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| yopnf5 ' | | yopnf5 ' |
| CAust sysTtu COMPoht NT Caust system COMF0htNT "h$C- O NPR ' | | CAust sysTtu COMPoht NT Caust system COMF0htNT "h$C- O NPR ' |
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| / y i I I I I I I I I I I I I I I I l l l l l l l l l i I I I ' | | / y i I I I I I I I I I I I I I I I l l l l l l l l l i I I I ' |
| E' SUPPLEMENTAL REPORT EXPECTED (141 MONTH DAY YEAR SUSMIS$10N YiS 199 ven. eemente tXPICTLD tvenetSSION DAfte f NO l l l Aest ACT esu.,1, ,e oa wueu e , eeanaav . rnee. e.,.wue avoe mo s. eei ns, l On November 13, 1989, with the plant in HOT SHUTDOWN, Channel Functional l | | E' SUPPLEMENTAL REPORT EXPECTED (141 MONTH DAY YEAR SUSMIS$10N YiS 199 ven. eemente tXPICTLD tvenetSSION DAfte f NO l l l Aest ACT esu.,1, ,e oa wueu e , eeanaav . rnee. e.,.wue avoe mo s. eei ns, l On November 13, 1989, with the plant in HOT SHUTDOWN, Channel Functional l |
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| RCIC Suppression Pool Suction Valve received signals to close. Valve ~ | | RCIC Suppression Pool Suction Valve received signals to close. Valve ~ |
| 1E51 F064 closed as designed and valve 1E51-F031 was already closed in accordance with the RCIC system lineup for the standby mode. The isolation had no. adverse impact on the RCIC system since the RCIC system was in standby at the time of the isolation. | | 1E51 F064 closed as designed and valve 1E51-F031 was already closed in accordance with the RCIC system lineup for the standby mode. The isolation had no. adverse impact on the RCIC system since the RCIC system was in standby at the time of the isolation. |
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| The C&I technicians immediately stopped surveillance 9532.18 when the ] | | The C&I technicians immediately stopped surveillance 9532.18 when the ] |
| RCIC isolation occurred. At 2239 hours, Control. Room Operators reset the RCIC isolation signal and pla.ced the RCIC system in the standby mode in | | RCIC isolation occurred. At 2239 hours, Control. Room Operators reset the RCIC isolation signal and pla.ced the RCIC system in the standby mode in |
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| ;gp- A . ... .,m i ...n.....,,oo>. | | ;gp- A . ... .,m i ...n.....,,oo>. |
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| anc e asna ' v.s cuctua urvonomv couwiesio= ! | | anc e asna ' v.s cuctua urvonomv couwiesio= ! |
| UCENSEE EVENT REPORT (LER) TEXT CONTINUATION emovio ove no. mo-oio. , | | UCENSEE EVENT REPORT (LER) TEXT CONTINUATION emovio ove no. mo-oio. , |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029A6421991-02-20020 February 1991 LER 91-001-00:on 910121,automatic Closure of Inboard MSIV 1B21-F022 A,B,C & D & Inboard Main Steam Drain Line Isolation Valve 1B21-F016 Occurred.Caused by Personnel Error.Maint Work Request Mwr D09786 revised.W/910220 Ltr ML20043H9231990-06-18018 June 1990 LER 90-012-00:on 900517,feedwater Sys Flow Channel Failed & Caused Sensed Low Feedwater Flow.Caused by Normal end-of- Life Failure for Converter.Power Converter Replaced & Preventive Maint Tasks established.W/900618 Ltr ML20043G1151990-06-14014 June 1990 LER 90-011-00:on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags replaced.W/900614 Ltr ML20043E4911990-06-0505 June 1990 LER 90-010-00:on 900508,Divs I & II Emergency Diesel Generators Declared Inoperable Due to Expansion Joints Not Having Required tie-rods Installed to Prevent Expansion. Caused by Const/Installation error.W/900605 Ltr ML20043C0211990-05-23023 May 1990 LER 89-038-01:on 891212,discovered That Only Two of Four Conductors of Cable to Div II Nuclear Sys Protection Sys Inverter Connected.Caused by Design Error.Design Drawings reviewed.W/900523 Ltr ML20043B5741990-05-21021 May 1990 LER 90-009-00:on 900427,discovered That Moving Filter Paper in Leak Detection Sys Drywell Air Particulate Sample Panel Not Collecting on take-up Reel.Caused by Loose Set Screw on Gear Train.Set Screw tightened.W/900521 Ltr ML20043A2351990-05-11011 May 1990 LER 90-008-00:on 900408,attempt Made for 14 Control Rod Withdrawals While Main Turbine Bypass Valves Were Open & Reactor Power Was Greater than Low Power Setpoint.Caused by Personnel Error.Reactor Shut down.W/900511 Ltr ML20042F4111990-04-30030 April 1990 LER 90-007-00:on 900331,inadequate Determination of Equipment Status Resulted in de-energization of Nuclear Sys Protection Sys.Caused by Personnel Error.Fact Sheet on Operation Issued & Personnel retrained.W/900430 Ltr ML20042E6781990-04-23023 April 1990 LER 90-005-00:on 900322,containment Penetration Identified to Have motor-operated Valve W/Inadequate Actuator on Inboard Isolation Valve.Caused by Failure to Consider Design Capabilities of Actuators.Actuators reworked.W/900423 Ltr ML20042E6791990-04-23023 April 1990 LER 90-006-00:on 900321,process Radiation Monitor Placed in Svc W/O Required Filter Due to Inadequately Specified Job Steps for Plant Mod.Caused by Personnel Error.Procedure 1502.01 to Be revised.W/900423 Ltr ML20042E1581990-04-0909 April 1990 LER 90-003-00:on 900212,determined That 13 safety-related Transmitters Inoperable Due to Housing Covers Found W/Torque Values Less than Required to Meet Environ Qualification. Corrective Actions Program enhanced.W/900409 Ltr ML20042E1551990-04-0606 April 1990 LER 90-004-00:on 900307,review of NRC Info Notice 88-024 Re Failures of air-operated Valves Determined Pressure Differential of 73 solenoid-operated Valves Less than Max Instrument Air Sys Pressure.Valves replaced.W/900406 Ltr ML20012C5831990-03-13013 March 1990 LER 90-001-00:on 900212,drywell Purge Sys Containment Penetration Failed Local Leak Rate Test.Caused by Failure to Remove Cosmolene from Surface of Valve Prior to Initial Installation.Valves replaced.W/900313 Ltr ML19354E1031990-01-18018 January 1990 LER 89-042-00:on 891219,false RCIC Div I Steam Line Differential Pressure High Signal Caused RCIC Turbine Steam Supply Isolation Valve to Shut & RCIC Sys to Trip.Caused by Sensor Design Error.Field Alteration begun.W/900118 Ltr ML19354D9161990-01-17017 January 1990 LER 89-041-00:on 891122,unit Entered Tech Spec 3.0.3 When RCIC & HPCS Sys Inoperable Simultaneously for 37 Minutes. Chiller Condensing Unit Tripped Due to Low Refrigerant Pressure.Refrigerant in Chiller recharged.W/900117 Ltr ML20005G3211990-01-11011 January 1990 LER 89-038-00:on 891212,discovered That Only 2 of 4 Cable Conductors for Div II Nuclear Sys Protection Sys Power Supply Connected.Caused by Design Drawing Deficiency.Power Supply Configurations reviewed.W/900111 Ltr ML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr ML20005G2951990-01-0808 January 1990 LER 89-039-00:on 891212,operations Shift Supervisor Notified That Three HPCS Suction Valves Not Tested within Max Surveillance Time Interval.Caused by Personnel Error. Surveillance Procedure revised.W/900108 Ltr ML20042D3011989-12-29029 December 1989 LER 89-037-00:on 891129,inboard Drywell post-LOCA Vacuum Relief Valve Failed to Indicate Fully Open During Valve Stroke Testing.Caused by Worn O-rings Allowing Air to Leak Around Solenoid piston.O-rings Replaced.W/Undated Ltr ML19354D6621989-12-21021 December 1989 LER 89-035-00:on 891129,during Channel Functional Test of ECCS Drywell Pressure Channel,Operator Selected Wrong Channel for Testing,Causing Isolation of Instrument Air Sys. Caused by Personnel Error.Briefing conducted.W/891221 Ltr ML19332F8981989-12-13013 December 1989 LER 89-036-00:on 891113,incorrect Connection of Source to Terminals Directly Below Correct Terminals Caused Div 1 Isolation of RCIC Sys.Caused by Personnel Error.Personnel Briefed on Need to Use ladders/stools.W/891213 Ltr ML19325E5841989-11-0101 November 1989 LER 89-034-00:on 891004,discovered That Inservice Station HVAC Exhaust Stack Process Radiation Monitor Had Not Been Verified as Operable,Contrary to Tech Spec 3.3.7.12.Caused by Lack of Training & Inadequate communication.W/891101 Ltr 1991-02-20
[Table view] Category:RO)
MONTHYEARML20029A6421991-02-20020 February 1991 LER 91-001-00:on 910121,automatic Closure of Inboard MSIV 1B21-F022 A,B,C & D & Inboard Main Steam Drain Line Isolation Valve 1B21-F016 Occurred.Caused by Personnel Error.Maint Work Request Mwr D09786 revised.W/910220 Ltr ML20043H9231990-06-18018 June 1990 LER 90-012-00:on 900517,feedwater Sys Flow Channel Failed & Caused Sensed Low Feedwater Flow.Caused by Normal end-of- Life Failure for Converter.Power Converter Replaced & Preventive Maint Tasks established.W/900618 Ltr ML20043G1151990-06-14014 June 1990 LER 90-011-00:on 900514,during Routine Testing,Diesel Generators 1A Tripped on High Coolant Temp.Caused by Lack of Procedures for Correctly Positioning Diesel Generator SX Throttle Valves.Caution Tags replaced.W/900614 Ltr ML20043E4911990-06-0505 June 1990 LER 90-010-00:on 900508,Divs I & II Emergency Diesel Generators Declared Inoperable Due to Expansion Joints Not Having Required tie-rods Installed to Prevent Expansion. Caused by Const/Installation error.W/900605 Ltr ML20043C0211990-05-23023 May 1990 LER 89-038-01:on 891212,discovered That Only Two of Four Conductors of Cable to Div II Nuclear Sys Protection Sys Inverter Connected.Caused by Design Error.Design Drawings reviewed.W/900523 Ltr ML20043B5741990-05-21021 May 1990 LER 90-009-00:on 900427,discovered That Moving Filter Paper in Leak Detection Sys Drywell Air Particulate Sample Panel Not Collecting on take-up Reel.Caused by Loose Set Screw on Gear Train.Set Screw tightened.W/900521 Ltr ML20043A2351990-05-11011 May 1990 LER 90-008-00:on 900408,attempt Made for 14 Control Rod Withdrawals While Main Turbine Bypass Valves Were Open & Reactor Power Was Greater than Low Power Setpoint.Caused by Personnel Error.Reactor Shut down.W/900511 Ltr ML20042F4111990-04-30030 April 1990 LER 90-007-00:on 900331,inadequate Determination of Equipment Status Resulted in de-energization of Nuclear Sys Protection Sys.Caused by Personnel Error.Fact Sheet on Operation Issued & Personnel retrained.W/900430 Ltr ML20042E6781990-04-23023 April 1990 LER 90-005-00:on 900322,containment Penetration Identified to Have motor-operated Valve W/Inadequate Actuator on Inboard Isolation Valve.Caused by Failure to Consider Design Capabilities of Actuators.Actuators reworked.W/900423 Ltr ML20042E6791990-04-23023 April 1990 LER 90-006-00:on 900321,process Radiation Monitor Placed in Svc W/O Required Filter Due to Inadequately Specified Job Steps for Plant Mod.Caused by Personnel Error.Procedure 1502.01 to Be revised.W/900423 Ltr ML20042E1581990-04-0909 April 1990 LER 90-003-00:on 900212,determined That 13 safety-related Transmitters Inoperable Due to Housing Covers Found W/Torque Values Less than Required to Meet Environ Qualification. Corrective Actions Program enhanced.W/900409 Ltr ML20042E1551990-04-0606 April 1990 LER 90-004-00:on 900307,review of NRC Info Notice 88-024 Re Failures of air-operated Valves Determined Pressure Differential of 73 solenoid-operated Valves Less than Max Instrument Air Sys Pressure.Valves replaced.W/900406 Ltr ML20012C5831990-03-13013 March 1990 LER 90-001-00:on 900212,drywell Purge Sys Containment Penetration Failed Local Leak Rate Test.Caused by Failure to Remove Cosmolene from Surface of Valve Prior to Initial Installation.Valves replaced.W/900313 Ltr ML19354E1031990-01-18018 January 1990 LER 89-042-00:on 891219,false RCIC Div I Steam Line Differential Pressure High Signal Caused RCIC Turbine Steam Supply Isolation Valve to Shut & RCIC Sys to Trip.Caused by Sensor Design Error.Field Alteration begun.W/900118 Ltr ML19354D9161990-01-17017 January 1990 LER 89-041-00:on 891122,unit Entered Tech Spec 3.0.3 When RCIC & HPCS Sys Inoperable Simultaneously for 37 Minutes. Chiller Condensing Unit Tripped Due to Low Refrigerant Pressure.Refrigerant in Chiller recharged.W/900117 Ltr ML20005G3211990-01-11011 January 1990 LER 89-038-00:on 891212,discovered That Only 2 of 4 Cable Conductors for Div II Nuclear Sys Protection Sys Power Supply Connected.Caused by Design Drawing Deficiency.Power Supply Configurations reviewed.W/900111 Ltr ML20005G2811990-01-0808 January 1990 LER 89-040-00:on 891206,discovered That Mode Limitations from Surveillance Procedure Omitted,Resulting in Inoperable ATWS Recirculation Pump Trip Sys Instrumentation.Caused by Inadequate Procedure.Surveillance revised.W/900108 Ltr ML20005G2951990-01-0808 January 1990 LER 89-039-00:on 891212,operations Shift Supervisor Notified That Three HPCS Suction Valves Not Tested within Max Surveillance Time Interval.Caused by Personnel Error. Surveillance Procedure revised.W/900108 Ltr ML20042D3011989-12-29029 December 1989 LER 89-037-00:on 891129,inboard Drywell post-LOCA Vacuum Relief Valve Failed to Indicate Fully Open During Valve Stroke Testing.Caused by Worn O-rings Allowing Air to Leak Around Solenoid piston.O-rings Replaced.W/Undated Ltr ML19354D6621989-12-21021 December 1989 LER 89-035-00:on 891129,during Channel Functional Test of ECCS Drywell Pressure Channel,Operator Selected Wrong Channel for Testing,Causing Isolation of Instrument Air Sys. Caused by Personnel Error.Briefing conducted.W/891221 Ltr ML19332F8981989-12-13013 December 1989 LER 89-036-00:on 891113,incorrect Connection of Source to Terminals Directly Below Correct Terminals Caused Div 1 Isolation of RCIC Sys.Caused by Personnel Error.Personnel Briefed on Need to Use ladders/stools.W/891213 Ltr ML19325E5841989-11-0101 November 1989 LER 89-034-00:on 891004,discovered That Inservice Station HVAC Exhaust Stack Process Radiation Monitor Had Not Been Verified as Operable,Contrary to Tech Spec 3.3.7.12.Caused by Lack of Training & Inadequate communication.W/891101 Ltr 1991-02-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARU-603277, Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Clinton Power Station,Unit 1.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers U-603267, Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Clinton Power Station,Unit 1.With U-603245, Monthly Operating Rept for Jul 1999 for CPS Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for Jul 1999 for CPS Unit 1.With ML20211C9621999-07-26026 July 1999 ISI Summary Rept U-603232, Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted1999-07-0909 July 1999 Special Rept:On 990531 Lpms Was Declared Inoperable Due to Receipt of High Vibration & Loose Parts Alarm Which Did Not Clear.Lpms Was Restored to Operable Status on 990707 After Alignment & Tension on Recorder Tape Drive Was Adjusted U-603233, Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Clinton Power Station,Unit 1.With U-603222, Monthly Operating Rept for May 1999 for Clinton Power Station.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Clinton Power Station.With ML20210K8391999-05-11011 May 1999 British Energy Annual Rept & Accounts 1998-99 ML20206H1231999-05-0505 May 1999 Illinois Power Co CPS Main CR Simulator Certification Rept U-603210, Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cps,Unit 1.With U-603204, Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR211999-04-30030 April 1999 Final Part 21 Rept 21-99-003 Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier Trentec for Westinghouse Breaker 1AP05EH.Issue Determined Not Reportable Per 10CFR21 U-603192, Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Clinton Power Station,Unit 1.With U-603182, Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue1999-03-12012 March 1999 Part 21 Rept Re Deficiency in Commercial Grade Dedication Process Used by Circuit Breaker Refurbishment Supplier, Trentec.Condition Rept 1-99-01-136 Was Initiated to Track Investigation & Resolution of Issue U-603176, Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Clinton Power Station,Unit 1.With ML20207F2031999-02-10010 February 1999 Rev 1 to CPS COLR for Reload 6 Cycle 7 ML20202J0181999-02-0303 February 1999 SER Accepting Changes in Quality Assurance Program,Which Continues to Meet Requirements of App B to 10CFR50 U-603144, Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Clinton Power Station,Unit 1.With U-603223, Illinova Corp 1998 Annual Rept. with1998-12-31031 December 1998 Illinova Corp 1998 Annual Rept. with U-603115, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components1998-12-0404 December 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps in Supplying SR Parts to Npps.Issue Is Not Reportable Under 10CFR21. Dedication Process Did Not Affect Ability of Components U-603124, Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Clinton Power Station,Unit 1.With U-603114, Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor1998-11-25025 November 1998 Part 21 Rept 21-98-049 Re W Dhp Circuit Breaker Refurbished by Nuclear Logistics,Inc Which Failed to Operate.Caused by Trip Latch out-of-adjustment & Incorrectly Sized Ratchet Lever Assembly Bushing.Breakers Were Returned to Vendor U-603103, Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Clinton Power Station,Unit 1.With U-603101, Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site1998-10-28028 October 1998 Special Rept:On 980918,discovered That Triaxial Seismic Accelerometers Had Not Been Properly Calibrated.Caused by Inadequate Calibration Procedure.Calibration to Be Performed off-site ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves U-603091, Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Clinton Power Station,Unit 1.With ML20153F9871998-09-17017 September 1998 Safety Evaluation Accepting 980225 Proposed Rev 26 to Illinois Power Nuclear Program Qam ML20151U1391998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Clinton Power Station,Unit 1 ML20237E3991998-08-27027 August 1998 SER Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode, for Clinton Power Station ML20237A1521998-08-0707 August 1998 SER Re Mgt Services Agreement at Clinton Power Station. Approval Under 10CFR50.80 Not Required ML20151Y6591998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Clinton Power Station,Unit 1 U-603033, Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals1998-07-20020 July 1998 Part 21 Rept 21-98-039 Re Shrinkage of Medium & High Density Silicone Seals Designed & Installed by Bisco Using Dow Corning Sylgard 170 Matl.Caused by Coefficient of Thermal Expansion.Will Inspect & Rework/Repair Suspected Seals U-603041, Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 ML20151U1501998-06-30030 June 1998 Revised Monthly Operating Rept for June 1998 for Clinton Power Station,Unit 1 U-603023, Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Clinton Power Station,Unit 1 U-603014, Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed1998-05-28028 May 1998 Special Rept:On 980512,lightning Struck Primary Meteorological Monitoring Instrumentation Tower Damaging 60- Meter Wind Speed & Associated Transmuter Circuit Card. Surveillance Testing Performed ML20236E7991998-05-26026 May 1998 Final Part 21 Rept Re W Dhp Circuit Breaker Auxillary Switch Operating Assembly Anomalies.Caused by Loss of Breaker Safety Function.Dhp Circuit Will Be Inspected ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted U-603004, Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable1998-05-15015 May 1998 Part 21 Rept Re 980107 Determination That Itt Barton Model 580A Series Differential Pressure Indicating Switches Operating Forces Too Low.Manufacturing Sys Allowed Switches to Be Mixed.Evaluation Concludes Issue Not Reportable ML20216A9601998-05-0808 May 1998 Part 21 Rept Re Failure of 12 Volt DC Inverter Power Supply. Caused by Inadequately Sized Output Transistor Pair Combined W/Degraded Capacitors.Licensee Plans to Replace All Output Transistors & Degraded Capacitors U-602995, Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts1998-05-0505 May 1998 Part 21 Interim Rept 21-98-021 Re Deficiencies in Matl Dedication Process Used by Goulds Pumps During Use of Portable Metal Analyzer.Util Identified Discrepancies Which Are Acceptable W/Some Exception of Some Replacement Parts U-603006, Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Clinton Power Station,Unit 1 U-602994, Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable1998-04-29029 April 1998 Part 21 Rept Re Final Rept 21-98-008,on 980113,reliance Electric Motors Supplied by Rockwell International for Hydrogen Recombiner Cooling Fans Do Not Have nameplate- Specified High Temperature Bearings.Fan Motors Acceptable ML20216B1351998-04-21021 April 1998 Rev 0 to Illinois Power Co Clinton Power Station SVC Design Rept U-602979, Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable1998-04-0707 April 1998 Final Part 21 Rept 21-97-059 Re Discrepancies Found During Receipt Insp of Three Refurbished safety-related W Dhp Circuit Breakers.Util Completed Evaluation,Per 10CFR21 & Concludes That Condition Is Not Reportable U-602976, Monthly Operating Rept for Mar 1998 for Clinton Power Station1998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Clinton Power Station ML20217H5771998-03-27027 March 1998 Safety Evaluation Concluding That No Significant Safety Hazards Introduced at CPS for Net 32% Ampacity Derating Factor for 1 H & 3 H Conduit Fire Barrier Sys & 1 H Cable Tray Fire Barrier Sys.Requests Response Addressing Issue U-602968, Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue1998-03-24024 March 1998 Interim Part 21 Rept 21-97-055 Re Westinghouse Dhp Circuit Breaker Auxiliary Switch Operating Assembly Anomalies. Initially Reported on 980116.Util Currently Evaluating Suppliers Response to Questions Re Issue U-602960, Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 9804111998-03-12012 March 1998 Part 21 & Deficiency Rept Re Commerical Grade Dedication Program of Sentry Equipment Corp.Initially Reported on 980217.IP Performed an Addl Assessment at Sentry Facility on 980226.Next Rept Will Be Submitted by 980411 U-602954, Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 9805131998-03-0909 March 1998 Interim Part 21 rept,21-98-008 Re Identification That Bearings Installed in Hydrogen Recombiner B Cooling Fan Motor 0HG04CB Were Not Same as Bearings Specified on Motor Nameplate.Will Complete Evaluation of Issue by 980513 1999-09-30
[Table view] |
Text
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, L45 89(12 13)-LP l
.20.220 -
,. -lLLIN0/8 POWER 00MPANY i
L December 13, 1989 !
j, 10CFR50.73 t.
!' Docket No. 50 461' U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 i
Subject:
Clinton Power Station . Unit 1 Licensee Event Reoort No. 89 036 00
Dear Sir:
Please find enclosed Licensee Event Report No. 89 036 00:
Failure to Perform Work at Eve Level Results in Connection of Test Eaulement to Incorrect Terminals and Automatic Isolation of Reactor Core Isolation Cooling System. This report is being submitted in accordance with the roquirements of 10CFR50.73.
Sincerely yours, b/ ~
D. L. Holtzscher Acting Manager -
Licensing and Safety RSF/kra I
i~ Enclosure
cc: NRC Resident Office NRC Region III,. Regional A&ainistrator INPO Records Center Illinois Department of Nuclear Safety l NRC Clinton Licensing Project Manager l-ik l 8912190273 891213
/ i
{DR ADOCK 05000461 l FDC !
b
6 pe.m See U g esuCLtL2 ht1UL. TORY COammenstm
, APPROVED oen8 NO. 3100410s
LICENSEE EVENT REPORT (LER) 9 ACILITV NAant til DOCkti NUGADER QI PACE (34 Clinton Power Station 01610 l 0 l 0141611 1 l0Fl0 le; m'* Failure to PerformWork at Eye Level Results in Connection of Test Equipment to I correct Terminals and Automatic Isolation of Reactor Qore Isolation Cooline System SVONT DATS ISI Lt R NUedDE R tel AtPont DAff (71 OTMt h 7 ACILittt$ INVOLVtD ISI MONTH DAv YtAR vlam St,0U k pyy gggyn gay yggq s actLif t h AMES DOCAtT NUM9tht$1 None 0l6l0 toto l l l 1l1 1l3 8 9 8l9 0 l3 l6 0l0 1l2 1l3 8l9 0 1 610 10 i 0, l l opt A Aflee0 THet mtPomT st SUtutTTED PUhsuANT TO TMt mLouentMENTS OF 10 C8R 6: (Chece pae er enew of sae rene.emas (11)
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NAME tt LtPHONE NUM98R Amt A COD 4 S. E. Resor, Director - Plant Maintenance, extension 3204 2 l 11 7 9I315I-l8I8I811 COMPLtit ONE LINE FOR E ACH COMPONtNT f A8tunt DiscRittD IN TMis atPon? (til MA C. oni "
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E' SUPPLEMENTAL REPORT EXPECTED (141 MONTH DAY YEAR SUSMIS$10N YiS 199 ven. eemente tXPICTLD tvenetSSION DAfte f NO l l l Aest ACT esu.,1, ,e oa wueu e , eeanaav . rnee. e.,.wue avoe mo s. eei ns, l On November 13, 1989, with the plant in HOT SHUTDOWN, Channel Functional l
Testing (CFT) of Division 1 differential temperaturo channel 1E31-N613A, Reactor Water Cleanup Pump "A" Room Differential Temperature, was in progress. The CFT procedure required connection of a millivolt source to the circuit to initiate a trip of channel 1E31-N613A. Control and Instrumentation (C&I) technicians identified and double verified the correct terminals to be connected to the millivolt source. The technician performing the connection looked away from the terminals to double check the procedure, then looked back and inadvertently connected the source to terminals directly below the correct terminals. The 3 incorrect connection caused a Division 1 isolation of the Reactor Core l Isolation Cooling (RCIC) system. The RCIC system was in standby at the time of the isolation. The cause of this event is attributed to the failure of the technician to perform the work at eye level. Contributing factors to the technician's error were the close arrangement of the terminal boards (tbs) and the similarity of the tbs. Corrective action includes briefing personnel on the need to use ladders / stools so that they perform work at eye level, applying various colored tape strips above and below terminal boards to enhance recognition of different terminal boards, and revising surveillance test procedures.
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DESCRIPTION OF EVENT On November 13, 1989, the plant was in Mode 3 (110T Sl!UTDOWN), at 330 degrees Fahrenheit and 107 pounds per square inch pressure, and a planned maintenance outage was'in progress. At 2207 hours0.0255 days <br />0.613 hours <br />0.00365 weeks <br />8.397635e-4 months <br />, an automatic Division 1 isolation of the Reactor Core Isolation Cooling (RCIC) system [BN) occurred because of an RCIC equipment area high differential temperature signal.
On November 13, 1989, utility Control and Instrumentation (C&I) maintenance technicians were preparing to perform Reactor Water Cleanup (RWCU) system [CE)/ Leak Detection (LD) system [IJ) surveillance test ,
procedure 9532.18, "RWCU Ventilation Differential Temperature '
E31-N612A(B) RWCU lleat Exchanger Room West, E31 N613A(B) RWCU Pump "A" Room E31-N613E(F) RWCU Pump "C" Poom E31 N614A(B) RWCU Pump "B" Room, E31-N618A(B) RWCU lleat Exchanger Room. East Channel Functional." The '
channel being tested was Division 1 differential temperature channel 1E31-N613A (RWCU Pump "A" Room Differentici Temperature). Surveillance ;
9532.18 requires that a trip of channel IE31 N613A be initiated by connecting the output leads of a millivolt source to terminals 4 and 5 of Terminal Board (TB) 018 in cabinet (CAB) lill3 P715E. Normally, a trip of channel IE31 N613A results in a Division 1 isolation of the RWCU system, however, durin6 surveillance 9532.18, this isolation function is i
bypassed, t
On November 13, 1989, at 2159 hours0.025 days <br />0.6 hours <br />0.00357 weeks <br />8.214995e-4 months <br />, the C&I technician responsible for p connecting the millivolt source to the terminals identified the correct terminals to be connected to the millivolt source. A second C&I technician correctly double verified these same terminals as the correct terminals for connecting the millivolt source. At this point, the second 7 C&I technician proceeded to the control room annunciator (ANN) panel (PL) to verify that the trip of channel 1E31-N613A occurred as expected.
At 2207 hours0.0255 days <br />0.613 hours <br />0.00365 weeks <br />8.397635e-4 months <br />, prior to making the connection, the C&I technician responsible for connecting the millivolt source to the terminals looked away from the terminals to double check the procedure. The technician
- looked back at the terminal boards and then inadvertently connected the leads of the millivolt source to terminals 4 and 5 of terminal board TB006 which are directly below terminals 4 and 5 of TB018 in cabinet 1}i13 P715E.
Connecting the leads of the millivolt source to terminals 4 and 5 of TB006 caused a trip of Division 1 differential temperature channel 1E31-N603A (RCIC Equipment Area liigh Differential Temperature) and resulted in an automatic Division 1 isolation of the RCIC system. (The Division 1 isolation function for the RCIC system was not in bypass status at the time of this isolation.) Because of the isolation, as designed, containment isolation valves [ISV] 1E51-F064, Residual lleat
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TEXT M mee apose h regwe( see esWeens/ NAC Farm J854 'st (1M Removal (RHR) [ESj and RCIC Steam Supply Isolation Valve, and 1E51 F031, ;
RCIC Suppression Pool Suction Valve received signals to close. Valve ~
1E51 F064 closed as designed and valve 1E51-F031 was already closed in accordance with the RCIC system lineup for the standby mode. The isolation had no. adverse impact on the RCIC system since the RCIC system was in standby at the time of the isolation.
The C&I technicians immediately stopped surveillance 9532.18 when the ]
RCIC isolation occurred. At 2239 hours0.0259 days <br />0.622 hours <br />0.0037 weeks <br />8.519395e-4 months <br />, Control. Room Operators reset the RCIC isolation signal and pla.ced the RCIC system in the standby mode in
. preparation for use to control Reactor Pressure Vessel [RPV) pressure. .
I No automatic or manually initiated safety system responses were necessary to place the plant in a safe and stable condition. No equipment or components were inoperable at the start of this event such that their inoperable condition contributed to this event. I l
CAUSE OF EVENT The cause of this event is attributed to personnel error by a utility C&I j maintenance technician. The technician identified the correct terminals >
in accordance with surveillance procedure 9532.18 prior to connecting the . )
millivolt source and then inadvertently connected the millivolt source to
=the terminals directly below the correct terminals.
The C&I technician's error was caused by his failure to perform the work at eye level. The terminals of TB018 were above the technicians head and <
therefore he had to reach to make the connection. The technician was familiar with this surveillance and had performed it many times without error prior to this event.
Contributing factors to the C&I technician's error were the close arrangement of the terminal boards and the similarity of the terminal boards in the cabinet. The terminal boards are mounted horizontally in a column approximately one inch apart. The terminals on the terminal boards are arranged in horizontal rows and are labelled identically which results in columns of terminalc close together with the same terminal numbers in each column.
CORRECTIVE ACTION The C&I maintenance technician who caused this event recognized his error '
in connecting the millivolt source to the wrong terminals; therefore, no specific corrective action was necessary with respect to this specific technician,
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0l 0 0l4 or 0 l5 f tKT t# e.one spese e tooemost esse es@,wist WRC perm Jap W (171 Illinois Power (IP) C&1 maintenance technicians, IP clectrical maintenance technicians, and the electrical personnel of IP's maintenance contractor (Stone and Webster Engineering Corporation) will be briefed on the need to use ladders / stools when working overhead so that they perform work at eye level.- This briefing is scheduled to be completed by December 18, 1989.
Various colored tape strips have been applied above and below the terminal strips of terminal boards in cabinets similar to illl3-P715E to enhance recognition of different terminal boards.
To provide additional assurance that an event similar to the event described in this LER will not recur. IP will revise four LD system temperature channel surveillance test procedures (including 9532.18) to include the temperature channels of each division in a single performance of the procedures. These revisions will result in a reduction in the number of times technicians must enter a cabinet to perform the surveillance tests. (The other LD system temperature channel surveillance test procedures are already formatted in this manner.)
These revisions are scheduled to be completed by March 1, 1990.
Additionally, eleven LD system temperature channel surveillance test .
procedures (including 9532.18) that do not require lifting of leads prior to connecting the millivolt source will be revised to require connection of the millivolt source leads and double verification of the connection before the millivolt source is energized. This requirement will provide additional assurance that the test leads are connected to the correct I terminals before signals are initiated to trip the temperature channels.
(The other LD system temperature channel surveillance test procedures that do require lifting of leads prior to connecting the millivolt source do not require this procedure revision, because if the leads are lifted from the wrong terminals, a trip would occur prior to connecting the millivolt source.) These revisions are scheduled to be completed by March 1, 1990.
ANALYSIS OF EVENT This event is reportable under the provisions of 10CFR50.73(a)(2)(iv) because of the automatic isolation of the RCIC system.
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0l0 0l5 or 0 l5 rens rae o no r.o.e. muncn mnsn Assessment of the nuclear safety consequences and implications of this i event indicates that this event is not nuclear safety significant. The )
RCIC system responded to the RCIC equipment area high differential :
temperature signal as designed by isolating the system. The RCIC system was in standby at the time of this event. The High Pressure Core Spray System [BC), the alternate means of providing reactor core cooling under high RPV pressure conditions, was available at the time of this event. .
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ADDITIONAL INPORMATION-No other reportable system isolations have occurred due to a similar root cause.
No components failed during this event. l l
For further information regarding this event, contact S. E. Rasor, Director - Plant Maintenance, at (217) 935-8881, extension 3204. l l
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