ENS 52347
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ENS Event | |
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08:04 Nov 5, 2016 | |
Title | Valid Actuation of Rps While Reactor Shutdown |
Event Description | On November 5, 2016 an RPS [Reactor Protection System] actuation occurred from an actual high scram discharge volume level reaching the RPS actuation setpoint. This actuation was the result of a Redundant Reactivity Control System (RRCS) signal inadvertently generated during excess flow check valve testing with the reactor in cold shutdown. At the time of the actuation, all control rods were inserted. RCS pressure was approximately 830 psig to support excess flow check valve testing and shutdown cooling was removed from service. When RRCS initiated, the B Reactor Recirculation Pump tripped as expected and the scram air header depressurized as expected, which caused the high level in the scram discharge volume. The cause of the RRCS signal is being investigated. The A loop of RHR was placed back into the Shutdown Cooling mode of operation with reactor temperature being maintained at approximately 150 degrees F. There were no injuries as a result of this event.
The licensee has notified Lower Alloways Creek Township and the NRC Resident Inspector. |
Where | |
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Hope Creek New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+2.2 h0.0917 days <br />0.0131 weeks <br />0.00301 months <br />) | |
Opened: | Mariaz Davis 10:16 Nov 5, 2016 |
NRC Officer: | Bethany Cecere |
Last Updated: | Nov 5, 2016 |
52347 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Not Critical |
Scram | No |
Before | Cold Shutdown (0 %) |
After | Cold Shutdown (0 %) |
WEEKMONTHYEARENS 541982019-08-03T23:47:0003 August 2019 23:47:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Manual Actuation of Reactor Core Isolation Cooling ENS 523472016-11-05T08:04:0005 November 2016 08:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Rps While Reactor Shutdown ENS 496082013-12-05T08:25:0005 December 2013 08:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Following Turbine Trip on High Moisture Separator Level ENS 491082013-06-12T17:33:00012 June 2013 17:33:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Circulating Water Pump Trip Leads to Reactor Scram ENS 450162009-04-23T13:10:00023 April 2009 13:10:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Auto Load Sequencer During Fast Bus Transfer Testing ENS 437532007-10-29T02:03:00029 October 2007 02:03:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Refuel Floor Exhaust Hi-Hi Radiation Alarms During Reactor Reassembly ENS 433952007-05-29T12:35:00029 May 2007 12:35:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Manual Reactor Scram Due to Loss of Feed Pumps After Electrical Transient ENS 411102004-10-11T01:53:00011 October 2004 01:53:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation a Rps Actuation Signal Occurred Due to Low Reactor Water Level While in Mode 3 ENS 411092004-10-10T22:14:00010 October 2004 22:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Manual Reactor Scram Due to a Steam Leak in the Turbine Building ENS 410942004-10-05T17:34:0005 October 2004 17:34:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Inadvertent Undervoltage Condition Initated Diesel Load Sequencer, Etc. Diesel Did Not Start. ENS 403782003-12-06T04:49:0006 December 2003 04:49:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation a Level 3 Low Reactor Water Level Was Reached During a Reactor Water Level Transient 2019-08-03T23:47:00 | |
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