ML20212M042
| ML20212M042 | |
| Person / Time | |
|---|---|
| Site: | Callaway |
| Issue date: | 08/31/1986 |
| From: | Evans S UNION ELECTRIC CO. |
| To: | |
| Shared Package | |
| ML20212M003 | List: |
| References | |
| NUDOCS 8701290478 | |
| Download: ML20212M042 (5) | |
Text
.-
,A-DOCKET NO.
50-483 UNIT NAME CALLAWAY UNIT 1 DATE 9/9/86 (Revised 11/7/86)
'00MPLETED BY S. R. EVANS
. TELEPHONE 314/676-8742 PART A
-OPERATIONS SUP9tARY' 8/1/86 - Power reduction to 45% for EHC leak and intake repairs. Began 10%/hr. power reduction at 2300 Repairs completed and loading commenced for full power operation at 1525, 8/2/86 Attained 100% power at 1200, 8/3/86.
8/25/86 - Manual reactor / turbine trip af ter a turbine runback and subsequent rod control problems during a controlled shutdown to repair an RCS RTD loop bypass valve leak.
8/31/86 - Power reduction to 75% due to turbine runback on loss of "B" circulating water pump.
Runback initiated on circulating water pump trip at 1308. Repairs completed and loading' commenced for full power operation at 1348. Attained 100% power at 1645.
I-PARI B PORY AND SAFETY VALVE SU)flARY I
None i
I CA-#804 04/10/85 QDP-ZZ-04204 Page 1 of 4 D
R
4..
~
- t Part C AVERAGE DAILY UNIT POWER LEVEL i
DOCKET NO.
50-483'
-UNIT NAME CALLAWAY UNIT 1 DATE 9/9/86 (Rev. 11/7/86)
.l Li.
COMPLETED BY S. R. EVANS TELEPHONE 314/676-8742 MONTH:
AUGUST 1986.
e AVERAGE DAILY POWER LEVEL.'s AVERAGE DAILY PCE'ER LEVEL DAY (MWe-Net)
DAY (HWe-Net)
)
r l'
1096 17 1089 2
531 18 1090 3
1026 19 1092 4-1099 20 1096 5
1102 21 1094
)
6 1100 22 1091 t
7-1095 23 1093 i
8 1099 24 1088 i
9 1101 25 289 i
10 1074 26 0
11
'1083 27 32 12 1102-28 497 13 1089 29 1055 14 1064 30 1098 4
15 1080
' 31 1084 16
'1084 i
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.8
. \\
p*
P:rt D OPERATING DATA REPORT DOCKET NO.
50-483 UNIT NAME CALLAWAY UNIT 1 DATE 9/9/86 (Rev. 11/7/86)
COMPLETED BY S. R. EVANS TELEPHONE 314/676-8742 OPERATING STATUS (YTD CUM )
1.
REPORTING PERIOD: August 1986 GROSS HOURS IN REPORTING PERIOD:
744 (5831 14893.5) 2.
CURRENTLY AUTHORIZED POWER LEVEL (MWt):
3411 MAX. DEPEND. CAPACITY (MWe-Net):
1120 DESIGN ELECTRICAL RATING (MWe-Net):
1171*
- At stretch power level which is not currently authorized under the Operating License.
3.
POWER LEVEL TO WHICH RESTRICTED (IF ANY) (MWe-Net):
100%
4.
REASONS FOR RESTRICTION (IF ANY):
THIS MONTH YR 10 DATE CUMULATIVE 5.
NUMBER OF HOURS REACIOR WAS CRITICAL...............
697.7 4379.0 12842.5 6.
REACIOR RESERVE SHUTDOWN HOURS.....................
0 0
0 7.
HOURS GENERATOR ON LINE...........................
687.9 4198.3 12385.7 8.
UNIT RESERVE SHUTDOWN HOURS........................
0 0
0 9.
GROSS THERMAL ENERGY GENERATED (ML11)...............
2,236,572 13,200,714 39,218,267
- 10. GROSS ELECTRICAL ENERGY GENERATED (MWII)............
748,806 4,428,667 13,242,610
- 11. NET ELECTRICAL ENERGY GENERATED (MWH)..............
710,711 4,200,894 12,569,681
- 12. REACTOR SERVICE FACIOR.............................
93.8%
75.1%
86.2%
- 13. REACTOR AVAILABILITY FACTOR........................
93.8%
75.1%
86.2%
- 14. UNIT SERVICE FACTOR................................
92.5%
72.0%
83.2%
- 15. UNIT AVAILABILITY FACIOR...........................
92.5%
72.0%
83.2%
- 16. UNIT CAPACITY FACTOR (Using MDC)...................
85.3%
64.3%
75.4%
- 17. UNIT CAPACITY FACTOR (Using Design MWe)............
81.6%
61.5%
72.1%
l 18.
UNIT R)RCED OUTAGt; HATE............................
7.5%
5.6%
6.0%
19.
SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH): None 20.
IF SHUT DOWN AT END OF REPORTING PERIOD, ESTIMATED DATE OF STARTUP:
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r Part E UNIT SHUTDOWNS AND POLTR REDUCTIONS DOCKET NO.
50-483 UNIT NAME CALLAWAY UNIT 1 DATE 9/9/86 (Rev. 11/7/86)
COMPLETED BY S. R. EVANS TELEPHONE 314/676-8742 REPORT MONTE AUGUST 1986 METHOD OF TYPE SHUTTING DOLW F: IVRCED IURATION THE REACIOR OR DATE S: SCHEDULED (HOURS)
REASON REDUCING POWER CORRECTIVE ACTIONS / COMMENTS 17.
8/1/86 S
0 B
4 Power reduced to 45% for repair of EHC Ieak, kTP, and intake repairs.
18.
8/25/86 F
56.1 A
2 Manual reactor / turbine trip due to turbine runback and rod control failure. LER 86-029-00 19.
8/31/86 F
0 A
4 Reduction in power to 75% due to turbine runback on loss of circulating water pump "B."
SUMMARY
REASON METHOD A: EQUIPMENT FAILUPI (EXPLAIN) 1: MAhTAL B: MAINT. OR TEST 2: MANUAL SCRAM C: REFUELING 3: AUTOMATIC SCRAM D: REGULATORY RESTRICIION 4: OTHER (EXPLAIN)
E: OPERATOR TRAINING AND LICENSE EXAMINATION F: ADMINISTRATIVE G: OPEEATIONAL ERROR (EXPLAIN)
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