05000382/FIN-2017002-04: Difference between revisions

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| identified by = NRC
| identified by = NRC
| Inspection procedure = IP 71111.19
| Inspection procedure = IP 71111.19
| Inspector = F Ramirez, C Speer, B Correll, S Graves, N Greene, R Kopriva, J O, 'Donnellg Miller
| Inspector = F Ramirez, C Speer, B Correll, S Graves, N Greene, R Kopriva, J O'Donnell, G Miller
| CCA = H.14
| CCA = H.14
| INPO aspect = DM.2
| INPO aspect = DM.2
| description = The inspectors identified a non-cited violation of Technical Specification 6.8, Procedures and Programs, and Regulatory Guide 1.33, Quality Assurance Program Requirements, for the licensees failure to perform operability testing on a safety-related component.  Specifically, following the coil replacement of main steam isolation valve 2 solenoid valve, a safety-related component, the licensee did not perform a retest of the solenoid valve.  As a result, main steam isolation valve 2 was returned to service without the assurance that no new deficiencies had been introduced, calling into question its operability. The licensee entered this condition into their corrective action program as Condition Report CR-WF3-2017-05507.  The licensees corrective action was to perform a voltage check of the solenoid valve to ensure it would energize in the event that a main steam isolation valve 2 closure was needed.The performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and adversely affected its objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  Specifically, the licensee restored main steam isolation valve 2 to an operable status without ensuring that its solenoid valve, which is a main steam isolation valve support system, was properly retested following maintenance.The inspectors screened the finding in accordance with NRC Inspection Manual Chapter 0609, Significance Determination Process.  Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, instructed the inspectors to use Appendix A, Significance Determination Process for Findings At-Power.  Using Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding to be of very low safety significance (Green) because it:  (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for greater than its technical specification allowed outage time or two separate safety systems out-of-service for greater than its technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more nontechnical specification trains of equipment designated as high safety-significant in accordance with licensees maintenance rule program for greater than 24 hours.The finding had a conservative bias cross-cutting aspect in the area of human performance because individuals did not use decision making-practices that emphasized prudent choices over those that were simply allowable.  Specifically, the licensee did not make a conservative decision when determining whether the main steam isolation valve or its solenoid valve should be tested prior to proceeding with plant startup [H.14].  
| description = The inspectors identified a non-cited violation of Technical Specification 6.8, Procedures and Programs, and Regulatory Guide 1.33, Quality Assurance Program Requirements, for the licensees failure to perform operability testing on a safety-related component.  Specifically, following the coil replacement of main steam isolation valve 2 solenoid valve, a safety-related component, the licensee did not perform a retest of the solenoid valve.  As a result, main steam isolation valve 2 was returned to service without the assurance that no new deficiencies had been introduced, calling into question its operability. The licensee entered this condition into their corrective action program as Condition Report CR-WF3-2017-05507.  The licensees corrective action was to perform a voltage check of the solenoid valve to ensure it would energize in the event that a main steam isolation valve 2 closure was needed.The performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and adversely affected its objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  Specifically, the licensee restored main steam isolation valve 2 to an operable status without ensuring that its solenoid valve, which is a main steam isolation valve support system, was properly retested following maintenance.The inspectors screened the finding in accordance with NRC Inspection Manual Chapter 0609, Significance Determination Process.  Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, instructed the inspectors to use Appendix A, Significance Determination Process for Findings At-Power.  Using Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding to be of very low safety significance (Green) because it:  (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for greater than its technical specification allowed outage time or two separate safety systems out-of-service for greater than its technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more nontechnical specification trains of equipment designated as high safety-significant in accordance with licensees maintenance rule program for greater than 24 hours.The finding had a conservative bias cross-cutting aspect in the area of human performance because individuals did not use decision making-practices that emphasized prudent choices over those that were simply allowable.  Specifically, the licensee did not make a conservative decision when determining whether the main steam isolation valve or its solenoid valve should be tested prior to proceeding with plant startup [H.14].  
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Latest revision as of 00:25, 22 February 2018

04
Site: Waterford Entergy icon.png
Report IR 05000382/2017002 Section 1R19
Date counted Jun 30, 2017 (2017Q2)
Type: NCV: Green
cornerstone Mitigating Systems
Identified by: NRC identified
Inspection Procedure: IP 71111.19
Inspectors (proximate) F Ramirez
C Speer
B Correll
S Graves
N Greene
R Kopriva
J O'Donnell
G Miller
Violation of: Technical Specification
CCA H.14, Conservative Bias
INPO aspect DM.2
'