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{{#Wiki_filter:ACCEI ERA>ED DOCUMENT DISTRIBUTION SYSTEM REGULRY INFORMATION DISTRIBUT+
{{#Wiki_filter:ACCEI ERA>ED DOCUMENT DISTRIBUTION SYSTEM REGULRY       INFORMATION     DISTRIBUT+     SYSTEM   (RIDE)
SYSTEM (RIDE)'CCESSION NBR:9306230022 DQC.DATE: 93/06/ll NOTARIZED:
'CCESSION NBR:9306230022             DQC.DATE: 93/06/ll NOTARIZED: NO                 DOCKET  ¹ FACIL.50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe                   05000397 AUTH. NAME           AUTHOR AFFILIATION MACKAMAN,C.D.       Washington Public Power Supply 'System PARRISHFJ.V.         Washington Public Power Supply System RECIP.NAME           RECIPIENT AFFILIATION
NO FACIL.50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe AUTH.NAME AUTHOR AFFILIATION MACKAMAN,C.D.
Washington Public Power Supply'System PARRISHFJ.V.
Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION DOCKET¹05000397


==SUBJECT:==
==SUBJECT:==
LER 93-002-01:on 930121,low RPV level reactor scram initiated by RPS in response to low water level condition.
LER   93-002-01:on 930121,low         RPV level reactor scram initiated by RPS in response           to low water level condition.
Caused by inadvertent actuation of deluge sys.Plant Procedure PPM 8.3.120 will be revised.W/930611 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), incident Rpt, etc.NOTES: RECIPIENT ID CODE/NAME PDV LA CLIFFORD,J INTERNAL: ACNW AEOD/DQA AEOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HICB NRR/DRIL/RPEB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB EXTERNAL: EG&G BRYCE,J.H NRC PDR NSIC POOREFW.COPIES LTTR ENCL 1 1 1 1 2 2 1 1 2 2 1 1 1 1 1 1 2 2 1 1 1 1 2 2 1 1 1 1 RECIPIENT ID CODE/NAME PDV PD ACRS AEOD/DSP/TPAB NRR/DE/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPW/OEAB NRR/DSSA/SPLB
Caused by inadvertent actuation of deluge sys.Plant Procedure   PPM   8.3.120     will be revised.W/930611   ltr.
~EG Fi 02 RGN5 FILE 01 L ST LOBBY WARD NSIC MURPHY,G.A NUDOCS FULL TXT COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 l 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
DISTRIBUTION CODE: IE22T         COPIES RECEIVED:LTR           ENCL       SIZE:
PLEASE HELP US TQ REDUCE WASTE}CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.504-2065)TO EUMINATE YOUR NAME FROM DISIRIBUTIQN LISTS FOR DOCUMENTS YOU DON'T NEED1 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32 i+~WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O.Box 968~3000 George Washington Way~Richland, Washington 99352 June 11, 1993 G02-93-148 Docket No.50-397 Document Control Desk U.S.Nuclear Regulatory Commission Washington, D.C.20555  
TITLE: 50.73/50.9 Licensee         Event   Report   (LER), incident Rpt,   etc.
NOTES:
RECIPIENT             COPIES              RECIPIENT          COPIES ID CODE/NAME           LTTR ENCL          ID CODE/NAME        LTTR ENCL PDV LA                     1      1    PDV PD                  1      1 CLIFFORD,J                 1      1 INTERNAL: ACNW                       2      2    ACRS                    2    2 AEOD/DQA                   1      1    AEOD/DSP/TPAB            1    1 AEOD/ROAB/DSP                             NRR/DE/EELB              1    1 NRR/DE/EMEB 2
1 2
1    NRR/DRCH/HHFB            1    l 1
NRR/DRCH/HICB               1      1    NRR/DRCH/HOLB            1 NRR/DRIL/RPEB               1      1    NRR/DRPW/OEAB            1    1 NRR/DRSS/PRPB               2      2    NRR/DSSA/SPLB            1    1 NRR/DSSA/SRXB               1      1    ~EG Fi          02      1    1 RES/DSIR/EIB               1      1    RGN5    FILE  01      1    1 EXTERNAL: EG&G BRYCE,J.H               2     2     L ST LOBBY WARD        1     1 NRC PDR                      1     1     NSIC MURPHY,G.A         1     1 NSIC POOREFW.              1     1     NUDOCS FULL TXT        1     1 NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TQ REDUCE WASTE} CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO EUMINATE YOUR NAME FROM DISIRIBUTIQN LISTS FOR DOCUMENTS YOU DON'T NEED1 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR               32   ENCL   32
 
i+~
WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 June 11, 1993 G02-93-148 Docket No. 50-397 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555


==Subject:==
==Subject:==
NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO.93-002-01 Transmitted herewith is Licensee Event Report No.93-002-01 for the WNP-2 Plant.This report is submitted in response to the report requirements of 10CFR50.73 and incorporates only minor administrative changes.Sincerely,.V.Parrish (Mail Drop 1023)Assistant Managing Director, Operations JVP/CDM/jd Enclosure CC: Mr.B.H.Faulkenberry, NRC-Region V Mr.R.Barr, NRC Resident Inspector (Mail Drop 901A, 2 Copies)INPO Records Center-Atlanta, GA Mr.D.L.Williams, BPA (Mail Drop 399)9'306230022 930611 PDR ADOCK 05000397 S PDR  
NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO. 93-002-01 Transmitted herewith is Licensee Event Report No. 93-002-01 for the WNP-2 Plant. This report is submitted in response to the report requirements of 10CFR50.73 and incorporates only minor administrative changes.
'LlCENSEE EAIT REPORT (LER)AGILITY NAHE (I)Wa'shin ton Nuclear Plant.-Unit 2 DOCKET NUHB R ()PAGE (3)0 5 0 0 0 3 9'7 ITLE (4)REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDW-ATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM EVENT DATE 5)HONTH DAY YEAR LER NUHBER 6)SEQUENTIAL NUHBER EVI SION UHBER REPORT DATE 7 OTHER FACILITIES INVOLVED 6)CKE YEAR FACILITY NAHES DAY HONTH NUHB R (5)0 1 2 I PERATING ODE (9)0 0 0 9 3 000 0 6 0 1 0 0 2 9 3 3 5 HIS REPORT IS SUBHITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR E: (Check one or more of the following)
Sincerely,
(11)I ONER LEVEL (10)0.402(b)0.405(a)(1)(i) 0.405(a)(1)(ii) 0.405(a)(1)(iii) 0.405(a)(1)(iv) 0.405(a)(1)(v) 0.405(C)50.36(c)(1).
      . V. Parrish (Mail Drop 1023)
0.36(c)(2) 0.73(a)(2)(i) 50.73(a)(2)(ii) 50.73(a)(2)(iii)
Assistant Managing Director, Operations JVP/CDM/jd Enclosure CC:     Mr. B. H. Faulkenberry, NRC - Region V Mr. R. Barr, NRC Resident Inspector (Mail Drop 901A, 2 Copies)
X 50.73(a)(2)(iv) 50.73(a)(2)(v) 0.73(a)(2)(vii) 0.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 0.73(a)(2)(x) 77.71(b)73.73(c)THER (Specify in Abstract elow and in Text, NRC orm 366A)LICENSEE CONTACT FOR THIS LER (12)C.D.Mackaman, Compliance Engineer REA CODE TELEPHONE NUMBER 0 9 7 7-4 4 5 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEH COMPONENT MANUFACTURER EPORTABLE 0 NPRDS CAUSE SYSTEH COMPONENT HANUFACTURER EPORTABLE TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (If yes, carpiete EXPECTED SUBHISSION DATE)NO TRACT nlO XPECTED SUBMISSION MONTH DAY YEAR ATE (15)On January 21, 1993, at 0948 hours, a low Reactor Pressure Vessel (RPV)level reactor scram was initiated by the Reactor Protection System (RPS)in response to an actual low water level condition.
INPO Records Center - Atlanta, GA Mr. D. L. Williams, BPA (Mail Drop 399) 9'306230022 930611 PDR   ADOCK 05000397 S                     PDR
The low RPV level was caused by a"high thrust bearing wear" trip of the Reactor Feedwater (RFW)Pump 1A turbine, The trip signal was generated as a result of wetted vibration sensing circuitry caused by an inadvertent actuation of the RFW Pump Room"A" fire protection deluge system.The remaining RFW pump was unable to supply enough water to maintain RPV level above the reactor scram setpoint.This was due to the failure of the Reactor Recirculation (RRC)Pump Flow Control Valves to automatically reposition (runback)to reduce'eactor power and steam flow to within the capacity of one RFW pump.The immediate corrective action was prompt response by the Plant Operators to bring the plant to a safe shutdown condition in accordance with approved Plant Operating Procedures.
 
                        'LlCENSEE       EAIT REPORT               (LER)
AGILITY NAHE     (I)                                                                               DOCKET NUHB R ( )                      PAGE  (3)
Wa'shin ton         Nuclear Plant .- Unit           2                                           0   5   0   0   0   3   9   '7 ITLE (4)
REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDW-ATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM EVENT DATE     5)               LER NUHBER   6)                 REPORT DATE     7                   OTHER FACILITIES INVOLVED 6)
HONTH      DAY            YEAR    SEQUENTIAL      EVI SION    HONTH    DAY    YEAR   FACILITY NAHES                                   CKE  NUHB R (5)
NUHBER          UHBER 0 0 0 0      1   2   I     3  9   3    0   0   2      0     1      0   6         9   3                                                   5 000 PERATING                  HIS REPORT IS SUBHITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR E: (Check one             or more of the following) (11)
ODE    (9)           I ONER LEVEL                     0.402(b)                       0.405(C)                  X  50.73(a)(2)(iv)                 77.71(b)
(10)                           0.405(a)(1)(i)                 50.36(c)(1).                 50.73(a)(2)(v)                  73.73(c) 0.405(a)(1)(ii)                 0.36(c)(2)                   0.73(a)(2)(vii)                 THER  (Specify in Abstract 0.405(a)(1)(iii)               0.73(a)(2)(i)                 0.73(a)(2)(viii)(A)             elow and in Text,    NRC 0.405(a)(1)(iv)               50.73(a)(2)(ii)               50.73(a)(2)(viii)(B)              orm 366A) 0.405(a)(1)(v)                 50.73(a)(2)(iii)               0.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER       (12)
TELEPHONE NUMBER REA CODE C. D. Mackaman,             Compliance Engineer 0   9       7   7   -     4   4   5   1 COMPLETE ONE LINE   FOR EACH COMPONENT   FAILURE DESCRIBED IN THIS REPORT       (13)
CAUSE       SYSTEH     COMPONENT     MANUFACTURER     EPORTABLE           CAUSE     SYSTEH       COMPONENT       HANUFACTURER       EPORTABLE 0  NPRDS                                                                        TO NPRDS SUPPLEMENTAL REPORT EXPECTED       (14)                                     XPECTED SUBMISSION        MONTH  DAY  YEAR ATE (15)
YES   (If yes,   carpiete EXPECTED SUBHISSION DATE)         NO TRACT nlO On January 21, 1993, at 0948 hours, a low Reactor Pressure Vessel (RPV) level reactor scram was initiated by the Reactor Protection System (RPS) in response to an actual low water level condition. The low RPV level was caused by a "high thrust bearing wear" trip of the Reactor Feedwater (RFW)
Pump 1A turbine, The trip signal was generated as a result of wetted vibration sensing circuitry caused by an inadvertent actuation of the RFW Pump Room "A" fire protection deluge system. The remaining RFW pump was unable to supply enough water to maintain RPV level above the reactor scram setpoint.
This was due to the failure of the Reactor Recirculation (RRC) Pump Flow Control Valves to automatically reposition (runback) to reduce'eactor power and steam flow to within the capacity of one RFW pump.
The immediate corrective action was prompt response by the Plant Operators to bring the plant to a safe shutdown condition in accordance with approved Plant Operating Procedures.
Three root causes for this event have been identified:
Three root causes for this event have been identified:
1.Personnel/work practices error causing the inadvertent actuation of the RFW Pump Room"A" fire protection deluge.
: 1.         Personnel/work practices error causing the inadvertent actuation of the RFW Pump Room "A" fire protection deluge.
LICENSEE EVENT REPOQLER)TEXT CONTINUATION ACILlTY MAME (i)Washington Nuclear Plant-Unit 2 DOCKET NUMBER (2)0 5 0 0 0 3 9 7 LER MUMBER (8)Year umber ev.Mo.3 02 01 AGE (3)2 F 7 iTLE (4)REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM 2.Management methods/work organization planning error in that there was no method in the painting pre-job planning process to provide the painters with precautionary information relating to sensitive equipment.
 
3.Plant equipment/design configuration and analysis error in that the RFW Pump Room fire protection manual discharge stations are not well suited for an industrial machinery environment.
LICENSEE EVENT REPOQLER)
TEXT CONTINUATION ACILlTY MAME (i)                               DOCKET NUMBER (2)               LER MUMBER (8)         AGE (3)
Year     umber       ev. Mo.
Washington Nuclear Plant - Unit          2 0  5  0  0  0 3 9  7 3      02       01       2   F 7 iTLE (4)
REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM
: 2. Management methods/work organization planning error in that there was no method in the painting pre-job planning process to provide the painters with precautionary information relating to sensitive equipment.
: 3. Plant equipment/design configuration and analysis error in that the RFW Pump Room fire protection manual discharge stations are not well suited for an industrial machinery environment.
This event posed no threat to the safety of the public or plant personnel.
This event posed no threat to the safety of the public or plant personnel.
P~~PI Power Level-100%Plant Mode-1 (Power Operation)
P~~         PI Power Level - 100%
Event Descri tion On January 21, 1993, at 0945 hours, the Plant Control Room Operators received a Reactor Feedwater Pump (RFW)Pump Room"A" fire protection deluge system actuation annunciator and several alarms relevant to the auto start of the fire pumps.At 0947 hours, the Control Room Operators received the RFW Pump 1A and 1B turbine vibration trouble annunciators, followed by the RFW Pump 1A and 1B turbine high thrust bearing wear annunciators.
Plant Mode - 1 (Power Operation)
At 09:47:57 hours, the RFW Pump 1A turbine tripped, and immediately, the Reactor Pressure Vessel (RPV)level decreased from+35 inches to+30 inches (Level 4).At which point, the Reactor Recirculation (RRC)System initiated an automatic RRC Flow Control Valve (FCV)Runback as designed.The"B" FCV repositioned to 26%open and the"A" FCV repositioned to 82%open.The setpoint for both valves was 20%open.The failure of the"A" and"B" Flow Control Valves to fully reposition caused reactor power and steam flow to remain significantly above the capacity of one operating RFW pump.As a result, the remaining RFW pump (1B)was unable to supply enough water to maintain RPV level above the reactor scram setpoint, and the RPS initiated an automatic Low RPV Level 3 (+13 inches)Reactor Scram at 09:48:20 hours.Following the reactor scram, RPV level continued to decrease due to the normally encountered post scram level transient.
Event Descri tion On January 21, 1993, at 0945 hours, the Plant Control Room Operators received a Reactor Feedwater Pump (RFW) Pump Room "A" fire protection deluge system actuation annunciator and several alarms relevant to the auto start of the fire pumps. At 0947 hours, the Control Room Operators received the RFW Pump 1A and 1B turbine vibration trouble annunciators, followed by the RFW Pump 1A and 1B turbine high thrust bearing wear annunciators.
The lowest RPV level reached was-19.4 inches at 09:48:55 hours.The main turbine tripped at 09:49:28 hours in response to the reactor scram, and immediately, RPV level began,to rapidly recover due to the reduced steam flow and the continuous RFW Pump 1B feed supply.The RFW pump turbine controls could not respond quickly enough to prevent a RPV high level overshoot, and at 09:49:35 hours, the RFW Pump 1B turbine tripped on a RPV Level 8 (+54 inches)trip signal.The highest RPV level reached during the transient was+63 inches at 09:49;40 hours.All Control Rods fully inserted and no Safety Relief Valves were actuated during this event.
At 09:47:57 hours, the RFW Pump 1A turbine tripped, and immediately, the Reactor Pressure Vessel (RPV) level decreased from +35 inches to +30 inches (Level 4). At which point, the Reactor Recirculation (RRC) System initiated an automatic RRC Flow Control Valve (FCV) Runback as designed.
LICENSEE EVENT REPOSER)TEXT CONTINUATION AGILITY NAHE (1)Washington Nuclear Plant-Unit 2 OOCKET NUHBER (2)0 5 0 0 0 3 9 7 Year LER NUHBER (8)umber ev.No.3 002 01 AGE (3)3 F 7 ITLE (4)REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM In accordance with 10CFR50.72(b)(2)(ii), this event was reported to the NRC Operations Center via the Emergency Notification System at 1034 on January 21, 1993, as an unplanned automatic actuation of the Reactor Protection System (RPS).Imm i t rrecive Ac i ns The immediate corrective action by the Plant Operators was to promptly enter Emergency Operating Procedure (EOP)5.1~1, Reactor Pressure Vessel Power, Level, and Pressure Control, and initiate a Manual Scram (four seconds after the automatic low RPV level scram).Pressure reduction was commenced at approximately 8 psi/min in anticipation of utilizing the Condensate Booster Pu'mps for level control.Reactor Core Isolation Cooling (RCIC)was manually initiated to maintain RPV level in the normal range, and the plant was brought to a safe shutdown condition in accordance with Reactor Scram Recovery Procedure PPM 3.3.1.F rther Evalu tion and rrective Action hrEv i n This event is being reported as an event that resulted in automatic actuation of the Reactor Protection System (RPS)in accordance with the requirements of 10CFR50.73(a)(2)(iv).
The "B" FCV repositioned to 26% open and the "A" FCV repositioned to 82% open. The setpoint for both valves was 20% open. The failure of the "A" and "B" Flow Control Valves to fully reposition caused reactor power and steam flow to remain significantly above the capacity of one operating RFW pump. As a result, the remaining RFW pump (1B) was unable to supply enough water to maintain RPV level above the reactor scram setpoint, and the RPS initiated an automatic Low RPV Level 3 (+13 inches) Reactor Scram at 09:48:20 hours.
2.There were no structures, components, or systems inoperable prior to this event that contributed to the event.3.The initial post scram investigation found that Supply System painters outside RFW Pump Room"A" had accidentally actuated a fire protection manual discharge station while preparing the area for painting.The discharge station actuation initiated the fire protection deluge system, which sprayed water on the RFW Pump turbine vibration monitoring cabinet.Water entered the cabinet causing the sensing circuitry to generate spurious RFW Pump turbine vibration trouble and high thrust bearing wear alarms, and finally, the high thrust bearing wear trip signal to the RFW Pump 1A turbine.4.Troubleshooting of the RRC Flow Control Valves found that a"Servo Error" trip of both Hydraulic Pump Units for the valves caused the incomplete automatic valve runbacks.The"Servo Error" trip signals were generated as a result of slow valve responses and reduced velocity feedback signal gains.The cumulative negative effect being enough to prevent the feedback signals from properly tracking the velocity demand signals.When the signal differentials reached their setpoints, indicating valve position control failures,"Servo Error" signals were generated to shutdown the Hydraulic Pump Units.
Following the reactor scram, RPV level continued to decrease due to the normally encountered post scram level transient. The lowest RPV level reached was -19.4 inches at 09:48:55 hours. The main turbine tripped at 09:49:28 hours in response to the reactor scram, and immediately, RPV level began,to rapidly recover due to the reduced steam flow and the continuous RFW Pump 1B feed supply. The RFW pump turbine controls could not respond quickly enough to prevent a RPV high level overshoot, and at 09:49:35 hours, the RFW Pump 1B turbine tripped on a RPV Level 8 (+54 inches) trip signal. The highest RPV level reached during the transient was +63 inches at 09:49;40 hours. All Control Rods fully inserted and no Safety Relief Valves were actuated during this event.
LICENSEE EVENT REPOQI ER)TEXT CONTINUATlON ACILITY NAME (i)Washington Nuclear Plant-Unit 2 DOCKET NUMBER (2).0 5 0 0 0 3.9 7 ev.No.3 002 01 LER NUMBER (8)ear'lumber AGE (3)4 F 7 ITLE (4)REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM Root Cause Three root causes for this event have been identified:
 
Personnel/work practices error causing the inadvertent actuation of, the RFW Pump Room"A" fire protection deluge system via the local manual discharge station.This initial root cause is considered by Supply System Management to be the primary cause of the chain of events that ultimately led to the reactor scram.2.Management methods/work organization planning error in that there was no method in the painting pre-job planning process to identify sensitive system specific equipment and provide the painters with precautionary information r'elating to the equipment.
LICENSEE EVENT REPOSER)
3.Plant equipment/design configuration and analysis error in that the RFW Pump Room fire protection manual discharge stations are of an older single action pull type not well suited for an industrial machinery environment.
TEXT CONTINUATION AGILITY NAHE (1)                                 OOCKET NUHBER   (2)               LER NUHBER (8)         AGE (3)
This type of pull station is designed for ease of manipulation (i.e., schools, public buildings, etc.), making it vulnerable to inadvertent actuation when located where incidental contact is likely during machinery maintenance and inspections.
Year      umber       ev. No.
WNP-2 has experienced inadvertent actuations of similar (alarm only)pull stations in the past.Two contributing causes for this event have been identified:
Washington Nuclear Plant - Unit          2 9
0  5  0    0  0 3   7 3    002       01         3   F 7 ITLE (4)
REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM In accordance with 10CFR50.72(b)(2)(ii), this event was reported to the NRC Operations Center via the Emergency Notification System at 1034 on January 21, 1993, as an unplanned automatic actuation of the Reactor Protection System (RPS).
Imm     i t   rrecive Ac i   ns The immediate corrective action by the Plant Operators was to promptly enter Emergency Operating Procedure (EOP) 5.1 1, Reactor Pressure Vessel Power, Level, and Pressure Control, and initiate a Manual
                        ~
Scram (four seconds after the automatic low RPV level scram). Pressure reduction was commenced at approximately 8 psi/min in anticipation of utilizing the Condensate Booster Pu'mps for level control.
Reactor Core Isolation Cooling (RCIC) was manually initiated to maintain RPV level in the normal range, and the plant was brought to a safe shutdown condition in accordance with Reactor Scram Recovery Procedure PPM 3.3.1.
F rther Evalu tion and       rrective Action hrEv       i n This event is being reported as an event that resulted in automatic actuation of the Reactor Protection System (RPS) in accordance with the requirements of 10CFR50.73(a)(2)(iv).
: 2.         There were no structures, components, or systems inoperable prior to this event that contributed to the event.
: 3.         The initial post scram investigation found that Supply System painters outside RFW Pump Room "A" had accidentally actuated a fire protection manual discharge station while preparing the area for painting. The discharge station actuation initiated the fire protection deluge system, which sprayed water on the RFW Pump turbine vibration monitoring cabinet.
Water entered the cabinet causing the sensing circuitry to generate spurious RFW Pump turbine vibration trouble and high thrust bearing wear alarms, and finally, the high thrust bearing wear trip signal to the RFW Pump 1A turbine.
: 4.         Troubleshooting of the RRC Flow Control Valves found that a "Servo Error" trip of both Hydraulic Pump Units for the valves caused the incomplete automatic valve runbacks. The "Servo Error" trip signals were generated as a result of slow valve responses and reduced velocity feedback signal gains. The cumulative negative effect being enough to prevent the feedback signals from properly tracking the velocity demand signals. When the signal differentials reached their setpoints, indicating valve position control failures, "Servo Error" signals were generated to shutdown the Hydraulic Pump Units.
 
LICENSEE EVENT REPOQI ER)
TEXT CONTINUATlON ACILITY NAME (i)                               DOCKET NUMBER  (2) .              LER NUMBER (8)        AGE (3) ear    'lumber      ev. No.
Washington Nuclear Plant - Unit         2 0   5   0   0   0   3 .9 7 3     002       01         4   F 7 ITLE (4)
REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM Root Cause Three root causes for this event have been identified:
Personnel/work practices error causing the inadvertent actuation of,the RFW Pump Room "A" fire protection deluge system via the local manual discharge station. This initial root cause is considered by Supply System Management to be the primary cause of the chain of events that ultimately led to the reactor scram.
: 2.         Management methods/work organization planning error in that there was no method in the painting pre-job planning process to identify sensitive system specific equipment and provide the painters with precautionary information r'elating to the equipment.
: 3.         Plant equipment/design configuration and analysis error in that the RFW Pump Room fire protection manual discharge stations are of an older single action pull type not well suited for an industrial machinery environment. This type of pull station is designed for ease of manipulation (i.e., schools, public buildings, etc.), making it vulnerable to inadvertent actuation when located where incidental contact is likely during machinery maintenance and inspections. WNP-2 has experienced inadvertent actuations of similar (alarm only) pull stations in the past.
Two contributing causes for this event have been identified:
The failure of system design reviews and,analyses to anticipate the negative effects of component interactions following system design changes, modifications and maintenance.
The failure of system design reviews and,analyses to anticipate the negative effects of component interactions following system design changes, modifications and maintenance.
The combined negative effects of the component interactions caused the"Servo Error" trip of both Hydraulic Pump Units for the RRC Flow Control Valves, which resulted in incomplete automatic valve runbacks.The design changes, modifications and maintenance to the Flow Control Valves, Hydraulic Power Units, and the associated electronics in 1989 and 1990 resulted in slowed valve responses and reduced velocity feedback signal gains.The affected components were satisfactorily retested in accordance with Maintenance Work Request (MWR)post maintenance test requirements.
The combined negative effects of the component interactions caused the "Servo Error" trip of both Hydraulic Pump Units for the RRC Flow Control Valves, which resulted in incomplete automatic valve runbacks. The design changes, modifications and maintenance to the Flow Control Valves, Hydraulic Power Units, and the associated electronics in 1989 and 1990 resulted in slowed valve responses and reduced velocity feedback signal gains. The affected components were satisfactorily retested in accordance with Maintenance Work Request (MWR) post maintenance test requirements. However, the Flow Control Valve Runback system was not reviewed for the cumulative effects of the component work, or functionally tested as a system, since full runback conditions could not be simulated during plant shutdown.
However, the Flow Control Valve Runback system was not reviewed for the cumulative effects of the component work, or functionally tested as a system, since full runback conditions could not be simulated during plant shutdown.2.The inability of the RFW pump vibration monitoring cabinet to protect the sensing circuitry from the fire protection deluge system water spray.Water entering the cabinet caused the sensing circuitry to generate a spurious high thrust bearing wear trip signal to the RFW Pump 1A turbine.
: 2.         The inability of the RFW pump vibration monitoring cabinet to protect the sensing circuitry from the fire protection deluge system water spray. Water entering the cabinet caused the sensing circuitry to generate a spurious high thrust bearing wear trip signal to the RFW Pump 1A turbine.
LICENSEE EVENT REPO LER)TEXT CONTINUATION AGILITY NAHE (1)Washington Nuclear Plant-Unit 2 DOCKET NUHBER (2)0 5 0 0 0 3 9 7 LER NUHBER (8)ear umber ev.No.AGE (3)3 002 01 5 F 7 ITLE (4)REACTOR'SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM Fu her rrective A ion Disciplinary action, including time off without pay, was taken against the painter who actuated the fire protection manual discharge station, his work partner and their supervisor.
 
Completed February 5, 1993.2.Conduct a"time out" session with the painters to re-emphasize the importance of constant vigilance when working around plant equipment.
LICENSEE EVENT REPO               LER)
Completed January 25, 1993.3.The RFW Pump vibration monitoring cabinet was inspected, dried'ut, cleaned, refurbished and tested with assistance from a manufacturer's representative called in for an independent system assessment.
TEXT CONTINUATION AGILITY NAHE (1)                               DOCKET NUHBER   (2)               LER NUHBER (8)        AGE (3) ear     umber       ev. No.
MWR AP2112 completed January 25, 1993.4 Proper operation of the RFW pump and turbine thrust bearing wear sensing circuits was verified.MWR AP2113 completed January 26, 1993.5.Velocity signal conditioning modules are located in the output circuits of the Flow Control Valve motion sensing Linear Variable Transformers to provide a velocity feedback signal output.The modules were readjusted and tested to produce the proper velocity feedback signal gains to track the velocity demand signals.MWR AP2142 completed January 29, 1993.NOTE: Supply System Management elected not to perform a runback test of the RRC Flow Control Valves since the test must be performed at full reactor power and could subject the plant to an undesirable transient; The runback control system is a commercial feature designed to enhance operational reliability, and not an engineered safety feature.Therefore, it is management's view that it would not be in the best interest of the plant to test a non-safety feature by potentially challenging safety features.However, the Supply System has the capability to evaluate system performance following future runback events.Furthermore, there was a significant amount of knowledge and information gained during the troubleshooting of the runback control system for this event..As a result, there is reasonable assurance that the post maintenance testing performed following completion of Corrective Action 5 (above)was adequate to ensure proper operation of the runback system.6.Design, fabricate and install a temporary water shield for the RFW Pump vibration monitoring cabinet.MWR AP2167 completed January 26, 1993.7.Procure and install permanent protective covers for the fire protection deluge system manual discharge stations located in RFW Pump Rooms A and B.This action to be completed by June 15, 1993.
Washington Nuclear Plant - Unit          2 0  0 3 9  7 0  5  0 3     002       01         5   F 7 ITLE (4)
LICENSEE EVENT REPOR ER)TEXT CONTINUATION AGILITY NAME (1)Washington Nuclear Plant-Unit 2 DOCKET NUMBER (2)0 5 0 0 0 3 9 7 Year LER NUMBER (8)umber ev.No.3 02 1 AGE (3)6 F 7 ITLE (4)REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM 8.Perform an evaluation to identify other systems and components important to plant operational reliability which are vulnerable to failure due to fire protection deluge system actuation.
REACTOR'SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM Fu her     rrective A ion Disciplinary action, including time off without pay, was taken against the painter who actuated the fire protection manual discharge station, his work partner and their supervisor.
Provide recommendations for corrective action.This action to be completed by March 15, 1993.9.Review the manual discharge stations located within the plant.Evaluate each station for proper mounting location and provide recommendations for either installation of permanent protective covers, or replacement with the'new'ual action type station.This action to be completed by March 15, 1993.10, Replace the temporary water shield for the RFW pump vibration monitoring cabinet with a permanent shield or vendor supplied weatherproof panels.This action to be completed by July 31, 1993.Evaluate current administrative controls and work practices for painting inside the power block..This action to be completed by April 15, 1993.12.Plant Procedure PPM 8.3.120, Recirculation Flow Control Valve-Alignment/Calibration, will be revised to include control system calibration and testing information gained during troubleshooting for this event.This action to be completed by April 15, 1993.~fi if'he Plant Operators reacted correctly in conjunction with installed plant safety systems to promptly bring the plant to a safe shutdown condition.
Completed February 5, 1993.
Although an actual RPV low level condition did exist for a short period, with vessel level decreasing to-19.4 inches, the transient was well within the bounds of WNP-2 safety analysis.A reactor scram was the appropriate plant response to an incomplete runback of the RRC Flow Control Valves during the loss of an RFW pump.In responding to the reactor scram, the plant satisfactorily demonstrated its ability to maintain adequate RPV water level under the resulting transient conditions.
: 2.         Conduct a "time out" session with the painters to re-emphasize the importance of constant vigilance when working around plant equipment. Completed January 25, 1993.
Accordingly, this event posed no threat to the safety of the public or plant personnel.
: 3.         The RFW Pump vibration monitoring cabinet was inspected, dried'ut, cleaned, refurbished and tested with assistance from a manufacturer's representative called in for an independent system assessment. MWR AP2112 completed January 25, 1993.
LICENSEE EVENT REPO+LER)TEXT CONTINUATION AGILITY NAME (1)Washington Nuclear Plant-Unit 2 DOCKET NUMBER (2)0 5 0 0 0 3 9 7 LER NUMBER (8)Year"/umber ev.No.3 02 1 AGE (3)7 F 7 ITLE (4)REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM imil r Ev n LER 89-031,"Reactor Scram Due to Low RPV Level as a Result of Loss of Reactor Feedwater Pump During Lube Oil Pump Surveillance Testing-Cause Indeterminate".
4           Proper operation of the RFW pump and turbine thrust bearing wear sensing circuits was verified. MWR AP2113 completed January 26, 1993.
The root cause of this event was'ndeterminate.
: 5.         Velocity signal conditioning modules are located in the output circuits of the Flow Control Valve motion sensing Linear Variable Transformers to provide a velocity feedback signal output. The modules were readjusted and tested to produce the proper velocity feedback signal gains to track the velocity demand signals. MWR AP2142 completed January 29, 1993.
However, a contributing factor for the reactor scram'as identified as the inappropriate RRC Flow Control Valve Runback setpoint of 30%open.This setpoint maintained reactor power and steam flow above the capability of one RFW pump, causing RPV level to decrease, resulting in a Low RPV Level 3 reactor scram.The corrective action was to reduce the valve runback setpoint to 20%open.Since no Hydraulic-Pump Units tripped, and runback appeared to function properly with the previous setpoint during the event, and during subsequent testing with the new setpoint, no further corrective action was identified.
NOTE: Supply System Management elected not to perform a runback test of the RRC Flow Control Valves since the test must be performed at full reactor power and could subject the plant to an undesirable transient; The runback control system is a commercial feature designed to enhance operational reliability, and not an engineered safety feature. Therefore, it is management's view that it would not be in the best interest of the plant to test a non-safety feature by potentially challenging safety features. However, the Supply System has the capability to evaluate system performance following future runback events. Furthermore, there was a significant amount of knowledge and information gained during the troubleshooting of the runback control system for this event.. As a result, there is reasonable assurance that the post maintenance testing performed following completion of Corrective Action 5 (above) was adequate to ensure proper operation of the runback system.
Apparently, the cumulative effects of later system work caused the current runback control system failure.~Sf*f f$ystem Q~m>~on en Reactor Pressure Vessel Reactor Recirculation System Reactor Protection System Reactor Feedwater Pump Turbine 1A Reactor Feedwater Pump Turbine 1B Reactor Feedwater Turbine I&C System Reactor Feedwater Control System Reactor Recirculation Flow Control Valve Fire Protection System (Water)AC AD JC SJ SJ JK JB AD KP RPV FU TRB TRB CAP FCV}}
: 6.         Design, fabricate and install a temporary water shield for the RFW Pump vibration monitoring cabinet. MWR AP2167 completed January 26, 1993.
: 7.         Procure and install permanent protective covers for the fire protection deluge system manual discharge stations located in RFW Pump Rooms A and B. This action to be completed by June 15, 1993.
 
LICENSEE EVENT REPOR                   ER)
TEXT CONTINUATION AGILITY NAME (1)                                   DOCKET NUMBER   (2)               LER NUMBER (8)         AGE (3)
Year      umber       ev. No.
Washington Nuclear Plant - Unit              2 0    0  0 3 9 7 0  5 3        02         1       6   F 7 ITLE (4)
REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM
: 8.         Perform an evaluation to identify other systems and components important to plant operational reliability which are vulnerable to failure due to fire protection deluge system actuation. Provide recommendations for corrective action. This action to be completed by March 15, 1993.
: 9.           Review the manual discharge stations located within the plant. Evaluate each station for proper mounting location and provide recommendations for either installation of permanent protective covers, or replacement with the 'new'ual action type station. This action to be completed by March 15, 1993.
10,           Replace the temporary water shield for the RFW pump vibration monitoring cabinet with a permanent shield or vendor supplied weatherproof panels. This action to be completed by July 31, 1993.
Evaluate current administrative controls and work practices for painting inside the power block.. This action to be completed by April 15, 1993.
: 12.           Plant Procedure PPM 8.3.120, Recirculation Flow Control Valve - Alignment/Calibration, will be revised to include control system calibration and testing information gained during troubleshooting for this event. This action to be completed by April 15, 1993.
      ~fi         if'he Plant Operators reacted correctly in conjunction with installed plant safety systems to promptly bring the plant to a safe shutdown condition. Although an actual RPV low level condition did exist for a short period, with vessel level decreasing to -19.4 inches, the transient was well within the bounds of WNP-2 safety analysis. A reactor scram was the appropriate plant response to an incomplete runback of the RRC Flow Control Valves during the loss of an RFW pump. In responding to the reactor scram, the plant satisfactorily demonstrated its ability to maintain adequate RPV water level under the resulting transient conditions. Accordingly, this event posed no threat to the safety of the public or plant personnel.
 
LICENSEE EVENT REPO+LER)
TEXT CONTINUATION AGILITY NAME (1)                               DOCKET NUMBER   (2)               LER NUMBER (8)         AGE (3)
Year   "/umber       ev. No.
Washington Nuclear Plant - Unit        2 0  5  0    0  0 3 9  7 3       02         1       7   F 7 ITLE (4)
REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM imil r Ev n LER 89-031, "Reactor Scram Due to Low RPV Level as a Result of Loss of Reactor Feedwater Pump During Lube Oil Pump Surveillance Testing - Cause Indeterminate". The root cause of this event was
  'ndeterminate. However, a contributing factor for the reactor scram'as identified as the inappropriate RRC Flow Control Valve Runback setpoint of 30% open. This setpoint maintained reactor power and steam flow above the capability of one RFW pump, causing RPV level to decrease, resulting in a Low RPV Level 3 reactor scram. The corrective action was to reduce the valve runback setpoint to 20%
open. Since no Hydraulic-Pump Units tripped, and runback appeared to function properly with the previous setpoint during the event, and during subsequent testing with the new setpoint, no further corrective action was identified. Apparently, the cumulative effects of later system work caused the current runback control system failure.
              ~Sf
                      *f                                                             f
                                                                      $ ystem         Q~m>~on en Reactor Pressure Vessel                                   AC                RPV Reactor Recirculation System                             AD                  FU Reactor Protection System                                 JC Reactor Feedwater Pump Turbine 1A                         SJ                TRB Reactor Feedwater Pump Turbine 1B                         SJ                TRB Reactor Feedwater Turbine I&C System                       JK Reactor Feedwater Control System                           JB                CAP Reactor Recirculation Flow Control Valve                   AD                FCV Fire Protection System (Water)                             KP}}

Latest revision as of 13:45, 29 October 2019

LER 93-002-01:on 930121,low RPV Level Reactor Scram Initiated by RPS in Response to Low Water Level Condition. Caused by Inadvertent Actuation of Deluge Sys.Plant Procedure PPM 8.3.120 Will Be revised.W/930611 Ltr
ML17290A456
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 06/11/1993
From: Mackaman C, Parrish J
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GO2-93-148, LER-93-002, LER-93-2, NUDOCS 9306230022
Download: ML17290A456 (9)


Text

ACCEI ERA>ED DOCUMENT DISTRIBUTION SYSTEM REGULRY INFORMATION DISTRIBUT+ SYSTEM (RIDE)

'CCESSION NBR:9306230022 DQC.DATE: 93/06/ll NOTARIZED: NO DOCKET ¹ FACIL.50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION MACKAMAN,C.D. Washington Public Power Supply 'System PARRISHFJ.V. Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 93-002-01:on 930121,low RPV level reactor scram initiated by RPS in response to low water level condition.

Caused by inadvertent actuation of deluge sys.Plant Procedure PPM 8.3.120 will be revised.W/930611 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), incident Rpt, etc.

NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PDV LA 1 1 PDV PD 1 1 CLIFFORD,J 1 1 INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DQA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP NRR/DE/EELB 1 1 NRR/DE/EMEB 2

1 2

1 NRR/DRCH/HHFB 1 l 1

NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 NRR/DRIL/RPEB 1 1 NRR/DRPW/OEAB 1 1 NRR/DRSS/PRPB 2 2 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 ~EG Fi 02 1 1 RES/DSIR/EIB 1 1 RGN5 FILE 01 1 1 EXTERNAL: EG&G BRYCE,J.H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 1 NSIC POOREFW. 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TQ REDUCE WASTE} CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO EUMINATE YOUR NAME FROM DISIRIBUTIQN LISTS FOR DOCUMENTS YOU DON'T NEED1 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32

i+~

WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 June 11, 1993 G02-93-148 Docket No. 50-397 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555

Subject:

NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO. 93-002-01 Transmitted herewith is Licensee Event Report No. 93-002-01 for the WNP-2 Plant. This report is submitted in response to the report requirements of 10CFR50.73 and incorporates only minor administrative changes.

Sincerely,

. V. Parrish (Mail Drop 1023)

Assistant Managing Director, Operations JVP/CDM/jd Enclosure CC: Mr. B. H. Faulkenberry, NRC - Region V Mr. R. Barr, NRC Resident Inspector (Mail Drop 901A, 2 Copies)

INPO Records Center - Atlanta, GA Mr. D. L. Williams, BPA (Mail Drop 399) 9'306230022 930611 PDR ADOCK 05000397 S PDR

'LlCENSEE EAIT REPORT (LER)

AGILITY NAHE (I) DOCKET NUHB R ( ) PAGE (3)

Wa'shin ton Nuclear Plant .- Unit 2 0 5 0 0 0 3 9 '7 ITLE (4)

REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDW-ATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM EVENT DATE 5) LER NUHBER 6) REPORT DATE 7 OTHER FACILITIES INVOLVED 6)

HONTH DAY YEAR SEQUENTIAL EVI SION HONTH DAY YEAR FACILITY NAHES CKE NUHB R (5)

NUHBER UHBER 0 0 0 0 1 2 I 3 9 3 0 0 2 0 1 0 6 9 3 5 000 PERATING HIS REPORT IS SUBHITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR E: (Check one or more of the following) (11)

ODE (9) I ONER LEVEL 0.402(b) 0.405(C) X 50.73(a)(2)(iv) 77.71(b)

(10) 0.405(a)(1)(i) 50.36(c)(1). 50.73(a)(2)(v) 73.73(c) 0.405(a)(1)(ii) 0.36(c)(2) 0.73(a)(2)(vii) THER (Specify in Abstract 0.405(a)(1)(iii) 0.73(a)(2)(i) 0.73(a)(2)(viii)(A) elow and in Text, NRC 0.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) orm 366A) 0.405(a)(1)(v) 50.73(a)(2)(iii) 0.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER (12)

TELEPHONE NUMBER REA CODE C. D. Mackaman, Compliance Engineer 0 9 7 7 - 4 4 5 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

CAUSE SYSTEH COMPONENT MANUFACTURER EPORTABLE CAUSE SYSTEH COMPONENT HANUFACTURER EPORTABLE 0 NPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14) XPECTED SUBMISSION MONTH DAY YEAR ATE (15)

YES (If yes, carpiete EXPECTED SUBHISSION DATE) NO TRACT nlO On January 21, 1993, at 0948 hours0.011 days <br />0.263 hours <br />0.00157 weeks <br />3.60714e-4 months <br />, a low Reactor Pressure Vessel (RPV) level reactor scram was initiated by the Reactor Protection System (RPS) in response to an actual low water level condition. The low RPV level was caused by a "high thrust bearing wear" trip of the Reactor Feedwater (RFW)

Pump 1A turbine, The trip signal was generated as a result of wetted vibration sensing circuitry caused by an inadvertent actuation of the RFW Pump Room "A" fire protection deluge system. The remaining RFW pump was unable to supply enough water to maintain RPV level above the reactor scram setpoint.

This was due to the failure of the Reactor Recirculation (RRC) Pump Flow Control Valves to automatically reposition (runback) to reduce'eactor power and steam flow to within the capacity of one RFW pump.

The immediate corrective action was prompt response by the Plant Operators to bring the plant to a safe shutdown condition in accordance with approved Plant Operating Procedures.

Three root causes for this event have been identified:

1. Personnel/work practices error causing the inadvertent actuation of the RFW Pump Room "A" fire protection deluge.

LICENSEE EVENT REPOQLER)

TEXT CONTINUATION ACILlTY MAME (i) DOCKET NUMBER (2) LER MUMBER (8) AGE (3)

Year umber ev. Mo.

Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 3 02 01 2 F 7 iTLE (4)

REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM

2. Management methods/work organization planning error in that there was no method in the painting pre-job planning process to provide the painters with precautionary information relating to sensitive equipment.
3. Plant equipment/design configuration and analysis error in that the RFW Pump Room fire protection manual discharge stations are not well suited for an industrial machinery environment.

This event posed no threat to the safety of the public or plant personnel.

P~~ PI Power Level - 100%

Plant Mode - 1 (Power Operation)

Event Descri tion On January 21, 1993, at 0945 hours0.0109 days <br />0.263 hours <br />0.00156 weeks <br />3.595725e-4 months <br />, the Plant Control Room Operators received a Reactor Feedwater Pump (RFW) Pump Room "A" fire protection deluge system actuation annunciator and several alarms relevant to the auto start of the fire pumps. At 0947 hours0.011 days <br />0.263 hours <br />0.00157 weeks <br />3.603335e-4 months <br />, the Control Room Operators received the RFW Pump 1A and 1B turbine vibration trouble annunciators, followed by the RFW Pump 1A and 1B turbine high thrust bearing wear annunciators.

At 09:47:57 hours, the RFW Pump 1A turbine tripped, and immediately, the Reactor Pressure Vessel (RPV) level decreased from +35 inches to +30 inches (Level 4). At which point, the Reactor Recirculation (RRC) System initiated an automatic RRC Flow Control Valve (FCV) Runback as designed.

The "B" FCV repositioned to 26% open and the "A" FCV repositioned to 82% open. The setpoint for both valves was 20% open. The failure of the "A" and "B" Flow Control Valves to fully reposition caused reactor power and steam flow to remain significantly above the capacity of one operating RFW pump. As a result, the remaining RFW pump (1B) was unable to supply enough water to maintain RPV level above the reactor scram setpoint, and the RPS initiated an automatic Low RPV Level 3 (+13 inches) Reactor Scram at 09:48:20 hours.

Following the reactor scram, RPV level continued to decrease due to the normally encountered post scram level transient. The lowest RPV level reached was -19.4 inches at 09:48:55 hours. The main turbine tripped at 09:49:28 hours in response to the reactor scram, and immediately, RPV level began,to rapidly recover due to the reduced steam flow and the continuous RFW Pump 1B feed supply. The RFW pump turbine controls could not respond quickly enough to prevent a RPV high level overshoot, and at 09:49:35 hours, the RFW Pump 1B turbine tripped on a RPV Level 8 (+54 inches) trip signal. The highest RPV level reached during the transient was +63 inches at 09:49;40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br />. All Control Rods fully inserted and no Safety Relief Valves were actuated during this event.

LICENSEE EVENT REPOSER)

TEXT CONTINUATION AGILITY NAHE (1) OOCKET NUHBER (2) LER NUHBER (8) AGE (3)

Year umber ev. No.

Washington Nuclear Plant - Unit 2 9

0 5 0 0 0 3 7 3 002 01 3 F 7 ITLE (4)

REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM In accordance with 10CFR50.72(b)(2)(ii), this event was reported to the NRC Operations Center via the Emergency Notification System at 1034 on January 21, 1993, as an unplanned automatic actuation of the Reactor Protection System (RPS).

Imm i t rrecive Ac i ns The immediate corrective action by the Plant Operators was to promptly enter Emergency Operating Procedure (EOP) 5.1 1, Reactor Pressure Vessel Power, Level, and Pressure Control, and initiate a Manual

~

Scram (four seconds after the automatic low RPV level scram). Pressure reduction was commenced at approximately 8 psi/min in anticipation of utilizing the Condensate Booster Pu'mps for level control.

Reactor Core Isolation Cooling (RCIC) was manually initiated to maintain RPV level in the normal range, and the plant was brought to a safe shutdown condition in accordance with Reactor Scram Recovery Procedure PPM 3.3.1.

F rther Evalu tion and rrective Action hrEv i n This event is being reported as an event that resulted in automatic actuation of the Reactor Protection System (RPS) in accordance with the requirements of 10CFR50.73(a)(2)(iv).

2. There were no structures, components, or systems inoperable prior to this event that contributed to the event.
3. The initial post scram investigation found that Supply System painters outside RFW Pump Room "A" had accidentally actuated a fire protection manual discharge station while preparing the area for painting. The discharge station actuation initiated the fire protection deluge system, which sprayed water on the RFW Pump turbine vibration monitoring cabinet.

Water entered the cabinet causing the sensing circuitry to generate spurious RFW Pump turbine vibration trouble and high thrust bearing wear alarms, and finally, the high thrust bearing wear trip signal to the RFW Pump 1A turbine.

4. Troubleshooting of the RRC Flow Control Valves found that a "Servo Error" trip of both Hydraulic Pump Units for the valves caused the incomplete automatic valve runbacks. The "Servo Error" trip signals were generated as a result of slow valve responses and reduced velocity feedback signal gains. The cumulative negative effect being enough to prevent the feedback signals from properly tracking the velocity demand signals. When the signal differentials reached their setpoints, indicating valve position control failures, "Servo Error" signals were generated to shutdown the Hydraulic Pump Units.

LICENSEE EVENT REPOQI ER)

TEXT CONTINUATlON ACILITY NAME (i) DOCKET NUMBER (2) . LER NUMBER (8) AGE (3) ear 'lumber ev. No.

Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 .9 7 3 002 01 4 F 7 ITLE (4)

REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM Root Cause Three root causes for this event have been identified:

Personnel/work practices error causing the inadvertent actuation of,the RFW Pump Room "A" fire protection deluge system via the local manual discharge station. This initial root cause is considered by Supply System Management to be the primary cause of the chain of events that ultimately led to the reactor scram.

2. Management methods/work organization planning error in that there was no method in the painting pre-job planning process to identify sensitive system specific equipment and provide the painters with precautionary information r'elating to the equipment.
3. Plant equipment/design configuration and analysis error in that the RFW Pump Room fire protection manual discharge stations are of an older single action pull type not well suited for an industrial machinery environment. This type of pull station is designed for ease of manipulation (i.e., schools, public buildings, etc.), making it vulnerable to inadvertent actuation when located where incidental contact is likely during machinery maintenance and inspections. WNP-2 has experienced inadvertent actuations of similar (alarm only) pull stations in the past.

Two contributing causes for this event have been identified:

The failure of system design reviews and,analyses to anticipate the negative effects of component interactions following system design changes, modifications and maintenance.

The combined negative effects of the component interactions caused the "Servo Error" trip of both Hydraulic Pump Units for the RRC Flow Control Valves, which resulted in incomplete automatic valve runbacks. The design changes, modifications and maintenance to the Flow Control Valves, Hydraulic Power Units, and the associated electronics in 1989 and 1990 resulted in slowed valve responses and reduced velocity feedback signal gains. The affected components were satisfactorily retested in accordance with Maintenance Work Request (MWR) post maintenance test requirements. However, the Flow Control Valve Runback system was not reviewed for the cumulative effects of the component work, or functionally tested as a system, since full runback conditions could not be simulated during plant shutdown.

2. The inability of the RFW pump vibration monitoring cabinet to protect the sensing circuitry from the fire protection deluge system water spray. Water entering the cabinet caused the sensing circuitry to generate a spurious high thrust bearing wear trip signal to the RFW Pump 1A turbine.

LICENSEE EVENT REPO LER)

TEXT CONTINUATION AGILITY NAHE (1) DOCKET NUHBER (2) LER NUHBER (8) AGE (3) ear umber ev. No.

Washington Nuclear Plant - Unit 2 0 0 3 9 7 0 5 0 3 002 01 5 F 7 ITLE (4)

REACTOR'SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM Fu her rrective A ion Disciplinary action, including time off without pay, was taken against the painter who actuated the fire protection manual discharge station, his work partner and their supervisor.

Completed February 5, 1993.

2. Conduct a "time out" session with the painters to re-emphasize the importance of constant vigilance when working around plant equipment. Completed January 25, 1993.
3. The RFW Pump vibration monitoring cabinet was inspected, dried'ut, cleaned, refurbished and tested with assistance from a manufacturer's representative called in for an independent system assessment. MWR AP2112 completed January 25, 1993.

4 Proper operation of the RFW pump and turbine thrust bearing wear sensing circuits was verified. MWR AP2113 completed January 26, 1993.

5. Velocity signal conditioning modules are located in the output circuits of the Flow Control Valve motion sensing Linear Variable Transformers to provide a velocity feedback signal output. The modules were readjusted and tested to produce the proper velocity feedback signal gains to track the velocity demand signals. MWR AP2142 completed January 29, 1993.

NOTE: Supply System Management elected not to perform a runback test of the RRC Flow Control Valves since the test must be performed at full reactor power and could subject the plant to an undesirable transient; The runback control system is a commercial feature designed to enhance operational reliability, and not an engineered safety feature. Therefore, it is management's view that it would not be in the best interest of the plant to test a non-safety feature by potentially challenging safety features. However, the Supply System has the capability to evaluate system performance following future runback events. Furthermore, there was a significant amount of knowledge and information gained during the troubleshooting of the runback control system for this event.. As a result, there is reasonable assurance that the post maintenance testing performed following completion of Corrective Action 5 (above) was adequate to ensure proper operation of the runback system.

6. Design, fabricate and install a temporary water shield for the RFW Pump vibration monitoring cabinet. MWR AP2167 completed January 26, 1993.
7. Procure and install permanent protective covers for the fire protection deluge system manual discharge stations located in RFW Pump Rooms A and B. This action to be completed by June 15, 1993.

LICENSEE EVENT REPOR ER)

TEXT CONTINUATION AGILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (8) AGE (3)

Year umber ev. No.

Washington Nuclear Plant - Unit 2 0 0 0 3 9 7 0 5 3 02 1 6 F 7 ITLE (4)

REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM

8. Perform an evaluation to identify other systems and components important to plant operational reliability which are vulnerable to failure due to fire protection deluge system actuation. Provide recommendations for corrective action. This action to be completed by March 15, 1993.
9. Review the manual discharge stations located within the plant. Evaluate each station for proper mounting location and provide recommendations for either installation of permanent protective covers, or replacement with the 'new'ual action type station. This action to be completed by March 15, 1993.

10, Replace the temporary water shield for the RFW pump vibration monitoring cabinet with a permanent shield or vendor supplied weatherproof panels. This action to be completed by July 31, 1993.

Evaluate current administrative controls and work practices for painting inside the power block.. This action to be completed by April 15, 1993.

12. Plant Procedure PPM 8.3.120, Recirculation Flow Control Valve - Alignment/Calibration, will be revised to include control system calibration and testing information gained during troubleshooting for this event. This action to be completed by April 15, 1993.

~fi if'he Plant Operators reacted correctly in conjunction with installed plant safety systems to promptly bring the plant to a safe shutdown condition. Although an actual RPV low level condition did exist for a short period, with vessel level decreasing to -19.4 inches, the transient was well within the bounds of WNP-2 safety analysis. A reactor scram was the appropriate plant response to an incomplete runback of the RRC Flow Control Valves during the loss of an RFW pump. In responding to the reactor scram, the plant satisfactorily demonstrated its ability to maintain adequate RPV water level under the resulting transient conditions. Accordingly, this event posed no threat to the safety of the public or plant personnel.

LICENSEE EVENT REPO+LER)

TEXT CONTINUATION AGILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (8) AGE (3)

Year "/umber ev. No.

Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 3 02 1 7 F 7 ITLE (4)

REACTOR SCRAM DUE TO LOW RPV LEVEL AS A RESULT OF LOSS OF REACTOR FEEDWATER PUMP CAUSED BY AN INADVERTENT ACTUATION OF THE DELUGE SYSTEM imil r Ev n LER 89-031, "Reactor Scram Due to Low RPV Level as a Result of Loss of Reactor Feedwater Pump During Lube Oil Pump Surveillance Testing - Cause Indeterminate". The root cause of this event was

'ndeterminate. However, a contributing factor for the reactor scram'as identified as the inappropriate RRC Flow Control Valve Runback setpoint of 30% open. This setpoint maintained reactor power and steam flow above the capability of one RFW pump, causing RPV level to decrease, resulting in a Low RPV Level 3 reactor scram. The corrective action was to reduce the valve runback setpoint to 20%

open. Since no Hydraulic-Pump Units tripped, and runback appeared to function properly with the previous setpoint during the event, and during subsequent testing with the new setpoint, no further corrective action was identified. Apparently, the cumulative effects of later system work caused the current runback control system failure.

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$ ystem Q~m>~on en Reactor Pressure Vessel AC RPV Reactor Recirculation System AD FU Reactor Protection System JC Reactor Feedwater Pump Turbine 1A SJ TRB Reactor Feedwater Pump Turbine 1B SJ TRB Reactor Feedwater Turbine I&C System JK Reactor Feedwater Control System JB CAP Reactor Recirculation Flow Control Valve AD FCV Fire Protection System (Water) KP