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| issue date = 07/05/1978
| issue date = 07/05/1978
| title = LER 78-036/03L-0 for Dresden, Unit 2 Re a SBGT Failed to Start Upon Auto Initiation from a Spurious Reactor Bldg. Hi Rad Signal
| title = LER 78-036/03L-0 for Dresden, Unit 2 Re a SBGT Failed to Start Upon Auto Initiation from a Spurious Reactor Bldg. Hi Rad Signal
| author name = Stephenson B B
| author name = Stephenson B
| author affiliation = Commonwealth Edison Co
| author affiliation = Commonwealth Edison Co
| addressee name = Keppler J G
| addressee name = Keppler J
| addressee affiliation = NRC/RGN-III
| addressee affiliation = NRC/RGN-III
| docket = 05000237
| docket = 05000237
Line 15: Line 15:
| page count = 3
| page count = 3
}}
}}
=Text=
{{#Wiki_filter:Comm&ealth Edison Dresden  ~ear    Power Station R.R. #1 Morris, Illinois 60450 Telephone 815 /942-2920 CJ
                                                                                      -'°
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                                                                                        --.J    ("")CJ July 5, 1978                ;;c :1: ;;.O
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                                                                                ..:*                    --1
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                                                                                        ">l James G. Keppler, Regional Director Directorate of Regulatory Operations - Region III U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL            60137 Reportable Occurrence Report #78-036/03L-0, Docket #050-237 is hereby submi.tted to your off:ice in accordance with Dresden Nuclear Power Station Technical Specification 6.6.B.2.(b), conditions leading to operation in a degraded mode permittedby a limiting condition for operation or plant shutdown required by a limiting condition for operation.
                                            ~m~
J.-.._ B.B~
r-                  Stephenson Superintendent Dresden Nuclear Power Station BBS/kmh Enclosure CC:  Director of Inspection & Enforcement Director of Management Information & Program Control File/NRC REGUU\TORY DOCKET .F'ltE COPY,
                                              ~ \ .. \;.*            .            .
1.---*-*--.----.
                                                                    ~ .782000097_
NRC FGRM 366 e
U.S. NUCl_EAR REGULATORY COMMISSION 17-77).
    '.                                                                LICENSEE EVENT REPORT I.
CONTROL BLOCK:                      I
                                        '---'-~.._~~~~~~6~
I t'0                  (PLEASE PRINT OR TYPE ALL RECtU.RED INFORMATION)
.~          I I I L I D I R I s I 2 101                  0  I 0 I - I 0 I 0 I 0 I 0 I 0 I - I 0 I 0 1014 I 1 I 1 I 1 I 1 101 I I 0 7      B  9        LICENSEE CODE            14      15                    'LICENSE NUMBER                      25      26      LICENSE TYPE        JO  57 CAT SB CON'T CIT!:]
7        B
:~~~~~    W© I o I 5 I o I o I o*I 2 I 3 I 1 60          61            DOCKET NUMBER 101 o I 6 I o I 5 I 1 I 8 '(V ill_ l z I 6 I s I 1 I a IG) 68    69      EVENT DATE            i'-      75      REPORT DATE        BO EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
I On    June 5,. 1978, while Unit 2 and 3 were in normal operation, "Av SBGT failed to C2:IIJ        start upon auto initiation from a spurious reactor bldg. Hi Rad signal.                                                                      'B' SBGT
  ~            auto started suc*cessfully.                          A tubing in the flow control panel was found broken.                                                The
*[QJ}]          flow control damper was left wide open until' new tubing could be obtained.                                                                      On
  ~            June 9, 1978,              I A' SBGT again failed to start upon auto initiation and 'B' SBGT auto
  ~            started.            Since the redundant system was available the safety significance of these
  ~            events was minimal.                      This event is -not repetitive.
6 9                                                                                                                                                                  BO SYSTEM            CAUSE          CAUSE                                                          COMP.          VALVE CODE              CODE        SUB CODE                    COMPONENT CODE                  SUB CODE          SUBCODE
  ~B                          Isl cl@ ~@
9          10 w@                11 IN 1s IT IR 1u 18                        ~@)            ~@
11          . 12                13                            18          19              20 SEQUENTIAL                            OCCURRENCE            REPORT                      REVISION
              ~      LER'RO LVENT YEAR                                  REPORT NO.                                CODE                TYPE                        NO.
              ~ :J~~~~          lz 21*
I a 22I        l.::::J 23 lo 13 I 2 I 24                26 I/I 27 lo I JI 2B      29 w
30 L=J 31 l.Q_J 32 ACTION    FUTURE            EFFECT          SHUTDOWN                              ~      ATTACHMENT        NPRD-4          PRIME COMP.          COMPONENT TAKEN    ACTION          ON PLANT            METHOD                      HOURS ~          SUBMITTED      FORM ::.Utl.        SUPPLIER          MANUFACTURER W@W@
33 .'      34 W@
35 W@)
36 Io lo Io Io I LLJ@
37                      40    41 IB_J@
42 LU            Ii I 9 I 9  19  I@
43            44              47 CAUSE DESCRIPTION .A,ND CORRECTIVE ACTIONS @
I After the second failure a blown fuse was found which                                                  tripped the train on auto start.I Q]JJ          It was replaced and the train was auto started *and ran successfully.                                                                    Apparently _the ITI2J        first failure                was also caused by this* blown fuse.                                  Because of the singularity of
[ill]          this event no future corrective action is deemed necessary.
rrm 7      B  9                                                                                                                                                                80 FACILITY                                                            t3()\      METHOD OF                                                          ~
STATUS            % POWER                        OTHER STATUS      ~          DISCOVERY                            DISCOVERY DESCRIPTION        (31
~ ~@                      I 0 I 8 I 6 l@)I          U3 at 55%                                ~~~l~_O_p_e_r_a_t_i_o_n_a_l~E_v_e_n~t--~~~~*~~~~~--'
B  9            10              12    11                                  44      45        46                                                                  BO ACTIVITY      CONTENT                                              ~
RELEASED OF RELEASE                    AMOUNT.OF      ACTIVITY~                                                    LOCATION OF RELEASE          @
~          tu@)          W@~'~N-=-A_ _ _ _ _ ___.                                                          NA B  9            10          11                                            44            45                                                                        80 PERSONNEL EXPOSURES                            ~
NUMBER      (.;:;\TYPE        DESC.:RIPTION ~
[Q2JB I9 0 I 0 I0 11k~LLJ@        12 NA i~3~~~~-"""~~~~~~~~~~~~~~~~~~~~~~-~~~~~~~~~~8~0 PERSONNEL INJURIES                Q NUMBER            DESCRIPTION6
~
7      8 9 I 0 I 0 I 0 11I@                              NA
                                    ~12:--~~~~-==-=-~~~~~~~~~~~~~~~~~~~~~~~-~~~~~~~~~~....JBO
            'Loss OF OR DAMAGE TO FACILITY          Q TYPE      DESCRIPTION                v::::J
[2J2Ja W@  g NA
                        ~10:--~~~__;~~~~~~~~~~~~~~~-
PUBL1c1TY            C\
so ISSUEDQ DESCRIPTION~                                                                                                                            NRC USE ONLY          "'
E2TIJ 7      8  lliJ6 9                        NA 1~0~~~_...,...._~~~~~~~~~~~~~~~~~~~~~~~~~~~....168                                                                          II II IIIIII 69                      i I I~
SO*;;
Joe Chan                                                                            265                            0 0.
NAME OF PREPARER                                                                                    PHONE:        -
.'="1' ATTACHMENT TO LICENSEE EVENT REPORT 78-036/031-0 COMHONWE.ALTH EDISON COMPANY (CWE)      -
DRESDEN UNIT -2 (ILDRS-2)
DOCKET if 050-237 On June 5,_ 1978 during normal plant operation, "A" SBGT system failed to start upon auto initiation from a spurious Reactor Building ventilation radiation monitor trip. "B" train auto started when the "A" train failed to supply the required flow rate. "B" train operated for 10 hrs. which proved its operability as required by Tech. Spec. 4.7.B.l.a.
It was determined that the flow through the "A" train wa.s low because the blower suction valve was slow to open. An investigation revealed that a piece of tubing in the flow control panel was broken causing the valve to open slowly. The "A" train blower suction valve was manually placed in the full open position and the "A" tr3in was declared operable after it was manually started and run seccessfully for 10 hours. The valve will be left in the full op~n position until replacemen~ tubing can be obtained and installed.
Since the redundant train auto* sta.rted and ran successfully, the safetysignificance of this event is minimal.
On June 9, 1978, the "A" SBGT failed to start again upon auto initiation when the Unit 3 instrument bus was deenergized. "B" SBGT auto started and ran successfully for 10 hours; It was then found th~t a fuse in the heater operation sensing circuit was blown which prevented the auto start of the tr~in. The train is designed to trip ~pan auto sta~t if the heater fails to operate, but is not tripped upon manual start by this fuse failure. The fus*:::! was replaced and the train was auto started and ran successfully. The failure of the fuse wa's probably caused by a dirty relay* .contact or by deterioration of" the contact. The relay contact was cleaned and properly adjusted. The fuse is.manufactured by BUSS. Apparently both failure[;! were due to the blown fuse. Because of the singular nature of this event no further corrective action is de~~d necessary.}}

Latest revision as of 07:29, 24 February 2020

LER 78-036/03L-0 for Dresden, Unit 2 Re a SBGT Failed to Start Upon Auto Initiation from a Spurious Reactor Bldg. Hi Rad Signal
ML17252B562
Person / Time
Site: Dresden Constellation icon.png
Issue date: 07/05/1978
From: Stephenson B
Commonwealth Edison Co
To: James Keppler
NRC/RGN-III
References
BBS 78-1019 LER 78-036/03L-0
Download: ML17252B562 (3)


Text

Comm&ealth Edison Dresden ~ear Power Station R.R. #1 Morris, Illinois 60450 Telephone 815 /942-2920 CJ

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_oo BBS Ltr. #78-1019  :::u -;C:

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">l James G. Keppler, Regional Director Directorate of Regulatory Operations - Region III U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 Reportable Occurrence Report #78-036/03L-0, Docket #050-237 is hereby submi.tted to your off:ice in accordance with Dresden Nuclear Power Station Technical Specification 6.6.B.2.(b), conditions leading to operation in a degraded mode permittedby a limiting condition for operation or plant shutdown required by a limiting condition for operation.

~m~

J.-.._ B.B~

r- Stephenson Superintendent Dresden Nuclear Power Station BBS/kmh Enclosure CC: Director of Inspection & Enforcement Director of Management Information & Program Control File/NRC REGUU\TORY DOCKET .F'ltE COPY,

~ \ .. \;.* . .

1.---*-*--.----.

~ .782000097_

NRC FGRM 366 e

U.S. NUCl_EAR REGULATORY COMMISSION 17-77).

'. LICENSEE EVENT REPORT I.

CONTROL BLOCK: I

'---'-~.._~~~~~~6~

I t'0 (PLEASE PRINT OR TYPE ALL RECtU.RED INFORMATION)

.~ I I I L I D I R I s I 2 101 0 I 0 I - I 0 I 0 I 0 I 0 I 0 I - I 0 I 0 1014 I 1 I 1 I 1 I 1 101 I I 0 7 B 9 LICENSEE CODE 14 15 'LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT SB CON'T CIT!:]

7 B

~~~~~ W© I o I 5 I o I o I o*I 2 I 3 I 1 60 61 DOCKET NUMBER 101 o I 6 I o I 5 I 1 I 8 '(V ill_ l z I 6 I s I 1 I a IG) 68 69 EVENT DATE i'- 75 REPORT DATE BO EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@

I On June 5,. 1978, while Unit 2 and 3 were in normal operation, "Av SBGT failed to C2:IIJ start upon auto initiation from a spurious reactor bldg. Hi Rad signal. 'B' SBGT

~ auto started suc*cessfully. A tubing in the flow control panel was found broken. The

  • [QJ}] flow control damper was left wide open until' new tubing could be obtained. On

~ June 9, 1978, I A' SBGT again failed to start upon auto initiation and 'B' SBGT auto

~ started. Since the redundant system was available the safety significance of these

~ events was minimal. This event is -not repetitive.

6 9 BO SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUB CODE COMPONENT CODE SUB CODE SUBCODE

~B Isl cl@ ~@

9 10 w@ 11 IN 1s IT IR 1u 18 ~@) ~@

11 . 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION

~ LER'RO LVENT YEAR REPORT NO. CODE TYPE NO.

~ :J~~~~ lz 21*

I a 22I l.::::J 23 lo 13 I 2 I 24 26 I/I 27 lo I JI 2B 29 w

30 L=J 31 l.Q_J 32 ACTION FUTURE EFFECT SHUTDOWN ~ ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM ::.Utl. SUPPLIER MANUFACTURER W@W@

33 .' 34 W@

35 W@)

36 Io lo Io Io I LLJ@

37 40 41 IB_J@

42 LU Ii I 9 I 9 19 I@

43 44 47 CAUSE DESCRIPTION .A,ND CORRECTIVE ACTIONS @

I After the second failure a blown fuse was found which tripped the train on auto start.I Q]JJ It was replaced and the train was auto started *and ran successfully. Apparently _the ITI2J first failure was also caused by this* blown fuse. Because of the singularity of

[ill] this event no future corrective action is deemed necessary.

rrm 7 B 9 80 FACILITY t3()\ METHOD OF ~

STATUS  % POWER OTHER STATUS ~ DISCOVERY DISCOVERY DESCRIPTION (31

~ ~@ I 0 I 8 I 6 l@)I U3 at 55% ~~~l~_O_p_e_r_a_t_i_o_n_a_l~E_v_e_n~t--~~~~*~~~~~--'

B 9 10 12 11 44 45 46 BO ACTIVITY CONTENT ~

RELEASED OF RELEASE AMOUNT.OF ACTIVITY~ LOCATION OF RELEASE @

~ tu@) W@~'~N-=-A_ _ _ _ _ ___. NA B 9 10 11 44 45 80 PERSONNEL EXPOSURES ~

NUMBER (.;:;\TYPE DESC.:RIPTION ~

[Q2JB I9 0 I 0 I0 11k~LLJ@ 12 NA i~3~~~~-"""~~~~~~~~~~~~~~~~~~~~~~-~~~~~~~~~~8~0 PERSONNEL INJURIES Q NUMBER DESCRIPTION6

~

7 8 9 I 0 I 0 I 0 11I@ NA

~12:--~~~~-==-=-~~~~~~~~~~~~~~~~~~~~~~~-~~~~~~~~~~....JBO

'Loss OF OR DAMAGE TO FACILITY Q TYPE DESCRIPTION v::::J

[2J2Ja W@ g NA

~10:--~~~__;~~~~~~~~~~~~~~~-

PUBL1c1TY C\

so ISSUEDQ DESCRIPTION~ NRC USE ONLY "'

E2TIJ 7 8 lliJ6 9 NA 1~0~~~_...,...._~~~~~~~~~~~~~~~~~~~~~~~~~~~....168 II II IIIIII 69 i I I~

SO*;;

Joe Chan 265 0 0.

NAME OF PREPARER PHONE: -

.'="1' ATTACHMENT TO LICENSEE EVENT REPORT 78-036/031-0 COMHONWE.ALTH EDISON COMPANY (CWE) -

DRESDEN UNIT -2 (ILDRS-2)

DOCKET if 050-237 On June 5,_ 1978 during normal plant operation, "A" SBGT system failed to start upon auto initiation from a spurious Reactor Building ventilation radiation monitor trip. "B" train auto started when the "A" train failed to supply the required flow rate. "B" train operated for 10 hrs. which proved its operability as required by Tech. Spec. 4.7.B.l.a.

It was determined that the flow through the "A" train wa.s low because the blower suction valve was slow to open. An investigation revealed that a piece of tubing in the flow control panel was broken causing the valve to open slowly. The "A" train blower suction valve was manually placed in the full open position and the "A" tr3in was declared operable after it was manually started and run seccessfully for 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />. The valve will be left in the full op~n position until replacemen~ tubing can be obtained and installed.

Since the redundant train auto* sta.rted and ran successfully, the safetysignificance of this event is minimal.

On June 9, 1978, the "A" SBGT failed to start again upon auto initiation when the Unit 3 instrument bus was deenergized. "B" SBGT auto started and ran successfully for 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />; It was then found th~t a fuse in the heater operation sensing circuit was blown which prevented the auto start of the tr~in. The train is designed to trip ~pan auto sta~t if the heater fails to operate, but is not tripped upon manual start by this fuse failure. The fus*:::! was replaced and the train was auto started and ran successfully. The failure of the fuse wa's probably caused by a dirty relay* .contact or by deterioration of" the contact. The relay contact was cleaned and properly adjusted. The fuse is.manufactured by BUSS. Apparently both failure[;! were due to the blown fuse. Because of the singular nature of this event no further corrective action is de~~d necessary.