ML20212M025
| ML20212M025 | |
| Person / Time | |
|---|---|
| Site: | Callaway |
| Issue date: | 06/30/1986 |
| From: | Evans S UNION ELECTRIC CO. |
| To: | |
| Shared Package | |
| ML20212M003 | List: |
| References | |
| NUDOCS 8701290473 | |
| Download: ML20212M025 (5) | |
Text
i DOCKET NO.
50-483 UNIT NAME CALLAWAY UNIT 1 DATE 7/14/86 (Revised 8/5/86)(Revised 11/7/86)
COMPLETED BY S. R. EVANS TELEP110NE 314/676-8742 PART A OPERATIONS SUdfARY Plant operated at 100% power with the following exceptions:
- 1) 6/06/86 - Low pressure reactor trip.
- 2) 6/21/86 - Reactor trip on S/C lo-lo level.
Reduced power due to the following:
- 1) 6/13/86 - Scheduled power reduction for maintenance.
- 2) 6/17/86 - Forced power reduction due to trip of circulating water pump.
PART B PORY AND SAFETY VALVE
SUMMARY
None CA-#804 04/10/85 QDP-ZZ-04204 fogK05000483-3 861117 D
R Page 1 of 4 PDR
,9 Part C AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-483 UNIT NAME CALLAWAY UNIT 1 DATE 7/14/86 (Rev. 8/5/86)
(Rev. 11/7/86)
COMPLETED BY S. R. EVANS TELEPHONE 314/676-6742 MONTH:
JUNE 1986 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe-Net)
DAY (MWe-Net) 1 994 17 1030 2
1082 18 1071 3
1077 19 1071 4
1074 20 1073 5
1083 21 183 6
777 22 0
7 265 23 0
8 899 24 0
9 1065 25 80 10 1066 26 424 11 1072 27 1015 12 1074 28 1094 13 1030 29 1095 14 717 30 1093 15 893 31 16 1062 CA-8804 04/10/85 QDP-Z2-04204 Page 2 of 4
,v P rt D OPERATING DATA REPORT DOCKET NO.
50-483 UNIT NAME CALLAWAY UNIT 1 DATE 7/14/86 (Rev. 8/5/86)
(Rev. 11/7/86)
COMPLETED BY S. R. EVANS TELEPHONE 314/676-8742 OPERATING STATUS (Y1D CUM )
1.
REPORTING PERIOD: June 1986 GROSS !!OURS IN REPORTING PERIOD:
720 (4343 13405.5) 2.
CURRENTLY AUT!!ORIZED POWER LEVEL (MWt):
3411 MAX. DEPEND. CAPACITY (We-Net):
1120 DESIGN ELECTRICAL RATING (HWe-Net):
1171*
- At stretch power level which is not currently authorized under the Operating License.
3.
POWER LEVEL TO WIIICH RESTRICTED (IF ANY) (MWe-Net):
100%
4.
REASONS MR RESTRICTION (IF ANY):
THIF MONTH YR TO DATE CUMULATIVE 5.
NUMBER OF HOURS REACTOR WAS CRITICAL...............
624.8 2962.7 11426.2 6.
REACTOR RESERVE SHUTDOWN HOURS.....................
0 0
0 7.
HOURS GENERATOR ON LINE............................
608 2812.5 10999.9 8.
UNIT RESERVE SHUTDOWN 110URS........................
0 0
0 9.
GROSS THER* AL ENERGY GENERATED (&11)...............
1,891,846 8,684,936 34,702,488 10 CROSS ELECTRICAL ENERGY GENERATED (511)............
620,885 2,918,138 11,732,081
- 11. NET ELECTRICAL ENERGY CENERATED (MWil)..............
586,973 2,766,355 11,135,142
- 12. REACTOR SERVICE FACTOR.............................
86.8%
68.2%
E5.2%
- 13. REACTOR AVAILABILITY FACTOR........................
86.8%
68.2%
85.2%
- 14. UNIT SERVICE FACTOR................................
84.4%
64.8%
82.1%
1
- 15. UNIT AVAILABILITY FACTOR...........................
84.4%
64.8%
82.1%
- 16. UNIT CAPACITY FACTun (Using MDC)...................
72.8%
56.9%
74.2%
- 17. UNIT CAPACITY FACTOR (Using Design MWe)............
69.6%
$4.4%
70.9%
1 18. UNIT FURCED OUTAGE RATE............................
15.6%
4.9%
5.8%
i 19 SHUTDOWHS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH): None i
20.
IF SHUT DOWN AT END OF REPORTING PERIOD, ESTIMAIID DATE OF STARTUP:
CA-8804 04/10/85 QDP ZZ 04204 Page 3 of 4
i Part E UNIT SHUIDOWNS AND POLTR REDUCTIONS DOCKET NO.
50-483 UNIT NAME CALIJLWAY UNIT 1 f
IlhM&)
l CXPfPLETED BY S. R. EVANS I
TELEPHONE 314/676-8742 i
REPORT MONTH: JUhT 1986 l
METHOD OF TYPE SHUITING DOLN F: FDRCED DURATION THE REACTOR OR NO.
DATE S: SCHEDULED (HOURS)
REASON REDUCING POWER CORRECTIVE ACTIONS / COMMENTS l
11.
6/6/86 F
7.5 G
3 Iow pressure reactor trip. LER 86-019-00 12.
6/13/86 S
O E
4 Reduced reactor power to 70% for maintenance on main feedwater pump, circulating water pump and feedwater heater string.
13.
6/17/86 F
0 A
1 Reduced reactor to 75% power due to trip of circulating water pump caused by phase unbalance relay, i
14.
6/21/86 F
104.5 A
3 Reactor trip on S/G lo-lo level due to circuit card failure. LER 86-022-00
SUMMARY
REASON METHOD i
l A: EQUIPMENT FAILURE (EXPLAIN) 1: MAhTAL B: MAINT. OR TEST 2: MANUAL SCRAM C: RETUELING 3: AUTOMATIC SCRAM D: REGUULIORY RESTRICTION 4: OTHER (EXPLAIN)
E: OPERATOR TRAINING AND LICENSE EXAMINATION F: ADMINISTRATIVE G: OPERATIONAL ERROR (EXPIAIN)
CA-#804 H: OTHIR (EXPLAIN) 04/10/85 QDP-ZZ-04204 Page 4 of 4
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