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| 05000373/LER-1985-001-01, :on 850102,level Switches LIS-B21-N100A & B for HPCS Injection Valve High Reactor Level Closure Found Out of Tolerance in Nonconservative Direction.Caused by Instrument Drift.Switch Setpoints Recalibr |
- on 850102,level Switches LIS-B21-N100A & B for HPCS Injection Valve High Reactor Level Closure Found Out of Tolerance in Nonconservative Direction.Caused by Instrument Drift.Switch Setpoints Recalibr
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| 05000374/LER-1985-001, :on 850107,HPCS Pump Suction Valve to Suppression Pool Opened,While Normal Suction Valve to Cycled Condensate Tank Closed.Caused by High Suppression Pool Level.Pool Level Lowered & HPCS Reestablished |
- on 850107,HPCS Pump Suction Valve to Suppression Pool Opened,While Normal Suction Valve to Cycled Condensate Tank Closed.Caused by High Suppression Pool Level.Pool Level Lowered & HPCS Reestablished
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| 05000373/LER-1985-002-01, :on 850105,condensate Pumps 1B & 1D Automatically Tripped,Resulting in Low Water Level Condition in Reactor Vessel.Caused by Increase in Stator Water Conductivity.Operator Involved Counseled |
- on 850105,condensate Pumps 1B & 1D Automatically Tripped,Resulting in Low Water Level Condition in Reactor Vessel.Caused by Increase in Stator Water Conductivity.Operator Involved Counseled
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| 05000373/LER-1985-003, :on 850106,reactor Water Cleanup Sys Isolated on High Differential Flow.Caused by Reactor Startup.Sys Restarted.Ge Investigating Design Basis for Isolation Setpoint |
- on 850106,reactor Water Cleanup Sys Isolated on High Differential Flow.Caused by Reactor Startup.Sys Restarted.Ge Investigating Design Basis for Isolation Setpoint
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| 05000374/LER-1985-004-03, :on 850114,automatic Depressurization Sys a & B out-of-svc Alarms Received from ESF Status Panel Accumulators E & V.Caused by Loosened Mounting Screws. Mounting Screws Tightened & Setpoints Verified |
- on 850114,automatic Depressurization Sys a & B out-of-svc Alarms Received from ESF Status Panel Accumulators E & V.Caused by Loosened Mounting Screws. Mounting Screws Tightened & Setpoints Verified
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| 05000374/LER-1985-005-02, :on 850121,reactor Bldg Closed Cooling Water Outlet Outboard Isolation Valve 2WR040 Closed.Caused by Physical Failure of Relay 2B214-K67X18 Due to Short Circuit & Burn Out of Coil Windings |
- on 850121,reactor Bldg Closed Cooling Water Outlet Outboard Isolation Valve 2WR040 Closed.Caused by Physical Failure of Relay 2B214-K67X18 Due to Short Circuit & Burn Out of Coil Windings
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| 05000373/LER-1985-005-01, :on 850114,unit Shut Down.Caused by Standby Gas Treatment Trains Declared Inoperable Due to Replacement Heaters Power Output Exceeding Tech Specs.Tech Spec 3.6.5 Will Be Revised to Clarify Output Requirements |
- on 850114,unit Shut Down.Caused by Standby Gas Treatment Trains Declared Inoperable Due to Replacement Heaters Power Output Exceeding Tech Specs.Tech Spec 3.6.5 Will Be Revised to Clarify Output Requirements
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| 05000374/LER-1985-006-02, :on 850122,HPCS Pump Suction Valve to Condesate Storage Tank Closed & Suction from Suppression Pool Opened. Caused by High Level of Water in Pool.Water Level Lowered. Normal Suction Reestablished |
- on 850122,HPCS Pump Suction Valve to Condesate Storage Tank Closed & Suction from Suppression Pool Opened. Caused by High Level of Water in Pool.Water Level Lowered. Normal Suction Reestablished
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| 05000373/LER-1985-006-01, :on 850112,calibr of Level Switch 1B21-N037B Exceeded Time Allowed,Per Tech Spec Tables 3.3.3-1 & 3.3.5-1.Caused by Switch Outside Desired Setpoints.Level Switches Replaced |
- on 850112,calibr of Level Switch 1B21-N037B Exceeded Time Allowed,Per Tech Spec Tables 3.3.3-1 & 3.3.5-1.Caused by Switch Outside Desired Setpoints.Level Switches Replaced
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| 05000374/LER-1985-007-02, :on 850205,high Pressure Core Spray Injection Valve Closure Switches 2B21-N100A & B Found Out of Tolerance Range in Nonconservative Direction.Apparently Caused by Instrument Drift |
- on 850205,high Pressure Core Spray Injection Valve Closure Switches 2B21-N100A & B Found Out of Tolerance Range in Nonconservative Direction.Apparently Caused by Instrument Drift
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| 05000373/LER-1985-007-01, :on 850116,Control Room a Ventilation/Auxiliary Equipment Room Ventilation Sys Chlorine Detector Alarmed. Cause Undetermined.Alarm Reset & Chlorine Detector Returned to Svc |
- on 850116,Control Room a Ventilation/Auxiliary Equipment Room Ventilation Sys Chlorine Detector Alarmed. Cause Undetermined.Alarm Reset & Chlorine Detector Returned to Svc
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| 05000373/LER-1985-008-01, :on 850202,exhaust Secondary Containment Isolation Dampers Inoperable.Caused by Failure of Solenoid Valves.Solenoid Valves Replaced |
- on 850202,exhaust Secondary Containment Isolation Dampers Inoperable.Caused by Failure of Solenoid Valves.Solenoid Valves Replaced
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| 05000374/LER-1985-008-02, :on 850213,high Chlorine/Ammonia Concentration Alarm Received for Train B of HVAC Sys.Caused by Chemcassette Being Out of Tape.Exhausted Chemcassette Replaced & Trip Reset |
- on 850213,high Chlorine/Ammonia Concentration Alarm Received for Train B of HVAC Sys.Caused by Chemcassette Being Out of Tape.Exhausted Chemcassette Replaced & Trip Reset
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| 05000373/LER-1985-009, :on 850122,no Assigned Calibr or Functional Test Procedure for Calibr RHR Shutdown Cooling Suction Pressure Switch.Caused by Improper Identification on Tech Spec Surveillance Matrix.Procedure Drafted |
- on 850122,no Assigned Calibr or Functional Test Procedure for Calibr RHR Shutdown Cooling Suction Pressure Switch.Caused by Improper Identification on Tech Spec Surveillance Matrix.Procedure Drafted
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| 05000373/LER-1985-009-01, :on 850122,investigation Determined That No Assigned Calibr or Functional Test Procedure for Suction Pressure Switch Existed as Required by Tech Specs.Caused by Improper Setpoint Info.Switches Calibr |
- on 850122,investigation Determined That No Assigned Calibr or Functional Test Procedure for Suction Pressure Switch Existed as Required by Tech Specs.Caused by Improper Setpoint Info.Switches Calibr
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| 05000374/LER-1985-009-06, :on 850301,reactor Water Cleanup Sys Isolated on High Differential Flow.Caused by Pressure Transient Created by Opening Vessel Head Vent Valves.High Differential Flow Isolation Signal Reset |
- on 850301,reactor Water Cleanup Sys Isolated on High Differential Flow.Caused by Pressure Transient Created by Opening Vessel Head Vent Valves.High Differential Flow Isolation Signal Reset
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| 05000374/LER-1985-010-02, :on 850215,CRD Hydraulic Control Unit Accumulator Pressure Switch Failures Occurred.Caused by Setpoint Drift.Low Pressure Accumulators Recharged & Accumulator Pressure Switches Recalibr |
- on 850215,CRD Hydraulic Control Unit Accumulator Pressure Switch Failures Occurred.Caused by Setpoint Drift.Low Pressure Accumulators Recharged & Accumulator Pressure Switches Recalibr
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) |
| 05000373/LER-1985-010-01, :on 850121,two Separate Ammonia Detector Alarms Occurred on Ammonia Detector a for Control Room B Ventilation/Auxiliary Electric Equipment Room Ventilation Sys.Caused by Freezing Ambient Temps |
- on 850121,two Separate Ammonia Detector Alarms Occurred on Ammonia Detector a for Control Room B Ventilation/Auxiliary Electric Equipment Room Ventilation Sys.Caused by Freezing Ambient Temps
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| 05000373/LER-1985-011-01, :on 850202,group 1 Isolation Occurred Due to High Main Steam Tunnel Ambient Air Temp,Causing Reactor Scram.Caused by Lack of Ventilation Flow to Steam Tunnel. Isolation Dampers Repaired |
- on 850202,group 1 Isolation Occurred Due to High Main Steam Tunnel Ambient Air Temp,Causing Reactor Scram.Caused by Lack of Ventilation Flow to Steam Tunnel. Isolation Dampers Repaired
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| 05000374/LER-1985-012-04, :on 850331,during Performance of RHR Injection Line Integrity Monitor Calibr & Functional Test, RHR Shutdown Cooling Isolation Occurred.Caused by Personnel Error.Personnel Will Be Trained |
- on 850331,during Performance of RHR Injection Line Integrity Monitor Calibr & Functional Test, RHR Shutdown Cooling Isolation Occurred.Caused by Personnel Error.Personnel Will Be Trained
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| 05000373/LER-1985-012-01, :on 850208,reactor Water Cleanup Sys Isolated on High Differential Flow.Caused by Sys Blowing Down to Main Condenser.Sys Restarted.Flow Elements Will Be Recalibr |
- on 850208,reactor Water Cleanup Sys Isolated on High Differential Flow.Caused by Sys Blowing Down to Main Condenser.Sys Restarted.Flow Elements Will Be Recalibr
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| 05000374/LER-1985-013-04, :on 850328,during Performance of Group V Isolation Sys Functional Test LES-PC-05,Group Vi,Div 2 Isolation Occurred.Caused by Relay deenergization.LES-PC-05 Being Revised to Prevent Recurrence |
- on 850328,during Performance of Group V Isolation Sys Functional Test LES-PC-05,Group Vi,Div 2 Isolation Occurred.Caused by Relay deenergization.LES-PC-05 Being Revised to Prevent Recurrence
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| 05000373/LER-1985-013-01, :on 850212,while Finishing Precoating of Filter Demineralizer,Reactor Water Cleanup Sys Isolated on High Differential Flow.Caused by Internal Accumulated Sys Leakage & Flow Perturbations |
- on 850212,while Finishing Precoating of Filter Demineralizer,Reactor Water Cleanup Sys Isolated on High Differential Flow.Caused by Internal Accumulated Sys Leakage & Flow Perturbations
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| 05000374/LER-1985-014-04, :on 850409,spurious Div I RHR Shutdown Cooling Isolation Occurred.Caused by Momentary Power Loss to Relay 2B21H-K74 During Installation of Environ Qualification Mod M-1-2-84-117.Work Completed 850414 |
- on 850409,spurious Div I RHR Shutdown Cooling Isolation Occurred.Caused by Momentary Power Loss to Relay 2B21H-K74 During Installation of Environ Qualification Mod M-1-2-84-117.Work Completed 850414
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| 05000373/LER-1985-014-01, :on 850204,vacuum Breaker Valve Opened & Reclosed to Equalize Pressure Between Suppression Pool & Drywell.Caused by Adding Nitrogen to Reduce Drywell Oxygen Concentration.Procedure Will Be Revised |
- on 850204,vacuum Breaker Valve Opened & Reclosed to Equalize Pressure Between Suppression Pool & Drywell.Caused by Adding Nitrogen to Reduce Drywell Oxygen Concentration.Procedure Will Be Revised
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| 05000373/LER-1985-015-01, :on 850217,vacuum Breaker C Opened & Closed. Caused by Differential Pressure.Procedures Revised |
- on 850217,vacuum Breaker C Opened & Closed. Caused by Differential Pressure.Procedures Revised
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| 05000374/LER-1985-015-03, :on 850401,control Room Conductivity Indication Inoperative for Greater than 31 Days.Caused by out-of-svc Sample Taps & Low Flow on Sys Where Sample Obtained.Recorder Repaired |
- on 850401,control Room Conductivity Indication Inoperative for Greater than 31 Days.Caused by out-of-svc Sample Taps & Low Flow on Sys Where Sample Obtained.Recorder Repaired
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| 05000374/LER-1985-016-02, :on 850418,valve 2E51-F091 Discovered Listed in Body of Operating Surveillance Procedure LOS-RI-Q2 W/O Place for Recording Stroke Time & Initials on Data Sheet. Caused by Word Processing Error |
- on 850418,valve 2E51-F091 Discovered Listed in Body of Operating Surveillance Procedure LOS-RI-Q2 W/O Place for Recording Stroke Time & Initials on Data Sheet. Caused by Word Processing Error
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| 05000373/LER-1985-016-01, :on 850208,Door 426 to Reactor Water Cleanup HX B Room Found Unsecured & Unattended.Caused by Personnel Error.Counseling Given to Individual Responsible |
- on 850208,Door 426 to Reactor Water Cleanup HX B Room Found Unsecured & Unattended.Caused by Personnel Error.Counseling Given to Individual Responsible
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| 05000374/LER-1985-017-02, :on 850413,Group 6 Isolation of RHR Shutdown Cooling Suction Inboard 2E12-F009 & Outboard 2E12-F008 Valves & Shutdown Cooling Injection Valve Occurred.Caused by Incorrect Wiring of Pressure Switch |
- on 850413,Group 6 Isolation of RHR Shutdown Cooling Suction Inboard 2E12-F009 & Outboard 2E12-F008 Valves & Shutdown Cooling Injection Valve Occurred.Caused by Incorrect Wiring of Pressure Switch
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| 05000373/LER-1985-017-01, :on 850208,reactor Scrammed on Low Reactor Vessel Level.Caused by Placing Defective Jumper in Feedwater Pump NPSH Trip Circuit.Circuit Modified.Oil Sys Flushed |
- on 850208,reactor Scrammed on Low Reactor Vessel Level.Caused by Placing Defective Jumper in Feedwater Pump NPSH Trip Circuit.Circuit Modified.Oil Sys Flushed
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| 05000374/LER-1985-018-02, :on 850413,isolation of Shutdown Cooling Initiated When Broken Lug on Pressure Switch Being Repaired Grounded,Blowing Fuse to Div I Group 6 Isolation Logic.Fuse Replaced & Lug Repaired |
- on 850413,isolation of Shutdown Cooling Initiated When Broken Lug on Pressure Switch Being Repaired Grounded,Blowing Fuse to Div I Group 6 Isolation Logic.Fuse Replaced & Lug Repaired
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| 05000373/LER-1985-018-01, :on 850216,H2 Grab Sample Obtained for Unit Offgas Hydrogen Recombiner Effluent.Caused by Inoperability of Hydrogen Analyzers.Sample Obtained at Greater than Allowable Frequency |
- on 850216,H2 Grab Sample Obtained for Unit Offgas Hydrogen Recombiner Effluent.Caused by Inoperability of Hydrogen Analyzers.Sample Obtained at Greater than Allowable Frequency
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| 05000373/LER-1985-019-01, :on 850212,Door 606 to High Radiation Area Boundary Found Ajar W/Radiation Protection Sign Between Door & Jamb.Caused by Equipment Attendant Opening Door.Alarm Reset.Sign Reposted |
- on 850212,Door 606 to High Radiation Area Boundary Found Ajar W/Radiation Protection Sign Between Door & Jamb.Caused by Equipment Attendant Opening Door.Alarm Reset.Sign Reposted
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| 05000374/LER-1985-019-02, :on 850412,Group I Isolation Occurred on Trip Sys a When OOS 2-481-85 Cleared to Place Main Condenser Low Vacuum Pressure Switches Back in Svc.Caused by Miswired Main Steam Line High Flow Switches |
- on 850412,Group I Isolation Occurred on Trip Sys a When OOS 2-481-85 Cleared to Place Main Condenser Low Vacuum Pressure Switches Back in Svc.Caused by Miswired Main Steam Line High Flow Switches
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| 05000374/LER-1985-020-03, :on 850424,svc Water Monitor Not Sampled Once Per 8 H While Inoperable.Caused by Personnel Mistakenly Told to Sample Unit 2 RHR Svc Water Monitor A.Memo Issued Re Effective Verbal Communication |
- on 850424,svc Water Monitor Not Sampled Once Per 8 H While Inoperable.Caused by Personnel Mistakenly Told to Sample Unit 2 RHR Svc Water Monitor A.Memo Issued Re Effective Verbal Communication
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| 05000373/LER-1985-020, :on 850214,gate to High Radiation Area Found Unlocked & Unattended.Caused by Individual Leaving High Radiation Gate Open & Unattended.Gate Closed & Secured & Personnel Counseled |
- on 850214,gate to High Radiation Area Found Unlocked & Unattended.Caused by Individual Leaving High Radiation Gate Open & Unattended.Gate Closed & Secured & Personnel Counseled
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| 05000374/LER-1985-021-03, :on 850503,during Cold Shutdown,Discovered That Cables from Sensors in Reactor Bldg Basement to Control Room Improperly Labeled.Probably Caused by Initial Const Error. Sensors Replaced |
- on 850503,during Cold Shutdown,Discovered That Cables from Sensors in Reactor Bldg Basement to Control Room Improperly Labeled.Probably Caused by Initial Const Error. Sensors Replaced
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| 05000373/LER-1985-021, :on 850220,high Radiation Area Gate Unsecured & Unattended.Caused by Contractors Leaving Area for Lunch Break W/O Securing Gate.Individuals Involved Counseled. Co-workers Counseled |
- on 850220,high Radiation Area Gate Unsecured & Unattended.Caused by Contractors Leaving Area for Lunch Break W/O Securing Gate.Individuals Involved Counseled. Co-workers Counseled
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| 05000374/LER-1985-022, :on 850510,while in Cold Shutdown,Intermediate Range Monitor C Spiked High,Initiating Full Scram Signal. Caused by Equipment Failure.Intermediate Range Monitor C Bypassed & Scram Reset |
- on 850510,while in Cold Shutdown,Intermediate Range Monitor C Spiked High,Initiating Full Scram Signal. Caused by Equipment Failure.Intermediate Range Monitor C Bypassed & Scram Reset
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| 05000373/LER-1985-022, :on 850222,RCIC Received Div 1 & 2 Isolation Signals on High RCIC Steam Line Flow.Caused by Release of Steam at Reactor Pressure Into RCIC Steam Line from Piping Between RCIC in- & Outboard Isolation Valves |
- on 850222,RCIC Received Div 1 & 2 Isolation Signals on High RCIC Steam Line Flow.Caused by Release of Steam at Reactor Pressure Into RCIC Steam Line from Piping Between RCIC in- & Outboard Isolation Valves
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| 05000374/LER-1985-022-03, :on 850510,reactor Scram Occurred Due to High Spikes on intermediate-range Monitor C.Caused by Equipment Failure.Nature of Failure Still Under Investigation |
- on 850510,reactor Scram Occurred Due to High Spikes on intermediate-range Monitor C.Caused by Equipment Failure.Nature of Failure Still Under Investigation
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| 05000373/LER-1985-023, :on 850223,door to High Radiation Area Discovered Unsecured & Unattended.Caused by Mechanical Failure of Door Latching Mechanism.Door Latch Adjusted & Lock Checked for Proper Functioning |
- on 850223,door to High Radiation Area Discovered Unsecured & Unattended.Caused by Mechanical Failure of Door Latching Mechanism.Door Latch Adjusted & Lock Checked for Proper Functioning
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| 05000374/LER-1985-023-03, :on 850523,safety Relief Valve 2B21-F013D Opened for No Apparent Reason,Then Reclosed.Thorough Investigation Discovered No Problems |
- on 850523,safety Relief Valve 2B21-F013D Opened for No Apparent Reason,Then Reclosed.Thorough Investigation Discovered No Problems
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| 05000373/LER-1985-024-01, :on 850303,reactor Scram Occurred,Resulting from Turbine Control Valve Fast Closure.Caused by Offsite Fault on 345-kv Transmission Line 0101.Lines 0101 & 0104 Inspected |
- on 850303,reactor Scram Occurred,Resulting from Turbine Control Valve Fast Closure.Caused by Offsite Fault on 345-kv Transmission Line 0101.Lines 0101 & 0104 Inspected
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| 05000374/LER-1985-024-03, :on 850531,primary Containment Isolation Sys Group I Isolation Occurred During Main Turbine Valve Testing W/Unit in Cold Shutdown.Caused by Auxiliary Transformer Being Backfed Through Main Power Transformers |
- on 850531,primary Containment Isolation Sys Group I Isolation Occurred During Main Turbine Valve Testing W/Unit in Cold Shutdown.Caused by Auxiliary Transformer Being Backfed Through Main Power Transformers
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| 05000374/LER-1985-025-03, :on 850606 & 07,full Reactor Scrams Occurred. Caused by MSIV Being Closed in Run.Corrective Actions Will Include Operator Training,Procedure Revs & New Mode Switch Procedure |
- on 850606 & 07,full Reactor Scrams Occurred. Caused by MSIV Being Closed in Run.Corrective Actions Will Include Operator Training,Procedure Revs & New Mode Switch Procedure
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| 05000373/LER-1985-025-01, :on 850304,drywell Vacuum Breaker Cycled Open & Closed.Caused by Steam from RCIC Turbine Causing Temp/ Pressure in Suppression Pool to Rise.Breaker Operated as Required |
- on 850304,drywell Vacuum Breaker Cycled Open & Closed.Caused by Steam from RCIC Turbine Causing Temp/ Pressure in Suppression Pool to Rise.Breaker Operated as Required
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| 05000374/LER-1985-026-03, :on 850522,diesel Generator 2B Tripped Approx 3 After Being Started Per Surveillance Procedure.Caused by Time Delay Relay for Low Lube Oil Pressure Switch Not Operating Correctly |
- on 850522,diesel Generator 2B Tripped Approx 3 After Being Started Per Surveillance Procedure.Caused by Time Delay Relay for Low Lube Oil Pressure Switch Not Operating Correctly
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| 05000373/LER-1985-026-01, :on 850313,shutdown Cooling Header Pressure Switch Not Tested within Allowable Time Limits.Caused by Error in Identifying Proper Switch to Meet Tech Spec Requirements.New Requirements Added to Program |
- on 850313,shutdown Cooling Header Pressure Switch Not Tested within Allowable Time Limits.Caused by Error in Identifying Proper Switch to Meet Tech Spec Requirements.New Requirements Added to Program
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