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 Discovered dateReporting criterionTitleEvent description
ENS 5723724 July 2024 12:02:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Notification of Unusual Event Due to Loss of Offsite Power

The following information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: A Notification of Unusual Event was declared by South Texas Project Unit 1 at 0718 CDT for emergency action level (EAL) SU.1, loss of all offsite power for greater than 15 minutes, following a fire in the switchyard. Unit 1 tripped following the loss of power and is stable in Mode 3. Unit 2 reduced power to 90 percent but was otherwise unaffected by this event. Offsite services responded to the switchyard fire. The fire was extinguished at 0925 CDT. There is no radioactive release and no threat to public safety. The licensee notified state and local authorities and the NRC senior resident inspector. Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email).

  • * * UPDATE ON 7/24/2024 AT 1154 EDT FROM CHRIS VAN FLEET TO ERNEST WEST * * *

The following information was provided by the licensee via phone and email: At 0702 CDT on 7/24/2024, with Unit 1 in Mode 1 at 100 percent power, the Unit 1 reactor automatically tripped due to loss of offsite power. The trip was not complex, with all systems responding normally post-trip. No equipment was inoperable prior to the event that contributed to the event or adversely impacted plant response to the scram. Operations responded and stabilized the plant. Decay heat is being removed by steam generator power operated relief valves (PORV). Unit 2 was reduced in power to approximately 90 percent power due to conditions in the switchyard. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. Notified R4DO (Azua)

  • * * UPDATE ON 7/24/2024 AT 1259 EDT FROM CHRIS MCRARY TO ERNEST WEST * * *

The following is a summary of information provided by the licensee via phone: At 1146 CDT, South Texas Project Unit 1 terminated the previously declared Notification of Unusual Event due to restoration of an offsite source of electrical power. Notified R4DO (Azua), NRR EO (McKenna), IR MOC (Crouch), DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email).

  • * * UPDATE ON 7/24/2024 AT 1555 EDT FROM CHRIS VAN FLEET TO ERNEST WEST * * *

The following information was provided by the licensee via phone and email: For the 10 CFR 50.72(b)(3)(iv)(A) reporting requirements: At 0702 CDT on 7/24/2024, with both Unit 1 and 2 in Mode 1 at 100 percent power, the South Texas Project (STP) north and south switchyard electrical buses were de-energized. In Unit 1, all emergency diesel generators (EDGs) 11, 12, and 13 automatically started in response to loss of offsite power on train `A', `B', and `C' engineered safety feature (ESF) buses. Also in Unit 1, trains `A', `B', and `C' of the auxiliary feedwater (AFW) system automatically started. In Unit 2, EDG 22 automatically started in response to loss of offsite power on the train `B' ESF bus. Also in Unit 2, train `B' of the AFW system automatically started. This event is reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in the valid actuation of a pressurized water reactor auxiliary feedwater system (50.72(b)(3)(iv)(B)(6)) and emergency alternating current (AC) electrical power system (50.72(b)(3)(iv)(B)(8)). There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. For the 10 CFR 50.72(b)(2)(xi) reporting requirement: A news release was completed at 1140 CDT on 7/24/2024, by South Texas Project on the declaration of the Unusual Event. This media release is being reported in accordance with 10 CFR 50.72(b)(2)(xi): Any event or situation, related to the health and safety of the public or onsite personnel, or protection of the environment, for which a news release is planned or notification to other government agencies has been or will be made. Notified R4DO (Azua)

ENS 572148 July 2024 19:21:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via phone and email: At 1521 EDT on July 8, 2024, with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main turbine trip. The (reactor) trip was not complex with all systems responding normally post trip. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the steam dump system and the auxiliary feedwater (AFW) system. Unit 2 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the AFW system (an engineered safety feature) is being reported as an eight-hour report under 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The specific cause of the turbine trip is under investigation by the licensee.
ENS 5719527 June 2024 12:04:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Start of Turbine Driven Auxiliary Feedwater PumpThe following information was provided by the licensee email: On June 27, 2024, at 0804 (EDT), D.C. Cook Unit 2 had an automatic start of the turbine driven auxiliary feedwater pump (TDAFP) following a controlled down power and manual reactor trip at approximately 17 percent power. The automatic start of the TDAFP was due to a steam generator water level 'low low' signal following the reactor trip. The down power and trip were performed in accordance with normal shutdown procedures to comply with the required action C.1 of technical specification 3.4.13, 'reactor coolant system operational leakage.' Reference event notification number EN57194. An automatic start of the TDAFP is an eight hour report per 10CFR 50.72(b)(3)(iv)(A). Unit 2 is being supplied by offsite power. All control rods fully inserted. Steam generators are being fed by both motor driven auxiliary feedwater pumps. Decay heat is being removed via the steam dump system to the main condenser. Preliminary evaluation indicates plant systems functioned normally following the reactor trip. D.C. Cook Unit 2 remains in Mode 3 to repair the previously reported reactor coolant system leakage through valve 2-QRV-251, 'CVCS (chemical and volume control system) charging pumps discharge flow control' valve packing. The NRC Resident Inspector has been notified.
ENS 5717718 June 2024 07:17:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip

The following information was provided by the licensee by email: On 06/18/2024 at 0317 EDT with Unit 2 at 18 percent power, the reactor was manually tripped due to elevated secondary chemistry levels (sodium and chlorides). The trip was uncomplicated with all systems responding normally post trip. Operations stabilized the plant in Mode 3. Decay heat is being removed by auxiliary feedwater and atmospheric dump valves. St. Lucie Unit 1 was unaffected and remains at 100 percent power. This event is being reported pursuant 10CFR 50.72(b)(2)(iv)(B). The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All rods fully inserted. An investigation is underway to determine the root cause of the elevated chemistry levels.

  • * * RETRACTION ON 6/24/2024 AT 1315 FROM BOB MURRELL TO ADAM KOZIOL * * *

The following retraction was provided by the licensee via email: The purpose of this notification is to retract a previous report made on 06/18/2024 at 0652 (EDT) (EN# 57177). Notification of the event to the NRC was initially made because of inserting a manual reactor trip due to elevated secondary chemistry levels (sodium and chlorides). After the initial report, Florida Power and Light has concluded that the event did not meet the reporting requirements on 10 CFR 50.72(b)(2)(iv)(B) since it was part of a normal plant shutdown. Therefore, this event is not considered an unplanned scram and is not reportable to the NRC as a Licensee Event Report per 10 CFR 50.73. The NRC Senior Resident Inspector has been notified.

ENS 571582 June 2024 21:08:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor TripThe following information was provided by the licensee via phone and email: Surry Unit 1 reactor automatically tripped at 1708 EDT on 6/2/24 due to a turbine trip (with the reactor operating at greater than 10 percent reactor power). The turbine control system is currently under investigation. Reactor coolant temperature is being maintained via main steam dumps with main feedwater supplying the steam generators. All systems operated as required. The trip was uncomplicated and all control rods fully inserted into the core. There was no emergency core cooling system (ECCS) or auxiliary feedwater system actuation. Offsite power remains available. There is no impact to Surry Unit 2. This notification is being made pursuant to 10 CFR 50.72(b)(2)(iv)(B) for 4-hour notification of reactor protection system activation. The NRC Resident Inspector has been notified. There were no radiation releases, personnel injuries, or contamination events due to this event.
ENS 5714829 May 2024 10:24:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via email and phone: On May 29, 2024, at 0624 EDT, Unit 1 automatically tripped from 100 percent power due to a negative rate trip. The unit has been stabilized in mode 3 at normal operating temperature and pressure. The reactor trip was uncomplicated and all control rods fully inserted into the core. This reactor protection system actuation is reportable per 10 CFR 50.72(b)(2)(iv)(B). The auxiliary feedwater pumps actuated as designed because of the reactor trip and is reportable per 10 CFR 50.72(b)(3)(iv)(A) for a valid engineered safety feature (ESF) actuation. Decay heat is being removed by the condenser steam dump system and Unit 1 is in a normal shutdown electrical lineup. Unit 2 was not affected by this event. The NRC Resident has been notified.
ENS 5713219 May 2024 04:30:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor TripThe following information was provided by the licensee via email: At 0030 (EDT) on 5/19/24, with Beaver Valley Unit 1 in mode 1 at 14 percent power, the reactor was manually tripped due to inability to control the A steam generator water level. The trip was not complex, with all systems responding normally post-trip. The turbine driven auxiliary feedwater pump automatically started on a valid actuation signal. All control rods inserted into the core. Operations responded and stabilized the plant. Decay heat is being removed by the feedwater system and the main condenser. Beaver Valley Unit 2 is unaffected. Due to the reactor protection system system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the emergency safety feature system actuation (automatic start of the turbine driven auxiliary feedwater pump) while critical, this event is being reported as an eight-hour, non-emergency notification per 10CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been verbally notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 1 is stable on off-site power, normal configuration. All emergency systems are available.
ENS 5712815 May 2024 08:27:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unit 2 Manual Reactor TripThe following information was provided by the licensee via email: On May 15, 2024 at 0427 EDT, DC Cooks Unit 2 reactor was manually tripped due to difficulty maintaining steam generator water levels. DC Cook Unit 2 had removed the main turbine from service at approximately 0354 EDT during a planned down-power to repair a steam leak on the high pressure turbine right outer steam/stop control valve upstream drip pot. Stable steam generator water levels were unable to be maintained. As a result, DC Cook Unit 2 was manually tripped with reactor power stabilizing at approximately 20 percent. This notification is being made in accordance with 10 CFR 50.72(b)(2)(iv)(B), Reactor Protection System actuation as a four hour report, and under 10 CFR 50.72(b)(3)(iv)(A), specified system actuation of the Auxiliary Feedwater System, as an eight hour report. The reactor trip was not complicated and all plant systems functioned normally. The DC Cook NRC Resident Inspector was notified.
ENS 571075 May 2024 08:38:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Lowering Steam Generator Water Level

The following information was provided by the licensee via email and phone: At 0338 CDT, with the unit 1 in mode 1 at 6 percent power, the reactor automatically tripped due to lowering steam generator water level. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for an actuation of the auxiliary feedwater system. Operations responded using procedure 1BwEP-0 and stabilized the plant in mode 3. Decay heat is removed by steam dumps via the main condenser. 1A and 1B auxiliary feedwater pumps were actuated manually prior to the reactor trip in an attempt to restore steam generator water level. Unit 2 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 07/05/2024 AT 0450 EDT FROM MATTHEW WHITE TO TENISHA MEADOWS * * *

The following information was provided by the licensee via email and phone: At 0338 CDT, with the unit 1 in mode 2 at 3 percent power, the reactor automatically tripped due to lowering steam generator water level. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and 10CFR50.72(b)(3)(iv)(A) for an actuation of the auxiliary feedwater system, eight-hour notification. Operations responded using procedure 1BwEP-0 and stabilized the plant in mode 3. Decay heat is being removed by steam dumps via the main condenser. 1A and 1B auxiliary feedwater pumps were actuated manually prior to reactor trip in an attempt to restore steam generator water level. Unit 2 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Notified R3DO (Hartman)

ENS 5709125 March 2024 01:56:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Automatic Turbine Driven Auxiliary Feedwater PumpThe following information was provided by the licensee via phone and email: This report is being made in accordance with 10 CFR 50.73(a)(2)(iv)(A), under the provision of 10 CFR 50.73(a)(1), detailing the event in which an unplanned actuation of the turbine driven auxiliary feedwater pump (TDAFP) at the Callaway plant occurred in response to an invalid actuation signal. The actuation occurred at 2056 (CDT) on 3/21/2024 during restoration from maintenance on the NN12 inverter. The actuation signal was received while closing breaker NK0211 (for connecting the inverter to its associated 125-VDC bus). In response to the TDAFP actuation, operators closed the flow control valves and reduced turbine load by approximately 10 MW electrical. Initial investigation showed that a spurious manual actuation signal had been received and cleared 5 seconds later. The direct cause of the event was due to a voltage transient generated on the NK02 125-VDC bus during closure of the NK0211 breaker. The actuation occurred due to degradation of a 48-VDC power supply (PS1) within engineered safety features actuation system (ESFAS) logic cabinet SA036C. The power supply exhibited elevated ripple during testing as part of troubleshooting efforts, which was indicative of degradation of the regulation circuitry within the supply. This degradation prevented the power supply from sufficiently filtering the transient that occurred on the 125-VDC bus associated with the NN12 inverter. The power supply was replaced. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee originally submitted this event under 10 CFR 50.72(b)(3)(iv)(A) in EN 57043. The licensee has retracted EN 57043.
ENS 5707513 April 2024 04:35:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via phone and email: At 0035 EDT on April 13, 2024, with Unit 1 at 97 percent power, the reactor automatically tripped due to 1 of 3 reactor coolant pump (RCP) low flow reactor trip (signal) associated with a loss of the A and B 4160 volt normal buses. Auxiliary feedwater and the 1-1 emergency diesel generator (EDG) automatically started on valid actuation signals. The 1-1 EDG sequenced on to supply all required loads per plant design. All control rods fully inserted and the trip was not complex with all systems responding normally post-trip. Operators have responded and stabilized the unit in Mode 3 (Hot Standby). Decay heat is being removed by discharging steam to the main condenser via the condenser steam dump system with steam generators being supplied by the main feedwater system. Unit 2 is not affected by the event. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the valid actuations of auxiliary feedwater and the 1-1 EDG, this event is reportable in accordance with 10 CFR 50.72(b)(3)(iv)(A). There was no impact to the health and safety of the public or plant personnel. The NRC senior resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Power for the A-E Bus is on the 1-1 EDG. The D-F Bus is on offsite power. One electrical train of offsite power is down.
ENS 5704724 March 2024 23:34:0010 CFR 50.72(b)(3)(iv)(A), System ActuationValid Specified System Actuations of Unit 2 Train B Emergency Diesel Generator and Train B Auxiliary FeedwaterThe following information was provided by the licensee via email: At 1634 MST on March 24, 2024, an engineered safety features (ESF) service transformer deenergized resulting in a loss of power to the Unit 2 Train B 4.16 kV Class 1E Bus. The Unit 2 Train B emergency diesel generator (EDG) automatically started and energized the Unit 2 Train B 4.16 kV Class 1E Bus. As a result of the loss of power on the Unit 2 Train B 4.16 kV Class 1E Bus and subsequent load sequencing after the Unit 2 Train B EDG started, the Unit 2 Train B auxiliary feedwater (AFW) pump automatically started as designed. The Train B AFW pump was not needed for steam generator level control and no auxiliary feedwater valves repositioned. The Train B AFW Pump did not supply feedwater to the steam generators. All systems operated as designed. Per the emergency plan, no classification was required due to the event. Units 1, 2, and 3 remain in Mode 1 at 100 percent power. The 4.16 kV Class 1E Buses in Units 1 and 3 were not affected by the deenergization of the ESF service transformer. The cause of the ESF service transformer being deenergized is under investigation. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of emergency AC electrical power systems and auxiliary feedwater system. The NRC Resident Inspectors have been informed.
ENS 5704322 March 2024 01:56:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Turbine Driven Auxiliary Feedwater Pump Actuation

The following information was provided by the licensee via email: At 2056 on 3/21/24, Callaway Plant was in Mode 1 at approximately 100 percent power when an automatic start of the turbine driven auxiliary feedwater pump occurred. The event occurred while restoring inverter NN12 from maintenance. NN12 is the normal in-service inverter for the group 2 120-VAC instrument bus (NN02). The actuation occurred while swapping from the swing inverter (NN18) to the normal in-service inverter (NN12). All safety systems responded as expected. At 2334, the turbine driven auxiliary feedwater pump was secured. The plant is being maintained in a stable condition, in mode 1. The NRC Resident Inspector was notified The licensee is investigating the cause of the automatic start.

  • * * RETRACTION ON 4/25/2024 AT 1432 EDT FROM GREG CIZIN TO ERNEST WEST * * *

Event Notification (EN) 57043, made on 03/21/2024 pursuant to 10 CFR 50.72(b)(3)(iv)(A), is being retracted based upon further investigation into the cause of the turbine driven auxiliary feedwater pump (TDAFP) actuation. The TDAFP received an invalid manual initiation signal caused by a voltage transient that was generated on the NK02 125-VDC bus upon closure of downstream breaker NK0211 (while restoring inverter NN12 from maintenance). This actuation signal was due to degradation of a 48-VDC power supply (PS1) within engineered safety features actuation system (ESFAS) logic cabinet SA036C. This degradation likely prevented the power supply from sufficiently filtering the transient that occurred on the 125-VDC bus associated with the NN12 inverter. Notified R4DO (Warnick)

ENS 5703317 March 2024 20:15:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Main Feedwater Pump TripThe following information was provided by the licensee via phone and email: On March 17, 2024, at 1515 CDT, the Comanche Peak Unit 2 reactor was manually tripped due to an anticipated automatic trip due to lo-lo steam generator (SG) water levels. Prior to the trip, main feedwater pump '2B' tripped and an auto runback to 700 MW (60 percent power) was in progress. Both motor driven auxiliary feedwater pumps and the turbine driven auxiliary feedwater pump started due to lo-lo level in all SGs. Unit 2 is being maintained in hot standby (Mode 3) in accordance with integrated plant operating procedures IPO-007B. The emergency response guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the '2B' main feed pump trip was due to loss of primary and redundant power to the servo control valve. The loss of power to the servo control valve is under investigation.
ENS 5702412 March 2024 13:16:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via phone and email: On March 12, 2024, at 0816 CDT, Comanche Peak Unit 2 reactor automatically tripped on lo-lo level in the 2-03 steam generator (SG). Prior to the trip, main feedwater pump (MFP) 2A speed reduced and a manual runback to 700 MW (60 percent) was in progress. Both motor driven auxiliary feedwater pumps and the turbine driven auxiliary feedwater pump started due to lo-lo level in all SGs. Concurrent with the loss of speed on MFP 2A, a servo filter swap was in progress on MFP 2A. Unit 2 is being maintained in hot standby (Mode 3) in accordance with integrated plant operating procedure IPO-007A. The emergency response guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the loss of the MFP is under investigation. Unit 1 was unaffected.
ENS 570065 March 2024 06:32:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via email: At 0132 EST, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main feedwater isolation signal which resulted in steam generator lo-level reactor trip. The reactor trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed using the auxiliary feedwater and steam dump systems. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the auxiliary feedwater system (an engineered safety feature) is being reported as an eight hour report under 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All control rods are fully inserted. The cause of the main feedwater isolation is being investigated.
ENS 570033 March 2024 17:42:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Loss of Main Feedwater Pump SuctionThe following information was provided by the licensee via email: At 1142 CST on 3/3/2024, with Unit 2 in Mode 1 at 29 percent power, the reactor automatically tripped due to a turbine trip caused by a loss of suction to the 22 main feedwater pump. All systems responded normally post trip. Decay heat is being removed via the auxiliary feedwater water system. Secondary steam control mechanism is the steam generator PORVs (power operated relief valves). Unit 1 remains at 100 percent power and is unaffected. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The resident NRC inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The trip occurred while the licensee was returning to power operations after a refueling outage. During the trip, all rods inserted into the core. The plant is in a normal shutdown electrical lineup with offsite power available. The plant will be maintained at normal operating temperature and pressure. There is no known primary to secondary leakage. The cause of the loss of 22 main feedwater pump suction is under investigation.
ENS 5699124 February 2024 20:46:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Steam Generator 22 Feed Pump TripThe following information was provided by the licensee via email: At 1546 EST, with unit 2 at 100 percent power, the reactor was manually tripped due to the '22' steam generator feed pump tripping. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Operations responded using emergency operation procedure EOP-0, Post Trip Immediate Actions and EOP-1, Uncomplicated Reactor Trip and stabilized the plant in mode 3. Decay heat is removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 is not affected. ESFAS (engineered safety features actuation systems) actuation (auxiliary feedwater manual actuation) is reportable under 10 CFR 50.72(b)(3)(iv)(A) 8-hour report. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5697116 February 2024 11:34:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip and Automatic Actuation of Auxiliary Feedwater SystemThe following information was provided by the licensee via email: At 0048 CST on February 16, 2024, with Unit 2 in mode 1 at 100 percent power, the reactor was manually tripped due to a loss of 2A 125V DC distribution panel. The trip was complex due to the loss of components associated with A-train DC power. Operations responded and stabilized the plant. Decay heat is being removed by the atmospheric relief valves. Unit 1 is not affected. An automatic actuation of the auxiliary feedwater system (AFW) occurred due to low-low steam generator levels. The AFW auto-start is an expected response with low-low steam generator levels from the reactor trip. AFW is still currently controlling steam generator levels. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the AFW System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5696815 February 2024 08:47:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Turbine Trip/Reactor TripThe following information was provided by the licensee via email: At 0247 CST on 2/15/2024, Callaway Plant was in mode 1 at approximately 100 percent power when a turbine trip and reactor trip occurred. All safety systems responded as expected with the exception of an indication issue on the feedwater isolation valves, which were confirmed closed. A valid feedwater isolation signal and auxiliary feedwater actuation signal were also received as a result of the reactor trip. The plant is being maintained stable in mode 3. All control rods fully inserted from the reactor trip signal and decay heat is being removed via the auxiliary feedwater system and steam dumps. The NRC Resident Inspector was notified.
ENS 5693528 January 2024 02:41:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via email: At 2141 EDT, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main turbine trip. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed using the auxiliary feedwater and steam dump systems. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the auxiliary feedwater system (an engineered safety feature) is being reported as an eight hour report under 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All control rods are fully inserted. The cause of the turbine trip is being investigated. The licensee notified the NRC Resident Inspector.
ENS 5689918 December 2023 06:00:0010 CFR 21.21(d)(3)(i), Failure to Comply or DefectInitial Part 21 Report - Deficient Fuel Injectors

The following is a synopsis of information was provided by the licensee via phone and email: Pursuant to 10 CFR 21.21(d)(3)(i), Paragon provided initial notification of a defect associated with the auxiliary feedwater pump diesel engine fuel injectors supplied to Constellation. The injectors were provided to Paragon for refurbishment. Constellation provided Paragon with root cause report # 4703982 on November 12, 2023. The associated failure analysis report documented potential defects with some fuel injectors supplied to Braidwood. These reported deficiencies allowed excessive fuel oil leakage which resulted in diesel lubricating oil system contamination above specified limits. Paragon concluded their evaluation on December 18, 2023, which determined that this condition, if left uncorrected, could contribute to a substantial safety hazard and is reportable in accordance with 10 CFR Part 21. The extent of condition is limited to the Constellation Braidwood and Byron plants. Paragon has entered this condition in their corrective action program. Affected injectors at Braidwood have been removed from service and returned to Paragon. Paragon is coordinating with Byron on recommended actions and will follow up with a final notification on or before 1/17/2024.

  • * * UPDATE ON 1/17/24 AT 1626 EST FROM RICHARD KNOTT TO ADAM KOZIOL * * *

Paragon Energy Solutions submitted a final report for this event. Notified R3DO (Orlikowski), R4DO (Josey), and Part 21 (email).

ENS 5685616 November 2023 07:27:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip

The following information was provided by the licensee via email: At 0227 EST on 11/16/23, Calvert Cliffs Unit 2 experienced an automatic trip from the reactor protection system (RPS) based on reactor trip bus undervoltage (UV). At that time, a loss of U-4000-22 (13 kV to 4 kV transformer) caused a loss of 22, 23, and 24 4 kV busses. This resulted in a loss of both motor generator (MG) sets causing the reactor trip bus UV. The loss of 22 and 23 4 kV non-safety related busses resulted in a loss of main feedwater. Auxiliary feedwater (AFW) was manually initiated and is feeding both steam generators. The 2B diesel generator (DG) started and restored the 24 4 kV safety related bus. Heat removal is via the normal turbine bypass valves to the main condenser. RPS actuation is reportable under 10 CFR 50.72(b)(2)(iv)(B) - 4 hour report ESFAS (engineering safety features actuation system) actuation (2B DG start on UV) is reportable under 10 CFR 50.72(b)(3)(iv)(A) - 8 hour report AFW operation is reportable under 10 CFR 50.73(a)(2)(iv)(A) - 60 day report The NRC Senior Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All rods fully inserted. There was no impact on Unit 1 operations. Unit 2 is stable in mode 3.

  • * * UPDATE ON AT 0940 EST FROM KERRY HUMMER TO ADAM KOZIOL * * *

ESFAS actuation (AFW manual initiation) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8 hour report Notified R1DO (Defrancisco).

ENS 5685214 November 2023 16:41:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor TripThe following information was provided by the licensee via phone and email: At 1041 CST on 11/14/23 with Farley Unit 2 in Mode 1 at 10 percent power, the reactor was manually tripped due to rising steam generator levels. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Auxiliary feedwater (AFW) was manually initiated in accordance with plant procedures and is feeding the steam generators. Heat removal is being provided via the atmospheric relief valves. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the auxiliary feedwater system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All rods fully inserted. The licensee attempted to take manual control of the feedwater control valves to lower steam generator level but, due to reaching a steam generator level that requires a manual trip, the licensee manually tripped the reactor.
ENS 568418 November 2023 11:45:0010 CFR 50.72(b)(3)(iv)(A), System ActuationManual Actuation of Auxiliary Feedwater System (AFW)The following information was provided by the licensee via phone and email: At 0645 EST, on November 8, 2023, with Unit 2 in Mode 3 at zero percent power, a manual actuation of the auxiliary feedwater system (AFW) occurred during a planned plant cooldown. The reason for the AFW manual-start was a trip of the 22 steam generator feed pump due to a high casing level. The 23 AFW motor driven pump was manually started in accordance with implementation of AOP-3G, Malfunction of Main Feedwater System to restore steam generator levels. There was no impact to Unit 1. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the AFW system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: No other systems were affected. No other compensatory or mitigation strategies implemented. Plant cooldown was the only significant evolution in progress. No impact to other technical specifications or limiting conditions for operation. All systems functioned as required. The electric plant is being supplied by offsite power with all diesel generators available. No significant increase in plant risk. There was nothing unusual or not understood.
ENS 568397 November 2023 21:17:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Trip Due to NON-SAFETY Related Bus Under VoltageThe following information was provided by the licensee via email: At 1617 on 11/7/2023, Calvert Cliffs Unit 2 experienced an automatic trip from a Reactor Protection System (RPS) based on reactor trip bus under voltage (UV). At that time a loss of U-4000-22 caused a loss of 22, 23, and 24 4kV busses. This resulted in a loss of both motor generator (MG) sets causing the reactor trip bus UV condition. The loss of 22 and 23 4kV non-safety related busses resulted in a loss of main feedwater. Auxiliary feedwater (AFW) was manually initiated and is feeding both steam generators. The 2B diesel generator (DG) started and restored the 24 4kV safety related bus. Heat removal is via the normal turbine bypass valves to the main condenser. RPS actuation is reportable under 10 CFR 50.72(b)(2)(iv)(B) - 4-hour report. ESFAS actuation (2B DG start on UV) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8-hour report. ESFAS actuation (AFW manual initiation) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8-hour report. Site Senior NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 1 was unaffected. Estimation of duration of shutdown is 24 hours.
ENS 568387 November 2023 17:00:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual HeatAuxiliary Feedwater System InoperableThe following information was provided by the licensee via email: On November 07, 2023 at 1200 EST, it was discovered that all pumps in the Auxiliary Feedwater system were inoperable due to the loss of control power to the 'B' train Emergency Feedwater (EFW) flow control valve which supplies the 'D' steam generator. The redundant 'A' train EFW control valve for the 'D' steam generator remains functional, as well as the capability of the Auxiliary Feedwater system to supply all steam generators. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(v)(B). The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The 'A' and 'B' EFW Flow Control Valves are arranged in a series configuration for each Steam Generator. Failure of any of the 8 EFW Flow Control Valves to meet its Surveillance Requirements will render all EFW Pumps inoperable per tech specs.
ENS 5680319 October 2023 16:10:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip

The following information was provided by the licensee via email: On 10/19/2023, at approximately 1110 (CST), with Unit 1 in mode 1 at 100 percent power, the reactor automatically tripped. All control rods fully inserted into the core following the trip. All safety functions operated as designed. The cause of the trip is being investigated. Operations responded and stabilized the plant. Auxiliary feedwater actuated as expected. Decay heat is being removed by the steam generator through the steam generator power operated relief valve. The trip was complex as non-safety related power was lost to both Unit 1 and Unit 2. Unit 1 is currently in mode 3 and on natural recirculation as both reactor coolant pumps are without power. Unit 2 is currently in a refueling outage with all fuel in the spent fuel pool (SFP). SFP cooling was lost for approximately 70 minutes. No impacts to the SFP temperature were observed. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the actuation of the auxiliary feedwater system following the reactor trip, this event is being reported as a specified system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 10/19/2023 AT 1646 EDT FROM MARTIN CABIRO TO ERNEST WEST * * *

The second paragraph of the original report is amended as follows to correct information regarding the spent fuel pool for Unit 2: Unit 2 is currently in a refueling outage with all fuel in the spent fuel pool (SFP). SFP cooling was maintained at all times with one train of SFP cooling. The second train lost power and was restarted approximately 70 minutes (after power was lost). No impacts to the SFP temperature were observed. Notified R3DO (Orth) and IR MOC (Crouch) and NRR EO (Felts) via email

ENS 5680218 October 2023 15:16:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Actuation of Auxiliary Feedwater SystemThe following information was provided by the licensee via email: On October 18, 2023, at 1116 (EDT), with Unit 1 in Mode 5, an automatic actuation of the 1A auxiliary feedwater motor driven pump occurred when an incorrect action resulted in an automatic start signal. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the auxiliary feedwater system. Feedwater is not needed for plant conditions, and the 1A auxiliary feedwater pump did not feed the steam generators. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 567691 October 2023 03:14:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor TripThe following information was provided by the licensee via email: At 2014 (PDT) on 09/30/2023, with (Diablo Canyon) Unit 1 in Mode 1 at 11 percent reactor power in preparation for a pre-planned manual reactor trip into a scheduled refueling outage, the reactor was manually tripped due to a failed secondary system dump valve. Auxiliary feedwater was manually started in accordance with plant procedures. This event is being reported in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). There was no plant or public safety impact. The NRC Senior Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Diablo Canyon Unit 2 was unaffected.
ENS 5669222 August 2023 21:24:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip and Automatic Actuation of Auxiliary Feedwater SystemThe following information was provided by the licensee via email: At 1724 EDT, on August 22, 2023, with Unit 1 in Mode 1 at 100 percent power, the reactor was manually tripped due to a failure of the non-safety heater drain pump 'B' and the failure of the non-safety condensate pump 'A' to automatically or manually start. At 1735 EDT, a fire was identified on heater drain pump 'B' and was extinguished by the onsite fire brigade at 1807 EDT. Operations responded and stabilized the plant. The trip was not complex, with all safety systems responding normally post-trip. Decay heat is being removed by the main steam system to the main condenser using the steam dumps. There was no impact to Units 2, 3, or 4. An automatic actuation of the auxiliary feedwater system (AFW) also occurred, as expected, due to lo-lo steam generator levels resulting from the reactor trip. AFW is currently controlling all steam generator levels at their normal levels. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the notification of another government agency, the Burke County Fire Department, this event is being reported as a four-hour, non-emergency notification under 10 CFR 50.72(b)(2)(xi). The Burke County Fire Department was not needed to extinguish the fire. This event is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the auxiliary feedwater system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 566604 August 2023 21:46:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via phone and email: At 1746 EDT on 08/04/2023, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to number 2 steam generator low low level. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed by using the auxiliary feedwater and steam dump systems. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the auxiliary feedwater system (an engineered safety feature) is being reported as an eight-hour report under 10 CFR 50.72 (b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All control rods are fully inserted. The cause of the number 2 steam generator low low level is being investigated.
ENS 566106 July 2023 16:32:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed ConditionThe following information was provided by the licensee via email: On July 6, 2023, at 1232 EDT, while operating in Mode 1 at 100 percent power, the supply check valve from the number 2 steam generator to the turbine driven auxiliary feedwater pump was determined during troubleshooting that it is not able to perform its isolation function. This failure would have resulted in the blowdown of both steam generators during a main steam line break in the number 2 steam generator main steam line upstream of the main steam isolation valves until the operators could isolate the faulted steam generator. Previous evaluation has determined that this condition constituted an unanalyzed condition that could impact containment pressure. There was no radioactive release to the environment. The steam line from the steam generator to the turbine driven auxiliary feedwater pump was isolated by use of a motor operated valve in the discharge line of the number 2 steam generator. There was no impact to Unit 3 which remains at 100 percent power. The NRC Senior Resident Inspector was notified. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B) as a condition that resulted in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety.
ENS 5659327 June 2023 20:26:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via phone and email: At 1626 EDT, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main turbine trip. The (reactor) trip was not complex with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed using the auxiliary feedwater and steam dump systems. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the auxiliary feedwater system (an engineered safety feature) is being reported as an eight hour report under 10 CFR 50.72 (b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All control rods are fully inserted. The cause of the turbine trip is being investigated.
ENS 5658016 June 2023 23:32:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to LO-LO Steam Generator LevelThe following information was provided by the licensee via email: (On June 16, 2023,) at 1832 CDT, Unit 1 reactor automatically tripped on lo-lo level in the '1-04' steam generator (SG). Prior to the trip, the 1B (main feedwater pump) (MFP) tripped due to speed oscillations and a runback to 700MW was in progress. Both motor driven auxiliary feedwater pumps started due to the lo-lo level in SG '1-04'. Unit 1 is being maintained in hot standby (Mode 3) in accordance with Integrated Plant Operating Procedure IPO-007A. The Emergency Response Guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves. The licensee notified the NRC Resident Inspector. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 1 is in a normal post-trip electrical line-up. There was no effect on Unit 2 due to the Unit 1 trip.
ENS 565512 June 2023 11:05:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via email: The following event description is based on information currently available. If through subsequent reviews of this event additional information is identified that is pertinent to this event or alters the information being provided at this time a follow-up notification will be made via the ENS (Emergency Notification System) or under the reporting requirements of 10 CFR 50.73. At 0405 MDT on June 2, 2023, the Unit 2 reactor automatically tripped on low steam generator water levels due to degraded flow from the A main feedwater pump. Steam generator water levels reached the automatic Auxiliary Feedwater Actuation System (AFAS) setpoint resulting in automatic AFAS-1 and AFAS-2 actuations and subsequent start of both class auxiliary feedwater pumps. Steam Generator water levels are being restored to normal band with the class 1E powered motor driven auxiliary feedwater pump. Following the reactor trip, all control element assemblies inserted fully into the core. No emergency plan classification was required per the Emergency Plan. Safety related buses remained powered from offsite power during the event and the offsite power grid is stable. Both emergency diesel generators automatically started on the AFAS-1 and AFAS-2 actuations as designed and are currently running unloaded. This event is being reported as a reactor protection system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B) and a specified system actuation in accordance with 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident Inspector has been informed. Unit 1 and 3 are in Mode 1 at 100 percent power. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Decay heat is being removed to main condenser via automatic steam bypass and B auxiliary feedwater pump.
ENS 5654430 May 2023 08:46:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor TripThe following information was provided by the licensee via email: At 0446 EDT on 5/30/2023, with Millstone Power Station Unit 3 operating at approximately 100 percent reactor power, an automatic reactor trip occurred due to a turbine trip caused by electrical protection. The reactor trip was uncomplicated and decay heat is being removed via steam dumps to the condenser. All systems responded as expected to the trip. Auxiliary feedwater actuated automatically as expected following the trip due to low-low levels in the steam generators. There was no risk to the public. There was no impact to Millstone Unit 2. This event is being reported as a four hour report under 10CFR50.72(b)(2)(iv)(B) as a condition that resulted in actuation of the reactor protection system while the reactor was critical, and as an eight hour report under 10CFR50.72(b)(3)(iv)(A) and 10CFR50.72(b)(3)(iv)(B) for actuation of the auxiliary feedwater system. The NRC Resident Inspector has been notified.
ENS 5654327 May 2023 23:34:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Notification of Unusual Event Due to Multiple Fire Alarms in Containment Not Verified within 15 Minutes

The following information was provided by the licensee via email: Notification of Unusual Event, HU4.1 declared based on multiple fire alarms in the containment building not verified within 15 minutes. Turbine trip causing reactor trip due to fault on 2GT transformer. At 1845 CDT, verification of no fire in the containment building. Notified DHS Senior Watch Officer, FEMA Operations Center, CISA Central watch officer, DOE Operations Center (email), HHS Operations Center (email), EPA Emergency Operations Center (email), USDA Operations Center (email), FDA EOC (email), FEMA NWC (email) and DHS Nuclear SSA (email), FEMA NRCC (email) and CWMD watch desk (email).

  • * * UPDATE AT 0148 EDT ON 5/28/23 FROM CHRIS BAARTMAN TO BILL GOTT * * *

The following information was provided by the licensee via email: This update is being made to report the actuation of the auxiliary feedwater system following the reactor trip at 1819 CDT. This event is being reported as a specified system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(3)(iv)(A). This update is also being made for the termination of the notification of unusual event at 2304 CDT on 5/27/2023. The basis for the termination was that there was no indication of a fire. Upon lockout of 2GT transformer, main to reserve power transfer did not occur on 3 of 4 non-safeguards buses. Subsequently, operator action successfully restored power to all non-safeguards buses at 1925 CDT. There was no impact to the health and safety of the public or plant personnel. The NRC resident inspector has been notified of the update. Notified R3DO (Benjam¡n), NRR EO (Walker), IRMOC (Grant), DHS Senior Watch Officer, FEMA Operations Center, CISA Central watch officer, DOE Operations Center (email), HHS Operations Center (email), EPA Emergency Operations Center (email), USDA Operations Center (email), FDA EOC (email), FEMA NWC (email) and DHS Nuclear SSA (email), FEMA NRCC (email) and CWMD watch desk (email).

ENS 5652719 May 2023 12:52:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Actuation of Auxiliary Feedwater System (AFW)The following information was provided by the licensee via email: At 0852 (EDT) on May 19, 2023, with Unit 2 in Mode 3 at zero percent power, an actuation of the auxiliary feedwater system (AFW) occurred. The reason for the AFW auto-start was a failed start attempt of the 'B' main feedwater pump. The 'A' and 'B' motor driven auxiliary feedwater (MDAFW) pumps automatically started as designed when the 'Loss of Both Main Feedwater Pumps' signal was received. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the AFW system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 564599 April 2023 04:44:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Loss of Reactor Coolant Pumps

The following information was provided by the licensee via email: The following event description is based on information currently available. If through subsequent reviews of this event additional information is identified that is pertinent to this event or alters the information being provided at this time a follow-up notification will be made via the ENS or under the reporting requirements of 10 CFR 50.73. At 2144 MST on April 8, 2023, the Unit 1 reactor automatically tripped due to the loss of reactor coolant pumps stemming from the loss of 13.8 kV power to the pumps. Prior to the reactor trip, the main turbine tripped due to a loss of hydraulic pressure. The main generator output breakers did not automatically open on the turbine trip as expected so the control room operators opened the breakers per procedural guidance. Once the breakers were opened, the two 13.8 kV electrical distribution buses failed to complete a fast bus transfer, which resulted in the loss of power to the reactor coolant pumps, initiating the reactor trip. The control room operators manually actuated a main steam isolation signal per procedure, requiring use of the atmospheric dump valves. Following the reactor trip, all control element assemblies inserted fully into the core. No automatic specified system actuation was required or occurred. No emergency plan classification was required per the Emergency Plan. Safety related buses remained powered from offsite power during the event and the offsite power grid is stable. Unit 1 is stable and in Mode 3. Decay heat is being removed by the atmospheric dump valves and the class 1E powered motor driven auxiliary feedwater pump. The loss of hydraulic pressure, the main generator output breakers failing to automatically open and the fast bus transfer not actuating are being investigated. This event is being reported as a reactor protection system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B). The NRC Senior Resident Inspector has been informed. Unit 2 is in a refueling outage in Mode 5 and Unit 3 is in Mode 1 at 100 percent power.

  • * * UPDATE ON 4/9/23 AT 0835 EDT FROM TANNER GOODMAN TO ADAM KOZIOL * * *

This update is being made to report the manual actuation of the B-train auxiliary feedwater pump and manual main steam isolation signal (MSIS) actuation affecting multiple main steam isolation valves (MSIVs) following the reactor trip. This event is being reported as a reactor protection system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B) and a specified system actuation in accordance with 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident Inspector has been informed of the update. Notified R4DO (Warnick)

  • * * UPDATE ON 5/3/23 AT 1945 EDT FROM LORRAINE WEAVER TO JOHN RUSSELL * * *

This update is intended to clarify the initial description of the event that occurred on 4/8/2023. Prior to the reactor trip, the main turbine tripped due to a loss of hydraulic pressure. The main generator output breakers did not automatically open on the turbine trip. The control room operators manually opened the breakers per procedural guidance. Once the breakers were opened, the two 13.8 kV electrical distribution buses de-energized. A fast bus transfer did not occur per design, which resulted in the loss of power to the reactor coolant pumps, initiating the reactor trip. The control room operators manually actuated a main steam isolation signal per procedure, requiring use of the atmospheric dump valves. The NRC Senior Resident Inspector has been informed of the update. Notified R4DO (Gaddy)

ENS 564512 April 2023 07:52:0010 CFR 50.72(b)(3)(iv)(A), System ActuationManual Actuation of Auxiliary Feedwater Motor Driven PumpsThe following information was provided by the licensee via email: On April 2, 2023, at 0341 EDT, with Unit 2 in Mode 3 and the 2B main feedwater pump feeding the steam generators, the 2A main feedwater pump recirculation valve, 2CF-76, failed. Further, observation of the operating 2B main feedwater pump recirculation valve, 2CF-81, called into question its functionality. At 0352 EDT, operations manually started the auxiliary feedwater motor driven pumps to feed the stream generators to allow maintenance on the main feedwater system. The auxiliary feedwater motor driven pumps started as designed. Flow to the steam generator was not adversely impacted during this sequence. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the auxiliary feedwater system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 563451 January 2023 11:04:0010 CFR 50.73(a)(1), Submit an LER60-DAY Optional Telephonic Notification of Invalid Actuation of Auxiliary Feedwater PumpThe following information was provided by the licensee via email: This 60-day optional telephone notification is being made in lieu of a Licensee Event Report as allowed by 10 CFR 50.73(a)(1). This notification is made pursuant to 10 CFR 50.73(a)(2)(iv)(A) for an invalid system actuation. On January 1, 2023, at approximately 0604 EST, static inverter KXA failed causing a loss of power to shared 120-VAC auxiliary control panel board KXA. Operations entered the appropriate procedures to assist in diagnosing and responding to the event. As expected, the solenoid valves in the instrument lines to steam supply valves 1SA-48ABC and 1SA-49AB deenergized, causing 1SA-48ABC and 1SA-49AB to open and admit steam to the unit 1 turbine driven auxiliary feedwater pump (TDAFWP). Operations reduced turbine load to maintain reactor power less than 100 percent. At approximately 0641 EST, power was restored to the KXA panelboard and the TDAFWP was secured. All systems functioned as required. Actuation of the TDAFWP was not initiated in response to actual plant conditions or parameters satisfying the requirements for initiation of the system nor was the actuation due to an intentional manual initiation. Therefore, this actuation is considered an invalid actuation. The NRC Resident Inspector has been notified.
ENS 563291 February 2023 15:56:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due and Automatic Actuation of Auxiliary Feedwater SystemThe following information was provided by the licensee via email: At 0956 CST with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped due to a turbine trip. The trip was not complex with all safety related systems responding normally post-trip. During the trip, the non safety related '1A' 4160V bus lost power resulting in the loss of one Reactor Coolant Pump (RCP-1A). Operations responded and stabilized the plant. The '1A' 4160V bus was re-energized at 1031 CST. Decay heat is being removed by steam dumps to the main condenser. Farley Unit 2 is not affected. An automatic actuation of (Auxiliary Feedwater) AFW also occurred, which is an expected response from the reactor trip. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour report per 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Auxiliary Feedwater System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 562944 January 2023 03:59:0010 CFR 50.72(b)(3)(iv)(A), System ActuationLoss of Offsite Power SourceThe following information was provided by the licensee via email: At 2259 EST on 1/3/2023, with Unit 1 and Unit 2 in Mode 1 at 100 percent power, an actuation of the Unit 1 B and Unit 2 A emergency diesel generator (EDG) systems, as well as an actuation of the associated auxiliary feedwater (AFW) systems on each unit occurred. The reason for the EDG auto-starts was due to a loss of an offsite power source (loss of one of the two reserve auxiliary transformers (RAT) on each unit) to the Unit 1 B and Unit 2 A safety related buses. The EDG and AFW systems automatically started as designed when the valid undervoltage signal on the affected safety related bus was received. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Emergency Diesel Generator and the Auxiliary Feedwater Systems for both Unit 1 and Unit 2. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5628624 December 2022 07:22:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripThe following information was provided by the licensee via email: At 0222 (EST) on 12/24/22, with Unit 2 at 100 percent power during steady state operation, the reactor automatically tripped and a safety injection actuated due to steam generator differential pressure. The trip and safety injection were not complex, with all systems responding normally post-trip. An actuation of the auxiliary feedwater system occurred following the reactor trip as expected due to low level in the steam generators. The unit is stable in Mode 3. The turbine bypass steam dumps and auxiliary feedwater system are removing decay heat. Salem Unit 1 was not affected. Due to the actuation of the reactor protection system while critical, this event is being reported as a four hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported as an eight hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the auxiliary feedwater system. There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5621610 November 2022 12:44:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip and Auxiliary Feedwater System ActuationThe following information was provided by the licensee via email: At 0744 EST on November 10, 2022, DC Cook Unit 2 tripped automatically on high-high level of number 23 steam generator (SG). The reason for the high-high level in SG 23 is under investigation. This notification is being made in accordance with 10 CFR 50.72(b)(2)(iv)(B), Reactor Protection System (RPS) actuation as a four (4) hour report, and under 10 CFR 50.72(b)(3)(iv)(A), specified system actuation of the Auxiliary Feedwater System, as an eight (8) hour report. The DC Cook NRC Resident Inspector has been notified. Unit 2 is being supplied by offsite power. All control rods fully inserted. All Auxiliary Feedwater Pumps started properly. Decay heat is being removed via the Steam Dump System. Preliminary evaluation indicates all plant systems functioned normally following the reactor trip. DC Cook Unit 2 remains stable in Mode 3 while conducting the post trip review. No radioactive release is in progress as a result of this event.
ENS 5619031 October 2022 00:57:0010 CFR 50.72(b)(3)(iv)(A), System ActuationSpecified System Actuation - Auxiliary Feedwater System ActuationThe following information was provided by the licensee via email: At 2057 Eastern Daylight Time (EDT), with Unit 1 in Mode 3 at 0 percent power, an actuation of the Auxiliary Feedwater (AFW) System occurred during an attempt to start the 'B' Main Feed Pump. The reason for the AFW system auto-start was due to the 'A' electrical bus being under clearance and the 'B' Main Feed Pump not starting, resulting in a valid actuation signal for loss of both Main Feedwater pumps. The 'A' and 'B' motor-driven AFW (MDAFW) pumps were running prior to the attempted start of the B Main Feedwater pump and continued to run. The MDAFW Flow Control Valves (FCVs) went full open automatically as designed when the MDAFW actuation signal was received. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the AFW System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5618930 October 2022 10:53:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip and Auxiliary Feedwater System ActuationThe following information was provided by the licensee via email: At 0653 Eastern Daylight Time (EDT), with Unit 1 in Mode 1, at 16 percent power, an automatic reactor trip occurred due to an under-voltage condition on the 'A' reactor coolant pump (RCP) and the 'C' RCP. Power was lost from the 'A' auxiliary bus while performing an operating procedure to transfer power from the 'A' start-up transformer to the 'A' unit auxiliary transformer. Operations responded and stabilized the plant. Decay heat is being removed by the main steam system to the atmosphere using the steam generator power-operated relief valves. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the auxiliary feedwater system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5618628 October 2022 00:50:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentAuxiliary Feedwater System InoperableThe following information was provided by the licensee via email: At 2050 EDT (on October 27, 2022), with Unit 1 in Mode 3, it was discovered that all auxiliary feedwater pumps were simultaneously inoperable and the capability to supply the 'B' steam generator was not maintained; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The function of the auxiliary feedwater pumps to supply the 'A' steam generator and 'C' steam generator was maintained. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5617724 October 2022 12:57:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip and Auxiliary Feedwater System ActuationThe following information was provided by the licensee via email: On 10/24/2022 at 0857 EDT, with Unit 2 in Mode 1 at 7 percent power, the reactor was manually tripped due to a 2B train main feedwater pump trip. The trip was not complex, with all systems responding normally post-trip. The auxiliary feedwater (AFW) system started automatically as expected. Operations responded and stabilized the plant. Decay heat is being removed by the steam generators and discharging to the condenser. Unit 1 is not affected. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The automatic start of the auxiliary feedwater system is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.