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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- AECM-83-0472, RO 83-067/0:on 830704,05 & 12,instruments on HPCS Spray Line,Lpcs Spray Line & Reactor Recirculation & Main Steam Piping,Respectively,Found Damaged.Caused by over-ranging. Instruments Will Be Replaced by 830826 + (ML20076F665)
- ML20076F667 + (ML20076F667)
- ML20076F670 + (ML20076F670)
- ML20076F673 + (ML20076F673)
- 05000338/LER-1983-053-03, /03L-0:on 830726,discharge Damper for 1-HV-F-40B Failed to Open While Running Associated Safeguards Exhaust Fan.Caused by Air Leak in Diaphragm of Actuating Mechanism for Damper AOD-HV-1301B.Damper Repaired + (ML20076F678)
- ML20076F680 + (ML20076F680)
- ML20076F682 + (ML20076F682)
- ML20076F683 + (ML20076F683)
- ML20076F686 + (ML20076F686)
- ML20076F687 + (ML20076F687)
- ML20076F691 + (ML20076F691)
- ML20076F694 + (ML20076F694)
- 05000296/LER-1983-041-03, /03L-0:on 830719,during Normal Operations,Control Rod Exercise SI 4.3.A.2 Not Performed within Required Schedule.Caused by Personnel Error.Personnel Counseled + (ML20076F703)
- ML20076F711 + (ML20076F711)
- AECM-83-0469, RO 83-069/0:on 830712,listed Penetrations,Cable Tray Cover & Access Hatch Barriers Opened to Support Planned Maint Activities.Hourly Fire Watches Established.Work Tasks Expected to Be Completed by 831130 + (ML20076F716)
- ML20076F731 + (ML20076F731)
- 05000338/LER-1983-050-03, /03L-0:on 830723,w/util Ramping Down & Reactor Power at 65%,axial Flux Difference Exceeded Target Band for 1 Minute.Caused by Tube Leak in Gland Steam Condenser.Axial Flux Returned to Required Band + (ML20076F734)
- ML20076F736 + (ML20076F736)
- ML20076F743 + (ML20076F743)
- A03174, Responds to 830406 SER Re Environ Qualification of Electrical Equipment for Facility.Corresponding Technical Evaluation Rept Contains No Proprietary Info & Can Be Released for Public Disclosure,Per 10CFR2.790 + (ML20076F745)
- 05000458/LER-1994-025, :on 940910,ADS Valve Inoperable Because Fire Wrap Not Replaced After Maint.Caused by Lack of Specific Rev for Connector Replacement.Administrative Procedure Developed + (ML20076F748)
- ML20076F757 + (ML20076F757)
- 05000315/LER-1983-069-03, /03L-0:on 830719,during Surveillance Testing on Diesel Generator Load Shedding Relays,Six GE Model NGV-13b Loss of Voltage Relays Exceeded Tech Spec Limit.Caused by Instrument Drift.Relays Readjusted + (ML20076F765)
- BSEP-83-1280, Responds to NRC Re Violations Noted in IE Special Training Assessment Repts 50-324/83-04 & 50-325/83-04. Corrective Actions:Orientation for New Employees Accomplished in Accordance w/TI-301 + (ML20076F766)
- ML20076F769 + (ML20076F769)
- ML20076F776 + (ML20076F776)
- 05000315/LER-1983-070-03, /03L-0:on 830723,during Refueling Operation,Fire Door 373 to Elevation 587 Vestibule Area Would Not Latch Properly.Caused by Barrel Retaining Ring in Contact W/Knob. Ring Adjusted & Set Screw Tightened + (ML20076F778)
- 05000260/LER-1983-043-03, /03L-0:on 830720,during Transient Operation, Following Control Rod Sequence Exchange,R Calculation Less than R Setpoint.Caused by Xenon Transient W/Operation Closer to Thermal Limits.Control Rods Repositioned + (ML20076F782)
- 05000302/LER-1983-029-03, /03L-0:on 830721 & 27,emergency Feedwater Ultrasonic Flow Indicator on Steam Generator B Inoperable. Caused by Electrical Malfunction in Transducers & Improperly Mounting Replacement Transducers,Respectively + (ML20076F784)
- ML20076F786 + (ML20076F786)
- 05000260/LER-1983-044-03, /03L-0:on 830712,during Performance of 4.2.B-26, Level Switches LS-73-56A & B Mfg by Robertshaw Failed to Operate Properly.Caused by Dirt in Mechanical Linkage. Switches Cleaned + (ML20076F787)
- ML20076F794 + (ML20076F794)
- ML20076F799 + (ML20076F799)
- 05000416/LER-1983-100-03, /03L-0:on 830718,during HPCS Monthly Functional Test,Diesel Generator Tripped While Attempting to Parallel Generator W/Bus 17AC.Caused by Operator Error.Engine Restarted + (ML20076F803)
- ML20076F805 + (ML20076F805)
- RA-20-0075, Response to NRC Regulatory Issue Summary 2020-01 Preparation and Scheduling of Operator Licensing Examinations + (ML20076F807)
- ML20076F809 + (ML20076F809)
- ML20076F813 + (ML20076F813)
- ML20076F814 + (ML20076F814)
- ML20076F820 + (ML20076F820)
- ML20076F821 + (ML20076F821)
- 05000302/LER-1983-027-03, /03L-0:on 830718,during Routine Sampling,Rcs Dissolved Oxygen Concentration at Approx 4 Ppm.Caused by Personnel Error.Hydrazine Added to Lower Dissolved Oxygen Concentration.Personnel Reinstructed + (ML20076F825)
- ML20076F826 + (ML20076F826)
- 05000369/LER-1983-058-03, /03L-0:on 830717,channel III Reactor Coolant Loop C Flow Instrumentation Read Low & Declared Inoperable.Caused by Out of Tolerance Westinghouse Veritrak 59DP4E99-7050 Flow Transmitter + (ML20076F827)
- 05000338/LER-1983-051-03, /03L-0:on 830723,post-reactor Shutdown Specific Activity RCS Samples Indicated Dose Equivalent I-131 Level Above Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core.Sampling Frequency Accelerated + (ML20076F829)
- 05000395/LER-1983-084-03, /03L-0:on 830722,licensee Notified NRC Inspector That Surveillance Test Procedure 115.001 Did Not Adequately Address Tech Spec.Caused by Inadequate Procedure.Revised Procedure to Be Issued 830820 + (ML20076F831)
- 05000348/LER-1983-040-03, /03L-0:on 830720,steam Generator 1B Level Transmitter LT-486 Instrumentation Channel Declared Inoperable Due to Loss of Power Supply.Caused by Power Supply Failure on Signal Comparator Card.Card Replaced + (ML20076F833)
- ML20076F834 + (ML20076F834)
- ML20076F835 + (ML20076F835)
- ML20076F839 + (ML20076F839)
- ML20076F840 + (ML20076F840)