ML17304A847

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Forwards SALP Board Repts 50-528/88-38,50-529/88-36 & 50-530/88-36 for Nov 1987 - Oct 1988.Events at Unit 1 Illustrative of Board Concern W/Early Criticality Event & Operation W/O HPSI Pump for 1.5 H
ML17304A847
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 12/23/1988
From: Martin J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Karner D
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
Shared Package
ML17304A848 List:
References
TAC-69593, TAC-69594, TAC-69595, NUDOCS 8901090153
Download: ML17304A847 (89)


See also: IR 05000528/1988038

Text

AC CELERY'TED

D1STMBt 'TlON

DEMONiTRXTION

SY~gy.

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8901090153

DOC.DATE: 88/12/23

NOTARIZED: NO

DOCKET

FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi

05000528

STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi

05000529

STN-50-530 Palo Verde Nuclear Station, Unit 3, Arizona Publi

05000530

AUTH.NAME

AUTHOR AFFILIATION

MARTIN,J.B.

Region 5, Ofc of the Director

RECIP.NAME

RECIPIENT AFFILIATION

R

KARNER, D. B.

Arizona Nuclear Power Project (formerly Arizona Public Serv

I

SUBJECT:

Forwards

SALP Board Repts 50-528/88-38,50-529/88-36

&

50-530/88-36 for Nov 1987

Oct 1988.

DISTRIBUTION CODE

IE40D

COPIES

RECEIVED:LTR

ENCL

SIZE:

TITLE: Systematic

Assessment

of Licensee

Performance

( ALP) Report

NOTES:Standardized

plant.

Standardized

plant.

Standardized

plant.

05000528/

05000529

050005'30~

RECIPIENT

ID CODE/NAME

PD5

LA

CHAN,T

DAVIS,M.J.

INTERNAL: ACRS

AEOD/DSP/TPAB

DEDRO

NRR/DLPQ/HFB 10

NRR/DOEA/EAB 11

NRR/DREP/RPB

10

NRR/DRIS/SGB

9D

NRR/PMAS/ILRB12

OE

B

,J

FIL

02

EXTERNAL: H ST

LOBBY WARD

NRC PDR

NOTES:

COPIES

LTTR ENCL

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1

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1

1

1

1

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RECIPIENT

ID CODE/NAME

PD5

PD

DAVIS,M

AEOD/DOA

COMMISSION

NRR SHANKMAN,S

NRR/DLPQ/PEB 11

NRR/DREP/EPB

10

NRR/DRIS DIR 9A

NRR/DRIS/SIB 9A

NUDOCS-ABSTRACT

OGC/HDS1

RGN5

FILE

01

LPDR

NSIC

COPIES

LTTR ENCL

1

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R

I

NIXIE K> ALL "RIDS" RECIPrWrS.

PLEASE HELP US TO REXJCE MSTE.'XM'ACT 'IHE DOCUMERZ CONTROL DESK,

ROOM Pl-37

(EXT. 20079)

KO ELQGXLTE %SR MNE HKH DISXVUBUTIGN

LISTS FOR DOCUMENTS YOU DGNiT NEED)

D

S

TOTAL NUMBER OF COPIES

REQUIRED:

LTTR

36

ENCL

35

Docket Nos. 50-528,

50-529

and 50-530

Arizona Nuclear

Power Project

P. 0.

Box 52034

Phoenix, Arizona

85072-2034

Attention:

Mr. D. B. Karner

Executive Vice President

Gentlemen:

SUBJECT:

SYSTEMATIC ASSESSMENT

OF LICENSEE

PERFORMANCE,

REPORT

NUMBERS

50-528/88-38,

50-529/88-36

AND 50-530/88-36

The

NRC Systematic

Assessment

of Licensee

Performance

(SALP) Board

has

completed its periodic evaluation of the performance of the Palo Verde Nuclear

Generating

Station for the period November

1,

1987 through October 31,

1988.

The performance of Palo Verde was evaluated

in the functional

areas

of plant

operations,

radiological controls, maintenance/surveillance,

emergency

preparedness,

security, engineering/technical

support,

and safety

assessment/quality

verification.

The criteria used in conducting this

assessment

and the

SALP Board's evaluation of your performance

in these

functional areas

are contained

in the enclosed

SALP report.

Based

upon discussions

with your staff,

a management

meeting to discuss

the

results of the

SALP Board's

assessment

has

been

scheduled for January

25,

1989, in the Region

V Conference

Room.

Arrangements for the management

meeting will be discussed

further with your staff in the near future.

Overall, the

SALP Board found the performance of licensed activities at Palo

Verde to be satisfactory

and directed

toward safe facility operation.

However,

as reflected

by the

SALP categories

assigned

to several

functional

areas,

the Board considered

the overall performance of activities to have

declined

when compared to the previous

SALP assessment

period.

Specific

areas

of concern are discussed

below.

In the functiphal.area

of operations,

the strong

performance of Unit 3

throughout )he assessment

period,

and the generally

good performance of Unit

2, particularly during the latter half of the assessment

period, were well

recognized

by the Board.

However, in assigning

a

SALP category of 3 to this

functional area,

the clearly poor performance of Unit 1 was heavily weighted

by the Board in their deliberations.

Events at Unit

1 which are illustrative

of the Board's

concern include:

(1) the early criticality event;

(2) the

sustained

inoperable condition of both trains of the safety related Essential

Chilled Mater System which occurred with the unit at full power; (3) the

~~0i0501s3 gq-23

PDR

AOOCK 0 <00052S

Q

PDC

. p)'

operation of the unit without an operable

High Pressure

Safety Injection

Pump

for about 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />

due to operator error; (4) the trip from 1005 power due to

operator error in turning the wrong disconnect

switch;

and (5) the trip from

12K power due to operator error in controlling temperature

and

power during

startup.

Additionally, the Board roted that Unit

1 tripped

on six separate

occasions

as

compared

to one trip at both Units

2 and 3.

The weak performance

of Unit I is considered

to be indicative of a failure by management

to

establish

the proper working atmosphere

at the unit in that

many of the events

which occurred at Unit

1 during the assessment

period

may have

been avoided

had the personnel

involved conducted

themselves

in

a more conservative,

questioning

manner.

The Board's

concern with your Radiation Protection

program extends

to all

three units.

Events

such

as the personnel

overexposure

at Unit 2, the

inappropriate

defeating of the lock on an entrance

to

a high radiation area at

Unit 3,

a locked high radiation area at Unit I being inadvertently left open,

and the failure of the

ALARA Board to meet for over

a year's

period, all led

the Board to conclude that

an appropriately

high level of respect for

radiation

has not been established

at Palo Verde, nor has

management

oversight

or line supervision

been sufficient to address

the numerous

problems in this

functional area.

The NRC's concern with your Radiation Protection

program is

best exemplified by our proposed

imposition of a

$200,000 civil penalty

on

December

1, 1988, for various violations of regulatory requirements

associated

with Radiation Protection.

In the functional

area of Safety Assessment/guality

Verification, the Board's

concerns

were primarily with your review of plant events

and the effectiveness

of the quality oversight groups.

Your reviews of several

significant events

were found to be weak.

These events

included the introduction of foreign

material into the reactor

vessel

at Unit 1 during refueling leading to a

stuck rod, the early criticality event at Unit I, and the personnel

overexposure

event at Unit 2.

The Board considers

the ability to thoroughly

learn -from experiences

to be critical in the operation of a nuclear reactor

facility, and, therefore,

recommends

that you consistently

demand that

critical, in-depth reviews

be conducted for all notable events.

With regard

to the quality oversight groups,

the Board concluded that they have not

demonstrated

an ability to identify major weaknesses

in the operation of the

facility prior to those

weaknesses

becoming self-revealing,

and

on occasions

where significant problem areas

were identified, the problems

were not always

elevated

to the proper level of management.

As we have discussed

with you recently,

we recognize

the plans you have

developed

to;=improve your performance

in various areas.

We generally regard

your proposed actions to be positive.

We encourage

you to follow through with

those actions, with particular attention to your efforts to recruit high

caliber personnel

to assume

presently vacant

management

positions.

l

t

t

t

~J

A management

summary of this assessment

is provided in Section II of the

enclosed

report.

Perceived

strengths

and weaknesses

and Board recommendations

are discussed

in Section

IV, Performance Analysis.

You are requested

to provide to this office, within 30 days of the management

meeting,

a written response

which addresses

the three functional

areas

assessed

by the

SALP Board as Category 3.

This response

should d'escribe

actions

which you have taken or plan to take to provide improved performance

in these functional areas.

Actions described

in previous

correspondence

may

be included

by reference if appropriate.

Your response

may also include

comments

on or amplification of the

SALP report in other areas,

as

appropriate.

In accordance

with Section

2.790 of the NRC's Rules of Practice,"

Part 2,

Title 10,

Code of Federal

Regulations,

a copy of this letter, the enclosed

SALP report,

and your response will be placed in the NRC's Public Document

Room,

The NRC's Office for Analysis

and Evaluation of Operational

Data performed

an

assessment

of licensee

event reports

submitted for Palo Verde.

This

assessment

was provided

as

an input to the

SALP process;

a copy is, therefore,

provided

as Attachment

1 to the enclosed report.

The response

requested

by this letter is not subject to the clearance

procedures

of the Office of Management

and Budget

as required

by the Paperwork

Reduction Act of 1980,

PL 96-511.

Should you have

any questions

concerning

the

SALP report,

we will be pleased

to discuss

them with you.

Sincer.e.ly,

.

~ ~

J.

B. Martin

Regional Administrator

Enclosure:

SALP Report

No. 50-528/88-38,

529/88-36,

530/88-36

Attachment

1 Enclosed in SALP Report

cc w/enclosures

( 1) and (2):

J.

G. Haynes","Vice President,

Nuclear Production

W.

F. guinnq;Director, Nuclear Safety

and Licensing

R. Papworth'",~Director, guality Assurance

State of Arizona

l

II

I'

I

1

bcc w/encl osures:

Project Inspector

Resident

Inspector

docket file

G.

Cook

B. Faulkenberry

J. Martin

Commissioners

T. Murley, Director,

NRR

M. Johnson,

OEDO

bcc w/o enclosures:

J. Zollicoffer

M. Smith

REGION V/ ot

JBurdoin

1

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125$ /88

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12@+88

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DKirsch

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COPY

7

REQUEST

COPY

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VEST COPY )

RE

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NO

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REQUEST

COPY ]

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PDR

3

YES /

NO

SALP

BOARD REPORT

U. S.

NUCLEAR REGULATORY COMMISSION

PEGION

V

SYSTEMATIC ASSESSMENT

OF LICENSEE

PERFOPMANCE

50-528/88-38,

529/88-36,

530/88-36

ARIZONA NUCLEAP,

POWER

PROJECT

PALO

VERDE NUCLEAR GENERATING STATION

NOVEMBER 1,

1987

THROUGH OCTOBER 31,

1988

TABLE OF

CONTENTS

I.

Introduction

A.

Licensee Activities

B.

Direct Inspection

and Review Activities.

II.

Summary of Results

A.

Effectiveness

of Licensee

Management

B.

Results of Board Assessment

C.

Changes

in,SALP Ratings

III. Criteria

I

IV.

Performance

Analysis

A.

. Plant Operations

B.

Radiological

Controls

C.

Maintenance/Surveillance

D.

Emergency

Preparedness

E.

Security

F.

Engineering/Technical

Support

G.

Safety Assessment/guality

Verification

V.

Supporting'ata

and Summaries

A.

Enforcement Activity

B.

Confirmation of Action Letters

C.

Other

TABLES

Table

1 - Inspection Activities and Enforcement

Summary

Table

2 - Enforcement

Items

Table

3 - Synopsis of Licensee

Event Reports

Attachment

1 - The Office for Analysis

and Evaluation of

Operational

Data

(AEOD) Input to SALP Review

Pa

e s)

1

-2

6

9

13

15

18

20

21

25

25

25

26

27-29

30-32

33-35

N/A

I

1

I .

INTRODUCTION

The Systematic

Assessment

of Licensee

Performance

(SALP) is

an

NRC staff

integrated effort to collect available observations

and data

on

a

pe'riodic'asis

and evaluate

licensee's

performance

based

on this

information.

The program is supplemental

to normal regulatory processes

used to ensure

compTia'nce with NRC rules

and regulations.

It is intended

to be sufficiently diagnostic to provide

a rational basis for allocatina

NRC resources

and to provide meaningful

feedback

to the licensee's

management

regarding

the

NRC's assessment

of their facility's performance

in each functional area.

An NRC

SALP Board,

composed of the members listed below, met in the

Region

V office on December

6,

1988, to review observations

and data

on

the licensee's

performance

in accordance

with NRC Manual Chapter 0516,

"Systematic

Assessment

of Licensee

Performance,"

dated

June

6,

1988.

The

Board's findings and

recommendations

were forwarded to the

NRC Regional

Administrator for approval

and issuance.

This report is the

NRC's assessment

of the licensee's

safety performance

at Palo Verde for the period November

1,

1987 through October

31,

1988.

The

SALP Board for Palo Verde was

composed of:

    • (i
  • S
  • +Q
  • R.
  • H
  • M

. **T

    • M
  • AT
    • J
  • p
  • L.

F. Kirsch, Director, Division of Peactor Safety

and Proiects,

Region

V (Board Chairman)

M. Knighton, Director, Project Directorate. V,

NRR

A. Richards, Acting Chief, Reactor Safety Branch

P.

Yuhas, Chief, Emergency

Preparedness

and Radiological Protection

Branch

F. Fish, Chief, Emergency

Preparedness

Section

S. North, Acting Chief, Facilities Radiological Protection Section

D. Schuster,

Chief, Safeguards

Section

L. Chan, Units

1 and

2

NRR Project Manager

J. Davis, Unit 3

NRR Project Manager

J. Polich, Senior Resident

Inspector

F. Burdoin, Project Inspector

Cillis, Senior Radiation Specialist

R. Norderhaug,

Safeguards

Inspector

  • Denotes voting member in functional area of cognizance.
    • Denotes voting member in all functional areas.

A.

Licensee Activities

In general, all three units operated satisfactorily during the

assessment

period.

Units

2 and

3 were relatively free of problems;

however,

the number

and type of events

which occurred at Unit I set

that Unit apart from Units 2 and 3.

Specific operational

events

were is follows:

I

Unit

1

Unit

1 was in its first refueling cycle at the beginning of this

assessment

period.

Startup following refueling was delayed until

March 8 because

of reactor coolant

pump shaft cracking problems

and

the binding of Control Element Assembly

(CEA) 56 during rod drop

testing.

A ball bearing

was found in the

CEA 56 Guide Tube.

On May

14 following a reactor trip, the reactor experienced

an early

criticality and

a subsequent

reactor trip while returning the unit

to service.

The reactor

was again returned to service

May 16.

On

July 6,

a

13.8KV bus fault resulted

in

a major electrical failure in

the unit auxiliary transformer,

which kept the uni t down until

Augus+

18.

The unit returned to power and operated

at essentially

100K power through the

end of the assessment

period.

Unit 2

Unit 2 entered

the assessment

period at

100K power and operated

essentially

at

1004 throughout the period until February

20,

when

the unit was

shutdown to commence its first refueling outage.

Startup initially scheduled for May 12 was delayed until early June

to complete

outage

maintenance

work and surveillance testing.

The

reactor went critical on June

18 and operated essentially

at

100K

power during the balance of the assessment

period.

Unit 3

Unit 3 was

shutdown

on the first day of the assessment

period after

having completed

low power physics testing associated

with the

issuance

of the initial low power license.

The unit was restarted

November

23 in anticipation of receiving

a full power license,

which

was issued

November 25.

Power was increased

to above

5X for the

first time on November 26.

Power ascension

testing continued with

some minor problems until January

1, when the unit was

opera+ed at

100% power for the first time.

The unit operated at essentially

full power until July 31,

when the "8" phase of the main transformer

faulted due to

a lightning strike,

and the unit was placed in

Mode 3.

The unit was returned to service

on August

18 following

repairs

to the main transformer

and the completion of other short

notice outage work.

The unit operated

at essentially

100% until the

end of the assessment

period except for a reduction to 50K on August

25 because

of a "8" main feedwater

pump problem and

a reduction to

204 on September

22 to repair

a main condenser

tube leak.

Palo Verde ended the evaluation period

on

a more positive note with

all three units operating at full power.

Unit

1 ended

the period in

its 61st continuous

day on line, Unit 2 with 131 continuous

days,

and Unit 3 with 74 continuous

days.

Direct Ins ection

and Review Activities

Approximately 5935 on-site inspection

hours

were spent in performing

a total of 49 inspections

by resident,

region-based,

headquarters,

t

and contract personnel.

Inspection activity in each functional

area

is summarized

in Table l.

II.

Summar

of Results

A.

Effectiveness

of Licensee

Manaqement

P

Overall site performance'during

.this

SALP period

has

been declining.

Since the. major- reorqanization=-of

the site in November

1987, that

separated

the single site organization into three separate

unit

organizations,

several

key manaqers

have left the organization.

The

former plant manager left the licensee after the reorganization

and

resulted

in the loss of a strong central directing force for the

site.

Other departures

from the licensee

management

team included

the sit. radiation protection manager,

central

chemistry

and

radiation protection manager,

emergency

planning manager,

and the

site maintenance

manager.

In the latter part of the

SALP period the

former Executive Vice President,

Mr. E.

E.

Van Brunt, announced

his

retirement.

The experience

level of licensee

upper management

has

.

been

a major

NRC concern for several

years.

The experience

level

has

not improved significantly as the individual units

came

on line;

and these

recent departures

have

caused

increased

concern.

The

reorganization

into three separate

unit organizations

has

placed

additional

demands

on the senior management.

There

appears

to be

a growing gap between

the site's

problems

and

the licensee 's capability to deal with them.

In response

to NRC's

concerns.

the licensee

has

announced

plans to add five senior

management

positions to the site organization.

The search for

-- - qualified personnel

to fill these positions is currently in

progress.

B.

Results of Board Assessment

Overa)1,

the

SALP Board found the performance of NRC licensed

activities by the licensee

to he acceptable

and directed

toward safe

'- operation of Palo Verde.

The

SALP Board has

made specific

recommendations

in most functional areas for licensee

management

consideration.

The results of the Board's

assessment

of the

licensee's

performance

in each functional area,

including the

previous

assessments,

are

as follows:

Functional

Area

A.

Plant Operations

B.

Radiological Controls

C.

Maintenance/Surveillance

D.

Emergency

Preparedness

E.

Securitv

F.

Engineering/Technical

Support

G.

Safety Assessment/equality

Verification

Rating

Last

Period

Ratina

This

Period

Trend

Improving

I

C.

An improvino trend is defined as:

Licensee

performance

was

determined

to be improving near the close of the assessment

period.

Chanqes

in SALP Ratinqs

The licensee's

performance

in the'lant operations

area

declined

.rom

a Cateqory

2 to

a Cateaory

3.

It is recognized that Unit 3

performance during'he

assessment

period

was

good

and several

siqnificant records. were set durina

power ascension

testinq

and

commercial operation.'nit

2 performance

was noted to have

improved

and unit management's

involvement in plant operations

increased

during the evaluation period.

The decline in performance

is

primari lv due to events

at Unit I and senior management 's irabi 1 ity

tn establish

a working atmosphere

which encourages

critical

assessment

during the conduct of operations

and is reflective of a

divergence

between

management

expectations

and staff performance.

Unit

1 operators

willingness to conduct safety significant

evolutions withou't

a questioning

and cautious attitude

overshadows

the acceptable

performance of operators

at the other two units.

The licensee's

performance

in the areas

of radiological controls

and

safety assessment/ouality

verification declined

from Category

2 to

Category

3 during this period.

The decline

in- the radiological

controls

area

is perceived

to be due to inadequate

technician

sta<fing levels, untimely replacement

of a permanent site radiatinr

protection

manager position,

and

weak training of technicians.

The licensee

performance

in the emergency

preparedness

area declined

from Category

1 to Category

2.

The cause of this is perceived to be

a reduction in upper management's

attention to the problems

in the

emergency

preparedness

program,

which contributed to

a failure to

understand

work requirements

and the necessity for adherence

to

procedures

in the

EP area.

The licensee's

performance

in the'Safety

Assessment/equality

Yerification area declined

from Category

2 to Category 3.

While'the

title of this section

changed

from the previous

SALP period the

items involved in the assessment

of this area

are essentially

the

same with the addition of licensing activities.

The decline is due

to several

failures of management

oversight

and direction,

some of

which resulted-in escalated

enforcement

actions

in the areas

of

plant operation,

radiological controls

and enqineering/technical

support.

In general,

management

failures

have combined to produce

situation's

which permit working level errors to continue to go

unchecked until the errors

are self-revealed

by events.

III. CRITERIA

,Licensee

performance

is assessed

in selected

functional areas,

depending

on whether

the facility is in

a construction or operational

phase.

Functional

areas

normally represent

areas significant to nuclear safety

and the environment.

Some functional areas

may not be assessed

because

of little or no licensee activities-or lack of meaningful observations.

Special

areas

may be added

to highlight significant observations.

The following evaluation criteria were used,

as applicable,

to assess

each functional area:

1.

Assurance of qualitv, including management

involvement

and control.

2.

Approach to resolution of technical

issues

from a safety standpoint.

3.

Pesponsiveness

to

NRC initiatives.

4.

Enforcement history.

5.

Operational

events

(including response

to, analysis of, reporting

of,

and corrective actions for events).

6.

Staffino (including management).

7.

Effectiveness

of the training and qualification program.

However, the

NRC is not limited to these criteria

and others

may have

been

used

where appropriate.

On the basis of the

NRC assessment,

each functional

area

evaluated

was

rated according

to three performance

categories.

The definitions of

these

performance

categories

are

as follows:

Cate or

1:

Licensee

management

attention

and involvement are readily

evident

and place

emphasis

on superior performance of nuclear safety or

safeguards

activiti'es, with the resulting performance substantially

exceeding

regulatory requirements.

Licensee

resources

are ample

and

effectively used

so that

a high level of plant and personnel

performance

is being achieved.

Reduced

NRC attention

may be appropriate.

Cate or

2:

Licensee

management

attention to and involvement in the

performance of nuclear safety or safeguards

activities are good.

The

licensee

has attained

a level of performance

above that needed

to meet

regulatory requirements.

Licensee

resources

are adequate

and reasonably

allocated

so that

good plant and personnel

performance is being achieved.

NRC attention

may be maintained at normal levels.

~Cate or

3:

Licensee

management

attention to and

invo1vement in the

performance

of nuclear safety

or safeguards

activities are not

sufficient.

The licensee's

performance

does

not significantly exceed

that needed

to meet minimal regulatory requirements.

Licensee

resources

appear

to be strained

or not effectively used.

NRC attention

should

be

increased

above

normal levels.

IV.

PERFORMANCE ANALYSIS

The following is the Board's

assessment

of the licensee's

performance

in

each of the ~unctional areas,

plus the Board's conclusions for each

area

t

I

}"

I

and its recommendations

with respect

to licensee

actions

and management

emphasis.

A.

Plant

0 erations

1.

~Ana1 sis

'Inaspite of'several-significant

operational

accomplishments

at

Units

2 and 3, plant operations

has declined from the previous

assessment

period.

This decline is primarily due to events at

Unit

1 and the lack of prompt and decisive efforts by corporate

senior

management

to establish

a working atmosphere

which

encourages

critical assessment

during the conduct of

operations.

This low level of self critical assessment

and

direction allowed individual unit performance

to diverge to the

'oint where Unit

1 performance

was clearly poor several

times

during this evaluation period.

Management.

also failed in their

responsibility to demand consistency

and accountability

of

overall site activities,

and failed,to take adequate, corrective

measures

when such actions

were clearly warranted.

Only in the

last month of the assessment

period were management

changes

made at Unit I and

a clear set of management

expectations

established.

During the assessment

period,

the licensee's

plant operations

activities

wer e observed routinely by both the resident

and the

regional staff.

A total of 2945 hours0.0341 days <br />0.818 hours <br />0.00487 weeks <br />0.00112 months <br /> of inspection effort

were devoted to this functional area.

The licensee

achieved

several

accomplishments

in the operations

area during this

SALP

period.

These

included

214 days of continuous

operation at

Unit 3 following a successful

power ascension

test. program

as

well as

a second

continuous

operating

run of 74 days following

only one reactor

shutdown during the commercial

operation

portion of the

SALP period.

Unit 2 had

131 days of continuous

operation following its first refueling outage.

Other positive

operational

experiences

were the problem free core reloads at

both Units

1 and 2; the core unloading,

inspection

and fuel

reconstitution at Unit 2; and the chemical

decontaminations

of

the primary coolant systems

at Units

1 and 2.

In spite of

these

accomplishments,

events did occur at Units

1

and

2 which

contribute'd negatively to the plant operating history.

These

events

were due in part to the lack of procedural

compliance,

personnel

errors,

and

a willingness

on the part of staff to

proceed with plant evolutions prior to having

a full

understanding

of the conditions relating to the evolution.

The licensee's

responsiveness

to

NRC initiatives was maintained

at about the

same level

as during the previous report.

The

licensee

accepted

NRC initiatives in a positive spirit.

While

resolution of some of the matters

are still in progress,

their

correction

has

proceeded

slower than expected.

Some of these

efforts include the need for correcting

bogus annunciators;

increasing

management

staffing; reducing

personnel

errors;

and,

in one significant case involvino an earlier than expected

H

l

)

t

criticality at Unit I, thoroughly Tdentifying the root cause of

the event.

In several

of the meetings

held between

the

NRC and

ANPP

management,

during which plant operations

were discussed,

the

licensee

expressed

a determination

to complete actions related

to initiatives wfiich would result in improved operations.

However, the repeated failure

o

managers

to devote significant

time to direct observation of plant activities is not

consistent

with ANPP management's

desire to improve activity

performance.

The licensee's

self-initiating approach

to the technical

resolution of plant problems resulting from operational

events

has

shown little improvement during the assessment

period.

Some examples of where licensee

management

resolutions

were

timely.-and technically sound

were related to the auxiliary

transformer fire (Unit I) and the replacement

of the reactor

coolant

pump shafts

(Units I and 2).

However,

both of these

issues

received

a high level of NRC attention,

and it is not

clear whether, left to their own initiative, the licensee

would

have arrived at the

same position.

Examples

where unconservative

actions

were taken'or

problem

identification was

weak included the early criticality at

Unit I where significant root causes

were not identified,

and

the failure of diesel

generator

intercooler drain plugs

on

Unit 2, three

months after the

same event occurred

on Unit 3.

.In several

of the meetings

held between

the-ANPP

and

NRC

management

the licensee

was informed that many of the problems

involving technical

issue resolutions

were related to

management's

failure to perform penetrating self-critical

assessments

of events,

and

demand that level of performance

from subordinates.

Escalated

enforcement

was taken in this functional area at

Units I and 2.

One such action dealt with

a series of

violations which were related to operating with an insufficient

number of auxiliary <eedwater

pumps,

due to an improper valve

alignment (Unit 2), failing to bypass

low pressurizer

pressure

protection

according

to procedures

which resulted

in an

engineered

safety feature actuation (Unit 2),

and entering into

Mode

4 without an operable

high pressure

safety injection pump

(Unit I).

A second

escalated

enforcement

action dealt with"

both trains of essential

chilled water inoperable

due to an

incorrect valving alignment (Unit I).

A third enforcement

action,

which is pending,

involved an earlier than expected

condition of criticality (Unit I).

In addition,

two other violations were identified in this

functional area.

These dealt with valving errors at Units I

and 3.

The number of LERs (25) submitted to the

NRC remained

the

same

as the

number submitted during the previous

SALP

period.

Nine were caused

by personnel

error.

However, of'he

operations

related

LERs, 60" (l5) of the total

and

78%%u (7) of

those

caused

by personnel

error were attributable to Unit 1.

During the

SALP period unplanned reactor trips were generally

associated

with Unit 1.

Four of the six trips which occurred

at Unit

1 were associated

with personnel

error or control

problems.

Units 2 and

3 experienced

only one unplanned

reactor

trip each during the period.

The Unit 3 trip-occurred during

power ascension

testing.and

the Unit 2 trip was

caused

by

control

prob1ems

during startup

from the refueling outage.

Four emergency diesel actuations

occurred durino the period.

One was related to an equipment malfunction, the other three

were due to personnel

or procedure

causes.

None of these

actuations

involved an interruption in plant operation.

One

safety injection/main steam isolation/containment

isolation

actuation

occurred at Unit 2 due to personnel

error.

During this

SALP period the regional licensing examiners

conducted

one replacement

examination

and

one licensed operator

requalification program evaluation.

The operator

replacement

examination results indicate that the trainino provided to

initial and upgrade

license candidates

is satisfactory.

However,

the pass/fail ratio has

decreased

during this

SALP

period from 19/1 to 18/3.

The licensed operator

requalification program evaluation indicates that the facility

training examination material, questions,

scenarios

and iob

performance

measures,

appear to be objective with evaluation

standards

that adeauately

evaluate

an operators

depth of plant

and operating

knowledge.

From the program evaluatior

and

operating

exams administered

the overall evaluation of the

licensed

operator requalification program appears

to be

satisfactory.

The licensee is involved in

a long term upgrade

program to

increase

simulator capability and fidelity to better reflect

actual plant responses.

The licensee

has

been

implementing

these

upgrades

slower than expected

due to debugging

problems

wi,th the more complex models

and the increased

licensed

operator simulator training time.

Licensed operator simulator

training time increased

from an average

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> per year

reported in the previous

SALP period to

a projected

60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br />

per year.

The narrowed window to implement the more complex

upgrades,

which require longer debugging

and testing times,

has

resulted in licensee

management

frequently having to delay

simulator training or extend

upgrade

schedules,

both of which

negatively impact effective training.

The licensee's fire protection

program has

remained

at

a high

level of performance.

Two major fires involving the Unit

1

auxiliary transformer

and the 525

KV switchvard transformer

were quickly extinguished

by the on-site fire department.

Two

ongoing unresolved matters still have not closed.

These

are

related

to inadequate fire door design

and ongoing work related

to sealing of penetrations.

Overa11,

operations

personnel

are knowledgeable

of plant system

performance

and generally

responded

properly to significant ard

complicated operational

transient

events

even

though

some of

the events

were self initiated.

Plant shift crews generally

conduct thorough shift turnovers/briefings

which include

discussions

not only with the operation staff but also include

other unit departments

such

as chemistry

and radiation

protection.

Also. t'here

have

been

several

events

during the

SALP period which led to improper isolation of equipment

due to

the failure of operating

personnel

to properly implement the

clearance

procedure.

2.

Performance

Ratin

Performance

Assessment

- Category 3, Improving

3.

Board Recommendations

The licensee

must strive to ensure

that operations

are

conducted

in

a formal, conservative

manner

at all units.

Licensee

management

should continue actions initiated to assure

that there is both sufficient management

staffing and

appropriate

management

involvement in problem evaluations

and

resolution, particularly at unit 1.

Priority attention

should

be given to conducting

thorough evaluations of problems

ard

establishing

a working atmosphere

which encourages

thoughtfully

critical assessments

of all phases

of plant operations.

B.

Radiological Controls

1.

A~nal sis

A total of eleven routine inspections

related to radiological

controls were performed

by the regional

and resident

inspection

staff during this, assessment

period.

Over 860 hours0.00995 days <br />0.239 hours <br />0.00142 weeks <br />3.2723e-4 months <br />

were

expended

in the areas of:

Organization

and Management

Occupational

Radiation Safety

Transportation of Radioactive Materials

Radiological Efflvent Control

and Monitoring

Radioactive

Waste

Management

Training and gualifications

LWR Water Chemistry Control

Licensee

Event and Special

Reports

During the previous

SALP period,

a total of three Severity

Level

IV and

one Severity Level

V violations were identified in

Unit 1, one Severity Level IV violation was identified in Unit

2 and

no violations were identified in Unit 3.

These

violations did not represent

a programatic

breakdown.

For +he

last assessment

period, the licensee

was assigned

a Category

2

rating and the board

recommended

that the licensee

improve

performance with respect

to the reduction of the numbers of

1

t

1

'I

l

10

license

event reports attributable to personnel

error, posting

requirements

and radiological controls.

During the last half of this 'assessment

period there

have

been

several

examples

where the level .of management

involvement has

not been sufficient to assure

a high level of quality

"

performance.

Specific examples

include:

key management

positions resulting from the November

1987 reorganization

remained unfilled for extended

periods,

the

ALARA-Committee

failed to meet for over

a year, ouality assurance

and other

internal audit findings were not resolved in a timely manner,

significant numbers of workers were unfamiliar with required

controls for entry into high radiation areas

and

some workers

perceived

a lack of commitment to good radiation protection

practices

on the part of ANPP management.

Following an unplanned

exposure

event in May 1988,

NRC

identified violations involving control, posting

and access

to

high radiation areas

in July, August

and September

1988.

An

Enforcement

Conference

was held

on August 17,

1988 to discuss

the unplanned

exposure

and other concerns.

The licensee's

presentation

of their assessment

of the radiation protection

program problems,

as highlighted by the unplanned

exposure

event,

was narrow and not adequate

to convince

NRC that

additional

enforcement

actions

would not be necessary.

A

second

more thorough review of the unplanned

exposure

event

was

presented

to

NRC on September

14,

1988.

This second

evaluation

was broader in scope

and indicated that the licensee

needed

to

expand

the investigative

process

in the area of problem

identification, deve1op

supervisory/management

skills and

increase

management's

awareness

of deficient conditions.

Subsequent

events

involving the prying open of a locked high

radiation area

gate at Unit 3, starting work prior to

completion'f required

ALARA reviews at Unit 2 and leaving

a

high radiation door open at Unit

1 indicated that initial

management

actions

were not fullv effective.

Following the

events

noted above,

the licensee initiated more aggressive

corrective actions including appointment of a,temporary site

Radiation Protection

Manager

and replacement

of the Unit 2

Radiation Protection

Manager.

The licensee's

resolution of a technical

issue associated

with

the decontamination

of the Unit 2 refueling cavity was

ineffective.

The planning

and schedule for accomplishing

the

work was not thorough, ponrly coordinated

and appeared

to place

operational

considerations

ahead of good radiation protection

practices.

Several

opportunities to decontaminate

the cavity

in accordance

with the nuclear industry standards,

such

as

performing

a thorough

vacuuming and/or hydrolazing of the

cavity, which could have prevented

the unplanned

exposure

event,

were missed during the refueling outage.

It appears

that additional effort is needed

in 'assuring that critical work

is thoroughly planned

and scheduled.

11

The program established

and

implemented for cortrolling hot

particles

was observed

to contain weaknesses

reflecting on the

resolution of technical

issues.

The licensee's initial program

for. controlling hot particles did not take into full account

requirements

for extremity monitoring of personnel

sorting hot

particle trash, training of personnel

in hot particle detection

and

a -rel'iable'method for calibration of instruments

used to

monitor for hot particles.

During this

SALP period the licensee

has

been generally

responsive

to

NRC initiatives and concerns.

These

included

management's

continued support of the reactor coolant

pump

bearing

and wear ring replacement

program to remove the

antimony .and cobalt containing material

in Unit 2 that had

been

conducted at Units I and

3 during the previous

SALP period.

The licensee

was effective in carrving forward to Unit 2 the

lessons

learned during the Units I and

3 antimony removal

process.

-Improved results

were obtained during the Unit'2

antimony clean-up

process

over those achieved

in Unit l.

Additional strengths

included

an

INPO accredited training

program and

an effective dosimetry program.

Housekeeping

was

effective in minimizing contaminated

areas.

As

a result of the

licensee's

efforts, discussed

above,

ANPP was well below the

1987 national

average collective dose of 371 person-rem

per

'react'or.

The licensee's

average collective dose

was

230

person-rem

per reactor,

despite

having

a partial refueling

outage in Unit I and

an initial refuelina outage in Unit 2.

The collective dose of ?.8 person-rem

in Unit 3,

a plant that

is scheduled

to undergo its first refueling outage

shor tlv,

indicates effective personnel

exposure

control consistent

with

the

ALARA concept.

This is considered

to be

a significant

-accomplishment.

Another improvement noted during this

SALP

period

was the licensee's

construction

and activation of a

permanent respiratory protection facility with state of the art

equipment for processing

respiratory equipment.

The licensee's

enforcement history during this

SALP period

included:

one apparent Severity Level III violation at Unit 2

as

a result of deficiencies identified'during the unplanned

exposure

event of Hav 23 and one apparent Severity Level III

violation .at Units

2 and

3 as

a result of the deficiencies

related

to the control, posting

and access

to high radiation

areas

which were identified during the third quarter of 1988.

The principal root causes for these

events

were attributed to

personnel

proceeding

in the face of uncertainty

and personnel

error.

These violations resulted

in an escalated

enforcement

act

on with imposition of civil penalties.

Additionally,

during this

SALP period,

there

were three Severity Level IV

violations

and two Severity Level

V violations identified at

Unit I, three Severity IV violations and one apparent Severity

Level

V violation identified at Unit 2 and one Severity Level

IV violation identified at Unit 3.

Corrective measures

for the

two apparent

Severity Level III violations were neither timely

or effective in that repeated

violations in the areas of ALARA

12

program implementation

ard posting

and control of high

radiation areas

were identified.

Additional weaknesses

identified during this

SALP period include:

(1) the use of

"permissive" terms

and lack of specificity in the radiation

protection program implementing procedures,

and (2) the failure

to implement

a coordinated,

consistent

radiation protection

prooram for the site and

each Unit.

The declining performance

in. the- radiation protection program was observed following the

,licensee's

site wide reorganization of November

1987.

Collectively, the above violations

and weaknesses

appear to

indicate that ther e has

been

a significant breakdown in the

radiation protection

program.

The number of reportable

events

in this functional area

included fourteen special

reports involving radiation

monitoring units which were reported to be inoperable for

greater

than

a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> period.

Additionally, there were

numerous

licensee

event reports

(LERs) involving the failure to

perform the sample analysis

required

by the

RETS and the

failure of process

and effluent monitoring

(PERM) equipment to

function properly.

Two of the reportable

events

were related

to the apparent Severity Level III violations that are

discussed

above.

Many of the

LERs were attributable to

personnel

error.

The number of reports attributable to

personnel

error was raised

as

a concern during the previous

SALP period.

In addition, of particular concern

was the high

incidence of reports involving the failure of PERMs to functior

properly.

It appears

that additional

management effort with

respect

to improving the reliability of the

PERMs and reducing

the number of reportable

events

due to personnel

error is

needed.

Experienced

technician staffing levels at each of the units

appeared

to be adequate

to support

normal plant operations.

Technician staffing levels of the central radiation protection

group technicians

appeared

to be marginal following the

reorganization of November 1987.

The licensee

became

aware of

this problem and took immediate action to supplement

the

central radiation group with additional

personnel

during the

last quarter of this

SALP period.

Managements

efforts to

secure

a permanent

replacement for the site Radiation

Protection

Manager position has not been effective or timely.

Weaknesses,

apparently attributable to traininq, were also

identified during this

SALP period.

These include the training

of technicians

in the methods for detecting hot particles

and

assuring that workers'nowledge

concerning control

and posting

of high radiation areas

is clearly understood.

Performance

Ratin

Performance

Assessment

- Category

3

ll

13

Based

on the serious

nature of events

and weaknesses

identified

the licensee's

performance

in this functional area

has

shown

a

significant decline from the rating assigned

during the

previous

SALP period.

3.

Board Recommendations

The licensee

should focus their immediate attention

on

completion of the assessment

of the radiation protection

program,and

implementation of corrective actions to assure

that

basic occupational

radiation protective

measures

are

accomplished.

The licensee

is encouraged

to create

a working

atmosphere

in which workers clearly understand

and discharge

their responsibilities,

are held accountable,

do not proceed

in

the face of uncertainty,

and feel comfortable

when bringing

concerns

to licensee

management

and to the NRC's attention.

Significant improvement is needed

to reduce

the

number of

events

leading to licensee

event reports attributable tn

personnel

error,-.and to improving the reliability of PERM

operatiors.

The licensee

is further encouraged

to improve the

scope

and quality of the evaluation of events

and in assuring

that corrective actions

are both timely and effective.

C.

Maintenance/Surveillance

1.

A~na1 sis

This functiona I area

was observed

routinely during the

assessment

period by both the resident

and regional

inspection

staff.

Approximately 712 hours0.00824 days <br />0.198 hours <br />0.00118 weeks <br />2.70916e-4 months <br /> of inspection effort were

devoted to this functional area.

Strengths

included the

successful

completion of several sigrificant maintenance

tasks

such

as the replacement

of the Units

1 and

2 reactor coolant-

pump shafts,

replacement

of the Units

1 and

2 auxiliary

feedwater

pump impellers within the

3 day Technical

Specification action time period

and the restoration of the

damaged auxiliary transformer

and related electrical

equipment

at Unit l.

Several

events

which reflect negatively

on the maintenance

fun'ctional" area

include the introduction of ball bearings

into

the Unit

1 Upper Guide Structure

(UGS) preventing

movement of a

Control Element Assembly

(CEA) (Unit 1), the bendino of a

CEA

extension

shaft (Unit 2) and the under torauing of the Reactor

Coolant

Pump shaft impeller nuts (Unit 2).

All of these

events

were caused

by inadequate

controls and/or insufficient

supervisory

involvement.

The first event also indicates

a

laxness

on the part of maintenance

personnel

in the reporting

of problems

to management.

The level of responsiveness

to

NRC initiatives was about the

same

as during the previous

SALP.

One concern which the

NRC

discussed

with the licensee

on several

occasions

was the

reduction of maintenance

backlog work items.

The licensee

implemented actions

to more closely monitor backlog.

h'hile the

backlog

has

decreased,

approximately half the site backlog is

associated

with Unit .1.

The control of work and the conduct of maintenance

continued to

be areas

of concern that

showed little improvement during the

assessment

period.

The work control procedures

were modified

during .the period.

The action was prompted in part by the

reorganization

and by the recoonition that changes

were

needed

to improve 'work coordination,

scheduling,

operations

involvement, retesting

and the quality of instructions.

Deficiencies in work controls resulted

in several significant

operational

problems during the period.

These

included

rendering auxiliary feedwater

pumps inoperable

(Units I and 2},

the introduction of ball bearings

into the

UGS (Unit I), the

tripping of a startup transformer (Unit 3),

and the bending

o<

a

CEA extension

shaft (Unit 2).

- Instances

of deficient post-

maintenance

retesting

were still being observed

during the

latter part of assessment

period.

The coordination with operations

on the issuance

of effective

clearances

continues

to require management's

attention

as

several

cases

of incomplete deactivation of equipment

associated

with work orders

were experienced

during the period.

There

have

been

no plant shutdowns directly attributable to

maintenance

personnel

errors,

although in one instance

a

turbine trip occurred

due to an incomplete troubleshooting

effort (Unit I) and

a secondary

plant transient

(loss of a Main

Feed

pump) occurred

due to poor job planning (Unit 2).

Two violations related to maintenance

were issued during the

SALP period.

One

was related to an incorrect restoration of an

access

door on

a vital static inverter (Unit 1), the other

was

due to

a failure to follow procedures

(Unit 2).

The quality of implementation of the surve'illance

program

has

been

equal

to that of the previous

assessment

period.

Of the

nineteen

LERs related to the functional area

seven

were due to

exceeding

the testing frequency time requirements.

The

ASYiE

Section

XI surveillance

program requirements

appear to be well

coordinated.

The licensee maintains

a qualified staff

dedicated

to this effort.

The licensee

has demonstrated

good performance

in chemistry

surveillance

and control to reduce degradation of the reactor

coolant, pressure

boundary.

Performance

weaknesses

were limited

to the sensitivity of reactor coolant system fluoride analysis

and control of condensate

polisher sodium ingress

to the

secondary

system.

The Chemistry Standards

Department

has

established

an aggressive

program for independent verification

of analytical

performance

using spiked

and replicate

samples.

I

15

Expertise within the maintenance

organization

generally

has

been

adequate

to repair

and maintain equipment in an operable

condition except

when multiple or extended

cutages

occur.

The

licensee

has contracted

assistance

from vendors

on work

requiring very specialized

knowledge.

An INPO accredited

maintenance

program for the crafts

was developed

and-

implemented during the period.

I'n spite

o'f this, several

observations

of inadequate

documentation

on work orders

were

made during the period.

Planner/coordinators

are

key personnel

in the proper implementation of the licensee's

work control

program;

however,

the experience

and training of these

individuals varies

great'1y

and

needs

improvement.

There is no

real engineering capability in the maintenance

organization,

and the'ork planners

only seek

help from system engineers if

thev see fit.

A decline in performance

was observed

due to the

significant organizational

and program changes

during

a period

of extended

workload (back to back refueling outages).

In the

later part of the assessment

period, while all three units have

operated

at essentially

fu11 power, conduct of maintenance

and

the control of work have not shown signs .of improvement.

2.

Performance

Ratin

Performance

Assessment

- Category

2

3.

Board Recommendations

Licensee

management

should strive to instill an inquisitive

attitude in their maintenance

personnel.

Maintenance craft and

work planners

must think beyond

the immediate work they do and

assess

how it affects

equipment operability.

Additionally,

planner coordinators

must

be more aggressive

in enlisting the

system engineers

support in the correction of non-routine

equipment

problems.

Maintenance

manaoement

must increase

efforts to observe

ongoing work and provide corrective feedback

into the maintenance

program.

0.

Emer enc

Preparedness

Analvsis

Approximately 313 hours0.00362 days <br />0.0869 hours <br />5.175265e-4 weeks <br />1.190965e-4 months <br /> of direct

NRC inspection effort was

spent

in this functional area during this

SALP period.

The

inspections

included

two annual

emergenc v preparedness

exercises

and

one routine preventive inspection.

h~hile management

has

been effectively involved in the emergency

preparedness

(EP) program,

the level of involvement appears

to

have diminished during this

SALP period.

For instance,

a

problem involving the delay of emergency

response

teams

being

processed

through security

was brought to management's

attention several

times through the licensee's

own

EP exercise

critiques,

NRC exit interviews

and

NRC inspection reports.

It

was also noted that firefighters responding

to the Unit

~

l

f

I

16

auxiliary transformer fire in July 1988 were unnecessarily

del.ayed

3-4 minutes while being processed

through the security

access

control point.

In another

instance,

congested

radio

traffic caused

bv routine use of an emergency

radio channel

was

brought to management's

attention during the licensee's

critique of the December

1987 exercise.

It has

been

noted that

congested

communications

occurred during the response

to the

1988 Unit -1 auxiliary transformer -fir'e.

Diminished management

involvement

,rom previous

SALP periods

was also 'indicated

by

the absence

of management

representatives

at the 'licensee's

latest

( 1988)

annual

exercise critique.

The only management

attendees

were from the

EP Department itself; no corporate

management

or representatives

from 'other departments

were

pr'esent.

(However, copies of the critique report were provided

to the various managers,

inc'luding those at the corporate

level. )

Corrective actions

are usually taken,

but there were instances

of ineffectiveness

in correcting 'the root cause of the problem.

As an example,

several

problems in identifying field monitoring

team locations

have

been identified during previous

annual'xercises.

Even after corrective actions weri taken, similar

problems

were identified in the

1988 exercise.

In another

instance,

the

NRC identified

a conflict between

procedural

protective action

recommendations

for the

same conditions.

After corrective actions

were taken,

the

NRC identified an

identical conflict in still another

procedure.

The licensee,

however,

has displayed

an above-average

capability of

self-assessment

of emergency

events.

The post trip report,

PTRR 1-88-004, of the July 6,

1988 Unit

1 Auxiliary Transformer

Fire and Reactor Trip is

a good example of this capability.

The occurrence

was analyzed,

cognizant individuals interviewed,

conflicting information identified and resolved,

and

documentation

provided to management

in clear

and objective

reports.

The licensee's effort to resolve technical

issues

from a safety

standpoint is generally

sound,

but resolutions

are not always

timely.

For instance,

a problem with providing reliable backup

emergency

communications

was first identified by the

NRC in

1986.

The:issue

was included in the 1987

SALP report because

the licensee still had

no concrete

plan of action to resolve

the issue.

It appeared

that the licensee

was attempting

a more

comprehensive

resolution

than

was actuallv required to satisfy

the concern.

Their plan for resolution called for purchasino

existing communications

lines from Mountain Bell and rerouting

them to a new facility constructed

to house the backup

comrunication svstem.

The licensee

now has installed

a number

of cellular portable

phones

as the backup

emergency

conmunications.

Implementation of NRC initiatives and policies

has

been timely

and effective,

and the licensee consistently

meets

expectations

with regard to schedule

or content.

17

There

have

been

no

NRC enforcement

actions

in this functional

area.

The

EP program staffino has

undergone

a major reorganization.

During this period the licensee's

executive vice president

retired,

the nuclear.,vice

president

was

removed from the

emergency

preparedness

chain of,responsibility,

and the

emergency

planning manager resigned.

The result

was

a

.considerabl.e.

aggregate

.l,oss .of. EP experience, within a short

period of'ime.

Expertise,

however,

has

been usually available

within the staff and consultants

have

been appropriately

used.

There

has

been

some

concern

about adequate staffing in the

emergency

response

organization.

The

NRC had expressed

in

a

report during the previous

SALP period

a concern that an

adequate

number of trained personnel

may not be available to

respond

to emergencies.

A licensee

post trip report,

No.

PTRR

1-88-004,

also indicated

a lack of staffing to respond to that

situation

when the services

of the Shift Technical Advisor was

unavailable

because

he was occupied maintaining communications

with the

NRC.

For some

time the emergency

planning department

has

been joined

with the fire department

under

a single manager.

The merged

departments,

along with the security,

nuclear trainirg,

material control,

and administration

departments

now operate

as

service organizations

under the Director of Site Services.

Organizationally,

these

are not associated

with the site

reactor operations.

It appears

that the present

organizational

setup provides little opportunity for direct site operations

interface with the emergency

planning program.

The licensee's

gA program continued to meet the

NRC re-

quirements

to provide

an independent

annual

review of the

emergency

preparedness

program

and evaluate

the adequacy of

interfaces

with State

and local governments.

Audits were

conducted

in

a timely manner

and audit

teams

were

composed of

members

who had

no direct responsibilities within the emergency

preparedness

program.

The training and qualification program contributes

to an

adequate

understanding

of work and adherence

to procedures.

Several training problems,

however,

were manifested

during the

Unit 1 auxi liarv transformer fire.

For instance, it was

necessary

several

times for firefighters to interrupt their

efforts to ask bystanders

to move back from the fire scene.

In

addition,

as previously mentioned,

unauthorized

use of an

emergency

radio channel for routine operations

disrupted

emergency

communications.

Both instances

are indicative of

inadequacies

in general

employee

emergencv

preparedness

training.

2.

Performance

Ratin

Performance

Assessment

- Category

2

18

3.

Board Recommendations

The licensee

is encouraged

to evaluate

the interface

between

the emergency

planning

and site operations

departments.

Additionally, emphasis

on timely resolution of identified

deficiencies seem-critically important to improving performance

in this area.

E.

~Securi t

A~ina 1

s i s

During the assessment

period from November I, 1987 throuqh

October 31,

1988,

Region

V conducted

three physical security

inspections.

A total of approximately

285 hours0.0033 days <br />0.0792 hours <br />4.712302e-4 weeks <br />1.084425e-4 months <br />

o+ direct

inspection effort was expended

by regional

inspectors.

In

addition,

the resident

inspectors

provided continuing

observations

in this area.

There were

no material control

and

accounting

inspections

conducted

during this assessment

period.

With regard to management's

involvement in assuring quality,

corporate

and plant management

continued to review the

operation of the overall securitv program.

They have generally

implemented

remedia1

measures

to correct deficiencies

identified in the course of both internal

and

NRC security

inspections.

The previous

SALP report encouraged

licensee

management

to

continue their augmented

support of the station security

program, particularly with respect to: engineering

support

of'he

security program

and the planned

upgrade of vehicle

and

personne1

access

control areas.

During this

SALP period

package

search

equipment

has

been

upgraded

and construction

was

begun

on

a

new vehicle access

portal.

Since February

1987, specific

NRC. concerns

with the suitability

of roll-up doors

as vital area barriers

has

been raised.

Although various design concepts

to improve the resistance

of

such doors to penetration

have

been considered,

each

has

been

evaluated

and rejected

by the licensee's

engineering staff and

the specific concern

remains

unsolved.

After nearly two years,

these potentially vulnerable barriers

remain

augmented

by

compensatory

measures.

The previous

SALP report identified major program upgrades

underwav (particularly in the area of alarm station operation,

access

control, radio communications,

and physical barrier

evaluation)

as requiring continued

management

attention.

During this assessment

period,

the security management

essentially

completed

the upgrade of their radio communication

equipment.

The alarm station

upgrade is nearly complete.

The

licensee

has initiated actions to incorporate suitable barrier

characteristics

into their security plan.

However,

19

considerable

engineering effort remains

to be completed

on the

development of the necessary

barrier evaluation criteria.

During the assessment

period, four information notices related

to security were issued;

. The licensee.'s; actions,

as reviewed

to date,

were found to be appropriate.

- As

a result of the.

NRC

Regulatory Effectiveness.

Review conducted

during the

SALP

period,

the licensee

has initiated an evaluation proiect to

consider

upgradinq

the perimeter barrier system to include

a

double fence barrier enclosing

an isolation zone with detection

systems

and continuous

CCTV surveillance

for immediate alarm

assessment.

In response

to the August 1986,

NRC policy statement

on Fitness

for Duty of Nuclear

Power Plant Personnel,

corporate

and plant

management

continued to support their established

Fitness for

Duty Program.

As designed,

this program requires that all

applicants

seeking onsite

employment must satisfactorily

complete

a pre-emp'loyment urinalysis test.

Individuals granted

unescorted

access

to the protected

area

are subject to annual,

but scheduled,

urinalysis drug screening.

The licensee's

current Fitness for Duty Program

does not follow the industrial

standards

published

by Edison Electric Institute (EEI) i.e.,

the requirement for random testing is not included.

The enforcement history for the period November

1,

1987 throuah

October 31,

1988 includes

two violations,

one related

to the

licensee's

failure to alarm all protected

area

access

portals

and the second

relates

to the licensee's

failure to properly

secure

safeguards

information.

During this

SALP period,

the licensee

reported

seven

safeguards

events.

Four of these

events

resulted

from personnel:

error

one from failed security compensatory

measures;"

one from

unauthorized

access

to a vital area

and

one from an

uncontrolled

pathway tn the protected

area.'ith

respect

to staffing,

key positions

were identified and

responsibilities

were generally well defined.

The security

training staff has initiated

a special

advanced training

program which exceeds

the requirements

of regulation,

and

augments

current offsite security resources

to meet the special

security

demands

wrought by the plant's isolated location.

2.

Performance

Ratin

'I

Performance

assessment

- Category 2.

3.

Board Recommendations

Licensee

management

is encouraged

to complete their

'construction project of an alternate

vehicle access

control

point and to expeditiously address

the engineering

issues

associated

with the evaluation of roll-up doors serving

as

I

20

vital. area barriers

and the upgrade of the perimeter barrier to

eliminate potential vulnerabilities identified hy,the

RER team.

Further,

the licensee

is encouraged

to reexamine their current

Fitness for Duty Program with respect

to the

EEI guidance

pertaining to chemical testing of body fluids.=

.

F.

En ineerin /Technical

Su port.

~Anal sls

This functional

area

was observed routinely during the

assessment

period by both the resident

and regional

inspectior

staff.

Approximately 184 hours0.00213 days <br />0.0511 hours <br />3.042328e-4 weeks <br />7.0012e-5 months <br /> of inspection effort were

devoted

to this functional area.

These

inspections

showe'd the

licensee's

engineering

and technical

support organizations

to

be staffed with experienced

personnel.

However,

a

number of

significant weaknesses

were observed.

These

include:

sionificant errors in design basis

documents;

engineers

lacked

a sufficient knowledge of the design basis;

inadequate

implementation of the design

change

process;

and management

inattention to the Technology Transfer

and System Engineer

Programs.

Technical

issues

have, generally,

been appropriately resolved

in a timely manner after identification.

However,

self-revealing

events

or inspection findings have surfaced

many

of the technical

issues.

The need for management

to insist

upon

a pro-active rather than reactive

approach

in identifying

technical

issues

has

been discussed

in several

inspection

reports

and management

meetings

during the assessment

period.

The licensee instituted

a Technology Transfer

program to assure

that design basis

documentation

developed

by Bechtel for Palo

Verde

was effectively transferred

to the cognizance

of ANPP

engineering

personnel.

The Safety System Functional

Inspection

(SSFI)

team found ANPP had not adequately

reviewed the design

basis analysis

to assure

that

a complete

and accurate

design

basis is available for use in future plant design

and

modification efforts.

This is one of several

areas

where

manaqement's

inattention to an established

proqram allowed

results

to diverge from management's

expectations.

The System Engineer

Prooram

has

been established

for several

years at Palo Verde.

However, management's

expectations

and

program performance

also diverged;

due, here,

to

a lack of

management

oversight.

This was evident from several

events

and

inspection findings including:

multiple failures withir. the

engineerinq

organization to identify work that rendered

the

steam driven Auxiliary Feedwater

pumps at Units I and

2

inoperable;

System Engineer lack of knowledge of design basis

and/or walkdown functions;

and the lack of system engineer

involvement with complex work planning

and significant

maintenance activities.

t~sanaaement's

poor definition of the

f

t

t

!

i

I

21

system engineer's

responsibilities

and duties in relation to

the workload appears

to be

a contributing factor to the

problems that occurred this assessment

period.

In response

to

NRC initiatives and inspection findings,

ANPP

management

instituted evaluation

and improvement

programs ir

the system-engineer,

design engineer,

and configuration

management

areas.

These

programs

required considerable effort

and re-evaluation of long range goals.

h'hile most of these

programs

began

in the first half of the

SALP period the initial

effort was spent in assessments,

evaluations

and long range

planning.

Thus,

most of the implementation will not

be

completed until well into the next

SALP period.

Although ANPP

management

has

been

involved in the early stages

of these

improvement

programs,

continuous

management

oversight will be

required to prevent

a relapse of the divergence

between

performance

and expectation.

No plant trips were attributable to the engineering

and

technical

support organizations

during the assessment

period.

However,

inadequate

technical

review of engineering

work did

play

a major role in rendering

the steam driven auxiliary

feedwater

pumps

inoperable at Units I and 2.

Escalated

enforcement

action resulted

from this event.

Engineering

involvement in trending

and performance monitoring of equipment

history and planning of significant maintenance

and testing

activities

was notably absent

when several

operational

events

and transients

were investigated (for example,

in the Unit

1

early criticality event deficiencies

were noted in the fuel

management

and reactor engineering

groups that contributed to

shortcomings

in the Cycle

2 Core Data

Book and the

Xenon

program

used in calculating the estimated critical conditions).

Staffing, qualifications

and training of both the site

and

corporate engineering

departments

has

been under review as part

of the System Engineer,

Technology Transfer

and Engineering

Excellence

programs.

These

reviews

have concluded that

increased

training and staffino are required to meet the long

range goals of ANPP management.

Thus,

management

has committed

to increase

both the site

and corporate engineering staffs to

better

manage

the workload of a three unit site

and reduce

the

current backlog.

2.

Performance

Patin

Performance

Assessment

- Cateoory

2

3.

Board Recommendations

The licensee

appears

to have initiated appropriate

programs

to

improve performance

in this area.

The licensee is encouraged

to closely monitor the implementation of these

programs.

G.

Safet

Assessment/Oualit

Verification

I

22

~Anal sis

This functional area

was observed routinely during the

assessment

period bv the resident

and reoional

inspection

staff.

In addition, several

inspections

focused specifically

on events

which were indicators of significant weakness

in this

area.

Over 636 hours0.00736 days <br />0.177 hours <br />0.00105 weeks <br />2.41998e-4 months <br /> of inspection effort were devoted to this

functiorial area.

This

SALP period evidenced significant

weaknesses

in problem identification, self-criticism of

identified problems

and management

oversight.

Underlvinq these

weaknesses

was the breakup

and re-formation of departmental

responsibilities

and lines, of communication,

brought about

by

the November

1987 reorgarization.

Furthermore,

the experience

level of upper management,

which has

been

a major

NRC concern,

was

reduced

when several

key managers left ANPP after the

reorganization

.

  • This reorganization left many licensee

personnel

unsure of their new responsibilities,

and unclear of

the expectations

held by the

new management

organization.

Without clear management

direction, institutionalized

'elf-critical

assessments

via Quality Assurance

(QA), Quality

Control

(QC), Independent

Safety Assessment

Group

(ISEG) ard

other problem finding arms of the organization failed to

identify operational

and engineering

weaknesses.

The lack of

strong

management

interest contributed substantially to

inaction

and subsequent

self-revealing

problems.

The licensee's

ability to initiate thorough

and self-critical

event assessments

was called into question

several

times during

this

SALP period.

These

included

an Auxiliarv Feedwater

pump

unknowingly rendered

inoperable following maintenance

(Units I

and 2), the loss of Multi Stud Tensioner

coaster

bearings

which

resulted

in

a stuck Control Element Assembly (Unit 1),

an early

criticality during reactor startup (Unit I), and

a radiation

overexposure

(Unit 2).

In each

case

the licensee's

assessment-

was found to be lacking or inadequate.

Although

QA inspected

in areas

such

as safety system

engineering

and radiation protection,

they have not been at the

forefront in assessing

the safety significance

o

their

results,

demandino

prompt and effective corrective action, or

aggressive

in clearly surfacing significant findings to senior

management

for resolution.

Furthermore,

management

review of

QA findings has not been sufficiently critical to require that

this

be routinely made

a part of QA audits.

In another

instance,

QA properly identified

a possible deficiency with

automatic pre-action fire suppression

systems;

however,

they

accepted

an engineering disposition which was incomplete in

addressing all the technical

issues.

On several

occasions,

the conduct of maintenance

proceeded

with

poor procedures

resulting in significant errors which failed tc

be questioned

by the involved maintenance,

operations,

engineering,

or QA/QC organizations.

Two steam driven

auxiliary feedwater

pumps were'endered

inoperable following

engineering

approved

adjustments

to the steam

admission

valves

(Units I and 2).

Reactor

Coolant

Pump

(RCP) impeller nuts were

under

torqued during assemblv

(Unit 2).

These

two situations

are

a demonstration

of poor performance

of technical

work by

engineering

and maintenance

organizations.

The licensee

was idertified as havinq good procurement qualitv

controls.

Also, the Nuclear Analysis department

identified

a

non-conservative

computer

code error which directly affected

shutdown margin calculations.

This is noteworthy

due to the

difficulty in locating such

an error in the extensive

computer

codes

used.

However, this detailed review was conducted after

and in response

to the early criticality event.

Response

to

NRC initiatives such

as Generic Letters,

NPC

Bulletins,

and

NRC Notices are adequate.

Past

licensee

practices of allowing regulatory issues,

such

as compliance

with the Anticipated Transient Without Scram

(ATWS) rule, to be

handled

by other parties (i.e. the

NSSS vendor),

are

now being

more aggressively

pursued

by the licensee's

own organization.

The licensee

continues

to be responsive

on

a daily basis

to

issues

NRC inspectors

bring to their attention.

In addition,

some

NRC concerns

in areas

such

as

improvements

in the

technical

adequacy of engineering

work, in general,

and in the

investigating

and root cause

methods

employed following events,

have resulted

in licensee efforts to institutionalize programs

meeting or exceeding

industry standards.

The. effects of these

and similar programs

have not yet been fully realized,

but

appear

to be

an in-depth

response

to these significant issues.

The licensee's

Compliance

department staff was

reduced

significantly after the reorganization

and resources

now appear

strained.

For example,

NRC open

item status

is tracked

as

a

collateral duty of a single compliance-engineer.

The status

of

licensee

followup to.these

items often requires

prompting by

NRC inspectors.

The events

discussed

in the enforcement

conferences

held during

the

SALP period appear to have resulted

from several

basic

failures

on the part of'NPP management.

These

include

an

inability"to establish

a, working atmosphere

.which encourages

step-by-step critical assessment

during the conduct of

operations,

an inability of gA and other oversight groups to

identify and correct significant problems prior to their

becoming self-revealing,

and

a failure to demand

thorough,

critical assessments

of events

such that root causes

can

be

clearly identified and effective corrective action taken.

Additionally, ANPP management

has

not devoted sufficient time

to direct observation

of plant activities during

a period when

programs

and policies were not being implemented to management

expectations.

Inspection findings throughout the

SALP period have indicated

a

high degree of non-compliance with established

procedures.

t

f

If,

]

I

24

Although this is sometimes

due to

a lack of knowledge or to

.. procedural

vagueness, it often appears

that the working

environment

and attitudes of first line supervisors,

gC

personnel,

and others

accept less-than-strict

adherence

as

an

acceptable

means of conducting business.

Contributing to this

a'ttitude is the unacceptably

high backlog of Procedure

Change

Requests

(PCR)

and

a growing frustration

on the part of

personnel

that their inputs are ineffective in creating

'constructive

change.

'he experience

level of the

gA organization is low in

operations

and engineering expertise,

contributing to

a lack of

confidence,

and

a reluctance,

to clearly identify poor

practices

when these

areas

are being assessed.

However,

following the inoperable auxiliary feedwater

pump event,

the

.NRC review determined

the need for better training to achieve

a

clearer understanding

of integrated plant operations,

  • fundamental

theory, procedural,

and regulatory requirements.

Although staffing of the

ISEG organization

meets

Technical

Specifications

minimum requirements, it has

been insufficient

to reduce

an administrative

backlog

and

has detracted

from

their ability to monitor plant activities

on

a routine basis.

The licensee's

approach

to the resolution of licensing

issues

generally exhibits conservatism,

timeliness,

and

an

understanding

of the issues.

Licensing activities at the

beginnino of the evaluation

period were focused primarily on

actions

in support of the issuance

of a full power license

on

Unit 3.

The full power license

was issued

on November 25,

1987.

This

SALP period

has

been

marked

by a series of events

and

inspection findings which, when taken

as

a whole, indicate

significant weakness

in the licensee's ability to self-identify

and effectively correct technical

and organizational

problems.

Organizations

such

as Operations,

Training, Maintenance,

and

Engineering

do not always work toward

common purposes,

nor do

functionally related entities,

such

as onsite

and offsite

enaineering,

communicate sufficiently to their mutual benefit.

Corrective actions

have

sometimes

failed to be effective

because

of inadequate

establishment

of root causes

and

insufficient communication of the actions

and the basis for

them to all affected organizations.

Senior

management

began to

strongly stress

the theme of teamwork,

communication,

and

attention to detail during the last portion of the

SALP period.

Performance

Ratin

Performance

Assessment

- Category 3.

Board Recommendations

Licensee

management

should continue to implement initiative

programs

such

as Radiation Protection

improvements,

the

gA

i

,k

25

Improvement

Program,

Engineering Excellence,

and Event

Investigation procedures.

The

new organizational

structure

must. be. solidified with clearly defined authority. and

accountability.

Management

must demonstrate

and encourage

increased self-criticism, at all organizational

levels,

but

particularly at the highest levels.

In parallel with increased

self-criticism must

be the creation of an atmosphere

where

such

criticism is eagerly sought,

analyzed,

and strongly acted

upon.

Corrective actions

must

be personally identified with by all

affected personnel.

Departmental

intercommunications

must

be

increased,

and

a

common goal to support safe plant operations

must

be strengthened.

The licensee

established

efforts to date

toward these

goals are noted

and encouraged.

The

QA organization

needs

to obtain personnel

experienced

in

operations

and engineering activities to enhance their

abilities tn effectively assess

these

areas.

Increased

inspection

coverage of daily in-plant activities is

recommended,

with emphasis

on procedure

compliance

and

communication.

Increased

inspection

by licensee

oversight

groups

(QA, QC,

QSEE,

ISEG,

NSG,

PRB) is also strongly

recommended.

V.

SUPPORTING

DATA AND SUMMARIES

A.

Enforcement Activit

Three resident

inspectors

were, essentially onsite during the

SALP

assessment

period.

Forty-nine inspections,

including

a team Safety

System Functional

Inspection

(SSFI) in Januar.v

and February

1988,

were conducted

during this period for a total of 5935 inspector

hours.

A summary of inspection activities is provided in Table I

along with a summary of enforcement

items from these

inspections.

A

description of the enforcement

items is provided in Table 2.

During

this

SALP period

a two part escalated

enforcement

item ($ 100,0000

Civil Penalty)

was identified concerning operating with turbine

auxiliary feedwater

(AFW) pump steam isolation valves

improperly

modified and operating with less

than three

AFW pumps operable

(units I and 2, November 1987).

A three part escalated

enforcement

item ($ 150,000 civil penalty)

was identified, concerning

an early

criticality event at Unit I (May 14);

a personnel

radiation

overexposure

event which occurred at Unit 2

(May 22-23);

and

an

inadvertent rendering

inoperable of the Essential

Chilled Water

System at Unit I, in violation of Technical Specification

reauirements

(May 20-29).

B.

Confirmation of Action Letters

One Confirmation of Action Letter was

issued

on June

23,

1988

concerning introduction of nonconservative

information into channel

B Core Protection Calculator.

The licensee's

letter of July 21,

1988 responded

to the concerns.

f

t

26

C.

Other

The Office for Analysis

and Evaluation of Operational

Data

(AEOD)

reviewed the licensee's

events at Palo Verde and prepared

a report

which is included

as Attachment I.

AEOD reviewed the

LERs

and

significant operating events for quality of reporting

and

effectiveness

of identified corrective actions.

'l

hi

lt

TABLE

1

INSPECTION ACTIVITIES AND ENFORCEMENT

SUMMARY (11/01/87 - 10/31/88

Pal o Verde Unit

1

Functional

Area

nspec-t

> on

Hours

ercent

of Effort

Ins ections

Conducted

Enforcement

Items

ever>ty Leve

I

II

III

IV

V

C'.

Radiological

Controls

345

A.

Plant Operations

1270

47.7

13.0

19

3

1

3

A

C.

Maintenance/

Surveillance

D.

Emergency

Prep.

E.

Security

F.

Engineering/

Technical

Support

G.

Sa fety Assessment/

Quality Verif.

374

105

143

74

351

14.0

3.9

5.4

2.8

13.2

3

1

1

1

Totals

2662

100.00

3

12

3

1

Allocations of inspection

hours to each functional area

are

approximations

based

upon

NRC form 766 data.

These

numbers

do not

include inspection

hours

by NRC contract personnel.

Severity levels are in accordance

with NRC Enforcement Policy (10 CFR Part 2, Appendix C).

No violation was issued,

but

a deviation

was identified.

9

-One

NOV pending in this area.

This violation which resulted

in a civil penalty also applies to Unit 2.

TABLE 1

INSPECTION ACTIVITIES AND ENFORCEMENT

SUMMARY (ll/01/87 - 10/31/88)

Palo Verde Unit 2

Functional

Area

Ins ections

Conducted

Inspection"

Percent

Hours

of Effort

Enforcement

Items

Severity

Leve

I

II

~

I I I

IV

V

A.'lant Operations

871

48.3

B.

C.

Radiological

Controls

Maintenance/

Surveillance

291

16.1

25

3

.1

200

D.

Emergency

Prep.

E.

Security

Engineering/

Technical

Support

104

86

5.8

5.3

4.8

Safety Assessment/

156

Quality Verif.

8.6

Total s

1804

100.00

4

3

1

If

Allocations of inspection

hours to each functional

area

are

approximations

based

upon

NRC form 766 data.

These

numbers

do not

include inspection

hours

by

NRC contract personnel.

Severity levels are in accordance'with

NRC Enforcement Policy (10 CFR Part 2, Appendix C).

No deviations

were identified during this

SALP

period.

This violation which resultd in a civil penalty also applies

to Unit l.

&

One of these violations which resulted in

a civil penalty also .applies to

Units

1 and 3.

29

TABLE

1

INSPECTION ACTIVITIES AND ENFORCEMENT SUMMARY (11/01/87 - 10/31/88)

Pal o Verde Unit 3

Functional

Area

Ins ections

Conducted

Enforcement

Items

Hours

of Effort

I

I I

III

IV

V

A.

Plant Operations

B.

Radiological

Controls

C.

Maintenance/

Surveillance

D.

Emergency

Prep.

E.

Security

F.

Engineering/

Technical

Support

804

224

138

104

56

54.7

15.2

'.4

7.1

3.8

1.0

1&

1

G.

Safety Assessment/

129

Quality Verif.

8.8

Totals

1469

100.00

1

2

Allocations of inspection

hours to each functional area

ar'

approximations

based

upon

NRC form 766 data.

These

numbers

do not

include inspection

hours

by

NRC contract personnel.

Severity levels are in accordance

with NRC Enforcement Policy (10 CFR Part 2, Appendix C).

No deviations

were identified during this

SALP

period.

&

This violation which resulted

in a civil penalty also applies to Units

1

and 2.

f

30

Table

2

Pa~oVer

e

Enforcement

Items

Report

Number

Unit

1

Subject

Severity

Functional

Level

Area

87-37

87-37

Limitorque valve operators

inside containment

were

4

not shown to be qua'lified because

of deviations

from qualification test

specimen configuration.

ANPP files di d not

a dequa te 1y document

qualification of skinner solenoid valves

because

design

and material differences

between

the plant

equipment

and test speciments

were not evaluated

in detail.

87-40

Radiation

areas within the west mechanical

penetration

access

room of the auxiliary building

were not conspicuously

posted.

87-40

88-01

88-01

88-01

West mechanical

penetration

access

room of the

auxiliary building had

two areas

where the

intensity of radiation measured

between

100 and

800

millirem per hour and were not posted

An access

door, vital static inverters,thumb

screws,and

battery spacers

were found contrary to

their respective

drawings. Eyewash station

installed without comparison

to seismic category

9

requirements.

Licensee did not consider or make calculations

to

demonstrate

that pressure relief valves were sized

to accommodate

flows from failure of upstream

regulating valves in the fully open position.

A temporary modification that installed tanks to

supply hypochlorite for emergency

spray

ponds

was

completed with an unacceptable

written safety

evaluation.

88-01

88-02

Spacers

were missing

between battery jars

and

eyewash stations

were installed without revising,

the calculation isometric drawing and were never

compared

to seismic category

9 requirements.

Unit

1 entered

mode

4 and operated for

approximately

one hour and twenty-five minutes

without an operable

HPSI

pump.

31

Tab'le

2

Pa~uuerde

E

Report

Number

~Sub 'ect

Severity

Level

Functional

Area

88-03

A copy of the notice of violation involving

"v'adiol'ogical working conditions received

by the

licenses

was not posted.

88-07

88-12

Contrary to tech specs,

unit I operated

with only

two operable

independent

steam generator

AFW

pumps. Modifications to valves were not reviewed

by

plant manager

or other proper authority.

Contrary to Reg Guide 1.97, wide range

steam

generator

level instrumentation

had

a range from

32

to 112K of the range described

in the

Reg

Guide.

88-13

88-14

Licensee

radwaste

shipments

were made with loose

chain restraints

and

had shifted during transport

as evidenced

by loosened

or broken bracing.

Nonconservative

operator

performance

combined with

errors in information used to calculate

boron

concentration

resulted

in an inadvertent

criticality.

88-15

Protected

area portals

were not alarmed

and

monitored

as required.

88-18

Contrary to stated

requirements,

a valve was found

4

to be in the open position following the addition

of chemicals

to the system.

88-24

Contrary, to specific technical specification

reouirements

while Unit

1 was operating in Mode I,

both loops of the essential

chilled water system

were rendered

inoperable.

88-27

No written safety evaluation

addressing

the

processing

of radioactive

equipment in

a trailer

recently converted into a respiratory processing

facility was performed.

88-31

Improper Protection of safeguards

information

Unit 2

88-02

Unit 2 operated with less

than

3

AFW pumps

operable

due to the discharge

valve, on

a

pump

being closed.

I[

32

Table

2

Palo Verde

Enforcement

Items

Report

doeber

88-OS

Sub.iect

Operation occurred with only two AFW independent

steam generator

pumps operable.

Valves were

modified without review by the proper

individual/group.

Severity

Functional

Level

Area

3

G

88-08

A principle

gamma emitter analysis

performed

on

a

gas

grab sample

from waste

gas

decay tank did not

achieve

the required

LLD.

88-14

Radioactive

noble fission product gases

were

vented

from portions of the gaseous

radwaste

system without prior evaluation of the potential

release.

88-22

An enclosed

area with a door which was not locked

had

an intensity of radiation accessible

to

a

major portion of the body measured

up to at least

3 Rem/hr.

88-26

Failure to provide

an exposure

report.

No written safety evaluation

addressing

the

processing

of radioactive

equipment in

a trailer

converted into a respiratory processing facility

was performed.

88-22, Occupational

radiation exposure

in excess

cf the

26/27

quarterly limit.

Failure to perform radiation

surveys.

Failure to implement the ALARA program.

Unit 3

88-18

Valves were found to be in the open position

following the addition of chemicals

to the system.-

88-25

No written safety evaluation

addressing

the

processing

of radioactive

equipment

in

a trailer

recently converted into

a respiratory processing

facility was performed.

88-33

Failure to control access

to high radiation area.

Enforcement action is being considered for this item.

(

U

Deviation from regulatory requirements.

t

I

1

1'

33

TABLE 3

SYNOPSIS

.OF PALO.,VERDE I LICENSEE

EVENT REPORTS

LERs)

Functional

Area

A.

Plant Operations

B.

Radiological

Controls

C.

Maintenance/

Surveillance

D.

Emergency

Prep.

E.

Security

F.

Engineering/

Technical

Support

G.

Safety Assessment/

equality Verification

SALP Cause

Code+

A

B

C

D

E

X

2

6

I

I

3

1

Totals

15

Totals

20

I

4

7

I

33

The above

data

are

based

upon

LERs 87-24 through 88-24

.

LERs 88-09, 88-20,

and 88-23 will be included in the next

SALP assessment

period.

LER 84-01

was

received during this

SALP assessment

period.

  • Cause

Code

A - Personnel

Error

8 - Design, Manufacturing or Installation Error

C - Externa,l

Cause

D - Defective Procedures"

E - Component Failure

X - Other

il

t

34

TABLE 3

SYNOPSIS

OF

PALO VERDE 2 LICENSEE

EVENT REPORTS

LERs

SALP Cause

Code*

Functional

Area

D

E

X

Tota1s

A.

Plant Operations

B.

Radiological

Controls

C.

Maintenance/

Surveillance

D.

Emergency

Prep.

E.

Security

2

I'

3

2

I

F.

Engineering/

Technical

Support

Safety Assessment/

equality Verification

Totals

9

2

2

3

I

16

The above

data

are

based

upon

LERs 87-18 through 88-13.

  • Cause

Code

A - Personnel

Error

B - Design, Manufacturing or Installation Error

C - External

Cause

D - Defective Procedures

E - Component Failure

X - Other

I

'I

li

TABLE 3

SYNOPSIS

OF

PALO VERDE 3 LICENSEE

EVENT REPORTS

(LERs)

Functional

-- Area=

A.

Plant Operations

B.,Radiological:."..

Controls

C.

Maintenance/

Surveillance

SALP Cause

Code*

--"A-

B

C

D

E

X

I

I

I

Total s

D.

Emergency

Prep.

E.

Security

F.

Engineering/

Technical

Support

G.

Safety Assessment/

equality Verification

Totals

5

I

2

I

The above data

are

based

upon

LERs 87-03 through 88-06.

  • Cause

Code

A - Personnel

Error

B - Design, Manufacturing or Installation Error

'C -'External

Cause

,D - Defective Pnocedures ..

'

- Component Failure

X - Other

I

n~,

~ s

~

n

I

ATTACHMENT 1

ENCLOSURE

AEOD INPUT TO SALP REVIEM FOR

PALO VERDE

Arizona Public Service

Company submitted about

52 reports for the three units

at Palo Verde, not including updates,

fn the

SALP assessment

period from.

November 1,

1987 to October 31, 1988.

This review fncluded the following LER

numbers:

Untt

1

87-025 to 87-028

88-001 to 88-024

Unit 2

87-018 to 87-021

88-001 to 88-012

Untt 3

87-004 to 87-005

88-001 to 88-007

Our findings from the'eview of these

LERs follows:

1.

Abnormal Occurrences

There were

no abnormal

occurrences

fn the assessment

period.

However,

an event

that occurred in late October

1987 (just prior to the start of the assessment

period) at Unit 1 was identified as

an Appendix

C item, and reported fn the

fourth quarter

1987 Report to Congress.

In the event, ultrasonic testing

revealed

cracks fn all four reactor coolant

pumps

(RCPs).

Althouoh the

failure of one

RCP is an analyzed accident,

concerns

were raised that there

could be

a potential for tultiple RCP shaft failures.

However, additional

analysis

concluded that once

a crack initiates, the crack propogates

slowly in

a circumferential

manner over millions of stress

cycles.

No LER was submitted

for this event.

2.

Si nfficant 0

ratino Events

There were four events,

each at Unit 1, fn the assessment

period that were

identified as particularly significant by the

ROAB screening

and review process.

These events were:

(a)

LER 88-010,

"Ground Fault in 13.8

KV Bus Causes

Fire fn Unit

Auxiliary Transformer

and Reactor Trip," on July 6, 1988;

(b)

LER 87-025 "Modfffcation to Steam to Turbfne Driven Auxiliary

Feedwater

Pump Isolation Valves Render

Pump Inoperable,"

dated

November 27, 1987;

(c)

LER 88-013 "Auxiliary Feedwater

Pump Degradation,"

dated March 25,

1988;

and

(d)

LER 88-022 "Shutdown Cooling Systems

Valve Bolting Failure," dated

July 25, 1988.

r

3.

AEOD Technical

Stud

Re orts

There were no events identified at any of the units that were considered

sufficiently, serious to merit an in-depth technical

study by AEOD in this

assessment

pe~iod.

4.

Pks Issued in Assessment

Period

There were many Preliminary kotification of Event or Unusual

Occurrence

issued for the three units.

For the

Pks that were issued for reportable

events,

the licensee

submitted

a

LER for each event,

so by this method of

verification, the licensee

appears

to be reporting all events that are

required to be reported.

The content of the information in the

LER was in

substantial

agreement with the event

as described in the

PH, so the licensee

appears

to be reporting these

events accurately.

5.

LER ualit

The

LER submittals for all units were identical,

so this review would be

applicable to any of the three units.

The licensee

used

two format styles in

the assessment

period;

a narrative form prior to about mid-1988 and

an outline

form subsequently.

Me found the narrative style to fully comply with the reporting guidelines

listed in pages

5 through 7 of NUREG-1022.

All aspects

of the event

were described in substantial

detail

and

we thought the submittals vere

uni formly outstanding.

The outline form of LER submittal

was an improvement over the previous

narrative form.

Me thought these later

LERs were the best of any. licensee

that we review.

Previous similar occurrences

were properly'referenced

in the

LERs as applicable.

The licensee

updated

several

LERs that were promised to be updated in the

assessment

period.

The updated

LERs provided

new information and the portion

of the report that was revised

was denoted

by a vertical line in the right

hand margin so the

new information could be easily determined

by the reader.

lio reports

were submitted

on a voluntary basis in the assessment

period.

As

stated

on page

10 of NUREG-1022, licensees

are encouraged

to report any event

that does not meet reporting criteria, if the licensee

believes that the event

might be of safety significance, might be of generic interest or concern

or

contains

a lesson to be learned.

6.

Effective Corrective Action

There were 43 events at the three units available for imnediate review where

a designated

root cause

had been fully determined for the event.

The casual

distribution of these

events were:

1

Human Factor Deficiency

32 events

74K

Equipment Failures

8 events

19K

Spurious Halfunctions

2 events

5X

Inadequate

Plant Design

'

" "

I events

2X

The

Human Factor Deficiencies would include:

personnel

errors

25 events,

inadequate

procedures

4 events,

bad engineering evaluation,

inadequate

administrative controls

and error in the work document, I each.

Although there

seemed to be

a relatively high frequency of human factor

deficiencies in the casual

pattern of LERs, only one of the events

rated

as

significant by ROAB was caused

by cognitive personnel

error

(LER 87-025).

The

root cause of the other three events

were equipment -failure.

p

I.