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Insp Repts 50-315/87-29 & 50-316/87-29 on 870929-1110. Violations Noted.Major Areas Inspected:Actions on Previously Identified Items,Plant Operations,Reactor Trips,Radiological Controls,Maint,Surveillance,Fire Protection & Cleanliness
ML17325A521
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 11/23/1987
From: Burgess B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17325A519 List:
References
50-315-87-29, 50-316-87-29, NUDOCS 8712110312
Download: ML17325A521 (27)


Text

U.S.

NUCLEAR REGULATORY COHHISSION

REGION III

Reports No. 50-315/87029(DRP);

50-316/87029(DRP)

Docket Nos. 50-315; 50-316 Licenses No. DPR-58; DPR-74 Licensee:

Indiana Hichigan Power Company 1 Riverside Plaza Columbus, OH 43216 Facility Name:

Donald C.

Cook Nuclear Power Plant, Units 1 and

Inspection At:

Donald C.

Cook Site, Bridgman, Hichigan Inspection Conducted:

September 29 through November 10, 1987 Inspectors:

Bruce L. Jorgensen James K. Heller Approved By:

Reactor rges

, Chief Proj cts Section 2A Date Ins ection Summar Ins ection on Se tember 29 throu h November

1987 (Re orts No. 50-315/87029(DRP)

No 50-316/87029(DRP))

Areas Ins ected:

Routine unannounced inspection by the resident inspectors of:

actions on previously identified items; plant operations; reactor trips; radiological controls; maintenance; surveillance; fire protection and cleanliness; security; Steam Generator Repair Project; and Information Notices and Generic Ietters.

Results:

Of the ll areas inspected, no violations or deviations were identified in ten areas.

One violation was identified (Level IV - failure to perform required reviews and approvals for substitute repair material - Paragraph 6.h)

in the remaining area.

8712110312 871204 PDR ADOCK 05000315

PDR

1.

Persons Contacted DETAILS W.

"A

'L AB T.

K.

AJ E.

T.

J J T.

L.

"M.

A.

D.

AJ Smith, Jr., Plant Manager Blind, Assistant Plant Manager - Administration Rutkowski, Assistant Plant Manager - Production Gibson, Assistant Plant Manager - Technical Support Svensson, Licensing Activity Coordinator Kriesel, Technical Superintendent

- Physical Sciences Baker, Operations Superintendent Sampson, Safety and Assessment Supervisor Morse, equality Control Superintendent Beilman, ISC/Planning Superintendent Droste, Maintenance Superintendent Postlewait, Technical Superintendent

- Engineering Matthias, Administrative Superintendent Horvath, (}uality Assurance Supervisor Tetzlaff, Performance Engineer Loope, Radiation Protection Supervisor Kauffman, Construction Manager The inspector also contacted a number of other licensee and contract employees and informally interviewed operations, maintenance, and technical personnel.

"Denotes some of the personnel attending Management Interview on November 10, 1987.

2.

Actions on Previousl Identified Items (Closed) Unresolved Item (315/86005-06):

the containment airlock door seal material needed to be changed, as the original seals were beyond the manufacturer's stated service life.

With seals of the original material no longer available, a design change (RFC-DC-2768)

was processed to install an acceptable substitute.

Action was completed on the last (Unit 1) airlock doors as of September 4,

1987.

b.

(Closed)

Open Item (315/86035-02; 316/86035-02): electrical shorting appeared coincident with hydro-lasing activities to decontaminate area surfaces.

Further review showed no circuits designed to be unaffected by water/steam had failed.

Improved controls of the activity were apparently effective in that no subsequent problems occurred despite widespread decontamination activities using both hydro-lasing and steam-cleaning techniques.

(Closed)

Open Item (315/86041-03; 316/86041-02):

the safety evaluation review sheet for lifted pressurizer heater leads determined remaining capacity was adequate by deducting lost capacity from total installed rather than from capacity accessible

to emergency power.

The emergency powered capacity establishes safety.

The licensee revised its evaluation, showing adequate capacity remains after deducting the disabled heaters from the emergency powered total.

d.

(Closed)

Open Item (315/87003-01; 316/87003-01):

the Component Cooling Water (CCW) system operating procedure contained a

precaution against operation below 70 degrees F., but the low temperature alarm setpoint

.was reduced to 60 degrees F. because alarms were common/continuous at the higher setpoint.

The licensee addressed this inconsistency by revising the operating procedure precaution to 60 degrees F, based on the facts that 70 degrees is not achievable during winter conditions and that no detriment to plant equipment had occurred in a number of years'xperience with colder operating periods.

No violations, deviations, unresolved or open items were identified.

3.

0 erational Safet Verification Routine facility operating activities were observed as conducted in the plant and from the main control rooms.

Plant startup, steady power operation, plant shutdown, and systems)

lineup and operation were observed as applicable.

The performance of licensed Reactor Operators and Senior Reactor Operators, of Shift Technical Advisors, and of auxiliary equipment operators was observed and evaluated including procedure use and adherence, records and logs, communications, shift/duty turnover, and the degree of professionalism of control room activities.

Evaluation, corrective action, and response for off normal conditions or events, if any, were examined.

This included compliance to any reporting requirements.

Observations of the control room monitors, indicators, and recorders were made to verify the operability of emergency systems, radiation monitoring systems and nuclear reactor protection systems, as applicable.

Reviews of surveillance, equipment condition, and tagout logs were conducted.

Proper return to service of selected components was verified.

'a

~

Unit 1 was taken critical at 6:42 p.m.

on October 4, 1987, ending a

scheduled refueling, maintenance, modification and testing outage which began on June 26.

I,ow power physics testing was completed on October 6 and power escalation for return to normal power operation commenced.

NRC review of low power physics testing is documented in I.E. Inspection Reports No. 315/87028(DRS);

No. 316/87028(DRS).

The Unit tripped (see Paragraph 4) on October 13, 1987 upon loss of one of two main feed pumps.

A restart followed later the same day and the Unit remained in normal power operation through the remainder of the inspection perio Unit 2 was taken critical at 1:52 a.m.

on October 10, 1987, ending an approximate six week maintenance and testing outage.

At 12:13 p.m.

the same day, the Unit tripped (see Paragraph 4) from about eight percent power.

A restart followed on October ll, and the Unit remained in normal power operation the remainder of the inspection period with a single substantial power reduction, as described below.

Following startup, the Unit experienced excessive leakage through the pressurizer spray system.

Pressure control required essentially all the pressurizer heaters be continuously energized.

Valve NRV-164 was suspected as the leak source, though the other valve (NRV-163) could not be excluded.

When attempts to rectify the situation from outside the containment failed, the licensee developed a preliminary plan to enter containment, inspect the situation, and (if no other course suggested itself) apply limited external mechanical force on the suspect valve with a jacking device.

The entry necessitated a power reduction to about 20 percent for radiation protection considerations, which was performed on October 28.

Upon entry, the inspection team found NRV-163 to be cycling erratically through a repetitive partial stroke cycle, while NRV-164 was found fully closed with operating (opening) air isolated by a local manual valve.

NRV-163 was secured and air valved in to NRV-164, restoring essentially normal pressure control with small controlled spray system leakage.

A return to normal power operation then followed.

The condition of the isolated air supply to NRV-164 was unexpected and the licensee is continuing to investigate the causal factors.

Items identified on plant tours for which some corrective action appeared appropriate were referred to plant management.

On some occasions, such items were noted during tours conducted with management representatives.

Examples noted during this inspection period included:

i)

an unsecured ladder left in an auxiliary feedwater pump room; ii)

vent lines/hoses attached to each Unit 2 RHR heat exchanger; plus, general clutter in the heat exchanger rooms.

Each of the above was noted prior to Unit startup and was expeditiously corrected.

iii) the inspector noted a lack of insulation on a line to a Unit 2 pressure instrument isolation valve, 2-MPI-lO-V1.

The line to the identical Unit 1 valve is insulated.

The Maintenance Superintendent initiated a review to determine which configuration is correc de A number of operating procedures were reviewed with results as described below:

01-OHP 4021.003.001

"Operation of I,etdown, Charging and Seal Water Systems",

Revision 9 dated 7/25/86 through Change Sheet

dated 8/28/87.

This procedure requires certain valve lineup checks, verification of oil level, flow and pressure, and verification of cooling water supply to auxiliaries.

These checks are made in the pump room and partially duplicate prior checks documented on an attached lineup sheets For those which exceed the scope of the lineup sheet, no provision exists to document they were done.

In fact, the procedure is not an "in hand" procedure, which is inconsistent with the concept of specifying local checks at the pump.

The procedure implies it is not necessary to run the associated auxiliary oil pump while -a centrifugal charging pump (CCP) is in service.

The auxiliary oil pump is to be run at least a

minute before starting an idle CCP and for at least five minutes after a

CCP is secured.

A caution tag was serving in lieu of specific procedure instructions for one of the pumps; e.g.

"operate the oil pump on the 1E CCP continuously while the CCP is in service".

This use of a caution tag in lieu of procedure instructions is inconsistent with the intent of the licensee's own administrative controls for caution tags.

The procedure is also either silent or provides ambiguous information concerning the single reciprocating charging pump in the Unit.

This is discussed further at iii) below.

01-OHP 4021.003.006

"Changing from a Reciprocating to a

Centrifugal Charging Pump", Revision 5 dated 10/9/54 through Change Sheet 1 dated 9/11/85.

iii) 01-OHP 4021.003.007

"Changing from a Centrifugal to a

Reciprocating Charging Pump", Revision 5 dated 8/14/84 through Change Sheet 1 dated 9/ll/85.

This procedure establishes an initial condition that the reciprocating charging pump (RCP) be filled, vented and available for standby operation per 1-OHP 4021.003.001.

This referenced procedure (003.001)

however, does not provide specific instructions for achieving standby readiness.

The text is silent with respect to the RCP.

The associated (003.001)

"Valve Lineup Sheet" does not specify valve positions as "open" or "closed", but says

"as required".

This does not achieve the objective presumed in (003.007) of preparing the RCP for operatio iv)

12-OHP 4021.005.001,

"Boron Makeup System Operation", Revision 9 dated 10/22/87.

v)

01-OHP 4024.109,

"Annunciator No.

9 Response:

Boric Acid",

Revision 3 dated 5/8/86 through Change Sheet 1 dated 8/28/87.

This alarm response procedure contained three apparent typographical errors in identification of relay numbers associated with the West Centrifugal Charging Pump motor instantaneous (drop 16)

and overload (drop 17) trips.

Three alarms (drop 31, 32 and 33) involve abnormal conditions associated with the "middle" Boric Acid Storage Tank ("M" BAST).

Though the tank can be aligned to either Unit, its conditions are monitored and alarmed only in the Unit 1 control room.

The alarm procedure lacks'instructions to check with or notify the Unit 2 control room concerning abnormal conditions for this tank.

vi)

02-OHP 4024.209

"Annunciator Response No. 9: Boric Acid",

Revision 2 dated 8/7/86 through Change Sheet 1 dated 8/28/87.

The inspector discussed observations from procedure reviews as described in i) through vi) ab'ove with the Operations procedure group.

Procedure change requests were initiated for deficiencies where deemed appropriate.

e.

Prior to the Unit 2 Mode change from MODE 5 to MODE 4'he inspector verified that containment integrity was established as required by the Technical Specifications.

The inspector verified the proper position of the valves associated with at least ten containment penetrations, observed that the Unit 2 upper airlock containment penetration was tested per plant procedure and that the ice condenser was maintained in accordance with plant procedures.

No violations, deviations, unresolved or open items were identified.

4.

Reactor Tri s or ESF Actuations a

Unit

Unit 1 tripped from about 69 per'cent power at 8:18 a.m.

on October 13, 1987, following loss of the 1E main feed pump.

The feed pump had tripped unexpectedly when an associated oil pump was secured per normal practice.

Operators immediately commenced pump recovery and reopening of the pump discharge valve, which closed as designed on the pump trip, but they were unable to maintain required steam generator levels and flow balances.

The reactor subsequently tripped on steam generator (No.

11) low level with steam/feed flow mismatch.

Control response of one feedwater regulating valve (FRV-210) was "ragged" and contributed to the event.

A detective circuit card was replace The inspector was onsite at the time of the trip and went to the control room to observe initial operator post-trip recovery actions and equipment performance.

All post-trip system responses were normal, and operator response was orderly, professional and "by the book".

b.

Unit 2 Unit 2 received a Train A safety injection actuation on October 2, 1987, at 4:57 p.m. while the Unit was in MODE 5 (cold shutdown).

Instrument and Control personnel had been performing surveillance testing of the Solid State Protection System (SSPS)

when a test failure occurred.

Investigation identified a faulted circuit board, which was replaced.

During the evolution of performing maintenance in the middle of testing, an error was made in the sequence for repositioning SSPS switches such that the "block" was not in effect for the streamline isolation signal input to safety injection.

In MODE 5, this signal is normal, so when the input error inhibit switch was returned to "normal" the Safety Injection signal act'uated.

No actual injection occurred because equipment was tagged out for low temperature overpressure protection as required.

The Train A emergency diesel (2 CD) started and the containment isolated as designed.

Upon assessment of the situation, operators terminated the signal and restored pre-event conditions.

The remaining instrument testing was then completed without further incident.

The resident inspectors will review adherence to applicable procedure controls during followup of the anticipated LER.

Unit 2 received a reactor trip/turbine trip signal at ll:28 p.m.

on October 8, 1987 while the Unit was in MODE 3 (hot shutdown)

with the reactor trip breakers closed but no control rods withdrawn.

Instrument and Control personnel were performing testing on excore nuclear instrument channels when, due to an error, channel 43 was placed in "Test" instead of channel 44.

The latter channel already had its bi-stables tripped in preparation for the testing, so two-of-four logic was satisfied and the trip signal resulted.

Both reactor trip breakers opened as designed.

Upon determination and discussion about what had happened, operators restored the. breakers and the remaining test was completed.

Unit 2 tripped (turbine trip/reactor trip) from about eight percent nuclear power at 12:13 p.m.

on October 10, 1987.

Operators were in the process of rolling the main turbine up to speed through about 1550 rpm when it tripped from an unknown cause.

Setpoint P-13 (establishing turbine/reactor trip off first stage pressure)

had been set rather low and had been blinking in and out with nuclear power around eight percen It happened to be instated when the turbine tripped, so reactor trip followed instantly.

Trip response was completely normal.

When the licensee was unable, despite extensive investigation and testing, (and consultation with a turbine vendor representative who witnessed the event) to determine the exact cause of the turbine trip, the start-up decision was referred, as required, to the Plant Nuclear Safety Review Committee (PNSRC)

and the Plant Manager.

They authorized restart conditioned on reverification and adjustment, if necessary, of setpoint P-13, and of the Brown-Boveri (turbine manufacturer)

vacuum trip circuits.

The trip circuits, which seemed the only remaining candidate/suspect, checked satisfactorily without adjustment.

Setpoint P-13 was raised to 8.7 percent.

The inspector went to the site October 11 to review the original records concerning the trip event and system response, to review the licensee's investigative scope and results, and to observe the restart.

No discrepancies prohibiting a Unit restart were noted.

Subsequently, the restart was observed through turbine roll, synchronization, and initial power escalation to 20 percent power. It was completely uneventful.

This occurrence, within a week of two Instrument and Control personnel errors which caused inadvertent safety system actuations, is of some concern to NRC.

The situation will be monitored carefully for a recurrence or for other related occurrences.

This was discussed at the management interview.

No violations, deviations, unresolved or open items were identified.

5.

Radiolo ical Controls During routine tours of radiologically controlled plant facilities or areas, the inspector observed occupational radiation safety practices by the radiation protection staff and other workers:

a.

proper wearing of personnel dosimetry; b.

correct use of step-off pads for contamination control; c.

adherence to assigned Radiation Work Permit; d.

proper Auxiliary Building exit, i.e. entering self reading dosimeter data to the REM computer and correctly using the high-sensitivity personnel contamination monitors.

Effluent releases were routinely checked, including examination of on-line recorder traces and proper operation of automatic monitoring equipmen Independent surveys were performed in various radiologically controlled areas, using a licensee-issued E-130 G-M detector.

No violations, deviations, unresolved or open items were identified.

6.

Maintenance Maintenance activities in the plant were routinely inspected, including both corrective maintenance (repairs)

and preventive maintenance.

Mechanical, electrical, and instrument and control group maintenance activities were included as available.

The focus of the inspection was to assure the maintenance activities reviewed were conducted in accordance with approved procedures, regulatory guides and industry.codes or standards and in conformance with Technical Specifications.

-The following items were considered during this review: the Limiting Conditions for Operation were met while components or systems were removed from service; approvals were obtained prior to initiating the work; activities were accomplished using approved procedures; and post maintenance testing was performed as applicable.

The following activities were inspected:

a

~

b.

The licensee recently named Mr.- J.

B. Droste to the position of Haintenance Superintendent.

This position is equivalent to the position of "Maintenance Hanager" as described in ANSI N18.1-1971, to which the licensee is committed.

Mr. Droste's training and experience were reviewed against the criteria of the ANSI standard with no deficiencies noted.

As part of a review of testing activities associated with containment isolation valves (see Paragraph 7.a) the inspector reviewed procedure PMI-2290 "Job Orders" and held discussions with Maintenance Department representatives concerning

"as found" testing of such valves before performance of work which could affect their performance as a leakage barrier.

The procedure contains a

generalized instruction to identify all required testing during the job order development process.

This is taken to include "as found" testing for containment'isolation valves.

The personnel who prepare the job orders have been informed and, reportedly, trained to include this testing for work on any containment boundary valve.

Specific written and/or computerized cross-check procedures to identify required testing as a function of the component being worked do not currently exist.

The licensee has an ongoing project to develop such a tool using the computerized plant equipment database, which is anticipated will be ready sometime around the middle of next year.

c

~

Procedure PMI-2160 "Control of Chemical Materials and Cleaning Agents" was reviewed and compliance to several of its attributes were verified during routine in-plant inspection activities.

No particular problem areas were noted by the inspector, although the

licensee's Quality Assurance audit/surveillance program has identified some problems in this area which the licensee is addressing.

RFC-DC-4033:

preliminary w'ork for relocating P-250 computer room

., exhaust vents.

RFC-DC-.2962:

preparatory grinding/cleaning activities in support of the project to strengthen the auxiliary building'rane and associated support structures; a subsidiary project of the Steam Generator Repair Project (SGRP)

on Unit 2 - see Paragraph 10.

Job Order JO 021122:

rebuild/retest of snubber.

A snubber located at the top of the pressurizer next to valve 2-NRV-152 was found leaking oil.

The snubber was removed and a replacement installed.

The removed snubber subsequently failed a functional bench test.

During discussion of the matter with licensee representatives, the inspector verified the test failure was being properly factored into the scheduling process for the next visual inspection period.

Job Order JO 726879:

repair post-accident sample sink.

Job Order JO 012282:

weld repair of the Unit 2 Component Cooling Water (CCW) return pipe from the West RHR heat exchanger.

This repair involved cutting out a rectangular piece atop the pipe to capture a through-wall crack which had developed in the heat-affected zone adjacent to a pipe weld.

The intent was to obtain a specimen perhaps representative of several cracks which developed in the Unit 2 CCW system and to perform metallurgical analysis on the specimen in an effort to determine the cause of the cracking.

The CCW investigatory project and the technical safety considerations associated with this repair are discussed in I.E.

Inspection Report

No

~ 50-315/87023(DRS);

50-316/87023(DRS).

Based

on questions

raised during the referenced

inspection it was learned

the licensee

had replaced

the cut out piece with a piece of ASTM

A-36 structural steel in lieu of the

ASTM A-106 Grade

B material of

which the pipe is made,

because

no A-106 material

was available.

Belated evaluation/documentation

concerning

the substitution

concluded

the repair

was satisfactory

from the standpoint of

strength

and weld compatibility.

This inspection

focused

on the administrative processes

established

to control substitutions

or other changes

to approved

design

conditions of plant safety systems.

The inspector

determined all

such

changes

are governed either by procedure

PMI-2140 "Temporary

Modifications" or (for permanent

changes)

by procedure

PMI-5040

"Design Change Control Program".

The former procedure at Paragraph

3.4.1,

requires prior evaluation

and approval

be performed

and

documented

before performing an activity which (temporarily) alters

a plant system,

component or structure

from its existing approved

condition.

A like requirement is contained in the latter procedure

(for permanent

changes)

at its Paragraph

4.4.3.

Thus, appropriate

controls exist to provide that alterations

to plant safety systems

receive

advance

review and approval.

In the subject repair, neither

of these controlling procedures

were applied.

Relatively concurrent with NRC inspection of this matter,

the

licensee's

onsite equality Assurance

(gA) Department

performed

an

audit of the maintenance

area which included the subject

Job Order

among many.

The gA audit report

(QA-87-26) was provided to and

reviewed by the inspector.

It contains

the

same finding that

administrative procedures

were violated when no documented prior

evaluation

and approval of the substitute

repair were completed.

Since Technical Specification 6.8.l.a requires

implementation of

such procedures

via reference

through Regulatory

Guide 1.33 Appendix

A, this matter is considered

a violation of the referenced

Technical

Specification (Violation: 316/87029-01).

Prior to the conclusion of the inspection,

both on the basis of the

gA audit finding and considering

an earlier Condition Report

initiated on the

same repair activity by the equality Control

Supervisor,

corrective actions

were implemented

as follows:

i)

a documented

safety analysis

was performed;

ii)

applicable

reviews

and approvals

were obtained;

iii) the applicable

documents

were updated

to show the current

modified condition.

Preventive

actions included:

iv)

requiring site Haintenance

Engineers

to have

documented

Engineering Evaluations vs. verbal instructions

from the

corporate

engineering

group for use in the development of work

packages;

v)

briefings/training for all welders

and supervisors

concerning

the need for documented

vs. verbal instructions;

and,

vi) utilization of a "traveler" form in preparation of Code weld

repair packages

to provide for specific advance identification

of the precise repair intended/required,

the applicable

Code,

the necessary

procedures

and the required testing.

The

"Traveler" is to receive prior review by equality Control and

Inservice Inspection personnel.

The last item is presently being implemented pursuant to an

instructional

memorandum

from the Haintenance

Engineer in charge of

this discipline.

A decision to make the process

permanent

has not

yet been

made

as the licensee is still considering if this system is

the most efficient one or whether

a better

(and perhaps

more

generic) alternative

may exist.

Also, subsequent

to the improper repair, but before its discovery,

the licensee

revised his procedure

PHI-5075,

"ASHE Section XI

Repair/Replacement

Program",

which governs

weld activities of this

type.

The new revision contains clearly stated

requirements

that all

materials

must conform to D.

C.

Cook plant specifications

and that

replacement

of any part or section requires

appropriate

reference

to

PHI-5040.

One violation (no licensee

response

required)

and

no deviations,

unresolved

or open items were identified.

7.

Surveillance

The inspector

reviewed Technical Specifications

required surveillance

testing

as described

below and verified that testing

was performed in

accordance

with adequate

procedures,

that test instrumentation

was

calibrated,

that Limiting Conditions for Operation were met, that removal

and restoration of the affected

components

were properly accomplished,

that test results

conformed with Technical Specifications

and procedure

requirements

and were reviewed by personnel

other than the individual

directing the test,

and that deficiencies identified during the testing

were properly reviewed

and resolved

by appropriate

management

personnel.

The following activities were inspected:

'<1

THP 4030 STP.203

"Surveillance Test Procedure

Type

BSC Leak

Rate Test" Revision

10 dated 5/28/87 through

Change

Sheet

13 dated

8/7/87.

Particular attention

was given to testing of valves in the Chemical

and Volume Control system

(CVCS) and the

Component

Cooling Water

(CCW) system,

to provide

some focus to the review, since the

procedure is an integrated

one (several

hundred pages,

counting

attachments)

covering all containment isolation valves.

Concerning

CVCS, the inspector verified:

i)

stipulated valve lineups

appeared

appropriate;

ii)

leakage

action guides

and limits were reasonable;

iii) data

and instructions

were consistent

among the various

attachments

and the procedure

body concerning

CVCS

penetrations;

and,

iv) justification/authorization

was provided for valves tested

by

"reverse direction" pressure,

consistent with 10 CFR 50,

Appendix J.

Concerning

CCW, attributes i) through iii) above were checked.

The

inspector noted

an apparent

inconsistency

between

the body of the

procedure

(Paragraph

5.9.3.3.C.2)

which excludes

ten

CCW valves

from

as-found vs. as-left "penalty" calculation, while Appendix I

includes

the valves.

Further discussion with Performance

Engineering established

the

CCW calculations, if performed,

are not

added into the total "penalty" applied to the subsequent

integrated

leak test.

Evaluation against criteria of 10 CFR 50 Appendix J,

considering function and design of the lines in question,

determined

the licensee's

practice is acceptable.

Some review was conducted

on

a licensee

Problem Report

(No.87-0846)

addressing

a failure to perform an "as-found" Type

C test

on

CVCS

letdown valve gCR-300 prior to maintenance.

The inspector verified

Procedure

STP.203 calls for an "as-found" leak rate test prior to

any piping or valve modifications or repair.

This is

a

Precaution/Limitation stated in Step 4.13 of the procedure.

As

noted in Paragraph

6.b above,

however,

the licensee

currently relies

on the knowledge

and experience

of the personnel

preparing job order

packages

to recognize, the need for such testing

so the Performance

Department is notified and can perform STP.203 before repairs begin.

Since the licensee identified this apparent

procedure violation,

corrected it, and it was neither safety significant nor repetitive,

only preventive actions

remain to be verified to establish

whether

a

NRC Notice of Violation should be issued.

Pending this review, this

is considered

an Unresolved

Item (315/87029-01).

- "12 HHP 5050 SPC.005

"Hydrostatic Test Procedure"

Revision

through

Change

Sheet

1 dated ll/3/87.

Setup for this procedure

to hydrostatically test essential

service

water to the containment

spray heat exchanger

was observed

on

November 3,

1987.

The test procedure

had just been revised to

incorporate

a

Code interpretation involving low temperature

(below

200 degrees

F.) systems with installed safety/relief valves.

It is

a generic procedure for testing multiple systems,

with the

applicable

system test pressure

calculated at the time the test is

done.

-12 THP 4030 STP.246

"Inspection of Ice Condenser Floor Drain

Valves".

Condition Report No. 2-10-87-1473 identified that two of twenty-four

Unit 2 floor drain valve gates

were not sealing properly during the

performance of STP.246.

The immediate corrective action documented

that the seating

surface

was sealed with grease

and

a Job Order

written to make permanent

repairs.

The inspector questioned

the use

of grease

as

a sealing

mechanism.

During discussion with cognizant

engineers

the inspector

was informed that the grease is routinely

applied,

by procedure,

to decrease

hot air inleakage,

during plant

operation,

from the lower containment to the ice condenser.

Thus,

all the gates

have greased

seating surfaces.

Air tightness is not

a

test criterion, however,

so grease is not required to pass

the test.

The inspector also found that the licensee

was aware of problems

encountered

by another utility when containment isolation valves

were greased prior to leak rate testing.

In addition, the inspector

verified that the grease

was compatible with the ice condenser

environment.

STP.246 at Step 4.4 states,

"Procedure test steps

can be performed

in any order".

The inspector questions if this is appropriate,

since

a primary objective of the procedure is to verify each drain

valve gate

opens within a specified opening force.

Since other

steps

involve exercising

the valve gates, it appears

inappropriate

to perform these

steps prior to determining the "as-found" opening

force.

This was discussed

with the cognizant engineer

who committed

to review/revise (if needed)

STP.246

':1

OHP 4030 STP.027AB

"AB Diesel Operability Test".

The Unit

1 AB

diesel generator failed

a start test under this procedure

on July

19,

1987.

The licensee

had intended to use

a successful

test to

declare

the machine "operable". Investigation

showed

fuses for the

generator field flashing circuits had been pulled by Instrument

and

Control personnel

on about July 15.

The purpose for pulling the

fuses

was to prevent

damage

during

a planned series of slow-speed

(non-synchronous)

runs of the engine.

The governing Haintenance

Department procedural instructions

were deficient in that they

neither specifically recognized

the actual pulling of the fuses

would be by the Instrument

and Control (ISC) group, nor were there

instructions to assure re-installation

on completion of the

slow-speed

runs'.

The ISC group

was not called upon in the interim

between July

15 and

19.

The licensee

issued

a Problem Report

(No.

87-0614)

on this matter which noted the above procedural

problems,

as well as other contributing factors.

The inspector

considered

the

evolution to reflect poorly on communication/co-ordination

among

plant departments,

but also to contain

some valuable lessons

learned.

The licensee identified this apparent

procedure deficiency and

corrected it, and the problem was neither safety significant nor

repetitive.

Pending final inspector review of preventive actions,

to determine

whether or not

a

NRC Notice of Violation should be

issue,

this matter is considered

an Unresolved

Item (315/87029-02).

12 MiP 4030 STP.029

"Functional Test of Hydraulic Snubbers".

-':1

OHP 4030 STP.004

"Centrifugal Charging

Pump Operability

Test-HODE

5 or 6".

As previously noted, Unit

1 was in an outage

throughout

September,

1987.

When this test

was run on September

4, acceptance

criteria in the form of updated differential pressure

graphs

were

not present in the Tech Data Book.

The pump could not be determined

to meet surveillance criteria on the basis of this test. Its condition

f'ollowing an earlier maintenance activity to modify the discharge

orifice remained indeterminate.

When updated

graphs

were received

by operators

on September

6, they showed the

pump failed with pressure

differential too high.

The

pump

was declared

inoperable.

Subsequently,

investigation

showed

the pressure

gauge

was reading

slightly high,

and

a retest after calibration (with no work on the

pump itself) succeeded

in qualifying the

pump for "operable" status

as required prior to

a

MODE change.

Retrospective

reviews also

showed

the other centrifugal charging

pump had remained

operable

while the subject

pump was unknowingly in a failed status.

A

licensee

Problem Report

(No. 87-0812)

documents

these

circumstances

which, in the view of the inspector,

resulted in inadvertant

compliance to requirements.

This was discussed

at the Management

Interview.

No violations, deviations,

unresolved

or open items were identified.

8.

Fire Protection

Fire protection program activities, including fire prevention

and other

activities associated

with maintaining capability for early detection

and

suppression

of postulated fires, were examined.

Plant cleanliness,

with

a focus

on control of combustibles

and

on maintaining continuous

ready

access

to fire fighting equipment

and materials,

was included in the

items evaluated.

a.

The licensee

reported

on October

12,

1987, that

a preplanned

maintenance activity to replace

a valve in the outside fire

suppression

water rising header necessitated

isolation of a portion

of the header.

Provision of backup suppression

capability and

followup written notification were both accomplished in accordance

with fire protection Technical Specifications.

b.

The inspector

informed the licensee

concerning discovery,

during

fire protection "safe shutdown" reviews at another plant, of a

potential

common mode postulated fire which could disable presumably

independent

emergency

power sources.

The licensee initiated

a

review of the matter to determine its applicability, if any, to the

D.

C.

Cook Units.

No violations, deviations,

unresolved

or open items were identified.

9.

~Securit

Routine facility security measures,

including control of access

for

vehicles,

packages

and personnel,

were observed.

Performance

of

dedicated

physical security equipment

was verified during inspections

in

various plant areas.

The activities of the professional

security force

in maintaining facility security protection were occasionally

examined or

reviewed,

and interviews were occasionally

conducted with security force

members.

No violations, deviations,

unresolved

or open 'items were identified.

10.

Steam Generator

Re air Pro'ect

(SGRP)

a.

Briefin

Meetin

The licensee visited

NRC Region III on October 23,

1987 to make

a

presentation

covering several

areas

of interest in the upcoming

(probable Spring 1988) project to replace

the Unit 2 steam

generators.

Specific topical areas

included

a schedule

overview,

which addressed

outage activities

and milestones.

,A presentation

was given on the radiological protection aspects

of the project,

as

were presentations

addressing

quality assurance

both from the

licensee

and from the primary contractor

(M-K Ferguson)

perspectives.

A scale

model was used to demonstrate

major aspects

of the physical disassembly,

component

movement,

and reassembly.

The licensee

also addressed

a variety of questions

from the

NRC

representatives.

A followup meeting is tentatively being considered

for March 1988.

b.

Or anization

and Staff

The inspector visited and toured the onsite offices for the

SGRP,

which occupy

somewhat

expanded facilities at the South

end of the

site formerly used

as the site training center.

Brief general

introductory meetings

were held with contractor,

licensee

corporate

and licensee site representatives.

c ~

Plant

Se re ation and La u

Plans

It will be necessary

while the

SGRP is ongoing to maintain clear and

positive segregation

of construction activities associated

with the

project from affecting the operating Unit

1 and those portions of

Unit 2 not involved with the project.

Licensee planning to

precisely identify the desired

boundaries

and to develop controls to

assure

compliance with the boundaries

were reviewed.

The licensee

has detailed

some experienced plant personnel

to the

SGRP primarily

to focus

on segregation

and

(as discussed

below) return to service.

The segregation

requirements

identified to date appeared

logical and

consistent.

Division of responsibilities

has

been established,

primary turnover preparation

milestones identified,

and individual

systems

reviewed.

A preliminary but quite detailed

clearance

setup

and valve position list has

been prepared.

During the layup portion of the

SGRP outage,

some current Technical

Specification testing will be impossible or illogical.

The licensee

intends,

however,

to maintain many Unit 2 systems

under appropriate

administrative controls to provide continuing "operability" by

performing applicable testing

and required maintenance.

A listing

of proposed

Technical Specifications

exemptions,

to omit impossible

or illogical testing,

has

been prepared

and submitted for NRC review

and approval.

Return to Service Plans

Preliminary Start-up

Program development,

for the return of Unit 2

to normal service after the

SGRP, is underway.

Organizational

responsibility and milestone

assignments

have been

made.

The

licensee

has

committed to complete Start-up

Program development,

including identification of applicable existing system performance

tests,

by the end of March,

1988, which is prior to commencement

of

the

SGRP outage.

This subject is likely to be addressed

in more

detail in future licensee/NRC meetings.

New Facilities

The inspector toured the newly constructed

temporary storage

facility which was completed during this inspection period.

Tours

were also conducted in a new radiation area

access

control facility

and

a

new security site access

control facility.

Each of these

facilities remained

under construction at the conclusion of the

inspection.

Both will be dedicated solely to

SGRP functions through

the completion of that project.

Details of their potential

utilization thereafter

have not yet been decided.

ll.

Information Notices

and Generic Letters

The inspector

reviewed the

NRC communications listed below and verified

that: the licensee

has received

the correspondence;

the correspondence

was reviewed by appropriate

management

representatives;

a written

response

was submitted if required;

and, plant-specific actions

were

taken

as described in the licensee's

response.

a.

(Closed) Information Notice (IN) 87-41, "Failures of Certain

Brown-Boveri Electric

(BBE) Circuit Breakers".

By memorandum

dated October 27,

1987,

the

NRC Region III requested

the inspector to review IN 87-41.to determine if the generic

implications had been considered

and (if necessary)

resolved

by the

licensee.

The IN identified two problems:

i)

The "close" latch in the breakers

should

be modified by

addition of a light spring.

The licensee's file on IN 87-41

states

this item is applicable for breakers

at D.

C.

Cook and

springs

are being added per design

change

RFC 12-2739,

"Modifications to BBE Circuit Breakers to Prevent Inadvertent

Opening".

The

RFC is complete for Unit

1 and is scheduled

for

the next refueling outage for Unit 2.

The inspector

reviewed

the

RFC file and verified a Brown-Boveri instruction (1B-8307,

"Installation of a Close Latch Anti-shock Spring in the

Mechanism" ) was incorporated.

ii)

A breaker failed to close because

of insufficient torquing of

the charging motor mounting bolts.

Maintenance

Procedure

MHP 5021.082.001,

"Maintenance Inspection

and Repair of 4 KV

Power Circuit Breakers",

was revised by Change

Sheet

2, dated

July 16,

1987, to require specific checks of the closing spring

charging motor mounting bolts.

b.

(Closed)

Generic Letter 81-21, "Natural Circulation Cooldown"

By memorandum

dated

May 15,

1987 and Temporary Instruction 2515/86,

Region III requested

that the inspector

review the licensee's

actions

taken to resolve

Generic Ietter

(GL) 81-21.

GL 81-21

describes

a

1980 natural circulation cooldown event at the St. Lucie

Unit

1 power plant which resulted in liquid flashing in the reactor

vessel

upper head region.

The Generic I,etter required

a response,

which was provided

on July 2,

1983 (Licensee file number

AEP:NRC:044A).

The

NRC Office of Nuclear Reactor Regulation

evaluated

the licensee's

response

and

a Westinghouse

Owners

Group

review of natural circulation and issued

a site specific Safety

Evaluation Report

(SER) dated

November

17,

1983.

The

SER discussed

different cooldown rates

and hold points

as they applied to the

availability of reactor vessel

head forced air cooling.

In

addition,

the

SER concluded that implementation of the NRC-approved

Westinghouse

Owners

Group Emergency

Response

Guidelines,

with

appropriate plant specific modifications,

would be adequate

to

perform

a safe natural circulation cooldown.

The inspector

reviewed the emergency procedures

listed below and

verified that the cooldown limits discussed

in the

SER are

addressed:

i)

Ol OHP 4023 ES-0.2

ii)

OHP 4023 ES-0.3

Natural Circulation Cooldown

Natural Circulation Cooldown

With Steam Voids in the Vessel

(with RVLIS)

iii) 01

OHP 4023 ES-0.4

Natural Circulation Cooldown

with Steam Voids in the Vessel

(without RVLIS)

The inspector interviewed the November 5,

1987 Unit

1 and Unit 2 day

shift operations

crew and determined that natural circulation

cooldown training had been performed

and that crew members

were

~ cognizant. of the St. Lucie event.

In addition, the inspector

confirmed that training had been p'erformed by review of natural

circulation lesson plans

RQ-C-EOPO;

RQ-C-EOP2;

RQ-R-1231;

RQ-R-1289,

and,

RQ-C-1291.

c.

(Open) Generic Letter 87-06, "Periodic Verification of Leak Tight

Integrity of Pressure

Isolation Valves"

This Generic Letter, dated

March 13,

1987,

was

one of two identified

for inspector followup via memorandum

from the Region III Director,

Division of Reactor Projects.

It identified information to be

submitted within 90 days; i.e. by about June ll, 1987.

During the

current inspection,

no record could be found that the requested

information had been provided.

The licensee is investigating

and

will develop

and provide the requested

information as

soon

as

possible.

Subsequent

to the exit interview, the licensee

confirmed

that the response

was not sent,

would be sent by November

11,

1987

and that

a Condition Report (internal corrective action document)

would be issued.

No violations, deviations,

unresolved

or open items were identified.

20.

Unresolved

Items

Unresolved

items are matters

about which more information is required in

order to ascertain

whether they are acceptable

items, violations, or

deviations.

Unresolved

items disclosed

during the inspection

are

discussed

in Paragraphs

7.a

and 7.d.

21.

Mana ement Interview

The inspectors

met with licensee

representatives

(denoted in Paragraph

1)

on November

10,

1987 to discuss

the scope

and findings of the inspection.

In addition,

the inspector

asked

those in attendance

whether they

considered

any of the items discussed

to contain information exempt from

disclosure.

No items were identified.

The following items were specifically discussed.

a

~

The inspector questioned

the review status

concerning

problems

experienced

with Unit 2 pressurizer

spray valve leakage

and

indicated it had been unclear

a safety evaluation would be performed

to justify a plan to apply force to

a valve with a jack.

,The

licensee

stated his investigation of the matter is continuing, that

use of a jack in the circumstances

discussed

was considered

analogous

to any other use of a tool but that it was understood

(and

some review actions

were initiated) that

a safety evaluation would

be required to justify leaving anything foreign in place

on or at

the valve (Paragraph

3.6).

Some of the observations

derived from operating procedures

reviews

were summarized

(Paragraph

3.d)

The inspector indicated close

NRC attention is being and will

continue to be paid to errors

by Instrument

and Control personnel

(Paragraph

4.b)

The apparent violation of administrative control requirements

in the

Maintenance

area

was reviewed

(Paragraph

6.h)

Poorly coordinated

charging

pump testing resulting in inadvertent,

rather than intentional,

compliance to

MODE change

requirements,

was

discussed

(Paragraph 7.f).

20