ENS 52576
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ENS Event | |
|---|---|
04:39 Feb 25, 2017 | |
| Title | Secondary Containment Differentail Pressure Exceeded Technical Specifications |
| Event Description | At approximately 2239 [CST] on 2/24/17, the Main Control Room received numerous annunciators that indicated a loss of the 138 kV off-site feed to the Emergency Reserve Auxiliary Transformer (ERAT). As a result of the voltage transient, the Division 1 Fuel Building ventilation (VF) system isolation dampers closed causing a trip of VF supply and exhaust fans. With no running VF fans, secondary containment differential pressure rose to slightly greater than 0 inches water gauge which exceeded the Technical Specification requirement of greater than 0.25 inches vacuum water gauge. The Control Room entered EOP-8, Secondary Containment Control. This event is being reported as a Condition that Could Have Prevented Fulfillment of a Safety Function under 10CFR50.72(b)(3)(v)(C). Secondary Containment differential pressure was restored within Technical Specification requirements at 2242 [CST] by starting the Standby Gas Treatment HVAC (VG) system.
The NRC Resident [Inspector] has been notified. |
| Where | |
|---|---|
| Clinton Illinois (NRC Region 3) | |
| Reporting | |
| 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material | |
| Time - Person (Reporting Time:+-0.27 h-0.0113 days <br />-0.00161 weeks <br />-3.69846e-4 months <br />) | |
| Opened: | Luke Echols 04:23 Feb 25, 2017 |
| NRC Officer: | Dong Park |
| Last Updated: | Feb 25, 2017 |
| 52576 - NRC Website
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Unit 1 | |
|---|---|
| Reactor critical | Critical |
| Scram | No |
| Before | Power Operation (99 %) |
| After | Power Operation (99 %) |
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