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| | issue date = 04/29/1991 | | | issue date = 04/29/1991 |
| | title = NPDES Noncompliance Notification:On 910310,bldg Sewage Collection Tank Pump Discovered to Be de-energized During Electrical Bus Outage.Caused by Inoperable Pump.Personnel to Refrain from Using Rest Rooms Until Power Restored | | | title = NPDES Noncompliance Notification:On 910310,bldg Sewage Collection Tank Pump Discovered to Be de-energized During Electrical Bus Outage.Caused by Inoperable Pump.Personnel to Refrain from Using Rest Rooms Until Power Restored |
| | author name = RICHEY R B | | | author name = Richey R |
| | author affiliation = CAROLINA POWER & LIGHT CO. | | | author affiliation = CAROLINA POWER & LIGHT CO. |
| | addressee name = | | | addressee name = |
Revision as of 07:36, 18 June 2019
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Category:NPDES NONCOMPLIANCE NOTIFICATION
MONTHYEARML18012A4201996-11-11011 November 1996 NPDES Noncompliance Notification:On 960930,exceeded Daily Max Limit & Monthly Average Limit of BOD5 During Reporting Period.Caused by Reduction in Chlorine Contact Time.Reviewed Operational Procedures ML18012A1931996-03-29029 March 1996 NPDES Noncompliance Notification:On 960326 Internal Audit Identified Concern W/Sampling Frequency for Fecal Coliform at Heec Outfall.Investigation in Progress & Upon Completion Results Will Be Communicated ML18011B0251995-09-13013 September 1995 NPDES Noncompliance Notification:On 950908,discovered Zinc Concentrations of Approx 3 Ppm in Cooling Tower Blowdown Discharge.Caused by Decrease in Ph of Cooling Tower Water. Cause of Ph Change Being Investigated ML18009A8811991-04-29029 April 1991 NPDES Noncompliance Notification:On 910310,bldg Sewage Collection Tank Pump Discovered to Be de-energized During Electrical Bus Outage.Caused by Inoperable Pump.Personnel to Refrain from Using Rest Rooms Until Power Restored ML19324B8051989-09-28028 September 1989 Forwards NPDES Wastewater Monitoring Repts for Listed Facilities 1996-03-29
[Table view] Category:TEXT-ENVIRONMENTAL REPORTS
MONTHYEARML18016A8211998-12-31031 December 1998 Number of Personnel & Man-Rem by Work & Job Functions, 1998,Harris Plant. with 990218 Ltr ML18016A9271998-12-31031 December 1998 1998 Annual Radiological Environ Operating Rept for Harris Nuclear Plant. with 990428 Ltr ML18016A9291998-12-31031 December 1998 Shnpp Unit 1 Annual Environ (Nonradiological) Operating Rept for Jan-Dec 1998. with 990428 Ltr ML18016A9331998-12-31031 December 1998 Annual Radioactive Effluent Release Rept for Jan-Dec 1998. ML18016B0191998-12-31031 December 1998 Corrected Pages to Annual Radioactive Effluent Release Rept, for 1998 for HNP ML18016A3301997-12-31031 December 1997 1997 Annual Operating Rept of Individuals Receiving Exposures Greater than 100Mr/Yr. W/980226 Ltr ML18016A4071997-12-31031 December 1997 Annual Environ (Nonradiological) Operating Rept,App B for 970101-1231. W/980427 Ltr ML18016A4081997-12-31031 December 1997 Radiological Environ Operating Rept for 1997. W/980428 Ltr ML18016A4121997-12-31031 December 1997 Annual Radioactive Effluent Release Rept for Jan-Dec 1997. ML18022B0141996-12-31031 December 1996 Annual Radioactive Effluent Release Rept 960101-1231. W/970414 Ltr ML18012A5401996-12-31031 December 1996 Numbers of Personnel & Man-Rem by Work & Job Function,1996 Harris Plant. W/970227 Ltr ML18012A6381996-12-31031 December 1996 Annual Environ (Non-Radiological) Operating Rept,App B for 960101-1231. W/970428 Ltr ML18012A7541996-12-31031 December 1996 Radiological Environ Operating Rept for Shearon Harris Nuclear Power Plant,Jan-Dec 1996. ML18012A7771996-12-31031 December 1996 Annual Radiological Environ Operating Rept for 1996. W/ 970428 Ltr ML18012A4201996-11-11011 November 1996 NPDES Noncompliance Notification:On 960930,exceeded Daily Max Limit & Monthly Average Limit of BOD5 During Reporting Period.Caused by Reduction in Chlorine Contact Time.Reviewed Operational Procedures ML18012A4281996-10-31031 October 1996 NPDES Discharge Monitoring Rept for Oct 1996 for Perry Nuclear Power Plant. W/961115 Ltr ML18012A1931996-03-29029 March 1996 NPDES Noncompliance Notification:On 960326 Internal Audit Identified Concern W/Sampling Frequency for Fecal Coliform at Heec Outfall.Investigation in Progress & Upon Completion Results Will Be Communicated ML18012A1471995-12-31031 December 1995 Number of Personnel & Man-Rem by Work & Job Function,1995. W/960221 Ltr ML18012A2401995-12-31031 December 1995 Annual Environ (Nonradiological) Operating Rept,App B for Jan-Dec 1995. W/960430 Ltr ML18012A2391995-12-31031 December 1995 Annual Radioactive Effluent Release Rept Jan-Dec 1995. W/ 960430 Ltr ML18012A2341995-12-31031 December 1995 1995 Annual Radiological Environ Operating Rept,Vols I- Iii. W/960429 Ltr ML18011B0251995-09-13013 September 1995 NPDES Noncompliance Notification:On 950908,discovered Zinc Concentrations of Approx 3 Ppm in Cooling Tower Blowdown Discharge.Caused by Decrease in Ph of Cooling Tower Water. Cause of Ph Change Being Investigated ML18022A9601994-12-31031 December 1994 Annual Environ (Nonradiological) Operating Rept for Jan -Dec 1994. W/ 950421 Ltr ML18022A9541994-12-31031 December 1994 Radiological Environ Operating Rept, Vols I,Ii & Iii.W/ 950421 Ltr ML18011B0801994-12-31031 December 1994 Revised Semi-Annual Effluent Release Rept for Period of Jul-Dec 1994. ML18011A8021994-12-31031 December 1994 Semiannual Radioactive Release Rept Jul-Dec 1994. ML18011A7961994-12-31031 December 1994 Annual Operating Rept, Consisting of Info Re Number of Individuals Receiving Exposures Greater than 100 Mrem/Yr, Primary Coolant Iodine Spikes & Challenges to PORVs & Safety Valves for 1994.W/950223 Ltr ML18011A5571994-06-30030 June 1994 Semiannual Radioactive Effluent Release Rept for Jan-June 1994. ML18011A3571993-12-31031 December 1993 Annual Operating Rept for 1993, Including Number of Personnel & man-rem by Work & Job Function,Primary Coolant Iodine Spikes & Primary Relief & Safety Valve challenges.W/940225 Ltr ML18011A3591993-12-31031 December 1993 Semiannual Radioactive Effluent Release Rept Jul-Dec 1993. W/940228 Ltr ML18011A4041993-12-31031 December 1993 Vols 1,2 & 3 of Radiological Environ Operating Rept 1993. ML18011A4241993-12-31031 December 1993 Shnpp Unit 1 Annual Environ (Nonradiological) Operating Rept,App B,Jan-Dec 1993. W/940428 Ltr ML18011A1171993-06-30030 June 1993 Semiannual Radioactive Effluent Release Rept Jan-June 1993. ML18010B0831992-12-31031 December 1992 Radiological Environ Operating Rept,1992 for Shearon Harris Nuclear Power Plant. W/930429 Ltr ML18010B0821992-12-31031 December 1992 Annual Environ (Non-Radiological) Operating Rept. W/930430 Ltr ML18010B0601992-12-31031 December 1992 1992 Statistical Summary Rept for Shearon Harris Nuclear Power Plant,Unit 1, Per 10CFR20.407.W/930312 Ltr ML18010B0181992-12-31031 December 1992 Semiannual Radioactive Effluent Release Rept,Jul-Dec 1992. W/930224 Ltr ML18010A7291992-06-30030 June 1992 Semiannual Radioactive Effluent Release Rept,Jan-June 1992. W/920827 Ltr ML18010A5491991-12-31031 December 1991 Personnel & Man-Rem by Work & Job Function for 1991. W/ 920224 Ltr ML18010A6301991-12-31031 December 1991 Amended Shearon Harris Annual Operating Rept for 1991. ML18010A6111991-12-31031 December 1991 Radiological Environ Operating Rept 1991,Harris Nuclear Project. ML18010A5341991-12-31031 December 1991 Annual Personnel Monitoring Rept for Shearon Harris Nuclear Power Plant for 1991. W/920218 Ltr ML18010A6141991-12-31031 December 1991 Radiological Environ Operating Rept,Vol III,Jul-Dec 1991 Sample Analyses Data. ML18010A6151991-12-31031 December 1991 Annual Environ (Nonradiological) Operating Rept,1991. W/920424 Ltr ML18010A5451991-12-31031 December 1991 Semiannual Radioactive Effluent Release Rept for Jul-Dec 1991. ML18010A3731991-06-30030 June 1991 Semiannual Radioactive Effluent Release Rept,Jan-June 1991. W/910830 Ltr ML18010A6131991-06-30030 June 1991 Radiological Environ Operating Rept,Vol II,Jan-June 1991, Sample Analyses Data. ML18009A8811991-04-29029 April 1991 NPDES Noncompliance Notification:On 910310,bldg Sewage Collection Tank Pump Discovered to Be de-energized During Electrical Bus Outage.Caused by Inoperable Pump.Personnel to Refrain from Using Rest Rooms Until Power Restored ML18009A8751990-12-31031 December 1990 Annual Environ (Nonradiological) Operating Rept for 1990. W/910422 Ltr ML18009A8221990-12-31031 December 1990 Semiannual Radioactive Release Rept,Jul-Dec 1990. W/910227 Ltr 1998-12-31
[Table view] |
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P~CCELERATED DI<UTION DEMONS'TION SYSTEM I'OTES:Application for permit renewal filed.RECIPIENT, COPIES ID CODE/NAME LTTR ENCL PD2-1 LA.1 1 BECKER,D 1 1 RECIPIENT'D CODE/NAME PD2-1 PD COPIES LTTR ENCL 1 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)4 ACCESSION NBR:9105060044 DOC.DATE: 91/04/29 NOTARIZED:
NO FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina AUTH.NAME AUTHOR AFFILIATION RICHEY,R.B.
Carolina Power 6 Light Co.RECIP.NAME RECIPIENT AFFILIATION-Document Control Branch (Document Control Desk)SUBJECT-: NPDES noncompliance notification:on 910310,bldg sewage collection tank pump discovered to be de-energized during electrical bus outage.Caused by inoperable pump.Personnel refrain from using rest rooms until power restored.DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR (ENCL C SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.DOCKET 05000400 D/05000400 A D D INTERNAL ACNW AEOD/DOA-AEOD/ROAB/DSP NRR/DET/EMEB 7E'RR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB 7E NRR/DST/SRXB 8E RES/DSIR/EIB EXTERNAL: EG&G BRYCE,J.H NRC PDR NSIC POORE,W.2 2 1" 1 2 2 1 1 1 1 2 2 1 1 1 1 1 1 3 3 1 1 1 1 ACRS AEOD/DSP/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFB11 NRR/DOEA/OEAB NRR/DST/SELB 8D NRR/DS PLB8D1 E 02~RG FILE 01 L ST LOBBY WARD NSIC MURPHYiG~A NUDOCS FULL TXT 2 2 1 1 1 1 1 1 1'1 1 1 1 1.1 1 1 1 1.1 1 1 1 1 R D NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE O'ASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM P!-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 33 ENCL 33 D D
Carolina Power&Light Company P,O.Box 165~New Hill;N.C.27562 R.B.RICHEY Vice President Harris Nuclear Project HARRIS NUCLEAR PROJECT PE 0.Box 165 New Hill, North Carolina 27562'PR 2 9 1991 Letter Number'.HO-910055 (0)United States Nuclear Regulatory Commission Document Control Desk Washington, D.C.20555 SHEARON HARRIS NUCLEAR POWER PLANT Docket No.50-400, License NPF-63 NONROUTINE REPORTEnclosed is a Nonroutine Report pursuant to Append'ix B, Section 5.4.2 of the plant Operating License.This report is a copy of the state NPDES Report as required by this Operating License subsection.
Very truly yours, MRH:kjc Enclosure Vice President Harris Nuclear Project cc: Mr.R.A.Becker Mr.S.D.Ebneter Mr.J.E.Tedrow 9105060044 91042x PDR ADOCK 0 000400 PDR MEM/HO-9100550/1/OS1
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~~*F 0 ATTACHMENT TO SHEARON HARRIS NUCLEAR POWER PLANT NPDES REPORT FOR MARCH 1991 Sewa e'Leaka e to Storm Drains At approximately 0845 on March 10,-1991, the K Building Sewage collection tank pump was discovered to be de-energized during an electrical bus outage.The inoperable pump caused the collection tank to overflow leaking about 50 gallons of raw sewage to the area catch basin.The catch basin already contained approximately 500 gallons of rain water.Upon high water level, the catcn basin pump automatically pumped the water to the storm drains.The spill was not detected in time to i'solate the catch basin since it was estimated that the power to the collection tank pump was off for about 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />'efore the spill was detected.Immediate action was taken to secure the K Building potable water supply at 0855.A plant wide announcement was made to alert K Building personnel to refrain from using the rest rooms until power was restored.The storm drain runoff collection dike at the plant boundary was checked for dissolved oxygen.This analysis showed an oxygen concentration of 3.2 ppm.A sample of a small nearby rain pool showed an oxygen concentration of 3.6 ppm, It was concluded that, the sewage would have only a minimum effect on the oxygen in the lake at the storm drain discharge point.Visual inspection of the storm drain discharge poi'nts at the plant boundary and Harris Lake showed no evidence of the sewage.The plane is evaluating this incident and will implement corrective actions as required.
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