05000374/LER-2021-002-02, Supplement to Reactor Protection System Half Scram Due to Motor Generator Set Output Breaker Trip
ML23145A012 | |
Person / Time | |
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Site: | LaSalle |
Issue date: | 05/25/2023 |
From: | Casey Smith Constellation Energy Generation |
To: | Office of Nuclear Reactor Regulation, Document Control Desk |
References | |
RA23-003 LER 2021-002-02 | |
Download: ML23145A012 (1) | |
Event date: | |
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Report date: | |
Reporting criterion: | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
3742021002R02 - NRC Website | |
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LaSalle County Station 2601 North 21 " Road Constellation. Marseilles, IL 61341 815 -415 -2000 Telephone
RA23-003
May 25, 2023
U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001
LaSalle County Station, 2 Renewed Facility Operating License No. NPF-11 NRC Docket No. 50-374
Subject: Licensee Event Report 2021-002-02, Supplement to Reactor Protection System Half Scram due to Motor Generator Set Output Breaker Trip
In accordance with 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(2)(i)(B),
Constellation Energy Generation, LLC (CEG) is submitting Licensee Event Report (LER) Number 2021-002-02 for LaSalle County Station, Unit 2.
There are no regulatory commitments in this letter. Should you have any questions concerning this report, please contact Mr. Dan Mearhoff, Regulatory Assurance Manager, at (815) 415-2800.
Respectfully,
Christopher J. Smith Plant Manager LaSalle County Station
Enclosure: Licensee Event Report
cc : Regional Administrator-NRC Region Ill NRC Senior Resident Inspector - LaSalle County Station RC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB : NO. 3160-0104 EXPIRES: 08/31/2023 (08-2020) Estimated bi,den per response to comply with t)P'*~<<. LICENSEE EVENT REPORT (LER) lessons l!a-ned ** inco,pora1Jld into Iha lcansing prooess and fed this mandatxy collection bad< to indus~. Send comments request 80 hoi,s. Reported
to the FOIA, IJlrary, 111d Information Collections Branch (T-8 A10M), U.S.
/¥.\\ regarding burden estimate (See Page 3 for required number of digits/characters for each block) Nuclea Regulatory Commission, Washingtm, DC 20555-0001, or by a-mail to.gov, and the OM! revlaww a: OM! Ofloe of lrtonnation and Regulatory
\\, ~i..... tlUR;l~ at!. llQ~ll~ ia11*(See NUREG -1022, R.3 for instruction and guidance for completing this fonn lnbcolects.ReSOll'oe@rrcAffairs, (3150-0104), Alln: Desk ait on submissoo@omb.eco.goy. The NRC may not oorduct or lllllll~ll~ illaiw1,1u:1111.!AlalflAtll22ZlQD sponoa-, and a parsa1 is not raqured b respond to, a colediol1 ol informaion unl!ss the dOQJ111811t requesting or requmg the colllction d"l)lays a a.nanlly vald OM! control numb<<.
- 1. Faclllty Name 2. Docket Number 3. Page LaSalle County Station, Unit 2 05000 -374 1 OF 5
- 4. Title Reactor Protection System Half Scram due to Motor Generator Set Output Breaker Trip
- 6. Event Date 6. LER Number 7. Report Date 8. Other Facilities Involved Month Day Year Year Number No. Month Day Year NA 05000 Sequential Revision Faclllty Name Docket Number
05 31 2021 2021 002 02 05 23 2023 Facility - - NA 05000 Name Docket Number
- 9. Operating Mode 1 110. Power Level 100 percent
- 11. This Report Is Submitted Pursuant to the Requirements of 10 CFR §: (Check all that apply) 10 CFR Part 20 D 20.2203(a)(2)(vi) D 50.36(c)(2) IZJ 50.73(a)(2)(Iv)(A) D 50.73(a)(2)(x) 20.2201(b) D 20.2203(a)(3)(I) D 50.46(a)(3)(ii) D 50.73(a)(2)(v)(A) 'fliO t1FR Pa rt i13 20.2201(d) 20.2203(a)(3)(il) 50.69(g) D 50.73(a)(2)(v)(B) D 73.71(a)(4)
D 20.2203(a)(1) D 20.2203(a)(4) 50.73(a)(2)(i)(A) D 50.73(a)(2)(v)(C) D 73.71(a)(5)
D 20.2203(a)(2)(i) 1110 \\lFIR ~ai't.2'1 IZJ 50.73(a)(2)(i)(B) D 50.73(a)(2)(v)(D) D 73.77(a)(1)(i)
D 20.2203(a)(2)(ii) D 21.2(c) 50.73(a)(2)(I)(C) D 50.73(a)(2)(vil) D 73.77(a)(2)(i)
D 20.2203(a)(2)(iii) 1O C AR Pa lt50 50.73(a)(2)(ii)(A) D 50.73(a)(2)(viii)(A) D 73.77(a)(2)(ii)
D 20.2203(a)(2)(iv) 50.36(c)(1)(i)(A) 50.73(a)(2)(ii)(B) D 50.73(a)(2)(viii)(B)
D 20.2203(a)(2)(v) 50.36(c)(1)(ii)(A) D 50.73(a)(2)(iii) 50.73(a)(2)(IX)(A)
D OTHER (Specify here, in abstract, or NRC 366A).
- 12. Licensee Contact for this LER Licensee Contact rhone Number (Include area code)
Joseph Reda, Director Site Engineering (815) 415-3800
- 13. Complete One Line for each Component Failure Described In this Report
Cause System Component Manufacturer Reportable to IRIS Cause System Component Manufacturer Reportable to IRIS X JE RHE 0026 y X MS ISV A415 y
- 14. Supplemental Report Expected Month Day Year 16. Expected Submlaalon Date
~ No I D Yes (If yes, complete 15. Expected Submission Date)
Abstract
On May 31, 2021, LaSalle Unit 2 was operating at 100 percent power, when the 2A reactor protection system (RPS) motor generator (MG) set output breaker tripped due to an overload condition, which resulted in a loss of 2A RPS bus. Loss of power to this bus created a half-scram and initiated closure of outboard isolation valves in multiple systems. The condition was an invalid actuation because it was not the result of actual plant conditions and not an intentional manual action. Actuations and isolations that occurred performed as designed, except for the outboard 2D main steam line isolation valve (MSIV) drain valve that was discovered later as having a slow closure time, rendering the component inoperable.
The cause of the MG set breaker trip was a degraded voltage adjustment potentiometer on the associated MG set, which caused the output voltage to fluctuate. The RPS bus loss resulted in general containment isolation signals that affected containment isolation valves in more than one system while the unit was critical. Therefore, the condition is reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A).
The cause of the MSIV drain valve slow closure was motor and bearing degradation from a nearby steam leak. There was no loss of safety function since an inboard isolation valve in the flow-path remained operable. However, the condition is reportable in accordance with 1 O CFR 50. 73(a)(2)(i)(B) as an operation or condition prohibited by technical specifications (TS) due to having an inoperable component longer than permitted by TS.
Plant and System Identification
LaSalle Country Station Unit 2 is a General Electric Boiling Water Reactor with 3546 Megawatts Thermal Rated Core Power.
The affected system was the " A " reactor protection system (RPS) logic and associated isolation functions. RPS initiates a rapid insertion of all the control rods (scram) when monitored variables exceed their pre-established limits, neutron flux instrumentation becomes inoperable, or a manual scram signal is inserted by the operator. In addition, the setpoints, power sources, and controls and instrumentation are arranged in such a manner as to preclude spurious scrams.
Condition Prior to Event
Unit(s) : 2 Date: May 31, 2021 Time : 19:26 CDT Reactor Mode(s) : 1 Mode(s) Name : Power Operation Power Level: 100 percent
Description
On May 31, 2021, the main control room (MCR) operating crew received an "A" RPS half scram due to loss of power to Unit 2 "A" (2A) RPS bus. The operating crew entered applicable abnormal operating procedure for the RPS power condition. Field operators determined that the 2A RPS MG set output breaker had overloaded and tripped. The loss of the power to the 2A RPS bus resulted in a half scram and closure of outboard isolation valves in multiple systems. The condition was considered an invalid actuation because it was not the result of a valid signal and not an intentional manual action. The actuations and isolations that occurred performed as designed except for the closure time of outboard main steam line isolation valve (MSIV) drain valve 2821-F067D.
The 2A RPS bus loss resulted in isolations of the reactor water cleanup system, main steam line (MSL) drains, RCS sampling, instrument nitrogen system, reactor recirculation hydraulic power unit outboard isolation valves, and containment monitoring valves. The condition also resulted in loss of power to portions of the average power range monitor, local power range monitor,
oscillating power range monitor, control rod block systems ; as well as portions of the radiation monitoring for main steam lines, reactor building ventilation, and fuel pool ventilation. Appropriate actuations and primary containment isolations occurred as designed.
Due to the 2A RPS bus loss of power, applicable technical specification (TS) timeclocks were entered. Power was restored to 2A RPS bus in accordance with station procedures by transferring 2A RPS bus to the alternate power supply and resetting the half scram. When power was restored and the isolations were reset, the affected equipment was returned to operable status and timeclocks were exited.
MSIV Drain Valve
Position indication was lost on the Unit 2 "D" outboard MSIV drain valve (2821-F067D) while power was being restored. This condition caused the station to enter TS Required Action (RA) to restore required post-accident monitor (PAM) instrumentat ion channel within 30 days. Position indication was restored after a reset of thermal breaker overloads. The 2D MSIV drain valve indicated in the closed position, verifying it performed its design function when 2A RPS power had been lost.
Subsequently, during reviews of computer traces from the loss of 2A RPS bus event, this valve was found to have exhibited closure time in excess of maximum isolation time limits spec ified in the technical requirements manual (TRM) and was declared inoperable as a primary containment isolation valve (PCIV). The station entered TS required actions to isolate the affected penetration flow path by use of at least one closed and de-activated automatic valve in four hours and to verify the affected penetration flow path is isolated once per 31 days. There was no loss of safety function as the penetration has two PCIVs in the flow-path, and the inboard PCIV remained operable.
Cause
The RPS MG set can trip on either over-voltage, under-voltage, or under-frequency. A review of plant data recorders and component testing determined that the cause of the issue was a degraded voltage adjustment potentiometer (device 1 P) on the 2A RPS MG set, which was causing intermittent resistance readings. The intermittent resistance caused the output voltage of the RPS MG set to fluctuate. As a result, the degraded potentiometer and the voltage regulator were replaced as part of the trouble shooting efforts, and the system was restored back to its original configuration.
MSIV Drain Valve
Following the loss of the 2A RPS bus, the 2D outboard MSIV drain valve, 2B21-F067D, was found tripped on thermals. Once the PCIS signal and breaker thermal overload was reset, position indication returned and showed the valve was in the full-closed position. Investigations performed during the 2023 Unit 2 Refueling outage found that the cause of the 2B21-F067D slow closure was motor and bearing degradation caused by an adjacent steam leak. This degradation is what caused the slow closure time and subsequent tripping of the thermal overloads.
Reportability and Safety Analysis
The RPS is divided into two trip systems that are physically and electrically independent. The design of this system is such that the loss of power to one of these trip systems neither prevents nor causes a reactor scram. Normal power to RPS buses A and B is supplied by two motor-generator (MG) sets. Alternate power for either RPS bus is from the Alternate Instrument and RPS Bus Transformer. The loss of an RPS bus and associated RPS actuation was considered an invalid actuation because it was not the result of a valid signal and not an intentional manual action. The RPS bus loss condition resulted in general containment isolation signals that affected containment isolation valves in more than one system or multiple main steam isolation valves while the unit was critical. Therefore, the RPS bus loss condition is reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A).
MSIY Drain Valve
The PCIS is designed to prevent the release of radioactive materials through containment penetrations in an accident where the primary system boundary has been lost and to prevent core damage when a major process line breaks outside primary containment. Major process lines are isolated automatically by PCIS on receipt of a trip signal. The PCIS logic is divided into two trip systems consisting of an inboard trip system and an outboard trip system. Main Steam is one of the several systems connected to the reactor which must close valves to isolate penetrations to the primary containment upon receipt of an isolation signal. The time required to close the Main Steam valves is designed to be short enough to minimize the loss of coolant from a steam line break. The 2D outboard MSIV drain valve indicated in the closed position, verifying it performed its design function when 2A RPS power had been lost. There was no loss of safety function as the penetration has two PCIVs in the flow-path, and the inboard PCIV remained operable.
The 2D outboard MSIV drain valve was subsequently found to have exhibited delayed closure time longer than the maximum isolation time limits specified in the technical requirements manual (TRM) and was declared inoperable as a primary containment isolation valve (PCIV). However, there was no loss of safety function as the penetration has two PCIVs in the flow-path, and the inboard PCIV remained operable. As a result of the inoperable valve, the condition is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as operation or condition prohibited by technical specifications.
Safety System Functional Failure Review
The system equipment responses did not result in a safety system functional failure (SSFF) as defined in accordance with NEI 99-02, "Regulatory Assessment Performance Indicator Guideline." The RPS logic safety function was satisfied by its actuation
for designed inputs, and the 2821-F067D delayed closure time did not result in prevention of associated safety systems to the control the release of radioactive material since this valve is located between the inboard and outboard MSIVs on the "D" MSL which would have been isolated by the inboard MSIV.
Corrective Actions
The station identified actions to restore the affected systems and perform maintenance activities including:
- Declaration of affected systems inoperable and applicable TS required actions
- Maintenance activities to restore the "A" RPS logic
- Restore system alignments for the affected PCIS group
- Completed repairs and failure analysis of valve in the 2023 Unit 2 refueling outage
The degraded potentiometer and the voltage regulator for the 2A RPS MG set were replaced as part of the troubleshooting efforts, and the RPS system was restored back to its original configuration. The station performed an extent of condition review to the Unit 1 RPS MG sets {1A and 1 B) and the other Unit 2 RPS (28), which included a review of trace recordings, which indicated less pronounced spiking for Unit 1 RPS {1A and 18). The most likely cause for the 1A and 18 RPS MG sets voltage fluctuations is the voltage adjust potentiometer and/or voltage regulator.
MSIV Drain Valve
Troubleshooting performed during the outage identified the 2821-F067D failure was caused by an adjacent steam leak from the 2821-F067A valve. Extent of condition testing was completed on nearby MSIV drain valves and repairs performed as necessary. All MSIV drain valves are included in station MOV testing program and will be periodically tested to monitor for effectiveness of actions.
Previous Occurrences
There have been no similar reportable events in the prior three-year period involving an RPS bus loss that resulted in TS actuations that did not meet applicable requirements. However, during that period there have been non-reportable component performance issues captured in the corrective action program via an Issue Report {IR) for RPS MG set output breaker or separately a containment isolation valve.
- IR 4166455 - On August 23, 2018, the 2A RPS MG set output breaker did not trip open due a surveillance test. All instruments powered by the associated RPS bus functioned as designed, and the output breaker was repaired. There was no loss of operability or past operability for this event.
- IR 4368877 - On September 11, 2020, the 1A RPS experienced a half-scram during maintenance activities to replace a relay, due to the 81 logic bypass circuit output contact de-energizing when the relay 's output contactor loosened. The RPS configuration was reset, and work planning instructions were revised to jumper this part of the circuit. There was no loss of operability or past operability for this event.
- IR 4407689-On March 9, 2021, during a refueling outage, the 20 inboard MSIV {2821-F022D) was unresponsive during maintenance testing to close this valve. There was no loss of function since the valve was not required in this mode operation.
Component Failure Data
Device: 2A RPS Logic MG Set Output Breaker - Voltage Adjustment Potentiometer Component Type: Rheostat/ Potentiometer [RHE]
Manufacturer: Ohmite [0026)
Part: RHSS00
Device: 20 Outboard MSIV Drain Valve Component Type: Motor Operated Isolation Valve [ISV]
Manufacturer: Anderson & Co., Greenwood [A415)
Part: GR12809F-6565-1M