ENS 56478: Difference between revisions
Jump to navigation
Jump to search
StriderTol (talk | contribs) (StriderTol Bot insert) |
StriderTol (talk | contribs) (StriderTol Bot change) |
||
(One intermediate revision by the same user not shown) | |||
Line 9: | Line 9: | ||
| unit = 1 | | unit = 1 | ||
| utype = GE-4, GE-4 | | utype = GE-4, GE-4 | ||
| cfr = 10 CFR 50.72(b)(2)(iv)(B) | | cfr = 10 CFR 50.72(b)(2)(iv)(B), 10 CFR 50.72(b)(3)(iv)(A) | ||
| emergency class = Non Emergency | | emergency class = Non Emergency | ||
| notification date = 04/20/2023 05:24 | | notification date = 04/20/2023 05:24 | ||
Line 22: | Line 22: | ||
Reactor water level reached low level 1 (LL1) following the reactor trip. The LL1 signal causes Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves), and Group 8 (i.e., shutdown cooling isolation valves) isolations. The LL1 isolations occurred as designed; the Group 8 valves were closed at the time of the event. Due to the valid Primary Containment Isolation System (PCIS) actuation and RPS actuation from the reactor pressure signal, this event is also being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A). | Reactor water level reached low level 1 (LL1) following the reactor trip. The LL1 signal causes Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves), and Group 8 (i.e., shutdown cooling isolation valves) isolations. The LL1 isolations occurred as designed; the Group 8 valves were closed at the time of the event. Due to the valid Primary Containment Isolation System (PCIS) actuation and RPS actuation from the reactor pressure signal, this event is also being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A). | ||
Unit 2 is not affected by this event. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. | Unit 2 is not affected by this event. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. | ||
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2023/ | | URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2023/20230424en.html#en56478 | ||
}}{{unit info | }}{{unit info | ||
| Unit = 1 | | Unit = 1 |
Latest revision as of 14:58, 4 January 2024
Where | |
---|---|
Brunswick North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.4 h-0.0167 days <br />-0.00238 weeks <br />-5.4792e-4 months <br />) | |
Opened: | Chris Denton 05:24 Apr 20, 2023 |
NRC Officer: | Thomas Herrity |
Last Updated: | Apr 20, 2023 |
56478 - NRC Website
| |