05000254/LER-2022-002, Low Pressure Coolant Injection Manually Isolated Due to Valve Test Equipment Issue
| ML22189A029 | |
| Person / Time | |
|---|---|
| Site: | Quad Cities |
| Issue date: | 07/08/2022 |
| From: | Wake B Constellation Energy Corp |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| SVP-22-040 LER 2022-002-00 | |
| Download: ML22189A029 (1) | |
| Event date: | |
|---|---|
| Report date: | |
| Reporting criterion: | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 2542022002R00 - NRC Website | |
text
Constellation,,,
SVP-22-040 July 8, 2022 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Quad Cities Nuclear Power Station, Unit 1 Renewed Facility Operating License No. DPR-29 NRC Docket No. 50-254 10 CFR 50.73
Subject:
Licensee Event Report 254/2022-002-00 "Low Pressure Coolant Injection Manually Isolated Due To Valve Test Equipment Issue" Enclosed is Licensee Event Report 254/2022-002-00 "Low Pressure Coolant Injection Manually Isolated Due To Valve Test Equipment Issue," for Quad Cities Nuclear Power Station, Unit 1.
This report is submitted in accordance with 10 CFR 50. 73(a)(2)(v)(B) and 10 CFR
- 50. 73(a)(2)(v)(D) for an event or condition that could have prevented the fulfillment of a safety function needed to remove residual heat and to mitigate the consequence of an accident.
There are no regulatory commitments contained in this letter.
Should you have any questions concerning this report, please contact Mark Humphrey at (309) 227-2800.
Brian Wake Site Vice President Quad Cities Nuclear Power Station cc:
Regional Administrator-NRC Region Ill NRC Senior Resident Inspector - Quad Cities Nuclear Power Station
Abstract
On May 10, 2022, with Unit 1 operating at 100% power, motor operated valve (MOV) thrust testing was being performed on Residual Heat Removal (RHR) Low Pressure Coolant Injection (LPCI) valve 1-1001-28B, 1B LPCI Loop Upstream Stop Valve. Inadequate thrust conditions were discovered on this valve, which also serves as a Primary Containment Isolation Valve (PCIV). Technical Specification (TS) 3.6.1.3 Condition A requires that a containment penetration with a degraded valve be manually isolated within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. Manual closure of the companion PCIV valve 1-1001-29B, 1 B LPCI Loop Downstream Stop Valve, including opening of the electrical breaker MCC 18/19-5 Cubicle F1 to the valve, rendered both loops of LPCI incapable of either manual or automatic injection as described in TS 3.5.1 Condition E for two LPCI Subsystems inoperable.
The cause of the low MOV thrust value was found to be insufficient installation bond between the valve stem and the thrust sensor instrument. Thrust was eventually found to be sufficient, but this was not identified prior to the 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> TS action requirement. A new sensor was installed, and the valve thrust results were found to be satisfactory. This report is being submitted in accordance with 10 CFR 50.73(a)(2)(v)(B) and 10 CFR 50.73(a)(2)(v)(D) for an event or condition that could have prevented the fulfillment of a safety function needed to (B) remove residual heat and (D) mitigate the consequences of an accident.
PLANT AND SYSTEM IDENTIFICATION
General Electric - Boiling Water Reactor, 2957 Megawatts Thermal Rated Core Power Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
EVENT IDENTIFICATION Low Pressure Coolant Injection Manually Isolated Due To Valve Test Equipment Issue
CONDITION PRIOR TO EVENT
Unit: 1 Event Date: May 10, 2022 Reactor Mode: 1 Mode Name: Run Event Time: 17 46 CST Power Level: 100%
002 REV NO.
00 No structures, systems or components were inoperable at the start of this event that contributed to the event.
A. DESCRIPTION OF EVENT
On May 10, 2022, Unit 1 was operating at 100% power. Motor Operated Valve (MOV) [VJ diagnostic testing was being performed on Residual Heat Removal (RHR) Low Pressure Coolant Injection (LPCI)
[BO] valve 1-1001-288, 1 B LPCI Loop Upstream Stop Valve, when a low thrust was measured at 1359 hours0.0157 days <br />0.378 hours <br />0.00225 weeks <br />5.170995e-4 months <br /> causing the valve to be declared inoperable. Inadequate grease volume was also identified in one chamber of the MOV actuator, which was considered an initial contributor to the insufficient thrust measurement. The grease was later eliminated as a cause or a contributor to this event. This valve is also a Primary Containment Isolation (PCIV) [BD] valve for containment penetration X-0138, resulting in TS 3.6.1.3 Condition A to be entered for a penetration flow path with one PCIV inoperable.
TS 3.6.1.3 Condition A requires that the affected flow path be isolated within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> by use of one closed and de-activated valve. Engineering review of thrust data and grease quantities did not reach a conclusion during the 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> window to provide confidence in valve performance. Operations de-activated the affected penetration at 1746 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.64353e-4 months <br /> by closing the 1-1001-298, 18 LPCI Loop Downstream Stop Valve, and electrically isolating it by opening breaker [BKR] MCC 18/19-5 Cubicle F1. LPCI Loop Select Logic will determine if LPCI flow is injected into the A or B loop of the Reactor Recirculation (RR) [AD] System depending upon the appropriate accident's line break location. The isolated penetration is part of the injection flow path into the B loop of the RR system with either the A or B loop of LPCI providing injection.
Because the LPCI injection path cannot be predicted ahead of an event, this penetration isolation renders both the A and B LPCI loops inoperable, causing entry into TS 3.5.1 Condition E for two LPCI subsystems inoperable.
SEQUENTIAL NUMBER 002 REV NO.
00 The valve thrust failure investigation concluded that there was no actual MOV thrust deficiency on the 1-1001-288 effecting valve functionality. The measurement and test equipment (M&TE) sensor was not bonded correctly to the valve stem. This cause was not identified until after TS 3.6.1.3 Condition A required isolation of the containment penetration. Following additional troubleshooting and repair activities, post maintenance testing indicated proper performance of both the M&TE sensor and all related MOV performance characteristics. At 1500 on May 11, 2022, the containment penetration was unisolated, and LPCI function was recovered.
The penetration de-activation took place on May 10, 2022 at 17:46 and was recovered on May 11, 2022 at 1500, for a total of twenty-one hours and fourteen minutes that LPCI was unavailable. Isolation of the containment penetration prevented both automatic and manual LPCI functions during this period.
Therefore, reportability is required under 10 CFR 50. 73(a)(2)(v)(8) and 10 CFR 50. 73(a)(2)(v)(D) - "Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: (8) remove residual heat," and "(D) mitigate the consequences of an accident."
B. CAUSE OF EVENT
The cause of the as-found low thrust was bad data obtained from an insufficient installation bond between the M& TE sensor and the valve stem and not a deficiency with the valve, thus this condition never actually prohibited proper valve performance.
The cause of the containment penetration and LPCI isolation was operator actions in accordance with Technical Specification (TS) requirements during the period that the 1-1001-288 valve performance was not clearly supported.
C. SAFETY ANALYSIS
System Design
Valves 1-1001-288 and 1-1001-298 provide both a PCIV function for penetration X-0138, as well as an injection path into the 8 RR loop for RHR pump low pressure Emergency Core Cooling System (ECCS) subsystem of LPCI to provide core cooling and residual heat removal during accident conditions. These valves receive automatic signals for both the PCIV function as well as the LPCI function and can also be manually controlled from the main control room.
Safety Impact Actual safety consequences of the event were minimal for both normal operation and design basis event operation based on the availability during this time of all High Pressure ECCS, as well as both loops of Low Pressure ECCS subsystem of Core Spray. The remaining functions of RHR including containment spray and suppression pool cooling remained available despite the loss of the LPCI subsystem ability to inject into RR Loop B. Based on the availability of these additional sources of coolant to the core, the consequences of this event were minimal. There was no impact on the health and safety of the public or plant personal.
00 This issue was evaluated for a Safety System Functional Failure (SSFF) in accordance with NEI 99-02 and 10 CFR 50. 73. Although the failure analysis determined that there was no MOV failure related to the function of the 1-1001-288 valve, the 1-1001-298 valve was still closed and electrically de-activated which resulted in the loss of the manual and automatic function of LPCI. Therefore, reportability under 50.73(a)(2)(v)(B) and 50.73(a)(2)(v)(D) - "Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: (8) remove residual heat" and "(D) mitigate the consequences of an accident" is required and this event is a Safety System Functional Failure (SSFF).
D. CORRECTIVE ACTIONS
Immediate:
- 1. Operations de-activated the affected penetration by closing the 1-1001-298 and electrically isolating it by opening breaker MCC 18/19-5 Cubicle F 1.
Follow up:
- 1. Replaced the M&TE sensor and re-perform the MOV 1-1001-288 As-left diagnostic test satisfactorily.
(Complete)
- 2. Procedure and training enhancements to be reviewed for detecting issues with sensor installation or performance issues.
E. PREVIOUS OCCURENCES
The station events database, LERs and INPO Industry Reporting Information System (IRIS) were reviewed for similar events at Quad Cities Nuclear Power Station. This event was caused by M&TE equipment installation issues that resulted in test data that prompted operations to isolate the LPCI system. No previous occurrences were identified.
F. COMPONENT FAILURE DATA
YEAR 2022 -
SEQUENTIAL NUMBER 002 Valve 1-1001-298 failed to perform its design function when de-activated by operations.
Failed Equipment: Motor Operated Valve Actuator Component Manufacturer: Limitorque Component Model Number: SMB-4 Component Part Number: N/A This event will be reported to IRIS.
The M&TE sensor was improperly installed but not failed.
REV NO.
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