported because the postulated terminal end break is required to be taken at the point of restriction. The inspectors concluded that the area in the middle of the collar could actually be an area with the lowest stress and likely would not see the full affects of thermal expansion and applied stress.

Analysis:

The finding is considered to be a performance deficiency in that although it is a design deficiency, the licensee failed to identify the problem during the six years of HELB design reconstitution. An unprotected terminal end line break would cause overpressurization of the East Penetration Room, loss of circuitry needed to mitigate a HELB, flooding of the HPI pump rooms, and structural damage to the East Penetration Rooms. Structural damage, jet impingement, and spray would damage systems such as building spray, letdown, low pressure service water, low pressure injection, emergency feedwater, instrument air, etc, since for many of these systems both trains are routed through the East Penetration Rooms. Damage to these systems would impact the ability to reach cold shutdown conditions. This performance deficiency was considered to be more than minor because an unprotected terminal end line break would impact the Reactor Safety Mitigating Systems Cornerstone objective for ensuring the availability, reliability and function of systems needed to respond to a HELB. For the Phase 1 review, the inspectors concluded that an unprotected terminal end line break would result in a loss of safety function of the Auxiliary Building, the multiple mitigation safety systems listed above, and containment cooling and containment integrity from unrestrained feedwater piping thrust. This would therefore impact mitigation and containment integrity. Based on this, a Phase 2 evaluation was required. The Phase 2 sequence for main steam line break was used because the postulated break is between the feedwater check valve and the steam generator. A break at this location would be similar to a steam line break. Based on the assumptions that the Auxiliary Building would be damaged, electrical indication and control circuits would be damaged and systems located in the East Penetration Room would be damaged, the Phase 2 sheet for main steam line break indicated that the issue could be greater than Green and that a Phase 3 analysis would be required. This finding involved the cross-cutting aspect of Problem Identification and Resolution.

Enforcement:

10 CFR 50 Appendix B, Criterion XVI, Corrective Action, requires that measures shall be established to assure that conditions adverse to quality are promptly identified. Contrary to the above, the licensee failed to identify that unprotected feedwater line terminal ends existed that could impact the mitigation systems needed to protect the plant from a HELB. Pending determination of the risk significance, this issue is being identified as URI 05000269,270,287/2005004-11, Failure to Identify Unmitigated/Unprotected Feedwater Line Terminal Ends.

.9 Summary of PI&R Cross-Cutting Findings

A Green NCV involving the cross-cutting aspect of PI&R is documented in Section

1R22.2. The licensee failed to develop and implement a program for the inspection and

cleaning of the containment electrical penetrations located in each units East and West Penetration Rooms, delaying the possible identification of conditions adverse to quality.

A second Green NCV involving the cross-cutting aspect of human performance is documented in Section 1R22.3. Licensee personnel failed to develop and implement a program for the inspection of the main steam lines located in each units East Penetration Rooms, delaying the possible identification of conditions adverse to quality.

A third Green NCV involving the cross-cutting aspect of PI&R is documented in Section 4OA2.6. The licensee failed to place a deficiency observed in the Unit 2 East Penetration Room floor into the corrective action program, delaying the identification of a condition adverse to quality, as well as, its resolution.

A URI involving the cross-cutting aspect of PI&R is documented in Section 4OA2.4. The licensee failed to take prompt and adequate corrective action for a deficient condition within each units East Penetration Rooms, that was identified in the Fall of 1999, resulting in all three Oconee Units operating outside their licensing basis since the units East Penetration Room blowout panels were improperly modified and have not been repaired.

A second URI involving the cross-cutting aspect of PI&R is documented in Section 4OA2.7. The licensee failed to identify a condition adverse to quality, in that, improperly maintained electrical penetration enclosures located within each units East and West Penetration Rooms had not be identified and placed into the licensees corrective action program; thereby, delaying resolution of this deficient condition.

A third URI involving the cross-cutting aspect of PI&R is documented in Section 4OA2.8.

The licensee failed to identify a condition adverse to quality, in that, the feedwater piping terminal ends located within each units East Penetration Room have not been properly identified.

4OA3 Event Followup

.1 Recent Events

a. Inspection Scope

The inspectors evaluated one licensee event and two degraded conditions for plant status and mitigating actions in order to provide input in determining the need for an Incident Investigation Team (IIT), Augmented Inspection Team (AIT), or Special Inspection (SI). As appropriate, the inspectors:

(1) observed plant parameters and status, including mitigating systems/trains and fission product barriers;
(2) determined alarms/conditions preceding or indicating the event;
(3) evaluated performance of mitigating systems and licensee actions;
(4) confirmed that the licensee properly classified the event in accordance with emergency action level procedures and made timely notifications to NRC and state/county governments, as required (10 CFR Parts 20, 50.9, 50.72);
(5) communicated details regarding the event to management, risk analysts and others in the Region and Headquarters as input to their determining the need for an IIT, AIT, or SI.
  • PIP O-05-5118, KHU-2 Emergency Lockout While Attempting to Generate to the Grid
  • PIP O-05-5365, KHU-2 Emergency Lockout While Performing PT/0/A/0620/016, Keowee Hydro Emergency Start Test

b. Findings

Except as identified in SI Inspection Report 05000287/2005010, no findings of significance were identified.

.2 (Closed) LER 05000269/2005-01-00, Exceeded TS: Emergency Power Path Aux Power

Source Inoperable The inspectors reviewed the circumstances surrounding the KHU overhead power path exceeding the TS allowed outage times due to a failed contactor for the overhead main step-up transformer cooling system normal power supply. The licensee also categorized this event as an unanalyzed condition due to a potential single failure vulnerability affecting both emergency power paths. This deficiency, its associated risk significance, and the licensees corrective actions were documented in Inspection Report 05000269,270,287/2005003 as a Green NCV of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action. This LER is closed.

.3 (Closed) LER 269/2004-04-01, Improper Overloads Installed on Control Room

Ventilation Filter Train

a. Inspection Scope

The inspectors reviewed the licensees TS LCO action statement entry, causal evaluation, corrective actions and operability assessment surrounding the unexpected tripping of the Unit 1 and 2, B Train, Control Room Outside Air Booster Fan (CROABF).

b. Findings

Introduction:

A Green self-revealing NCV of 10 CFR 50 Appendix B, Criterion X, Inspection, was identified for an inadequate quality control (QC) inspection associated with the incorrect installation of the Unit 1 and 2 CROABF, B Train, motor thermal overload relays.

Description:

On November 17, 2004, the filters of the B Train, outside air portion of the Unit 1 and 2 Control Room Ventilation System were replaced, and the associated booster fans motor bearings were lubricated as part of a preventive maintenance task.

During the subsequent post-maintenance testing, the fan tripped unexpectedly after 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> of operation. As documented in PIP O-04-7937, a licensee investigation determined that the apparent cause of the tripping of the B CROABF was the use of undersized heater overloads (S4.0) on the fans motor. The fans overloads were replaced with larger S4.4 heater overloads, and a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> post-maintenance test was conducted satisfactorily. The inadequate design controls associated with this issue were previously documented as NCV 05000269/2005002-02, Improper Thermal Overloads Installed in the Unit 1 and 2, B Train, CROABF.

At 3 p.m. on April 10, 2005, the B CROABF was found tripped. Troubleshooting efforts revealed that the B CROABF center phase overload relay had tripped. The licensees root cause evaluation concluded that the cause of the fan tripping was the off-center installation of S4.4 heater element within the thermal overload relay. This heater element was previously replaced as part of the recovery from the November 17, 2004, trip of the B CROABF. The replacement heaters were installed per IP/0/A/3011/015, Removal and Replacement of Motor Control Center, Panelboards and Remote Starter Components, which required the installer and QC inspectors to verify that the overload heaters were properly centered; however, the as-found heater position was off-center.

As determined by subsequent testing, an off-center heater element will cause the overload relay to trip at a lower current than a relay with the heater element properly centered. The licensee replaced the S4.4 overload relay heater elements on the A and B CROABFs with S37.5 heater overloads, which are rated at 25 amps. The A and B CROABFs were then operated satisfactorily for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Analysis:

The finding was considered to be a performance deficiency because the licensee failed to conduct an adequate QC inspection of the installation of the S4.4 overload relay heater elements on the safety-related B CROABF. The licensees failure to correctly install the thermal overloads on the Unit 1 and 2, B Train, CROABF was considered to be more than minor because it affected the Barrier Integrity Cornerstone attribute of maintaining control room habitability. The inspectors reviewed this finding in accordance with IMC 0609, Significance Determination Process. Similar to NCV 05000269/2005002-02, this finding represented a similar degradation of the barrier function of the control room against smoke and/or a toxic atmosphere; thereby, requiring a Phase 3 evaluation be performed. However, since the exposure time associated with this CROABF finding is shorter than that used in the Phase 3 evaluation of NCV 05000269/2005002-02, it too is considered to be of very low safety significance (Green).

This finding involved the cross-cutting aspect of human performance.

Enforcement:

10 CFR 50 Appendix B, Criterion X, Inspection, requires, in part, that inspection of activities affecting quality be executed in conformance with the documented instructions, procedures, and drawings. IP/0/A/3011/015 required that the overload heaters be installed correctly, centered, and inspected by QC. Contrary to the above, the licensee failed to perform adequate QC inspections of the Unit 1 and 2, B Train, CROABF, in that, the center phase thermal overload was not properly centered within the relay housing, resulting in the center phase overload tripping prematurely at a lower current than the fans operating motor current. Because this issue was of very low safety significance and was placed in the licensees corrective action program as PIP O-05-2361, this violation is being treated as an NCV in accordance with Section VI.A.1 of the Enforcement Policy: NCV 05000269,270/2005004-12, Inadequate QC Inspection Results in the Improper Installation of Thermal Overloads on the Unit 1 and 2 B Train, CROABF.

4OA4 Summary of Human Performance Cross-Cutting Findings

A Green Finding involving the cross-cutting aspect of human performance is documented in Section 1R13. Licensee personnel failed to fully understand the scope of maintenance on a Unit 3 secondary system makeup valve, resulting in an inadequate maintenance tagout. This nearly resulted in a Unit 3 trip with a loss of normal heat sink.

A Green NCV involving the cross-cutting aspect of human performance is documented in Section 4OA3.3. A licensee QC inspectors failed to properly inspect the installation of a heater element within the thermal overload relay for the Unit 1 and 2, B Train CROABF, resulting in the overload relay tripping at a reduced current.

A URI involving the cross-cutting aspect of human performance is documented in Section1R14. Licensee personnel failed to update procedural guidance for the control of the newly installed equipment, Unit 3, SSF-powered Pressurizer Heater Bank 2, Group C, resulting in the supply breaker, PXSF-4A, not being closed prior to entering Mode 3.

A second URI involving the cross-cutting aspect of human performance is documented in Section 1R23. Licensee personnel improperly blocked the ventilation paths into and out of Auxiliary Building Room 81 (Train B, LPI/RBS pump room). This ventilation path is required for heat removal from the room during the recirculation phase of a LOCA to ensure that the LPI and RBS pump and motor bearings do not exceed maximum operating temperatures.

4OA5 Other Activities

Operational Readiness of Offsite Power (Temporary Instruction (TI) 2515/163)

Completion of this TI was documented in Inspection Report 05000269,270,287/

2005003. However, after NRC headquarters review of the information provided, additional information related to the TI was requested. The inspectors collected this information from licensee discussions, site procedures, and other licensee documentation. The information was provided to the headquarters staff for further analysis.

4OA6 Management Meetings (Including Exit Meeting)

.1

Exit Meeting Summary

The inspectors presented the inspection results to Mr. Bruce Hamilton, Station Manager, and other members of licensee management at the conclusion of the inspection on October 4, 2005. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.

.2 Regulatory Performance Meeting Summary

On September 20, 2005, NRC Region II (RII) held an Oconee regulatory performance meeting with Duke Energy to discuss the results of a supplemental inspection (IR 05000269,270,287/2005010) conducted May 31 - June 2, 2005. That inspection assessed the licensees problem identification, root cause evaluation, extent of condition determination, and corrective actions associated with two White findings in the Mitigating Systems Cornerstone, which placed the performance of Oconee Units 1, 2 and 3 in the Degraded Cornerstone Column of the NRCs Action Matrix for the third quarter 2004. The two findings involved:

(1) pressurizer ambient heat losses in all three Oconee units exceeding the capacity of the pressurizer heaters powered from the SSF; and
(2) procedural criteria for manning the SSF during a fire in certain areas. The meeting focused on the corrective actions associated with these White findings, as well as with the supplemental inspection, in order to arrive at a shared understanding of the performance issues, underlying causes, and planned licensee actions.

This meeting was opened to the public. Attendees included: Oconee site management and staff (indicated on the Attachment to this report); NRC Region II management (indicated on Attachment to this report); and the resident inspectors. The presentation material used for the discussion is available from the NRCs document system (ADAMS)as Accession Number ML052650202. ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

L. Azzarello, Modification Engineering Manager
S. Batson, Superintendent of Operations
D. Baxter, Engineering Manager
R. Brown, Emergency Preparedness Manager
S. Capps, Mechanical/Civil Engineering Manager
N. Clarkson, Regulatory Compliance*
N. Constance, Operations Training Manager
C. Curry, Maintenance Manager
G. Davenport, Compliance Manager
C. Eflin, Requalification Supervisor
T. Gillespie, Reactor and Electrical Systems Manager
T. Grant, Engineering Supervisor, Reactor & Electrical Systems
R. Griffith, QA Manager
B. Hamilton, Station Manager*
D. Hubbard, Training Manager
R. Jones, Site Vice President*
T. King, Security Manager
L. Nicholson, Safety Assurance Manager*
B. Spear, Engineer, Reactor & Electrical Systems
J. Twiggs, Manager, Radiation Protection
J. Weast, Regulatory Compliance*

NRC

M. Ernstes, Chief of Reactor Projects Branch 1*
C. Casto, Director RII Division of Reactor Projects*
W. Travers, Regional Administrator, RII
  • Note: Personnel indicated with an asterisk attended the regulatory performance meeting on

September 20, 2005. (See section 4OA6.2 for further details.)

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000287/2005004-03
05000287/2005004-06
05000269,270,287/2005004-07
05000269,270,287/2005004-08
05000269,270,287/2005004-10
05000269,270,287/2005005-11 URI URI URI URI URI URI Failure to Maintain Design Control of the SSF Supply Power Breaker for Unit 3, Bank 2, Group C Pressurizer Heaters (Section 1R14)

Inadequate Design Control of Unit 3 LPI/RBS Room Ventilation Pathways (Section 1R23)

Untimely Corrective Actions in Correcting the East Penetration Room Blowout Panel Deficiency (Section 4OA2.4)

Failure to Meet the Reportability Requirements of 10 CFR 50.73 for the East Penetration Room Blow Out Panel Deficiency (Section 4OA2.5)

Failure to Maintain Containment Electrical Penetration Enclosures (Section 4OA2.7)

Failure to Identify Unmitigated/Unprotected Feedwater Line Terminal Ends (Section 4OA2.8)

Opened and Closed

05000269,270,287/2005004-01
05000287/2005004-02
05000269,270,287/2005004-04
05000269,270,287/2005004-05 NCV FIN NCV NCV Performing Licensed Duties While Medically Unqualified (Section 1R11.2)

Inadequate Maintenance and Oversight Increased the Likelihood of a Unit 3 Reactor Trip with a Loss of Normal Heat Sink (Section 1R13)

Failure to Develop and Implement a Cleanliness Inspection Program for the Containment Electrical Penetrations (Section 1R22.2)

Failure to Implement an Inspection Program for the Main Steam Lines (Section 1R22.3)

05000270/2005004-09
05000269,270/2005004-12 NCV NCV Untimely Corrective Actions for Repairs to a Unit 2 East Penetration Room Floor Seal (Section 4OA2.6)

Inadequate QC Inspection Results in the Improper Installation of Thermal Overloads on the Unit 1 and 2, B Train, CROABF (Section 4OA3.3)

Closed

05000269/2005-01-00
05000269/2004-04-01 LER LER Exceeded Tech Spec: Emergency Power Path Aux Power Source Inoperable (Section 4OA3.2)

Improper Overloads Installed on Control Room Ventilation Filter Train (Section 4OA3.3)

Items

Discussed

2515/163 TI Operational Readiness of Offsite Power (Section 4OA5)

DOCUMENTS REVIEWED