ENS 56543
ENS Event | |
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23:34 May 27, 2023 | |
Title | Notification of Unusual Event Due to Multiple Fire Alarms in Containment Not Verified within 15 Minutes |
Event Description | The following information was provided by the licensee via email:
Notification of Unusual Event, HU4.1 declared based on multiple fire alarms in the containment building not verified within 15 minutes. Turbine trip causing reactor trip due to fault on 2GT transformer. At 1845 CDT, verification of no fire in the containment building. Notified DHS Senior Watch Officer, FEMA Operations Center, CISA Central watch officer, DOE Operations Center (email), HHS Operations Center (email), EPA Emergency Operations Center (email), USDA Operations Center (email), FDA EOC (email), FEMA NWC (email) and DHS Nuclear SSA (email), FEMA NRCC (email) and CWMD watch desk (email).
The following information was provided by the licensee via email: This update is being made to report the actuation of the auxiliary feedwater system following the reactor trip at 1819 CDT. This event is being reported as a specified system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(3)(iv)(A). This update is also being made for the termination of the notification of unusual event at 2304 CDT on 5/27/2023. The basis for the termination was that there was no indication of a fire. Upon lockout of 2GT transformer, main to reserve power transfer did not occur on 3 of 4 non-safeguards buses. Subsequently, operator action successfully restored power to all non-safeguards buses at 1925 CDT. There was no impact to the health and safety of the public or plant personnel. The NRC resident inspector has been notified of the update. Notified R3DO (Benjam¡n), NRR EO (Walker), IRMOC (Grant), DHS Senior Watch Officer, FEMA Operations Center, CISA Central watch officer, DOE Operations Center (email), HHS Operations Center (email), EPA Emergency Operations Center (email), USDA Operations Center (email), FDA EOC (email), FEMA NWC (email) and DHS Nuclear SSA (email), FEMA NRCC (email) and CWMD watch desk (email). |
Where | |
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Prairie Island Minnesota (NRC Region 3) | |
Reporting | |
10 CFR 50.72(a) (1) (i), Emergency Class Declaration 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000306/LER-2023-001 Gt/Xfmr Lockout Due to Failure of Lightning Arrester Caused Unit 2 Reactor Trip |
Time - Person (Reporting Time:+-3.1 h-0.129 days <br />-0.0185 weeks <br />-0.00425 months <br />) | |
Opened: | Chris Baartman 20:28 May 27, 2023 |
NRC Officer: | Donald Norwood |
Last Updated: | May 28, 2023 |
56543 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Prairie Island with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 574042024-10-29T15:23:00029 October 2024 15:23:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 570032024-03-03T17:42:0003 March 2024 17:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Main Feedwater Pump Suction ENS 568032023-10-19T16:10:00019 October 2023 16:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 565432023-05-27T23:34:00027 May 2023 23:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Notification of Unusual Event Due to Multiple Fire Alarms in Containment Not Verified within 15 Minutes ENS 555032021-10-03T20:25:0003 October 2021 20:25:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation ENS 548592020-08-26T18:19:00026 August 2020 18:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Flux Rate ENS 534082018-05-17T16:15:00017 May 2018 16:15:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of Emergency Diesel Generator ENS 521782016-08-14T04:59:00014 August 2016 04:59:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Due to Excessive Reactor Coolant System Leakage ENS 516092015-12-17T19:18:00017 December 2015 19:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Fire Alarm in Containment Not Verified within 15 Minutes ENS 511362015-06-07T12:35:0007 June 2015 12:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Resulting from Turbine Trip on Low Oil Pressure ENS 511072015-06-01T03:20:0001 June 2015 03:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Trip of Condensate and Main Feedwater Pump ENS 509502015-04-03T11:52:0003 April 2015 11:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Loss of Main Feedwater Pump ENS 508662015-03-05T10:06:0005 March 2015 10:06:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unit 2 Declares Unusual Event Due to Inability to Validate a Containment Fire Alarm within 15 Minutes ENS 502212014-06-23T16:07:00023 June 2014 16:07:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Auto Start Due to Degraded Bus Voltage Signal ENS 484642012-10-31T19:18:00031 October 2012 19:18:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Notice of Unusual Event Due to Security Condition ENS 481862012-08-14T08:12:00014 August 2012 08:12:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Based on Both Emergency Diesels Being Declared Inoperable ENS 477202012-03-06T12:24:0006 March 2012 12:24:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Notification of Unusual Event Due to Unidentified Rcs Leakage Greater than 10 Gpm ENS 476832012-02-22T05:42:00022 February 2012 05:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Feedwater Heater Hi Hi Alarm ENS 475692012-01-05T09:53:0005 January 2012 09:53:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Sodium Hypochlorite Leak Resulted in Airborne Concentrations Potentially Dangerous to Life and Health ENS 470172011-07-01T20:52:0001 July 2011 20:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Manual Trip Due to Electro-Hydraulic Control Fluid Leak on Turbine Stop Valve ENS 468302011-05-09T12:22:0009 May 2011 12:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Upon Turbine Trip Due to Main Generator Lockout ENS 459522010-05-25T08:14:00025 May 2010 08:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 458512010-04-17T03:37:00017 April 2010 03:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip Due to Turbine Trip ENS 450772009-05-18T18:05:00018 May 2009 18:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip/Reactor Trip Due to Condenser Vacuum ENS 449202009-03-19T20:32:00019 March 2009 20:32:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Start of a Cooling Water Pump During Testing ENS 446152008-10-30T19:17:00030 October 2008 19:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Manually Tripped Due to Failure in Rod Control System ENS 443802008-08-03T08:52:0003 August 2008 08:52:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event - Hydrazine Leak in Non-Vital Area of the Turbine Building ENS 443772008-07-31T13:17:00031 July 2008 13:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip During Testing ENS 432802007-04-05T14:08:0005 April 2007 14:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Reactor Trip Caused by Spurious Safety Injection During Testing ENS 425042006-04-14T19:25:00014 April 2006 19:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Condensate Pump and Feedwater Pump Trip 2024-03-03T17:42:00 | |