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 Issue dateTitleTopic
ML18153B1353 November 1994Ro:On 941028,total Suspended Solids Concentration in Spoil Discharge Reached 820 Mg/L.Permit Limitations Expressed as Values Exceeding Ambient Levels
ML18153B41115 December 1993Ro:On 931215,discovered Fault in Control Rod Drive Sys, Rendering Control Rod Assemblies in Shutdown Bank a Immovable W/Group 2 at 222 Steps & Group 1 Rods of Control Banks a & C Immovable by Faulted ConditionsShutdown Margin
Enforcement Discretion
ML18153D13115 September 1992Update to 920703 Special Rept Re Operational Difficulties W/ Waste Gas Decay Tank Hydrogen Monitors.Operability Intermittent & Reliability Not Yet Achieved.Ts Change to Delete Requirement to Monitor Hydrogen Sent on 920628Grab sample
ML18153D0563 July 1992Special Rept:Waste Gas Decay Tank Monitoring Instrumentation Out of Svc for More than 30 Days as Result of Replacement of Pressure Sensors Due to Instrument Drift.Replacement Pumps Received in June 1992.Updated Rept to Be Sent by 920731Grab sample
ML18153D0223 June 1992Special Rept:On 920503,quadrant to Average Power Tilt Exceeded 2% for Greater than 24 H.Caused by Loop Inlet Temp Imbalance.Power Range Nuclear Instruments Recalibr
ML18153C90724 February 1992Ro:On 920106,discovered That Portion of Wall Separating Cable Vault & Auxiliary Bldg Was of 4-inch Block Const Instead of Being Designated as Separate Fire Areas.Fire Watches Established Per Station Operating ProceduresFire Barrier
Exemption Request
ML18153C73713 September 1991Special Rept:On 910815 & 24,quadrant-to-average Power Tilt Exceeded 2% for More than 24 H.Caused by Blown Fuse & Dropped Rod Runback.Cable W/Insulation Damage & Rod Control Cabinet RepairedShutdown Margin
ML18153C54415 February 1991Special Rept:On 901220,spurious Alarms Received Shortly After Placing ATWS Mitigation Sys Actuation Circuitry in Svc.From 901222-28,spurious Trouble Alarms Received.On 901231,improper Voltage Ratings Found on Relay Modules
ML18153C50723 January 1991Special Rept:On 901224,quadrant to Average Power Tilt Exceeded 2.0% for Greater than 24 H.Caused by Xenon Transient & Change in Tave Coupled w/pre-existing Core Asymmetry.Isophase Bus Duct Shunts Repaired
ML18152B1335 May 1988Ro:Safety Evaluation of Steam Generator Tube Rupture Accident.Continued Operation of Station Based on Continuing Reanalysis of Impact of Steam Generator Tube Uncovery Justified for Listed Reasons
ML18150A1639 June 1987Ro:On 870516,automatic Shutdown on Low Reactor Coolant Flow in One Loop Experienced.Caused by Mechanical Failure of Reactor Coolant Loop Stop Valve.Effects of Event from Core DNB Standpoint Evaluated,Per 870527 Telcon W/Nrc
ML18139B9885 August 1982Ro:On 820721,rate of Exchange of Condenser Cooling Water Outlet Temp Reached Max of 12 F/Hour Exceeding Max Rate of Change of 3 F/Hour Per Tech Spec 4.14.A.3.Caused by Loss of Electrical Power to Four of Eight Circulating Water Pumps
ML18139B84616 April 1982Ro:On 820403,average Rate of Change of Condenser Cooling Water Outlet Temp Exceeded Permitted Rate.Caused by Operator Error.Personnel Reinstructed
ML18139B82726 March 1982Ro:On 820212,w/Unit 1 at 100% Power & Unit 2 at Hot Shutdown,Average Rate of Change of Condenser Cooling Water Outlet Temp Exceeded Tech Specs.Caused by Failure of Vacuum Priming Sys at River Intake.Sys Repaired
ML18139B7245 February 1982Ro:On 820122,average Rate of Change of Condenser Cooling Water Outlet Temp Exceeded Tech Spec Limit.Caused by Throttling of Water Flow Through Condenser Boxes to Preserve Reduced Canal Water Due to Vacuum Priming Pump Failure
ML18139B49925 August 1981Ro:On 810813,condenser Cooling Water Outlet Temp Exceeded Max Rate of Change of 3 F Per Hour Permitted by Tech Spec 4.14.A.3.Caused by Sheared Pin on Condenser Inlet Screen.No Damage to River Environ Found During Search
ML18139B49725 August 1981Ro:On 810810,rate of Change of Condenser Cooling Water Outlet Temp Reached Max of 7 F/Hr Exceeding Tech Specs, & Causing Loss of Electrical Svc to 4 of 8 Circulating Water Pumps.Loss of Svc Caused by Ground Fault in Transformer
ML18139B32613 May 1981Ro:On 810428,condenser Cooling Water Outlet Temp Exceeded Max Average Rate of Change.Caused by Lack of Svc Water Flow. Event Caused No Detrimental Effect on River Environ
ML18139B2871 May 1981Ro:On 810418,condenser Cooling Water Outlet Temp Exceeded Max Average Rate of Change of 3F/hr Per Tech Spec 4.14.A.3. Lack of Svc Water Flow Believed to Be Contributing Factor. Tube Leaks Repaired.River Environ Not Affected
ML18139B25016 April 1981Ro:On 810406,condenser Cooling Water Outlet Temp Exceeded Max Average Rate of Change Permitted by Tech Specs.Lack of Svc Water Flow Believed to Be Contributing Factor.Search Conducted to Determine Temp Change Effect on River Environ
ML18139B2311 April 1981Ro:On 810322,condenser Cooling Water Outlet Temp Exceeded Tech Spec Limit.Caused by Lack of Svc Water Flow. Investigation Is in Progress
ML18139A9645 January 1981Ro:On 801220 at Full Power,Condenser Cooling Water Outlet Temp Exceeded Max Rate of Change Per Tech Specs.Cause Not Stated.Temp Decreased When Waterbox Outlet Valves Throttled Due to Vacuum Priming Problems
ML18139A84819 November 1980Ro:On 801102,during Cold Shutdown,Condenser Cooling Water Outlet Temp Exceeded Max Rate of Change of 3 F/Hr.Caused by Lack of Svc Water Flow Through Unit 1.No Detrimental Evidence Found Re River Environ
ML18139A2996 June 1980Ro:Several Lines in Low Head & High Safety Injection Sys Were Not Analyzed for Effects of Fluid Temp Below 70 F. Review of New Nozzle Loads Showed Load on Pump Exceeded Vendor Allowable Load.Multiphase Program Proposed
ML18139A27423 May 1980Ro:On 800512,condenser Cooling Water Outlet Temp Exceeded Temp Change Rate of 3 F/H.During Power Escalation W/Only Three Circulating Water Pumps in Operation,Canal Intake Level Dropped & Groin Temp Reached Change Rate of 5.5 F/H
ML18139A17322 April 1980Ro:While Conducting PT 25.12,pump 1-FP-P2 in Fire Protection Sys Failed to Meet Acceptance Criteria of 250 Ft at 2500 Gallons Per Minute.Cause Not Determined.Vendor Will Participate in Insp.Local Fire Depts Will Supply Assistance
ML18136A40318 January 1980Ro:On 800108,while Unit 1 Was Operating at 50% Power,Cooling Water Outlet Temp Exceeded 3 F/Hour Change Rate.While Returning Unit 1 to Svc,Discharge Coolant Temp Increased to 7 F/Hour.No Temp Effects on River
ML18136A45916 January 1980Ro:On 800116,during Power Operation,Boric Acid Flow in One of Two Required Flow Paths to Core Was Blocked for Approx 3-h.Caused by Inadvertent Closing of Discharge Valve.Valve Immediately Opened & Boric Acid Flow VerifiedBoric Acid
ML18136A33727 December 1979Ro:On 791217,condenser Cooling Water Outlet Temp Exceeded Max Temp Rate Change Permitted by Tech Specs.Caused by Removing Waterbox from Svc Too Rapidly.No Adverse Impact on Environ
ML18136A34710 December 1979Ro:On 791207,when Radiation Alarm Setpoint Reached in Discharge Line of Air Ejectors,Trip Valves Diverted Air Into Containment.Caused by Improper Initial Design Concept.Mods to Maintain Valve Closed Initiated
ML18136A23126 November 1979Ro:On 791110,condenser Cooling Water Outlet Temp Exceeded Temp Change Rate of 3 F/H While Unit 1 Was at 100% Power & Unit 2 Was in Cold Shutdown.Caused by Valve Misalignment Permitting Sodium Fluid to Enter Sys
ML18136A1789 November 1979Ro:On 791026 & 27,condenser Cooling Water Outlet Temp Exceeded Temp Change Rate of 3 F/H.Caused When Waterbox Was Removed from Svc on 791026 & When Returned to Svc on 791027.No Detrimental Effects Found on River Environ
ML18116A17425 June 1979RO on 790622:radiography of Facility Steam Generator Feedwater Nozzles & Reducers Revealed Crack Indications at Counterbore Region.Westinghouse & Util to Evaluate Problem
ML18116A17522 June 1979RO on 790621:Westinghouse Notified Util of Nonconservatism in Accident Analysis.Increase in Steam Generator Ref Resulted from Rise in Containment Temp Not Properly Accounted For.Corrective Action Being Evaluated
ML18114A6986 June 1979RO on 790606:abnormal Degradation of Cable Insulation in Emergency Power Sys Battery Charges.Cause Unknown But Manufacturer Will Be Contacted