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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 541983 August 2019 23:47:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip and Manual Actuation of Reactor Core Isolation CoolingAt 1947 (EDT) on 8/3/19, with Hope Creek in Mode 1 at 37 percent power, the reactor was manually scrammed due to loss of condenser vacuum. All control rods fully inserted into the core. All safety systems responded as designed and expected. Reactor level was stabilized using Reactor Core Isolation Cooling (RCIC) and Reactor Feedwater Pumps. Currently reactor water level is being maintained by the feedwater system and decay heat is being removed by the main condenser using the main turbine bypass valves. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the manual actuation of RCIC, this event is also being reported as an eight-hour, non-emergency notification per 10 CFR 50. 72(b )(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The plant is in its normal shutdown electrical lineup with all safe shutdown equipment available. The licensee will be notifying the state of Delaware, state of New Jersey and the Lower Alloway Creek township.Feedwater
Reactor Protection System
Reactor Core Isolation Cooling
Main Condenser
Control Rod
ENS 523475 November 2016 08:04:0010 CFR 50.72(b)(3)(iv)(A), System ActuationValid Actuation of Rps While Reactor ShutdownOn November 5, 2016 an RPS (Reactor Protection System) actuation occurred from an actual high scram discharge volume level reaching the RPS actuation setpoint. This actuation was the result of a Redundant Reactivity Control System (RRCS) signal inadvertently generated during excess flow check valve testing with the reactor in cold shutdown. At the time of the actuation, all control rods were inserted. RCS pressure was approximately 830 psig to support excess flow check valve testing and shutdown cooling was removed from service. When RRCS initiated, the B Reactor Recirculation Pump tripped as expected and the scram air header depressurized as expected, which caused the high level in the scram discharge volume. The cause of the RRCS signal is being investigated. The A loop of RHR was placed back into the Shutdown Cooling mode of operation with reactor temperature being maintained at approximately 150 degrees F. There were no injuries as a result of this event. The licensee has notified Lower Alloways Creek Township and the NRC Resident Inspector.Shutdown Cooling
Reactor Recirculation Pump
Control Rod
ENS 496085 December 2013 08:25:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram Following Turbine Trip on High Moisture Separator Level

While operating at 76% power on 12/5/13 at 0325 EST, the main turbine tripped on moisture separator hi level. The reactor scrammed along with the main turbine trip. All safety systems responded as designed and expected. There was no radiological release. There were no injuries. During the scram, all rods inserted into the core. Plant is stable in Mode 3 in its normal S/D (shutdown) electrical line up. Decay heat is being removed via the turbine bypass valves dumping steam to the main condenser. At 0505 EST while securing from cooldown in an attempt to start a recirc pump, BPVs (Bypass Valve) opened causing reactor level swell and subsequent shrink. During this time, RPV (Reactor Pressure Vessel) level lowered to below RPV level 3 and caused a RPS (Reactor Protection System) actuation. RPV level was recovered and is now stable in normal band. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE ON 12/5/13 AT 1000 EST FROM LINDSAY KOBERLEIN TO DONG PARK * * *

This update to ENS #49608 adds reporting criterion 10CFR50.72(b)(3)(iv)(A) for the RPS actuation at 0505 EST during post-scram recovery.

The licensee notified the NRC Resident Inspector and the Lower Alloways Creek township. The licensee will be making a press release. Notified R1DO (Cook).

Main Turbine
Main Condenser
05000354/LER-2013-009
ENS 4910812 June 2013 17:33:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Circulating Water Pump Trip Leads to Reactor ScramThis is a report of a manual RPS actuation and manual RCIC actuation per 10CFR50.72(b)(2)(iv)(B) and 10CFR50.72(b)(3)(iv)(A). At 1332 (EDT), on 6/12/13, the 'B' Circulating Water Pump tripped with a stuck open discharge valve resulting in a vacuum transient. Operators lowered reactor power from 100% in an effort to stabilize condenser vacuum. When vacuum reached 6.5 inches, the operators inserted a manual reactor scram at 1333 (EDT). All control rods inserted as required. No automatic ECCS or RCIC initiations occurred. No primary or secondary containment isolations occurred. The plant is stable in OP CON 3 HOT SHUTDOWN with the condensate pumps in service. The Reactor Recirculation Pumps are in service. At the time of the event, a RCIC surveillance was in progress, but did not contribute to the event. The RCIC pump was secured and subsequently placed in service for inventory control. The only safety-related equipment out of service at the time of the scram was the C Service Water Pump, which was tagged for scheduled maintenance. No personnel injuries occurred. No radiation releases occurred. The NRC Resident Inspector has been informed.Secondary containment
Service water
Reactor Recirculation Pump
Control Rod
05000354/LER-2013-002
ENS 4501623 April 2009 13:10:0010 CFR 50.72(b)(3)(iv)(A), System ActuationActuation of Auto Load Sequencer During Fast Bus Transfer Testing

At 0910 during planned testing of the 10A401 vital bus, an unplanned momentary loss of power was experienced when testing the fast transfer function. A delay of approximately 1 second was experienced when forcing a fast transfer (simulating a transformer lockout via the 86 device) from the alternate to the normal 4KV bus infeeds. This condition resulted in an initiation of the 'A' channel LOP sequencer (ELS) as a direct result of bus under voltage and is considered valid ESF actuation. All other equipment operated as expected that was available for service. The bus de-energized for <1 second and restored power automatically from the bus normal infeed. No major loads were lost. The channel is currently inoperable for planned maintenance and is not required per tech specs. Prior to the transient, the reactor was shut down, in operational condition 5, with all control rods fully inserted, and the reactor cavity flooded and communicating with the spent fuel pool. All other 'A' and 'C' channel equipment, including the 'A' and 'C' emergency diesel generators are inoperable for maintenance. Decay heat is being removed by the 'B' loop of residual heat removal operating in the shutdown cooling mode. No personnel were injured. The licensee is conducting an investigation to understand the response and cause. The licensee has notified the NRC Resident Inspector and will notify the township.

  • * * RETRACTION ON 5/7/2009 AT 1309 FROM TOM FOWLER TO MARK ABRAMOVITZ * * *

During a subsequent review of the event, it has been determined that this was not a valid actuation of one of the systems listed in 10CFR50.72(b)(3)(iv)(B). The original report was made based on the event being an actuation of (8) Emergency AC electrical power systems, including: emergency diesel generators (EDGs); hydroelectric facilities used in lieu of EDGs at the Oconee Station; and BWR dedicated Division 3 EDGs'. The Hope Creek (HC) Updated Final Safety Analysis Report (UFSAR) �8.3.1.1.2 states that there are three potential power sources for the Class 1E AC power system: (a) normal power source, (b) alternate power source and (c) dedicated standby diesel generator (SDG). The HC UFSAR �8.3.1.1.3 lists the components of the 'Standby Power System' (Emergency AC Power System). The ELS is not one of the components listed. Additionally, the sequence of events did not complete the required logic to actuate a start of the EDG. Since no EDG actuation signal was generated, this was neither a valid nor invalid actuation of a system listed in 10CFR50.72(b)(3)(iv)(B) and is not reportable. The licensee notified the NRC Resident Inspector. Notified the R1DO (Caruso).

ENS 4375329 October 2007 02:03:0010 CFR 50.72(b)(3)(iv)(A), System ActuationRefuel Floor Exhaust Hi-Hi Radiation Alarms During Reactor Reassembly

On 10/28/07 at 2203 in Operational Condition 5, two of three Refuel Floor Exhaust Radiation Monitors actuated on HI-HI Radiation during the Moisture Separator lift for Reactor Pressure Vessel Reassembly. Reactor Building Ventilation was procedurally secured at the time of the actuation to minimize the potential for airborne contamination. The cause of the elevated radiation levels at the Refuel Floor Exhaust Radiation Monitors is currently attributed to the lifting of the Moisture Separator closer to the surface of the water to obtain an unobstructed underwater path to the Reactor Pressure Vessel. The resulting ESF signal yielded an automatic start of the 'A' and 'D' Station Service Water Pumps, the Filtration Recirculation and Ventilation System, and load-shed of non-1E breaker loads. All systems responded as expected. Systems and components actuated by the condition have been restored to a normal stand-by alignment as required. No other systems were affected and the plant is stable in Operational Condition 5. The licensee will notify the NRC Resident Inspector. The licensee notified the Lower Alloways Creek Township.

  • * * RETRACTION AT 1554 ON 11/13/2007 FROM MICHAEL REED TO MARK ABRAMOVITZ * * *

Follow up investigation has revealed that the initiation of the signals was the result of radiation levels outside of the Refuel Floor Exhaust duct, and not from the in-duct activity. This would not be considered the parameter satisfying the requirements for initiation of the safety function of the system. The actual plant condition that satisfies the requirements for initiation of the safety function of the system is to detect conditions and initiate protective actions due to a release of steam or radioactive material internal to the duct that could result in the release of fission products to the environment. As a result, this is not considered a 'valid actuation' and is being retracted. Also, upon review of the refuel floor camera system, the reason for the HI-HI actuation was that during the Moisture Separator lift, the Moisture Separator broke the surface of the water by approximately 24 inches. This caused the radiation monitors to alarm on radiation shine from the moisture separator rather than airborne activity in the exhaust duct. This notification also provides telephone notification of an invalid actuation other than actuation of the reactor protection system instead of submitting a written LER 1. This is not considered an LER 2. This report is being made under 10 CFR 50.73(a)(2)(iv)(A). 3. The resulting ESF signal yielded an automatic start of the 'A' and 'D' Station Service Water Pumps, the Filtration, Recirculation and Ventilation System (FRVS), and load-shed of non-1E breaker loads: all systems responded as expected. This was a complete actuation. All required systems started and functioned successfully. The licensee notified the NRC Resident Inspector. Notified the R1DO (Holody).

Service water
Reactor Protection System
Reactor Pressure Vessel
Reactor Building Ventilation
ENS 4339529 May 2007 12:35:0010 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Manual Reactor Scram Due to Loss of Feed Pumps After Electrical TransientOn 5/28/07 with Hope Creek in Operating Condition 1 at 100% Reactor power, an electrical transient and loss of 'A' and 'B' reactor feed pumps resulted in lowering reactor water level. Operators inserted a manual reactor scram at 0835 in response to the lowering reactor water level. Reactor water level lowered to (-) 38 inches subsequent to the manual scram, resulting in initiation of High Pressure Coolant Injection (HPCl) and injection to the reactor vessel. The Reactor Core Isolation Cooling (RCIC) system also initiated but tripped. Investigation of the cause of the electrical transient, loss of the 'A' and 'B' RFP's, and trip of the RCIC system are currently in progress. Initial review of the event indicates that all other systems operated as expected. Current plant conditions as of 1100 are: Hope Creek is in mode 3 at 715 psig with heat removal to the main condenser via the Main Turbine Bypass valves. All control nods fully inserted on the scram. This report also documents a 4 hour report under 10CFR50.72(b)(2)(iv)(A) for valid ECCS initiation and injection to the reactor vessel (RAL 11.3.1). The reactor is stable with the water level currently at 17 inches and feedwater being supplied by the 'C' feed pump. No Safeties lifted during the transient. All systems functioned as required except for the trip of the RCIC. The licensee was not in any major technical specification LCO at the time of the trip. The licensee notified the NRC Resident Inspector. The licensee will also notify the States of NJ and Delaware, and Lower Alloways Creek Township.Feedwater
High Pressure Coolant Injection
Reactor Core Isolation Cooling
Main Condenser
ENS 4111011 October 2004 01:53:0010 CFR 50.72(b)(3)(iv)(A), System Actuationa Rps Actuation Signal Occurred Due to Low Reactor Water Level While in Mode 3At 2153 (hrs. EDT) on October 10, 2004, the Hope Creek Generating Station experienced an automatic reactor scram signal on low reactor level +12.5 inches (Level 3) while cooling down following a manual scram. As previously reported under Event Notification 41109, the Main Steam Isolation Valves (MSIV's) were closed as the result of a steam leak in the Turbine Building. The +12.5 inch (Level 3) scram occurred from the manual closure of a Safety Relief Valve (SRV) while it was being manually operated to reduce reactor pressure. The SRV was closed when reactor level was +24 inches, resulting in a reactor level shrink. Reactor level lowered to +8 inches, and stabilized. The secondary condensate pumps immediately restored reactor level to its normal band following the scram signal. SRV's were being utilized to assist the plant cool down because the High Pressure Coolant Injection (HPCI) system had been manually taken out of service. The HPCI vacuum tank vacuum pump tripped on an overload/power failure condition, and use was not desired. The Reactor Core Isolation Cooling (RCIC) system was out of service because of a high reactor level condition, due to plant cool down. Also, the Reactor Water Cleanup (RWCU) system was out of service due to the initial manual scram that occurred at 1814 hours which prevented normal reactor level blow down. The NRC Resident Inspector was notified and Lower Alloway Creek Township will be notified. HOO note: See Event # 41109High Pressure Coolant Injection
Main Steam Isolation Valve
Reactor Core Isolation Cooling
Reactor Water Cleanup
Safety Relief Valve
ENS 4110910 October 2004 22:14:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Manual Reactor Scram Due to a Steam Leak in the Turbine Building

At 1814 (hrs. EDT) on October 10, 2004, Hope Creek Generating Station was manually scrammed due to a steam leak in the Turbine Building. All Control Rods inserted fully. Subsequent to the manual actuation of the Reactor Protection System, reactor pressure was reduced to minimize the effects of the steam leak. Degrading Main Condenser Vacuum following the scram resulted in trips of all operating Reactor Feed Pump Turbines at 10 (inches) HgA. The High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) Systems were manually initiated for reactor level control and the Main Steam Isolation Valves (MSIV's) were closed to isolate the leak - MSIV closure was completed prior to reaching the Main Condenser Vacuum isolation setpoint of 21.5 (inches) HgA. During plant stabilization, Reactor Water Level lowered below the RPS actuation setpoint of 12.5 inches four separate times. First, following the initial scram. Second, immediately following initiation of the HPCI and RCIC systems, when the 'A' and 'B' Reactor Water Level channels lowered to -38 inches (Level 2). Level 2 is the HPCI and RCIC actuation setpoint and Primary Containment Isolation actuation setpoint for Groups 2, 7, 8, 9, 12, 13, 14, 17, 18, 19, and 20 valves. Because only two of the four Level 2 instrument channels actuated, the isolation of these systems was channel dependent and occurred as required by the respective isolation logic. Third, following manual closure of the MSIVs. Finally, Reactor Water Level lowered below 12.5 inches following reset of the original manual scram signal which resulted in an automatic scram signal. RCIC was re-initiated manually to restore Reactor Water Level. No personnel were injured during this event. The plant is currently stable in OPCON 3 with reactor pressure at 615 psig. Pressure control (decay heat removal) was transitioned to HPCI in pressure control mode during plant stabilization. Reactor Water Level is being maintained with the Secondary Condensate Pumps. Two loops of RHR in Suppression Pool Cooling mode are in service with Suppression Pool Temperature at 110 degrees F in compliance with Technical Specification 3.6.2.1 Action b.2. Actions to determine the cause of the steam leak and effect repairs are in progress. The licensee will inform Lower Alloway Creek Township and has informed the NRC resident inspector.

  • * * UPDATE ON 10/11/04 @ 0049 HRS EDT BY BAUER TO GOULD * * *

On steam leak investigation, a walk down of the turbine building condenser bay determined the source of the leak to be a failure of an 8 inch moisture separator dump line. The line break is located approximately one foot from the condenser shell penetration. An additional investigation into the root cause of the failure has commenced. The NRC Resident Inspector was notified and Lower Alloway Creek Township will be notified. The Reg 1 RDO (Richard Barkley) and EO (Chris Grimes) were informed. HOO Note: See Event # 41110

High Pressure Coolant Injection
Reactor Protection System
Main Steam Isolation Valve
Reactor Core Isolation Cooling
Primary containment
Decay Heat Removal
Main Condenser
Control Rod
ENS 410945 October 2004 17:34:0010 CFR 50.72(b)(3)(iv)(A), System ActuationInadvertent Undervoltage Condition Initated Diesel Load Sequencer, Etc. Diesel Did Not Start.

At approximately 1334, during realignment from monthly surveillance testing of the normal and alternate power supply breakers to the 10 A404 vital 4 Kv bus, an inadvertent undervoltage condition appears to have occurred. This condition resulted in initiation of the diesel load sequencer and tripping of the normal loads supplied by this bus. The undervoltage condition was momentary in nature, the load sequencer stopped upon restoration of voltage prior to starting the emergency diesel generator and operators successfully restarted the equipment that had tripped and restored the load sequencer. The D Emergency Diesel Generator is considered to be operable at this time. The cause of the occurrence is under investigation. The plant is stable in Operational Condition 1 at 100% power. This event is being reported in accordance with 10CFR50.72(b)(3)(iv)(A) 'Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) subsection 8', specifically in this case, Emergency ac electrical power systems." LAC Township notified by licensee. The NRC Resident Inspector was notified of this event by the licensee.

  • * * RETRACTION PROVIDED FROM BRADDICK TO KNOKE AT 1503 ON 11/25/04. * * *

Upon further review this event was determined to not meet the reportability requirements of 10CFR50.72. The event that caused the momentary interruption to the 10A404 vital bus (i.e., less then a second) did not result in an actuation of a listed system (Emergency ac electrical power systems, including: Emergency diesel generators (EDGs)). Because the event did not meet the NUREG 1022 reporting requirement specified in 10CFR50.72 (b)(3)(iv)(A) it has been determine to not be reportable." The NRC Resident Inspector was notified of this event by the licensee. LAC Township notified by licensee. Notified R1DO (Dimitriadis)

Emergency Diesel Generator
ENS 403786 December 2003 04:49:0010 CFR 50.72(b)(3)(iv)(A), System Actuationa Level 3 Low Reactor Water Level Was Reached During a Reactor Water Level Transient

The reactor was being shutdown as part of a planned evolution to allow repairs on the Reactor Water Cleanup flange leak. After the Reactor Protection System Mode Select Switch had been placed in shutdown, the resulting reactor level transient caused the Level 3 low reactor level set point to be reached. The Reactor Protection System had already been de-energized and the lowest level reached during the transient was +2 inches. This level transient is a normal occurrence on a reactor shutdown, and level was restored to the normal operating band. There was no effect on the plant due to reaching the low level set point. No other abnormal plant response was noted. The licensee will notify the NRC Resident Inspector

  • * * RETRACTION ON 1/9/04 AT 1310 FROM CLYDE BAUER TO E. THOMAS * * *

Upon further review of this event, the resulting Level 3 low reactor water level signal following the manual scram is considered part of the pre-planned sequence in accordance with the guidance of NUREG-1022. Therefore, this event is not reportable under 10 CFR50.72(b)(3)(iv)(A) and is being retracted. Notified R1DO (J. Noggle)

Reactor Protection System
Reactor Water Cleanup