ENS 51845
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ENS Event | |
|---|---|
17:57 Apr 2, 2016 | |
| Title | Insulator Failure on Reserve Auxiliary Transformer |
| Event Description | At approximately 1257 [CDT] on 4/02/16, the Main Control Room received numerous annunciators that indicated a trip of the Reserve Auxiliary Transformer (RAT) Static VAR Compensator (SVC) that was caused by an insulator failure of the 'A' phase 345kV Circuit Switcher. As a result of the voltage transient, the Division 1 Fuel Building Ventilation (VF) system isolation dampers closed causing a trip of VF supply and exhaust fans. With no running VF fans, secondary containment differential pressure rose to slightly greater than 0 inches water gauge which exceeded the Technical Specification requirement of greater than 0.25 inches vacuum water gauge. The Control Room entered EOP-8, Secondary Containment Control. This event is being reported as a 'Condition that Could Have Prevented Fulfillment of a Safety Function' under 10CFR50.72(b)(3)(v)(C). Secondary Containment differential pressure was restored within Technical Specification requirements at 1300 [CDT] by starting the Standby Gas Treatment HVAC (VG) system.
The NRC Resident Inspector has been notified. |
| Where | |
|---|---|
| Clinton Illinois (NRC Region 3) | |
| Reporting | |
| 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material | |
| Time - Person (Reporting Time:+0.5 h0.0208 days <br />0.00298 weeks <br />6.849e-4 months <br />) | |
| Opened: | Justin Reynolds 18:27 Apr 2, 2016 |
| NRC Officer: | Mark Abramovitz |
| Last Updated: | Apr 2, 2016 |
| 51845 - NRC Website
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Unit 1 | |
|---|---|
| Reactor critical | Critical |
| Scram | No |
| Before | Power Operation (99 %) |
| After | Power Operation (99 %) |
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