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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5330330 March 2018 18:05:0010 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Primary Containment Declared Inoperable Due to Both Airlock Doors Open SimultaneouslyOn March 30, 2018 at 1305 CDT, with the reactor at 98 percent core thermal power and steady state conditions, plant personnel identified that both doors of the containment personnel airlock were open simultaneously due to failure of the interlock. Personnel were at both the outside and inside doors. Immediate action was taken to close the inner containment personnel airlock door and it was verified closed. Both doors of the containment personnel airlock were open for less than one minute. There was no radioactive release as a result of the event. The cause of the interlock failure is under investigation. This condition requires an 8-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(ii)(A), the condition of the nuclear power plant, including its principal safety barriers (primary containment), being seriously degraded. This condition is also reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material. The NRC Resident Inspector was notified.Primary containment
ENS 531109 December 2017 19:48:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Manual Reactor Scram Due to Loss of Division 1 Ac Power to Numerous Components

At approximately 1347 (CST) on 12/09/17, the Main Control Room received annunciators that indicated a trip of the 4160 V 1A1 breaker 1AP07EJ, 480V XFMR 1A and A1 breaker. Numerous Division 1 components lost power (powered from unit subs 1A and A1). The Division 1 containment Instrument Air isolation valves had failed closed by design due to the loss of power. Due to the loss of containment instrument air, several control rods began to drift into the core as expected and, by procedure, the reactor mode switch was placed in the shutdown position at 1353 (CST). All control rods fully inserted. Also due to the loss of power, the Fuel Building ventilation dampers failed closed by design. With the normal ventilation system secured, secondary containment differential pressure rose to slightly greater than 0 inches water gauge which exceeded the Technical Specification requirement of greater than 0.25 inches vacuum water gauge at 1348 (CST). The Control Room entered EOP-8, Secondary Containment Control. Secondary Containment differential pressure was restored within Technical Specification requirements at 1351 (CST) by starting the Division 2 Standby Gas Treatment system. This event is being reported as a manual actuation of the Reactor Protection System (RPS) and as a Condition that Could Have Prevented Fulfillment of a Safety Function.

The cause is currently under investigation. The NRC Resident has been notified. The licensee informed the NRC Resident Inspector.

  • * * UPDATE FROM DALE SHELTON TO VINCE KLCO AT 1658 EST ON 12/10/2017 * * *

During a review of plant logs it was identified that the primary to secondary containment differential pressure was identified to be outside of Technical Specification 3.6.1.4 limits of 0 plus or minus 0.25 psid at 2009 on 12/9/17 due to the primary containment ventilation system dampers closing as a result of the loss of power. This parameter is an initial safety analysis assumption to ensure that primary containment pressures remain within the design values during a Loss of Coolant Accident (LOCA). As a result, this condition is reportable as an unanalyzed condition that significantly degrades plant safety. The NRC Senior Resident Inspector has been notified. Notified the R3DO (Stone).

  • * * UPDATE FROM MICHAEL ANTONELLI TO VINCE KLCO ON 12/11/17 AT 1805 EST * * *

During the post transient review of the trip of the 4160 V 1A1 breaker 1AP07EJ, 480V XFMR 1A and A1, it was identified that the unplanned INOPERABILITY of the Low Pressure Core Spray (LPCS) system due to the loss of power to the injection valve constitutes an event or condition that could have prevented fulfillment of a safety function and is reportable under 10CFR50.72(b)(3)(v)(D) for Accident Mitigation. The High Pressure Core Spray (HPCS) remained available to perform the core spray function, if necessary, during a design basis Loss of Coolant Accident (LOCA), however HPCS and LPCS are each considered single train safety systems. The NRC Senior Resident Inspector has been notified. Notified the R3DO (Stone).

Secondary containment
Reactor Protection System
Primary containment
High Pressure Core Spray
Core Spray
Standby Gas Treatment System
Control Rod
ENS 530545 November 2017 18:40:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Pressure Due to Voltage TransientAt approximately 1240 CST on 11/05/17, the Main Control Room received numerous annunciators that indicated a trip of the Emergency Reserve Auxiliary Transformer (ERAT) Static VAR (volt-ampere reactive) Compensator (SVC) caused by a voltage transient on the 138 kV feed due to thunderstorms in the area. As a result of the voltage transient, the Division 1 Fuel Building ventilation (VF) system isolation dampers closed causing a trip of VF supply and exhaust fans. With no running VF fans, secondary containment differential pressure rose to slightly greater than 0 inches water gauge which exceeded the Technical Specification requirement of greater than 0.25 inches vacuum water gauge at 1241. The Control Room entered EOP-8, Secondary Containment Control. This event is being reported as a Condition that Could Have Prevented Fulfillment of a Safety Function under 10CFR50.72(b)(3)(v)(C). Secondary Containment differential pressure was restored within Technical Specification requirements at 1242 by starting the Standby Gas Treatment HVAC (VG) system. The NRC Resident Inspector has been notified.Secondary containment
HVAC
ENS 527822 June 2017 07:41:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Declared InoperableOn 6/2/2017 at 0241 CDT, Clinton Power Station entered Mode 2 with secondary containment boundary doors propped open. Specifically, both doors for Reactor Water Cleanup (RT) 'B' pump room were propped open with welding cables routed through pump room doors to perform welding in the RT pump room. At 0300 CDT, a Senior Reactor Operator identified that the doors were propped open and Secondary Containment was declared inoperable. LCO 3.6.4.1 Required Action A.1 was entered to restore Secondary Containment to Operable in four hours. At 0324 CDT, the cabling for the welding machine was removed and the doors were closed. Investigation determined that authorization had been granted while in mode 4, when secondary containment was not required to be operable. The doors were propped open at the beginning of the shift, prior to the mode change to mode 2 (0241 CDT). This loss of secondary containment is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material. The NRC Resident Inspector has been notified.Secondary containment
Reactor Water Cleanup
ENS 5257625 February 2017 04:39:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Differentail Pressure Exceeded Technical SpecificationsAt approximately 2239 (CST) on 2/24/17, the Main Control Room received numerous annunciators that indicated a loss of the 138 kV off-site feed to the Emergency Reserve Auxiliary Transformer (ERAT). As a result of the voltage transient, the Division 1 Fuel Building ventilation (VF) system isolation dampers closed causing a trip of VF supply and exhaust fans. With no running VF fans, secondary containment differential pressure rose to slightly greater than 0 inches water gauge which exceeded the Technical Specification requirement of greater than 0.25 inches vacuum water gauge. The Control Room entered EOP-8, Secondary Containment Control. This event is being reported as a Condition that Could Have Prevented Fulfillment of a Safety Function under 10CFR50.72(b)(3)(v)(C). Secondary Containment differential pressure was restored within Technical Specification requirements at 2242 (CST) by starting the Standby Gas Treatment HVAC (VG) system. The NRC Resident (Inspector) has been notified.Secondary containment
HVAC
ENS 5204324 June 2016 20:11:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment

On 06/24/2016 at 1511(CDT), an unexpected trip of a Fuel Building ventilation supply fan occurred followed by an exhaust fan trip and secondary containment differential pressure became positive.

At 1512 (CDT), the standby fuel building ventilation fans auto started and secondary containment differential pressure was restored to Technical Specification required conditions. Secondary containment was declared INOPERABLE when Technical Specification-required differential pressure was not being maintained and LCO 3.6.4.1 Action A.1 was entered and exited for the given time period. Emergency Operating Procedure (EOP) - 8 was entered due to Secondary containment differential pressure reading positive (greater than 0 inches of water). This loss of secondary containment is reportable under 10CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material. The cause of the fuel building supply fan trip is under investigation. The NRC Resident Inspector has been informed.

Secondary containment
ENS 518452 April 2016 17:57:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialInsulator Failure on Reserve Auxiliary TransformerAt approximately 1257 (CDT) on 4/02/16, the Main Control Room received numerous annunciators that indicated a trip of the Reserve Auxiliary Transformer (RAT) Static VAR Compensator (SVC) that was caused by an insulator failure of the 'A' phase 345kV Circuit Switcher. As a result of the voltage transient, the Division 1 Fuel Building Ventilation (VF) system isolation dampers closed causing a trip of VF supply and exhaust fans. With no running VF fans, secondary containment differential pressure rose to slightly greater than 0 inches water gauge which exceeded the Technical Specification requirement of greater than 0.25 inches vacuum water gauge. The Control Room entered EOP-8, Secondary Containment Control. This event is being reported as a 'Condition that Could Have Prevented Fulfillment of a Safety Function' under 10CFR50.72(b)(3)(v)(C). Secondary Containment differential pressure was restored within Technical Specification requirements at 1300 (CDT) by starting the Standby Gas Treatment HVAC (VG) system. The NRC Resident Inspector has been notified.Secondary containment
HVAC
ENS 5183630 March 2016 20:45:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Differential Pressure Outside Required Technical Specification ValueAt approximately 1545 CDT on 3/30/16, the Main Control Room received numerous annunciators that indicated a trip of the Emergency Reserve Auxiliary Transformer (ERAT) Static VAR Compensator (SVC) caused by a voltage transient on the 138 kV feed due to thunderstorms in the area. As a result of the voltage transient, the Division 1 Fuel Building ventilation (VF) system isolation dampers closed causing a trip of VF supply and exhaust fans. With no running VF fans, secondary containment differential pressure rose to slightly greater than 0 inches water gauge which exceeded the Technical Specification requirement of greater than 0.25 inches vacuum water gauge. The Control Room entered EOP-8, Secondary Containment Control. This event is being reported as a condition that could have prevented fulfillment of a safety function under 10 CFR 50.72(b)(3)(v)(C). Secondary Containment differential pressure was restored within Technical Specification requirements at 1550 CDT by starting the Standby Gas Treatment HVAC (VG) system. The NRC Resident has been notified.Secondary containment
HVAC
05000461/LER-2016-004
ENS 5173213 February 2016 08:06:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Inoperable

On 02/13/2016 at 0206 CST, an unexpected trip of a Fuel Building ventilation exhaust fan occurred and secondary containment differential pressure became positive. Secondary containment was declared INOPERABLE when Technical Specification-required differential pressure was not being maintained and entered LCO 3.6.4.1 Action A.1

At 0256 (CST), the standby gas treatment system was started and secondary containment differential pressure was restored to Technical Specification requirements at 0257 CST. This loss of secondary containment is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material. The cause of the fuel building exhaust fan trip is unknown at this time. The NRC Resident Inspector has been notified.

Secondary containment
Standby Gas Treatment System
05000461/LER-2016-002
ENS 5117925 June 2015 08:01:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Pressure Increase Due to Voltage TransientAt approximately 0301 (CDT) on 6/25/15, the Main Control Room received numerous annunciators that indicated a trip of the Emergency Reserve Auxiliary Transformer (ERAT) Static VAR Compensator (SVC) caused by a voltage transient on the 138 kV feed due to thunderstorms in the area. The Division 1 Safety Bus was manually aligned from the reserve source to its normal source. As a result of the voltage transient, the Division 1 Fuel Building Ventilation (VF) system isolation dampers closed causing a trip of VF supply and exhaust fans. With no running VF fans, secondary containment differential pressure rose to slightly greater than 0 inches water gauge and which exceeded the Technical Specification requirement of greater than 0.25 inches vacuum water gauge. The Control Room entered EOP-8, Secondary Containment Control. This event is being reported as a condition that could have prevented fulfillment of a safety function under 10 CFR 50.72(b)(3)(v)(C). Secondary Containment differential pressure was restored within Technical Specification requirements at 0319 (CDT) by reopening the VF isolation dampers and restarting the VF supply and exhaust fans. The ERAT SVC was returned to service at 0457 (CDT). The NRC Resident Inspector has been notified.Secondary containment
ENS 507947 February 2015 05:55:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLeakage Detection System InoperableOn 2/6/15 at 2300 (CST) the Division 1 Reactor Water Cleanup (RT) system differential flow instrument was declared inoperable due to erratic indication. The Division 1 RT differential flow instrument was declared inoperable in accordance with Technical Specification 3.3.6.1 Action D.1. At time 2355 Division 2 RT differential flow instrument failed downscale and was declared inoperable in accordance with Technical Specification 3.3.6.1 Action D.1 and also Technical Specification 3.3.6.1 Action E.1 (entered due to Division 1 RT differential flow already inoperable). Since this condition renders the Leakage Detection System incapable of performing its safety function, it is reportable under 10CFR50.72(b)(3)(v)(C). Division 1 RT differential flow was declared Operable at time 0036 on 2/7/15. Division 2 RT differential flow was restored to Operable at time 0225 on 2/07/2015. The NRC Resident (Inspector) has been notified.Reactor Water Cleanup05000461/LER-2015-001
ENS 4975823 January 2014 01:56:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Differential PressureA spurious closure of a Secondary Containment isolation damper caused a trip of the Fuel Building ventilation system and a loss of Secondary Containment differential pressure. Secondary Containment differential pressure exceeded -0.25 inches of water vacuum rendering Secondary Containment inoperable between the time of 1956 and 2003 (CST). The damper re-opened, fuel building ventilation was restarted and Secondary Containment differential pressure was restored to normal. This event is reportable under 10CFR50.72(b)(3)(v)c. The Licensee will be notifying the NRC Resident Inspector". Investigation for the spurious closure of a Secondary Containment isolation damper is in progress.Secondary containment05000461/LER-2014-001
ENS 496179 December 2013 02:27:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Manual Scram Due to Loss of Division 1 480 Vac Power Causing Loss of Instrument Air to Containment and Scram Air HeaderWhile operating at rated electrical power, the station experienced a transformer fault which resulted in a loss of Division 1 480 VAC power. This resulted in the operators inserting a Manual Scram due to loss of Instrument Air to Containment and the scram air header. On the scram, all control rods fully inserted and no safety relief valves lifted. Reactor vessel level is being maintained by normal feedwater and decay heat is being removed via steam to the main condenser through the steam bypass valves. The plant is currently in Mode 3 and proceeding to Mode 4 to comply with Technical Specification requirements. The plant is in a normal shutdown electrical lineup with the exception of the loss of Division 1 480 VAC power. Reporting in accordance with 10CFR50.72(b)(3)(v)(C) due to loss of normal ventilation to secondary containment which resulted in a positive secondary containment pressure for approximately 15 minutes. Secondary Containment required pressure was restored at 2043 CST. Reporting in accordance with 10CFR50.72(b)(3)(v)(D) due to loss of Division 1 480 VAC power resulting in loss of a single train of Low Pressure Core Spray. The licensee has notified the NRC Resident Inspector.Feedwater
Secondary containment
Core Spray
Safety Relief Valve
Main Condenser
Control Rod
05000461/LER-2013-008
ENS 4853324 November 2012 02:08:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Inadvertent Loss of Instrument AirOn 11/23/2012 at approximately 1956 CST, it was reported that the Control Room (VC) B Chiller breaker was cycling open and closed. In order to stop the cycling, Control Building Unit Sub B was manually tripped causing the following isolations/actuations: loss of power to instrument air (IA) system containment isolation valves causing the Division 2 valves to isolate; loss of power to the low pressure switch that resulted in an automatic start of Division 2 Shutdown Service Water (SX) system; and loss of power to fuel building (VF) system ventilation Division 2 dampers resulting in a trip of the VF system. High Pressure Core Spray (HPCS) became inoperable based on inoperability of the room cooler for the associated Division 4 inverter and battery charger. Operations entered the Loss of AC Power and Automatic Isolation off-normal procedures. Following the loss of power to the VF system ventilation, at 2008, secondary containment differential pressure became positive. At 2009, power was restored to Control Building Unit Sub B and HPCS was restored to operable. At 2011, the standby gas treatment system (VG) was started and at 2013, secondary containment differential pressure was restored. Following re-energization of Unit Sub B, the IA containment isolation valves were re-opened, VG was secured, VF restarted and the Division 2 SX pump was secured. The loss of secondary containment differential pressure is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material An unplanned inoperability of HPCS reportable under 10 CFR 50.72(b)(3)(v)(D) as HPCS is a single train safety system The cause of the breaker cycling is unknown at this time. The NRC Resident has been informed.Secondary containment
Service water
High Pressure Core Spray
Standby Gas Treatment System
ENS 482693 September 2012 03:04:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Transfer of Emergency Reserve Auxiliary Transformer Isolating Fuel Pool Cooling and Cleanup System, and Fuel Building Ventilation System

At 22:04 CDT on 9/02/2012, the Emergency Reserve Auxiliary Transformer (ERAT) transferred unexpectedly to the Reserve Auxiliary Transformer (RAT). During this transfer, the Fuel Pool Cooling and Cleanup (FC) system pump 'A' tripped and the Fuel Building Ventilation (VF) system isolated. Upper containment pool level dropped below the minimum required level per Technical Specifications (TS) 3.6.2.4 and Secondary Containment differential pressure increased above 0.25 inches vacuum per TS 3.6.4.1. Upper Containment Pool level was restored above the minimum level at 01:27 CDT on 9/3/2012 within the 4 hour completion time. The Upper Containment Pool is a part of the suppression pool makeup system used to ensure the Primary Containment function. Secondary Containment differential pressure was restored at 22:19 on 9/2/2012 when the Standby Gas Treatment System was started. Maintaining secondary containment differential pressure helps to control the release of radioactive material. This event is being reported as a condition that could have prevented the fulfillment of a safety function per 10 CFR 50.72(b)(3)(v)(B) and 10 CFR 50.72(b)(3)(v)(C). The station is currently in a 72-hour action to restore the ERAT to an operable status per TS LCO 3.8.1 Required Action A.2. Plant conditions are stable and actions are underway to repair the ERAT. The NRC Resident (Inspector) has been notified.

  • * * RETRACTION ON 10/26/12 AT 1322 EDT FROM KEN LEFFEL TO DONG PARK * * *

Upper Containment Pool level dropped below the normal pool level of 827 feet-3 inches when the Fuel Pool Cooling and Cleanup system pump 'A' tripped, and was initially reported as dropping below the minimum level (825 feet-6 inches) required by Technical Specification (TS) 3.6.2.4. However, subsequent reports from the field confirmed that the lowest level reached was 827 feet 0 inches, which is greater than the minimum required TS level. Therefore, no loss of safety function occurred for the Upper Containment Pool level as a result of this event, and the event is not reportable under 50.72 (b)(3)(v)(B). The NRC Resident (Inspector) has been notified." Notified R3DO (Pelke).

Secondary containment
Primary containment
Standby Gas Treatment System
Fuel Pool Cooling and Cleanup
ENS 4753318 December 2011 15:30:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Loss of Rhr Cooling Due to Incorrect Reactor Water Level IndicationOn 12/18/11 at approximately 0930 CST, with the plant in Mode 4, while Operations was lowering reactor water level as part of restoration activities following the Reactor Pressure Vessel hydrostatic test, an automatic reactor scram and Residual Heat Removal (RHR) 'A' pump trip occurred due to a valid Reactor Water Level Low (Level 3) signal. The cause of the low level appears to be due a significant disparity between the Upset and Shutdown Range level instrumentation and the Level 3 RPS (Reactor Protection System) instrumentation. No rod motion occurred during the reactor scram as all control rods were fully inserted at the time of the event. Operations immediately entered the station off-normal procedures for Loss of Shutdown Cooling and Reactor Scram. The 'A' RHR pump was restored at 0956 CST. Reactor coolant temperature increased from approximately 128.7 deg F to 131.7 deg F during the event. At 1112 CST, the scram was reset and at 1216 CST, the off-normal procedures were exited. Following the event as part of trouble shooting, maintenance personnel performed a fill and vent of reactor water level transmitter, 1B21N027. At the completion of this fill and vent, indicated water level changed from 195" to 86" on Shutdown Range and from off-scale high (>180") to 103"on Upset Range. No change in other reactor water level indication was observed. This event is reportable under 10 CFR 50.72 (b)(3)(v)(B), as an event or condition that could have prevented the fulfillment of a safety function needed to remove residual heat, and 10 CFR 50.72 (b)(3)(iv)(A), event or condition that results in a valid actuation of the reactor protection system (RPS). The licensee has notified the NRC Resident Inspector.Reactor Protection System
Shutdown Cooling
Reactor Pressure Vessel
Residual Heat Removal
Control Rod
05000461/LER-2011-008
ENS 4677120 April 2011 14:15:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual HeatWatertight Doors Left Ajar Simultaneously During Room Checks

During the performance of operator rounds in the Lake Screenhouse Safe Shutdown System (SX) pump rooms, two water tight doors were left opened simultaneously during the room checks. These two doors opened simultaneously (which) allowed for communication between the Division 1 SX room and Division 2 SX pump room. The operator was in constant attendance in the Division 2 SX pump room during the performance of the equipment checks. During site review, it was determined that a flood in either the Division 1 or Division 2 SX pump rooms would not be isolated to the initiating room, but potentially affect both trains of SX. This could result in a loss of cooling for both Residual Heat Removal systems, therefore, a condition that could have prevented fulfillment of a safety function under 10CFR50.72(b)(3)(v)(B). The NRC Senior Resident has been notified. Offsite power is normal and emergency diesel generators are operable and available.

* * * RETRACTION FROM ED TIEDEMANN TO PETE SNYDER ON 6/8/11 AT 1141 EDT * * * 

A subsequent plant barrier impairment evaluation consistent with Exelon Procedure CC-AA-201, 'Plant Barrier Control Program' has determined that no loss of safety funct ion would have occurred. Each of the following door functions and related postulated events were reviewed for impact: ventilation; flooding, internal and external; high energy line breaks; missiles; radiation protection; and fires. For the condition with the SX pump room water tight doors being open with an operator in the area, the conclusion is an SX division remains protected to ensure that in any of the evaluated events the safety function of SX has been maintained. The licensee has notified the NRC Resident Inspector.

Emergency Diesel Generator
Residual Heat Removal
ENS 456763 February 2010 17:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Feedwater Check Valve Leak Rate Exceeded Technical Specification RequirementAt 1100 (CST) on February 3, 2010, it was discovered that a primary containment local leak rate test performed on feedwater check valve 1B21-F032B exceeded its acceptance criteria. Technical Specification Surveillance Requirement (SR) 3.6.1.3.11 requires that the combined leakage rate for both primary containment feedwater penetrations to be less than or equal to 2 gallons per minute. The measured leakage for 1B21-F032B was reported to be 2.5 gallons per minute (gpm). Operations immediately declared 1B21-F032B inoperable and initiated action to close the feedwater inlet shutoff valve 1B21-F065B to isolate the affected penetration. At 1136 (CST), 1B21-F065B was closed and its breaker was turned off to comply with TS 3.6.1.3, Condition C required actions. At 1447 (CST), the Feedwater Leakage Control System (FWLCS) was declared inoperable in accordance with LCO 3.6.1.9 and the plant entered a 30-day action to restore FWLCS to an operable condition. After performance of a line flush, plans are underway to attempt to re-perform the local leak rate test for the feedwater check valve, 1B21-F032B. If unsuccessful, further corrective actions will be taken. The NRC Senior Resident has been informed.Feedwater
Primary containment
ENS 4216121 November 2005 16:42:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual HeatDivision 3 Emergency Diesel Generator Declared Inoperable

The Division 3 Emergency Diesel Generator (EDG) was declared INOPERABLE following a trip during a routine monthly surveillance run. As soon as the Division 3 EDG was at full load it tripped off line (output breaker tripped). The Division 3 EDG supplies electrical power to the High Pressure Core Spray System in the event of a loss of offsite power. No problems occurred on the Division 3, 4160 volt, safety related bus. This event is being reported in accordance with 10CFR50.72(b)(3)(v)(B), Event or Condition That Could Have Prevented Fulfillment of a Safety Function for a single-train system failure. The NRC Resident inspector has been notified.

  • * * THIS EVENT IS BEING RETRACTED ON 12/20/05 AT 1557 * * *

Subsequent trouble-shooting and testing determined that the cause of the engine trip on 11/21/05 was an invalid high coolant temperature trip signal. This trip is bypassed during a Loss of Coolant (LOCA) initiation of the system, therefore, it was determined that the EDG would have been able to perform its safety function during a LOCA. Following a Loss of Offsite Power (LOOP), reactor water level is expected to reach Reactor Pressure Vessel (RPV) Water Level Low Low (Level 2) within 30 seconds of the initiating signal. Once Level 2 is reached, both the EDG and the LOCA Trip bypass signals are actuated. It was determined that the bypass would have occurred prior to the high coolant temperature trip. Based on the above, it was determined that the Division 3 EDG would have been fully capable of performing its safety function under both LOCA and LOOP. The Division 3 EDG was restored to an operable condition at 0214 on 11/22/05. The NRC Senior Resident Inspector has been notified. Notified R3DO (H. Peterson).

Emergency Diesel Generator
Reactor Pressure Vessel
High Pressure Core Spray