ML18139B326

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Ro:On 810428,condenser Cooling Water Outlet Temp Exceeded Max Average Rate of Change.Caused by Lack of Svc Water Flow. Event Caused No Detrimental Effect on River Environ
ML18139B326
Person / Time
Site: Surry Dominion icon.png
Issue date: 05/13/1981
From: Sylvia B
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To: Harold Denton, Varga S
Office of Nuclear Reactor Regulation
References
314, NUDOCS 8105270285
Download: ML18139B326 (1)


Text

e VIRGINIA ELECTR.Ic AND PoWER COMPANY RICRMOND,VIRGJ:N.IA 23261 May 13, 1981 Mr. Harold R. Denton, Director Serial No. 314 Office of Nuclear Reactor Regulation NO/RMT:ms Attn: Mr. Steven A. Varga, Chief Docket No. 50-281 Operating Reactors Branch No. 1 License No. DPR-37 Division of Licensing U. S. Nuclear Regulatory Commission Washington, D. C. 20555 Gentlemen:

This letter report is submitted in accordance with the provisions of Surry Power Station Technical Specification 4.14.C.1.

During the period of 0150 to 0250 on April 28, 1981, the condenser's cooling water outlet temperature exceeded the maximum average rate of change of 3°F/hr permitted by Technical Specification 4.14.A3. The average rate of change dur-ing this period was 5°F/hr. At the time of this event, Unit No. 1 was at cold shutdown and Unit No. 2 was at 40% escalating to full power.

The lack of service water flow through Unit No. 1 is believed to be a major contributing factor to this event. It should be recognized that all due care and caution were exercised during the power escalation.

A search was conducted to determine if the temperature change had affected the river environment. No detrimental evidence was found.

Very truly yours, B. R. Sylvia Manager - Nuclear Operations and Maintenance cc: Mr. James P. O'Reilly s