Search by property
Jump to navigation
Jump to search
This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ENS 50055 +
- 05000286/LER-2003-002, From Indian Point Unit 3 Regarding Manual Reactor Trip for Fire in Main Turbine Insulation Due to Rearing Oil Leak +
- 05000390/LER-2001-003 +
- IR 05000416/2006010 +
- ML17317B203 +
- ML101590078 +
- ML19337B054 +
- 05000499/LER-1990-001-01, :on 900108,Train Low Steam Line Pressure Blocking Switch Placed in Blocked Position,Causing Actuation of Safety Injection & ESF Sys.Caused by Lack of Instructions.Training Program Modified +
- ML19317F534 +
- ML20082S956 +
- ML20078H071 +
- ML20117N208 +
- ML20147E199 +
- ML20141B350 +
- ML20128K650 +
- 05000461/LER-1992-010, Re-isssed LER 92-010-00:on 921122,turbine Driven RFP B Min Flow Valve Failed Open Due to Broken Instrument Air Supply Line.Copper Tubing Air Supply Line Replaced W/Flexible Stainless Steel Hoses +
- ML20198Q125 +
- ML20197H633 +
- ML20236N986 +
- IR 05000416/1985024 +
- ML20211A495 +
- 1CAN028605, Monthly Operating Rept for Jan 1986 +
- ML21116A176 +
- ML22026A206 +
- ST-HL-AE-4165, Suppl to 920430 Special Rept:On 920408,nonvalid Failure of Sdg 21 Occurred When Sdg Tripped When Released from Emergency Mode.Cause Not Determined.Power Supply Mfg by Beta Products.No Corrective Actions Warranted +
- ST-HL-AE-4094, Special Rept:On 920408,SDG 21 Tripped When Released from Emergency Mode.Cause Has Not Been Determined.Further Analysis & Investigation Performed on Sdg 21.Supplemental Rept Will Be Submitted by 920730 +
- ST-HL-AE-4065, Special Rept:On 911206,emergency Mode Sdg 23 Tripped W/No Test Mode Trips Indicated.Caused by Foreign Matl Under Seat of Check Valves Allowing Decrease in Air Pressure. Troubleshooting for Sdg 23 & 24 Has Been Completed +
- ST-HL-AE-3955, Special Rept:On 911206 & 07,standby DGs 23 & 21 Tripped W/ No Test Mode Trips Indicated When Released from Emergency Mode.Cause Not Known.Work Packages Developed to Troubleshoot Standby DGs & to Determine Causes of Trips +
- 1CAN059501, Monthly Operating Rept for Apr 1995 for ANO Unit 1 +
- ML24059A034 +
- ML24213A020 +
- 05000278/LER-1998-003-03, :on 980328,identified Failure to Meet TS for IST Stroke Timing of Msivs.Caused by Incorrect Interpretation of Required Testing Frequency.Reset Subject Surveillances to Appropriate TS Frequency +
- 05000395/LER-1987-027, :on 871029,primary & Backup Power Supply Failure Occurred Resulting in Reactor Trip & Loss of Control Functions.Caused by Failed Capacitor in Process Rack Panel Xpn 7008.Design Change Being Investigated +
- 05000335/LER-1986-010-03, :on 861006,discovered That Surveillance Interval for Testing of Charcoal Absorbers in ECCS Area Ventilation Sys Exceeded.Caused by Personnel Error.Test Sample Indicated Iodine Removal within Limits +
- 05000324/LER-1987-004-02, :on 870311,reactor Scram on Low Level Due to Loss of Uninteruptible Power Supply & Subsequent Loss of Feedwater.Caused by Noncompliance W/Procedure to Transfer Power.Motor Replaced & Sys Returned to Normal +
- 05000338/LER-1988-005, :on 880113,turbine Trip,Reactor Trip & Main Feedwater Isolation Occurred.Caused by hi-hi Level in Steam Generator Which Resulted from Generator Level Oscillations. Main & Auxiliary Feedwater Secured & Restored +
- 05000254/LER-1986-004, :on 860119,reactor Scram Occurred Due to Atws/Alternate Rod Insertion Sys Initiation.Caused by Deficiency in Procedure Used to Drain Vessel.Procedure Revised +
- 05000341/LER-1996-007, :on 960419,RCIC Sys Declared Inoperable Due to Turbine Shaft Gland Leakage.Caused by Steam Leakage Past Seat of RCIC Turbine Steam Admission Valve +
- 05000368/LER-1993-002-02, :on 931022,discovered That Containment Sump Integrity Inadequate to Prevent Entry of Foreign Matl. Caused by Initial Const Deficiency.Temporary Mod Installed to Provide Plates Over Holes +
- 05000498/LER-1991-004, :on 910215,loss of Offsite Power Actuation Occurred During Routine Maint.Caused by Lack of Attention to Work Performance Methods.Training Conducted for Maintenance Personnel +
- ML20005G490 +
- IR 05000244/1986011 +
- 05000389/LER-1999-005, :on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With +
- IR 05000410/1986009 +
- 05000440/LER-2013-003, Shutdown Required by Technical Specifications Due to RCS Pressure Boundary Leakage +
- ML19098A806 +
- ML17304A847 +
- ML20012G476 +
- ML20247K564 +
- 05000324/LER-1992-001-01, Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled +