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Issue date | Title | Topic | |
---|---|---|---|
ML20204G246 | 22 March 1999 | Audit Rept on Implementation of GL 98-01, 'Year 2000 Readiness of Computer Sys at Nuclear Power Plants.' | |
ML20151W180 | 25 August 1998 | Rev 2 to BYR98-109/BRW-98-0339-E, Base Line Ampacity Values for Std Fire Wrap Configurations | |
ML20198L818 | 10 December 1997 | Rev 5 to Calculation 95-011, Control Room Thyroid Dose from Main Steam Line Break Event | |
ML20198L828 | 10 December 1997 | Rev 4 to Calculation BRW-97-0798-M, Allowable Leak Rate Calculation for SG Interim Plugging Criteria | |
ML20203J750 | 9 December 1997 | Plant Issues Matrix | Hot Short Safe Shutdown Unanalyzed Condition Boric Acid Loop seal Packing leak High Radiation Area Grab sample Offsite Dose Calculation Manual Fire Barrier Stroke time Weld Overlay Anchor Darling Emergency Lighting Locked High Radiation Area Foreign Material Exclusion Scram Discharge Volume Annual Radiological Environmental Operating Report Battery sizing Earthquake Fire Protection Program Fire Watch Downpower Reverse polarity |
IA-97-451, Plant Issues Matrix | 9 December 1997 | Plant Issues Matrix | Hot Short Safe Shutdown Unanalyzed Condition Boric Acid Loop seal Packing leak High Radiation Area Grab sample Offsite Dose Calculation Manual Fire Barrier Stroke time Weld Overlay Anchor Darling Emergency Lighting Locked High Radiation Area Foreign Material Exclusion Scram Discharge Volume Annual Radiological Environmental Operating Report Battery sizing Earthquake Fire Protection Program Fire Watch Downpower Reverse polarity |
ML20211H294 | 30 September 1997 | Rev 4 to Allowable Leakrate Calculation for SG Interim Plugging Criteria | |
ML20211H302 | 30 September 1997 | Rev 2 to CR Dose for MSLB Accident | |
ML20211H308 | 30 September 1997 | Rev 3 to Allowable Leakrate Calculation for SG Interim Plugging Criteria | |
ML20211H321 | 30 September 1997 | Rev 4 to CR Thyroid Dose from MSLB Event | |
ML20216F162 | 29 August 1997 | Rev 0 to Allowable Leakrate Calculation for SG Interim Plugging Criteria | |
ML20216F169 | 29 August 1997 | Rev 3 to CR Thyroid Dose from MSLB Event | |
ML20210P139 | 22 August 1997 | Rev 0 to BYR97-332, CR Dose for MSLB Accident | |
ML20210P160 | 21 August 1997 | Rev 1 to ATD-0410, Allowable Leakrate Calculation for Steam Generator Interim Plugging Criteria | |
ML20149H742 | 10 July 1997 | Rev 0 to 5.2.2-BRW-97-0667, Evaluate Tendon H4ED for Broken/Unseated Wires | |
ML20148T728 | 27 June 1997 | Rev 4 to BWR-97-0339-M, Byron & Braidwood CR Heat Up Evaluation | Coast down |
ML20148T742 | 25 June 1997 | Rev 4 to BRW-97-0624-M, Determination of Div 11 & 12 Miscellaneous Electrical Equipment Rooms Transient Temp Profiles Following Loss of Ventilation | |
ML20140D390 | 12 March 1997 | Determination of 2-Dimensional Pressure Distribution on Byron/Braidwood D4 SG Tube Support Plate During Mslb | |
ML20133K462 | 17 January 1997 | Press Release III-97-05, NRC to Hold Predecisional Enforcement Conference W/Comm Ed on Apparent Violations at Byron Plant | |
ML20133E740 | 31 December 1996 | Flaw Evaluation of Line 1SX933AA-8 Per GL 90-05 Guidelines | Nondestructive Examination Earthquake |
ML20129G522 | 2 October 1996 | Press Release III-96-61, Byron Nuclear Plant Rated Superior in Two Areas, Good in Two Areas in NRC Performance Assessment | Systematic Assessment of Licensee Performance |
ML20115F368 | 3 June 1996 | Ampacity Derating for Std Fire Wrap Configurations | Fire Barrier |
ML20115F353 | 19 April 1996 | Verification of Models for Fire-Wrapped Conduits & Cable Trays Against Test Data | Fire Barrier Thermoset |
ML20092B161 | 4 September 1995 | Calculation of Byron D4 SG Tube Support Plate Differential Pressures During MSLB W/RELAP5M2 | |
ML20080H523 | 23 January 1995 | Darmatt Firewrap Matl Cable Ampacity Derating Factor Calculation | Fire Barrier |
ML20062N819 | 29 December 1993 | Battery Sizing Calculation | Battery sizing |
ML20062N821 | 9 December 1993 | Battery Sizing Calculation | Battery sizing |
ML20085M469 | 11 November 1991 | Responds to Aquatic Resource Questions Re NUMARC Survey in Support of NRC License Renewal Rulemaking | Weld Overlay License Renewal Scaffolding |
ML20133P093 | 1 August 1985 | Rev 0 to Calculation Q-14, Calculation for Justification for Electrical Separation Between Safety-Related & Nonsafety-Related Cables When One in Free Air & Other in Raceway | |
ML20133P046 | 1 August 1985 | Rev 0 to Calculation Q-13, Calculations for Justification of Electrical Separation Distance Between Safety-Related & Nonsafety-Related Raceways | |
ML20104A712 | 6 December 1984 | Viewgraphs from Braidwood Const Assessment Program (Bcap) Monthly Briefing | |
ML20079F856 | 20 December 1983 | Transparencies Presented at NRC 831220 Enforcement Conference Re Const & QA Activities at Facility | |
ML20091M861 | 28 January 1983 | Comparison of Ringhals & Transflo Pressure Drops Through D-3 Preheater | |
ML20091M839 | 28 January 1983 | Model D-3 Preheater Temps | |
ML20091M822 | 28 January 1983 | D-3 SG Downcomer Flow Rates | |
ML20011A559 | 2 October 1981 | Transcript of 811002 Telcon W/Aslb,Util,Nrc Ofc of Executive Legal Director,Dekalb Area Alliance for Responsible Energy & Safe Energy for New Haven.Notice of Filing & Certificate of Svc Encl |