ML20209H777

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SALP Rept 50-382/87-03 for Jan 1986 - Jan 1987
ML20209H777
Person / Time
Site: Waterford Entergy icon.png
Issue date: 04/30/1987
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20209H774 List:
References
50-382-87-03, 50-382-87-3, NUDOCS 8705040120
Download: ML20209H777 (37)


See also: IR 05000382/1987003

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APPENDIX

>SALP BOARD REPORT:

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION IV..

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SYSTEMATIC ASSESSMENT.OF LICENSEE-PERFORMANCE

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50-382/87-03

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Louisiana Power & Light Company

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- Wate'rford Steam Electric ' Station

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January 1,1986, through January 31, 1987

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I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated Nuclear Regulatory Commission (NRC) staff effort to collect

available observations and data on a periodic basis and to evaluate

licensee performance based upon this information. SALP is supplemental to

normal regulatory processes used to ensure compliance to NRC rules and

regulations. SALP is intended to be sufficiently diagnostic to provide a

rational basis for allocating NRC resources and to provide meaningful

guidance to the licensee's management to promote equality and safety of

plant operation.

An NRC'SALP Board, composed of the staff members listed below, met on

March 27, 1987, to review the collection of performance observations and

data, and to assess the licensee performance in accordance with the

guidance in NRC Manual Chapter 0516, " Systematic Assessment of Licensee

Performance." A summary of the guidance and evaluation criteria is

provided in Section II of this report.

This report is the SALP Board's assessment of the licensee's safety

performance at Waterford 3 Steam Electric Station (W3 SES) for the period

January 1,1986, through January 31, 1987.

SALP Board for W3 SES included:

E. H. Johnson, Director, Division of Reactor Safety and Projects, Region IV

R. L. Bangart, Director, Division of Radiation Safety and Safeguards,

Region IV

G. W. Knighton, Director, PWR Project Directorate No. 7, Nuclear Reactor

Regulation

J. E. Gagliardo, Chief, Reactor Projects Branch, Region IV

G. L. Constable,- Chief, Project Section C, Reactor. Projects Branch,

Region IV

J. H. Wilson, Project flanager, Nuclear Reactor Regulation

J. G. Luehman, Senior Resident Inspector, W3 SES

The following personnel also participated in the SALP. Board meeting:

W. C. Seidle, Chief, Technical Support Staff, Region IV

J. P. Jaudon, Chief, Reactor Project Section A, Reactor Projects

Branch, Region IV

B. Murray, Chief, Facilities Radiological Protection Section, Radiological

and Safeguards Programs Branch, Region IV

R. E. Ireland, Chief, Engineering Section, Reactor Safety Branch, Region IV

L. A. Yandell, Chief, Emergency Preparedness and Safeguards Programs Section,

Radiological and Safeguards Programs Branch, Region IV

R. P. Mullikin, Project Inspector, Region IV

M. E. Skow, Project Inspector, Region IV

T. R. Staker, Resident Inspector, W3 SES

II. CRITERIA

Licensee perfonnance was assessed in eleven selected functional areas.

Each functional area normally represents areas significant to nuclear

safety and the environment at operating plants.

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One or more of the following evaluation criteria were used to assess each

functional area:

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1.

Management involvement and cont'rol in assuring quality.~

2.

Approach to resolution of technic ~al issues from a safety. standpoint.

3.

Responsiveness to NRC initiatives.

4.

Enforcement history.

5.

Operational events (including response to, analysis of, and

corrective actions for).

6.

Staffing (includingmanagement).

However, the SALP Board was not limited to these criteria and others may

have been used where appropriate.

Based on the SALP Board Assessment, each functional area' evaluated is

classified into one of three performance categories. The definitions of

these performance categories are:

Category 1.

Reduced NRC attention may be appropriate. Licensee

management attention and involvement are aggressive and oriented toward

nuclear safety; licensee resources are ample and effectively used so that

a high level of performance with respect to operational safety is being

achieved.

Category 2.

NRC attention should be maintained at normal levels.

Licensee management attention and involvement are evident and are

concerned with nuclear safety; licensee resources are adequate and are

reasonably effective so that satisfactory performance with respect to

operational safety is being achieved.

Category 3.

Both NRC and licensee attention should be increased.

Licensee management attention or involvement is acceptable and considers

nuclear safety, but weaknesses are evident; licensee resources appear'to

be strained or not effectively used so that minimally satisfactory

performance with respect to operational safety is being achieved.

III. SUMMARY OF RESULTS

Significant improvement was achieved in the area of Plant Operations,

Surveillance, Fire Protection, Outages, Licensing Activities, and Training

and Qualification Effectiveness.

Improvement was also noted in the Maintenance

functional area.

Performance in the area of Security and Safeguards has

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declined, in part, due to the failure of plant personnel outside the

security organization to carry out their responsibilities to this program.

The licensee's performance is summarized in the table below, along with

the performance categories from the previous SALP evaluation period.

Previous

Present

Performance

Performance

Category

Category

(12/18/84 to

(1/1/86 to

Functional Area

(12/31/85)

(1/31/87)

A.

Plant Operations

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2

B.

Radiological Controls

2

2

C.

Maintenance

3

2

D.

Surveillance

2

1

E.

Fire Protection

2

1

F.

Emergency Preparedness

2

2

G.

Security and Safeguards

1

2

H.

Outages

Not Assessed

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I.

Quality Programs and

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2

Administrative Controls

Affecting Quality

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Licensing Activities

2

1

K.

Training and Qualification

2

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Effectiveness

The total NRC inspection effort during this SALP evaluation period

consisted of 35 inspections, including ~ resident inspector inspections and

emergency exercises, for a total of 4300 direct inspection hours. The

plant availability factor was 72.8 ' percent.

IV.

PERFORMANCE ANALYSIS

A.

Plant Operation

1.

Analysis

This area has been inspected on a continuing basis by the NRC

resident inspectors and on a periodic basis by region-based NRC

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inspectors. Licensee management involvement in the area of

plant operations was evident during this appraisal period. This

involvement was, to a large extent, responsible for the

substantial decrease in the number of both reactor trips and

licensee event reports (LERs).

The licensee management established a group responsible for the

review and reporting of potentially reportable events. This

group, which is headed by a ~ senior reactor operator (SR0), has

provided improved event analysis and higher quality LERs as

evidenced by the LER analysis performed by the 11RC Office of

Analysis and Evaluation of Operational Data (AE00). This

analysis was provided to LP&L under a cover letter dated

March 5, 1987.

There was a low turnover of personnel in the operations department

during this appraisal period.

The licensee instituted a

college degree program for licensed operators which should, in

part, encourage a continued low turnover. The increase in the

number of available licensed operators has produced a number of

benefits for the operations department.

First, it has allowed

the operations superintendent to allocate additional resources

to ongoing projects such as upgrading of operating procedures

and improving the labelling of plant equipment. Secondly, it

has made possible the transfer of a number of very experienced

licensed operators to the training department.

Upgrading of the control room and the control room panels

progressed, as conditions permitted, throughout the appraisal

period. The improvements made in the control room included

panel relabeling, painting, recarpeting, and the addition of

normal operating bands to many control room meters. Also, new

distinctive clothing, desinned based on operator suggestions,

was introduced for the on-watch licensed operators.

The licensee's program to reduce the number of illuminated

annunciators during power operations made progress during the

appraisal period; however, additional work remains to be done.

Efforts to reduce the overall number of temporary plant

alterations have also had some success, but many remain in place

with the majority awaiting completion of 'a particular plant

modification. Substantial progress was made in improving the

reliability of the engineered safety system features portion of

the control room ventilation system by replacing the chlorine

detection system. At the same time, however, during extended

shutdowns the containment purge isolation system has exhibited

operational problems. Spurious termination of containment purge

has caused diversion of the reactor operator's attention from

monitoring overall plant operations and caused high humidity in

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the containment. This made for uncomfortable working conditions

as well as condensation on equipment.

The licensee's efforts to reduce the high concentrations of

short-lived, airborne radioactivity in the reactor auxiliary

building have been fairly successful but maintaining

consistently low levels will require a continuation of the joint

effort between plant operations and health physics personnel.

Numerous-NRC inspections during the appraisal period have

identified deficiencies in system valve lineup procedures, the

referenced plant drawings, and the labelling of plant equipment.

As discussed previously, the operations superintendent has

assigned additional manpower to upgrading these areas, but these

efforts have concentrated largely on the correction of

previously identified discrepancies and not on the equally

important correction of discrepancies noted as the system

lineups are performed.

Based, in part, on observations made by the NRC resident

inspectors, the licensee has recognized that the administrative

burden on the shift technical advisors (STA) has at times

diverted them from their prime responsibility of providing the

shift supervisor with an independent engineering appraisal of.

operational situations.

Licensee management has taken a number

of steps to refocus the STA's efforts to providing the needed

technical reviews and recommendations. The steps taken included

trying to reduce STA involvement in the plant temporary

alteration request system and moving toward fully staffing all

of the approved STA positions. Overall, the STAS were well

integrated into the operating shift organization and continuing

the practice of having STAS obtain senior reactor operator

licenses should improve the operations department.

During the appraisal period, the licensee deviated from two

commitments made to the NRC in the area of plant operations.

These deviations resulted, in part, from a lack of direct

involvement of plant operations personnel in providing input to

commitments made to the NRC.

Furthermore, the lack of a

central point, responsible for ensuring the accuracy of

responses made to NRC Region IV and the NRC Office of Inspection

and Enforcement, contributed to the deviations. Without such

central coordination, there was apparently no assurance that all

the necessary departments fully understood their commitments

relative to the responses.

The licensee has made a number of changes in hardware to reduce

the number of reactor trips due to drcppcd ccr. trol element

assemblies (CEA). Additionally, core protection

calculator (CPC) software changes have been made to reduce the

impact of a dropped CEA on plant operations.

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2.

Conclusions

The NRC staff is encouraged by the large decrease in the number

of reactor trips and licensee event reports that occurred during

this appraisal period. The morale of the operations staff is

considered very high, and the confidence of the staff continues

to grow with operating experience.

Operator distractions in the control room such as various

illuminated annunciators, as well as the temporary alterations

existing throughout the plant, are avoidable potential problem

areas that operators must contend with on a daily basis.

The licensee is considered to be in Performance Category 2 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this area should be consistent

with the basic inspection program.

Emphasis should focus

on monitoring of licensee efforts to eliminating operator

distractions such as spurious annunciators, inadvertent

ventilation actuations, and existing temporary plant

al terations.

b.

Recommended Licensee Actions

Continued efforts to clear. illuminated annunicators, remove

temporary plant alterations, and eliminate spurious

ventilation actuations should be given priority.

Additionally, shift technical advisors should be removed

from duties involving largely_ administrative functions so

they can concentrate on the duties and responsibilities

outlined in Technical Specifications. Licensee management

should ensure preparation, tracking, and closure of

regulatory compliance issues are pursued with the same

systematic approach normally taken in the licensing area.

B.

Radiological Controls

1.

Analysis

Six inspections in the general functional area of radiological

controls were performed by regional radiation specialist

inspectors during the assessment period. The inspections

included the following specific areas: occupational radiation

safety, radioactive waste management, radiological effluent

control and monitoring, transportation of radioactive materials,

and water chemistry controls.

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a.

Occupational Radiation Safety

This area was inspected three times during the assessment

period. These inspections included two inspections during

routine operations and one refueling outage inspection.

Management involvement was evident by the performance of

comprehensive audits of radiation protection activities.

The licensee's program is considered adequate in the areas

of radiological training for the plant staff, stability of

the health physics staff at the technician level, and the

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development of radiation protection procedures. The

licensee demonstrated good planning and preparation for the

1986 refueling outage. The licensee's response to NRC

initiatives is considered above average.

Problems continue to exist concerning the release of

airborne and liquid radioactive contaminates from valves

and fittings in various plant systems. The licensee made

some progress to repair leaky valves and fittings during

the recent refueling outage. However, additional repair

work is needed in order to reduce the amount of leakage

that currently exists. This problem area was identified in

the previous SALP report.

The new Radiation Protection Manager (RPM) was hired during

the assessment period. The new RPM has previous

experience, with INP0, evaluating radiation protection

programs at several utilities.

A large turnover rate was experienced among the

professional health physics technical staff. Almost a

complete turnover occurred within the onsite and corporate

staff during 1985-86.

First-line, onsite supervisors are

burdened with excessive administrative duties which prevent

them from spending adequate time in the plant supervising

radiation protection activities.

Several problems were

identified concerning the failure to follow Radiation Work

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Permit instructions and the proper control of contaminated

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workers leaving the site which reflects the need for more

direct supervisory oversight of the radiation protection

program.

The person-rem exposure for 1986 was 270. This compares to

an estimated national average for PWR reactors of 'about

270 person-rem.

b.

Radioactive Waste Management

The licensee's program concerning the processing and onsite

storage of gaseous liquid and solid radioactive waste was

inspected once during the assessment period.

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The licensee had not established a permanent low-level

radioactive waste storage' facility. Low-level waste is

currently stored in various temporary areas throughout the

plant. A protected storage area had not been established

for radioactive waste containers.

Containers are presently

stored outside and exposed to environmental conditions.

c.

Radiological Effluent Control and Monitoring

The liquid and gaseous effluent control and monitoring

program was inspected once during the assessment period.

Effluent sampling and analyses activities were well defined

in plant procedures to ensure compliance with the

Radiological Effluent Technical Specifications. Gaseous

and liquid release permit programs were established to

ensure that planned releases receive the necessary review

and approval prior to~ release.

The radiochemistry / confirmatory measurements program was

inspected once during the assessment period. The

inspection included onsite confirmatory measurements with

NRC Region IV mobile laboratory. The results of the

confirmatory measurements values indicated 98 percent

agreement between the NRC's and licensee's measurements.

This percent agreement is above an expected industry

average of about 90 percent.

The radiochemistry / confirmatory measurements inspection

also included a review of the post accident sampling

system (PASS). Several major problems had been encountered

while attempting to obtain liquid and containment air PASS

samples.

In order to correct these problems, extensive

modifications to the PASS system were performed during the

1986 refueling outage.

The radiological environment monitoring program was

inspected once during the assessment period.

No problem

areas were identified. The licensee has established a well

documented program to ensure compliance with the offsite

dose calculation manual and Technical Specification

requi rements. All NRC identified matters have been

resolved.

d.

Transportation of Radioactive Materials-

This area was not inspected during the assessment period.

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The previous inspection was performed in October 1985, and

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the next inspection is scheduled for March 1987.

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Water Chemistry Controls

The primary and secondary systems affecting plant water

chemistry were inspected once. No problem areas were

identified.

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Conclusions

Leakage from liquid,and gaseous systems has resulted in

unnecessary personnel exposure and excessive contamination of

plant areas.

First-line health physics supervisors have not

spent adequate time in the plant overseeing ~ radiation protection

activities. The'large turnover rate among the professional

staff has reduced the- technical review of radiation protection

work.

No problems were identified in the areas of enforcement,

training, resolution of technical issues, or responsiveness to

NRC initiatives.

The licensee is considered to be in Performance Category 2 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should be

consistent with the basic inspection program. An

inspection of the new PASS should be conducted in early

1987.

b.

Reconmended Licensee Actions

Management attention is needed to:

(1)ensureappropriate

action is taken to reduce the radioactive leakage.from

liquid and gaseous systems to an acceptable level,

(2) ensure that first-line health physics supervisors spend

adequate time in the plant overseeing radiation protection

work activities, (3) ensure that stability is maintained-

~ with the health physics professional staff, and

(4) evaluate the benefits of establishing a permanent

low-level radioactive waste storage facility.

C.

Maintenance

1.

Analysis

This functional area was periodically inspected by region-based

NRC inspectors and on a continuing basis by the NRC resident

inspectors. During this appraisal period, the region-based

inspection efforts-included a maintenance program assessment

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which was performed by NRC and contractor personnel.

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A number of major maintenance efforts were accomplished during

the appraisal period. Many of these efforts, which included

main turbine. inspection / maintenance, replacement of reactor

coolant pump seals, and repairs of the . reactor coolant pump seal

water heat exchangers, were accomplished during the refueling

outage.

The licensee: continued efforts toward implementation of the

maintenance segment of the station information management

system (SIMS), a project that was begun late in the last

appraisal period.

In general, preventive maintenance

initiatives such as SIMS and routine corrective maintenance have

consistently been delayed in favor of priority corrective

maintenance.

Early in the appraisal period, the licensee continued to have

problems with the measuring and test equipment (M&TE) program.

The NRC resident inspectors identified a number of pieces of

M&TE in use or available for use in the plant well past their

calibration expiration dates. These problems were corrected

near the end of the appraisal period through implementation of

strict procedural controls and retraining of personnel.

In

general, routine corrective'and preventive maintenance was

performed satisfactorily. Work observations indicated that

maintenance personnel were well prepared and trained.

Maintenance activities did not directly contribute to any

reactor trips.

It is not uncommon for emergent containment maintenance to be

performed in areas where temperatures reach the 130-140 degrees

Fahrenheit range. During the plant's refueling outage, the

spurious terminations of containment purge, discussed in the

Plant Operations section of this report, compounded existing

temperature and humidity problems.

Events such as those

described in LER 382/86-15 illustrate the role environmental

factors can have both in operations and maintenance related

activities.

2.

Conclusions

Improvement was noted in the licensee's maintenance program.

Given the tempo of activity dictated by t.*o major outages,

efforts in the area of corrective maintena.'ce were considered

generally well coordinated and performed. However, a

significant backlog of corrective maintenance items of a routine

nature continued to exist.

The existence of some of these

outstanding items contributed to the large number of temporary

plant modifications discussed in the Plant Operations section of

this report.

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Programmatic planned maintenance' initiatives such as SIMS have

not been fully implemented due, in part, to the attention given

outage activities. Licensee management has been very responsive

to NRC inspection findings and concerns in this functional area.

Both, through telephone conversations and written correspondence,

the licensee has attempted to close out many issues, some of

which had been under review for long periods of time.

The licensee is considered to be in Performance Category 2 in

this functional area.

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Board Recommendations

a.

Recommended NRC Actions

The NRC inspection efforts in this functional area should

be consistent with the basic inspection program. These

efforts should, however, include followup of the licensee's

efforts to implement preventive maintenance initiatives.

b.

Recommended Licensee Actions

Licensee management should work toward reduction of the

outstanding routine maintenance backlog and implementation

of programs such as SIMS. Additionally, initiatives to

improve the~ containment working environment should be

considered.

D.

Surveillance

1.

Analysis

This functional urea was inspected on a continuing basis by the

NRC resident inspectors and periodically by region-based NRC

inspectors. Additionally, during the refueling outage, an

inspection was performed using the facilities of'the NRC

nondestructive examination mobile van.

The W3 SES surveillance program accomplished the required

testing in a timely manner in accordance with required

procedures. The activities performed by the licensee in the

area of inservice inspection were well prioritized, well

controlled, and executed using explicit procedures. Although

timely completion of nonroutine surveillances continue to be a

problem, the frequency of such problems has declined.

The Health Physics and Chemistry departments are responsible for

a large number of the very frequently performed nonroutine

surveillances which provide the most opportunities for missed

surveillances.

Licensee management has taken a number of

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positive-steps to minimize such problems including the

installation of an automatic hydrogen / oxygen sampling system for

various plant storage tanks.

However, there are other problems

such as the baron management / blowdown radiation monitors that

need attention. .These monitors have' proven to be unreliable,

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various nonroutine surveillances thereby setting up the

possibility of missing a required sample or failing to verify a

lineup.

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Conclusions

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Licensee management has taken positive actions to improve

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performance in the. functional' area of surveillance, and these

actions have helped reduce problems in the area. Problems with

nonroutine surveillance exist but have declined in number.

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The performance and tracking of surveillances has been good as

has the licensee's evaluation and resolution of problems

discovered during surveillance testing.

.The licensee is considered to be in Performance Category 1 in

this functional area.

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3.

Board Recommendations

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a.

Recommended NRC Actions

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The NRC should consider reduced inspection effort in this

functional area; however, a review of the licensee's

compliance with nonroutine surveillance requirements should

still be accomplished,

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b.

Recommended Licensee Actions

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The licensee should continue to pursue procedural as well'

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as equipment changes needed to eliminate nonroutine

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surveillance problems.

Evaluation ~of the long-term

reliability of the boron management / blowdown' system

radiation monitoring equipment, and the placement of the

new hydrogen / oxygen analyzing system into routine

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operational service are two actions that will assist in

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this effort.

E.

Fire Protection

1.

Analysis

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This functional area was inspected on a continuing basis by the

NRC resident inspectors, and one-inspection of the fire

protection / prevention program was performed by a region-based

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NRC inspector. These inspections verified that the licensee was

maintaining a fire protection / prevention program that met the

requirements of Branch Techntcal Position 9.5-1, the Plant Final

Safety Analysis Report, the Plant Fire Hazards Analysis, and

Technical Specifications.

In general, housekeeping and cleanliness controls were adequate

throughout the plant.

Fire brigade training and fire

detection / suppression surveillances were performed in accordance

with TS (except as described in LER 382/86-27). During the

refueling outage, the licensee installed the fire protection

hardware required by license conditions and made the

modifications resulting from the spurious signal analysis.

By the end of the appraisal period, the licensee was making a

concerted effort to reduce the number of fire impairments

existing throughout the plant and this, in turn, reduced the

need for compensatory fire watches.

2.

Conclusions

Licensee management demonstrated a definite commitment to having

an effective fire protection / prevention program. However, for

much of the appraisal period, the use of fire watches, in place

of barriers / detection equipment, was very routine. As noted in

the Quality Programs and Administrative Controls Affecting

Quality area of this report, the licensee created a single fire

protection / industrial safety group. Such a consolidated

organization will provide quicker resolution to problems in the

areas of fire protection / prevention by placing these areas and

the functionally related area of safety under a single

supervisor.

The licensee is considered to be in Performance Category 1 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC should consider a reduction of inspection effort in

this functional area.

b.

Recommended Licensee Actions

Licensee management should continue to stress the reduction

of the number of inoperable fire barriers and work toward

the elimination of routine fire watches in areas containing

safety-related equipment.

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F.

Emergency Preparedness

1.

Analysis

This area was inspected on a periodic basis by NRC region-based

inspectors and contract personnel. During the assessment

period, three emergency preparedness inspections were conducted.

Two violations and one deficiency were identified.

The two violations identified during this assessment period were

failure to follow document change procedure and failure to

provide adequate training to emergency response personnel. The

licensee took immediate corrective action in response to

personnel making hand written procedure changes.

The previous SALP assessment had identified that the licensee

had reduced the retraining program. During this assessment

period, it was determined that the licensee's training program

still was weak. A sampling of operations personnel indicated

some were unable to demonstrate adequate knowledge of the

protective action decision-making procedures. Health physics

technicians were unable to adequately demonstrate fundamental

radiation protection techniques in determining habitability of

emergency response facilities and performing offsite surveys to

characterize a radioactive plume released in an accident. The

licensee has not conducted a review of the training program to

be assured that it is adequate for emergency response personnel.

One deficiency identified during the emergency exercise

concerned communications and the Emergency Operations

Facility (E0F) organization.

During the exercise, the licensee

encountered problems in demonstrating comand and control of the

Emergency Operations Facility (E0F). The command and control

problem, in turn, precipitated onsite communication poblems with

the E0F support groups.

In response to the training violation,

the licensee committed to training seminars for the health

physics personnel and for other emergency response personnel on

an as-needed basis.

The licensee conducted a joint emergency response exercise with

the NRC, state, and local parish participation. The results of

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this exercise indicated that there was reasonable assurance that

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the licensee could adequately protect the health and safety of

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the public during an emergency. One unresolved item concerning

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the size of the Technical Support Center (TSC) and the resulting

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overcrowded conditions in the TSC was identified. This item

will be resolved during the NRC Emergency Response Facility

Appraisal.

During this assessment period, the licensee improved the station

emergency personnel callout system. The licensee had identified

areas for improving the callout system during several unannounced

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drills. The licensee has maintained sufficient depth in the

emergency response organization. Additionally, the licensee

exercised several different emergency response teams.

The licensee entered this assessment period with approximately

40 deficiencies. Thirty-eight deficiencies were closed during

the annual emergency preparedness exercise.

During this assessment period, the licensee improved the station

emergency personnel callout system. The licensee had

identified areas for improving the callout system during

several unannounced drills. The licensee has maintained

sufficient depth in the emergency response organization. During

this assessment period, the licensee exercised several different

emergency response teams.

2.

Conclusions

Training in emergency preparedness continues to be a weakness in

the W3 SES program. This has reduced program effectiveness

as evidenced during NRC walk-throughs and annual exercise.

The finding of the NRC inspections conducted during the

evaluation period indicate that overall the licensee's emergency

preparedness program is adequate to protect the public health

and safety.

The licensee is considered to be in Performance Category 2 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

i

The level of NRC inspection effort in this functional area

should be consistent with the basic inspection program.

b.

Recommended Licensee Actions

)

Upper level management's attention to the implementation of

the emergency preparedness program should be increased to

ensure proper response to NRC identified items.

The

licensee management should evaluate the emergency

preparedness initial training and retraining program as to

i

training frequencies, scope, and depth for all emergency

response personnel.

.

_

_

- - . -

.

.

.

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.

-16-

G.

Security and Safeguards

1.

Analysis

This area was inspected on a continuing basis by the NRC

resident inspector and periodically by NRC region-based

inspectors. Several violations that were identified resulted

from activities performed by personnel other than the security.

force, indicating the failure by management to make everyone

onsite aware of their security responsibilities. The licensee

has taken extensive corrective action to train everyone on the

security requirements at W3 SES.

It was noted that the

number and severity of violations decreased during the latter

part of this assessment period, indicating strong management

support of the security program.

Weaknesses were identified in the areas of physical barriers and

the closed circuit television system. Several passive barriers

have been corrected, and the closed circuit television is being

evaluated for upgrading.

2.

Conclusions

While there was an increase in the nuaSer of ser mity violations,

most of' the violations were discovered as a result of the

licensee's own initiative and an excellent record-keeping

capability. The violations encountered during these inspections

were promptly corrected. The licensee undertook and completed

an extensive training and briefing program for all employees

with access to the protected or vital areas. There was ample

evidence of the effectiveness of the program during an early

1987 inspection which encountered no violations.

The licensee

continues to be very responsive to NRC concerns and initiatives.

The licensee is considered to be in Performance Category 2 in

this functional area.

3.

Board Recommendations

I

a.

Recommended NRC Actions

i

The level of NRC inspection effort in this functional area

should be consistent with the basic inspection program.

b.

Recommended Licensee Actions

The licensee should continue to enhance the security

training of nonsecurity personnel in order to prevent

recurrence of the physical barrier violations.

Additionally, licensee management should ensure the

evaluation of the closed circuit television system is

completed and appropriate modifications are made.

.

4

.-.

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s

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+--

a

_

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i

,

H.

~ 0utages

' 1.

Analysis

-This functional area was inspected on a continuing basis by the

j

NRC resident inspectors during the mid-cycle outage of March 8

through March 30, 1986,~and the first plant refueling outage

starting November 26, 1986, and continuing through the end of

-

the SALP period. These inspections included verification that

outage management, repairs and modifications to equipment, and-

refueling activities were -performed in accordance with plant

procedures, regulatory requirements, and Technical

Specifications.

.

l~

During both the mid-cycle and refueling outages, planning and

~

scheduling 'of operations and maintenance activities were very

good. The licensee's use of containment coordinators, as well

as floor and assigned area radiation control technicians,

resulted in effective control and coordination of all work

performed in the containment during the refueling outage.

However, a violation (382/86-33) for failure to follow radiation

j

work permit requirements discussed the fact'that radiation

technician control of work in progress was'not always performed

l

in strict conformance'with established procedures. This problem

led the licensee to promptly pursue revision of established

procedures and to retrain personnel.

,

'

Prior to the refueling outage, a weakness in the organization

and supervision during receipt of new fuel was identified. The

weakness, in conjunction with poor layout of the fuel handling

<

building, led to damage to a new fuel element which was

discussedinviolation(382/86-29). At the beginning of the

i

fuel shuffle, a boraflex plate wa's'~1nadvertently pulled out of

the spent fuel storage rack by the_ spent: fuel handling machine

af ter it caught on the spent fuel : tool. The remainder of the

fuel shuffle was revised.in order to accommodate the above

. problem as well as the extensive search (in the core barrel and

.

lower structure' sections of'the reactor vessel) .for missing

j

steam generator tube plugs (LER 382/86-28). The revised

evolutions were completed without incident.

,

.

During both~ the mid-cycle and refueling ' outages, problems With

j

coordination maintenance and testing.were observed on the

individual component level. Certain pieces of equipment were

'

taken out of service more than once in order to accomplish'

,

j

assigned work.

For instance, a piece of equipment would first

be taken out for preventive maintenance, then again for

j

i

equipment qualification inspection, and finally for surveillance

i

testing.

In many cases, all the work could have been

accomplished during a single period of inoperability.

In efforts to minimize nonproductive time during the beginning

of unplanned / forced outages, the licensee has developed a

i

- _ _ .

.

-

.

..

-18-

detailed forced outage list that includes, not only the work to

be accomplished, but other information such as who to contact to

get the work started promptly.

2.

Conclusions

Licensee management involvement was effective and aggressive in

keeping informed, keeping control, and solving of problems as

they developed during the outages. This involvement, along with

good planning and scheduling, resulted in overall outage

management that is considered above average for a licensee

conducting an initial refueling outage. As noted, coordination

of work activities between disciplines could have been better

controlled on the individual component level.

The licensee is considered to be in Performance Category 1 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

Although a performance rating of one would suggest that

reduced NRC inspection might be appropriate, the NRC

inspection effort in this functional area should be

consistent with the basic inspection program as major

outages involve numerous, infrequently performed

activities.

b.

Recommended Licensee Actions

Licensee management should continue with aggressive

involvement in outages. Some improvement could be made in

scheduling of equipment testing / inspection so that multiple

equipment outages could be avoided.

Progress of the

revision of the radiation work permit procedures should be

closely monitored so that the revised program is in place

and functioning well before the next scheduled outage.

I.

Quality Programs and Administrative Controls Affecting Quality

,

1.

Analysis

Activities under this functional area were inspected by

region-based NRC inspectors and by the NRC resident inspectors.

During this appraisal period, the licensee's nuclear

organization underwent a number of changes.

First, a new senior

vice president was appointed, and then a major reorganization

was executed. As part of the reorganization, a vice

president (site director) position was created. The guality

control group was placed under the quality assurance (QA)

,

.

.

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l

manager, the Independent Safety' Evaluation Group (ISEG) was

'

elevated in the-corporate structure, and a consolidated fire

protection and safety group was established.

4

This functional area includes all verification and oversight

activities which effect or ensure quality of plant activities,

structures, systems, and components. The work of organizations

such as the Plant Operations Review Committee (PORC), the

Quality Assurance (QA) organization, the Safety Review

Committee (SRC), and the ISEG form the basis for much of the

l

evaluation. Specific activities which were evaluated included

procurement control, control of design changes, audits, inspections,

records, and corrective action systems. One area needing

improvement was noted in a number of NRC inspections.

In

'

certain plant procedures, informational cautions / notes were used

as procedural' action steps.

Considering procedures on a broader

basis, it was noted in review of violations and LERs that in a

number of functional areas two specific weaknesses existed.

First, LERs such as 382/86-15 and 382/86-24 demonstrated that

the understanding of the basis / intended use of procedures was

not always adequate on the part of the users. While an LER such

as 382/87-03 or a violation such as the failure to follow

procedures, described in NRC Inspection Report 50-382/86-02,

i

demonstrated individual failures to implement the established

l

procedures.

,

Licensee management has effectively implemented a program to

reduce the large backlog of outstanding station modifications,

however, continuing effort in this area is needed as evidenced

by the large number of temporary alterations still in place

l

dwaiting permanent changes.

Further, NRC inspections indicated

'

that although procedures, specifications, and drawings were in

place for station modification, the instructions in some

modification packages were poorly stated, and retrieval of

documents associated with a particular modification was

sometimes a problem.

Problems with reliability of the plant monitoring computer that

were evident during the last appraisal period have not been

fully remedied. The licensee has gotten an approved change to

l

the TS which reduces the operational impact of a core operating

limit supervisory system (COLSS) failure, but this change has

'

done nothing to' improve overall computer reliability.

In

addition to operating the COLSS, the plant computer supports a

portion of the licensee's plant / environmental assessment

capabilities, and regular losses of some or all of capabilities

supported by the plant monitoring computer have resulted.

During this appraisal period, an inspection was performed to

determine the status of the licensee's implementation of

10 CFR 50.49 requirements.

It was determined that the licensee

.

L

.

.-

.-

-20-

has established an equipment qualification (EQ) program that

meets the applicable regulatory requirements. Additionally,

staffing and training in the EQ area were adequate.

Some specific problems were identified in the licensee's EQ

program. These problems included: no records to demonstrate

qualification for equipment subject to submergence under design

'

basis accident conditions, improper temperature lag analysis,

and inadequate schedules for replacement of components

susceptible to aging effects at elevated service temperatures.

Licensee management was very responsive in addressing these

issues, and responses were both technically sound and thorough.

2.

Conclusions

Licensee management adequately implemented programs and controls

designed to ensure quality including the EQ program.

The

'

completion of a large number of station modifications during the

first refueling outage will place extra demands on the

licensee's system for modification closeout and drawing update.

Even though the licensee has made some improvements, plant

computer reliability continued to be a problem.

The licensee is considered to be in Performance Category 2 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

The level of NRC inspection effort in this functional area

i

should be consistent with the basic inspection program with

particular emphasis on the station modification program,

b.

Recommended Licensee Actions

Licensee management needs to resolve the lingering problems

associated with the plant computer system. Licensee

management has taken steps to minimize the impact of plant

computer outages but such outages continue to occur.

Additional reviews of plant procedures need to be done to

eliminate the practice of using informational notes as

procedural requirements.

Followup of the concerns

identified in the NRC EQ inspection should be monitored by

licensee management to ensure continued compliance in this

area. Careful monitoring of the station modification

program also needs to be a priority so that progress made

in reducing the number of outstanding station modifications

in the review cycle continues even with the added volume of

post refueling outage reviews.

.

- -

-

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-21-

l

J.

Licensing Activities

1.

Analysis

The licensing activities at W3 SES during the current SALP

appraisal period have been characterized by a high level of

dCtivity targeted toward preparation and conduct of the first

reload, closure of license conditions imposed by the operating

license, completion of commitments made prior to licensing, and

,

l

modifications to streamline and upgrade operations and increase

plant reliability.

A total of 54 licensing actions were completed during the rating

period, many of which were associated with the first reload.

In

addition to the 39 Technical Specification changes in support of

the reload-analysis, the licensee closed out 4 multi-plant

actions and carried out programs and commitments as required by

11 license conditions.

During_ the assessment period, the licensee's management has

demonstrated a high level of involvement and control in assuring

quality.

Prior planning and assignment of priorities were

consistently evident.

Regarding multi-plant actions, the

licensee's management actively participated in efforts to work

closely with the NRC staff and there were no backlogs over which

the licensee had control. With regard to plant-specific

t

activities, the licensee has consistently demonstrated a high

degree of planning and prioritization of actions to resolve

plant-specific issues. TF.i; was especially evident during the

staff review of Technical Specification amendment requests for

Cycle 2 reload to increase the cycle length to 18 months and the

implementation of actions to close out commitments and license

conditions for the Broad Range Toxic Gas Detection System, axial

l

fuel growth, smoke detection in the control room, spurious

l

signal analysis modifications, neutron flux indication, and

Increased enrichment evaluation of the spent fuel storage racks.

l

l

The licensee has well-stated and understandable policies

'

disseminated throughout their Nuclear Operations organization

through a system of Nuclear Operations Directives established

dnd controlled through the office of the Senior Vice

President-Nuclear. The licensee reorganized during the SALP

evaluation period to redefine organizational reporting-

responsibilities which places decisionmaking consistently at a

i

l

level to ensure adequate, thorough, and technically sound

management review.

In general, the new organization places

plant operations, design engineering and construction under a

site director (the Vice President-Nuclear Operations), expands

the role of training, consolidates similar functions, and places

l

increased emphasis ~on important functions, such as events

!

analysis, trending, industrial safety, and fire protection.

- -

-

.

.

.

.

-22-

The Senior Vice President - Nuclear maintains a site office for

his frequent visits and is involved in site activities. The

Vice President-Nuclear Operations, in his function as site

director, maintains his office on site on a full-time basis

and is involved on a day-to-day basis with plant and site

activities.

In order to enhance their involvement and increase

their control of licensing activities, LP&L management has

maintained an office in Bethesda. This licensing presence near

NRC, which includes both technical and administrative liaison,

has enabled LP&L management to be highly responsive to staff

concerns and has expedited the resolution of licensing issues.

The licensee has demonstrated sound and thorough approaches with

regard to almost all issues and has resolved the issues in a

timely and responsible manner. Where additional information was

needed by the staff to complete their reviews, the licensee

demonstrated a responsive and aggressive role in reaching timely

dnd thorough resolution, especially where there was a potential

for safety significance. This immediate approach to resolution

of the technical issues was particularly evident during the

period from August 1986 through January 1987, when the safety

analysis and 39 Technical Specification change requests were

processed to support an 18-month Cycle 2.

The continuation of a

licensing presence in Bethesda has enabled LP&L to focus quickly

and accurately on technical issues and to determine which

resources need to be brought to bear to reach timely resolution

based on sound communications.

There is, however, one area where LP&L could have been more

responsive in following guidance provided by the staff. During

review of the licensee's implementation of the SPDS, repeated

discussions at meetings and during telecons have not been

effective in directing LP&L's efforts to come up with a design

that meets the intent of NUREG-0737, Supplement 1.

In fairness

to the licensee, it should be noted that many of the staff's

criticisms of Safety Parameter Display System (SPDS) design have

arisen because LP&L's design of the system preceded issuance of

detailed guidance by the staff.

In view of the high level of

responsiveness on a very large number of issues exhibited by

LP&L during the rating period, failure to close out this single

difficult issue is not judged to be a significant performance

decrement.

The licensee has an apparently effective system for tracking and

responding to NRC requests and, in nearly all cases, meets

regulatory deadlines and commitments for timely resolution of

issues. The licensee infrequently requires extensions to meet

submittal dates, but is timely in alerting the staff in the rare

instances when an extension is needed. Through meetings with

the NRC staff, and through their Bethesda Licensing Office, the

licensee has maintained an effective line of communications.

_ _ _

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t

.

-23-

The licensee is always cooperative in meeting with the NRC staff

whenever the circumstances warrant. The licensee has been

responsive to first-of-kind programs, audits, and surveys. The

Operational Licensing Group, located at the plant site, was

instrumental in responding to NRC requests for plant performance

and operating data by bridging communications with operations,

engineering, and technical groups.

Corrective action is effective, as indicated by a lack of

repetition. The licensee has conducted licensing activities in

such a manner as to allow adequate time for staff review and

approval. No emergency Technical Specification changes were

necessary during the rating period. The trip reduction program

implemented by the licensee has been effective in reducing the

number of reactor trips from 22 in the previous rating period to

7 this rating period. Plant modifications to increase

reliability have been implemented and include:

modifications to

feedwater systems, rework of the turbine governors, replacement

of CEDM cards and power supply, and an extensive valve

replacement program to reduce RAB airborne activity.

2.

Conclusions

Management involvement and control in licensing activities is

effective in assuring quality. The licensee has consistently

demonstrated a high degree of planning and prioritization of

actions to resolve plant-specific issues, particularly during

the recent first refueling outage. The licensee has well stated

and understandable policies disseminated throughout its nuclear

operations and has an effective system for tracking commitments

and responding to NRC requests. The licensee's organization is

configured such that reporting responsibilities consistently

place decision making at a level to insure adequate, thorough

and technically sound management review. The licensee has

demonstrated sound and thorough approaches to almost all issues

and has resolved the issues in a tiraely and responsible manner.

The licensee is considered to be in Performance Category 1 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

NRC efforts should continue at the present level, or

possibly be reduced in recognition of the completion of the

first refueling outage.

Continued emphasis should be given

to assure that no declining performance trends develop in

any of the licensee's programs.

- -

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-24-

b.

Recommended Licensee Actions

The licensee should continue to maintain a high level of

management involvement to assure continued improvement in

this functional area. Continued emphasis should be placed

to assure that supporting analyses continue to be thorough,

complete, and accomplished in a timely manner. The

licensee should focus on the expeditious resolution of the

SPDS issues to achieve an acceptable design and operation.

K.

Training and Qualification Effectiveness

1.

Analysis

The licensee has made substantial progress in certain aspects of

the plant training programs. The skills training center was not

only used for a broader scope of normal training activities, but

it also provided the classrooms and equipment to perform much of

the specialized training needed to support the refueling outage.

The plant licensed operator training program had an overall

success rate of greater than 90 percent on three NRC

administered examinations performed during the appraisal period.

Finally, the licensee had all plant-training programs covered by

the Institute for Nuclear Power Operation (INP0) guidelines

i

ready for accreditation by the December 1986 target date.

An NRC inspection performed on selected aspects of the

licensee's training programs did identify a-number of

deficiencies in the area of training administration /

documentation; however, content and scope were adequate. The

delivery of the plant specific simulator did not take place as

scheduled, and the simulator was not on site at the end of the

appraisal period.

2.

Conclusions

The licensed operator training program is functioning very well;

however, ' administration / documentation of the 10 CFR Part 55

requalification program and other training programs could be

improved. As evidenced by comments in )ther portions of this

report, as well as in LERs and potentially reportable

events (PRES), training for a number of unlicensed plant staff

positions still needs strengthening. Though the licensee has

' devoted a large number of man-hours to the plant simulator

project, problems with the project contractor have again delayed

the delivery date.

The licensee is considered to be in Performance Category 1 in

this functional area.

.I

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.

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-25-

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC should consider a reduction of inspection effort in

this functional area.

b.

Recommended Licensee Actions

LP&L management attention should focus on delivery of the

plant specific simulator to the site and all efforts

necessary to make the unit fully operational. As discussed

above, additional emphasis _should be placed on training of

nonlicensed plant staff personnel.

Finally, licensee

management should direct the correction of the identified

deficiencies in training program administration / documentation

and ensure periodic reviews of these programs are performed

to identify any future problems.

l

V.

Supporting Data and Sumaries

A.

Licensee Activities

During this appraisal period, W3 SES was involved in two significant

outages. The first outage to occur was a mid-cycle maintenance

outage, and the second, which was reaching completion at the end of

the appraisal period, was the plant's first refueling outage.

During the refueling outage, numerous modifications were made to meet

!

license conditions. Additionally, during the outage, inspection of

l

the steam generator tubes was performed, plant snubbers were

l

inspected / tested, and extensive work was done on both the reactor

coolant pumps and main steam isolation valve hydraulic systems.

B.

Inspection Activities

1.

Violations

See Table I and II

2.

Major Inspections

i

Three major inspections were conducted during the assessment

period. These were a maintenance program review (November 1986,

50-382/86-28), the independent verification inspections of plant

modifications and inservice inspection using the NRC nondestructive

examination mobile van (December 1986,50-382/86-31), and the

equipment qualifications inspection (December 1986,50-382/86-32).

.

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-26-

C.

Investigations and Allegations Review

1.

One major investigation was completed during this assessment

period. This related to possible misrepresented facts in

October 1984 concerning managers (November 1986,50-382/86-30).

2.

Three allegations were reviewed and closed (January and

February 1986, 50-382/86-02 and 50-382/86-05).

D.

Escalated Enforcement Actions

1.

Civil Penalties

Actions (EA)ppraisal period, two Escalated Enforcement

During the a

were issued involving W3 SES. Ona of these EAs did

not impose a civil penalty. On April 16, 1986, EA 86-50

involving the inoperability of a containment spray pump was

issued. The licensee responded to EA 86-50 and the proposed

civil penalty of $50,000 in a letter dated May 16, 1986. The

letter imposing the civil penalty was subsequently issued on

August 27, 1986.

2.

Enforcement Orders

None.

E.

Licensee Conferences Held During Appraisal Period

A management meeting was held on January 8,1986, to discuss facility

and programs status and planning. An enforcement conference was held

on March 5, 1986, to discuss apparent violations concerning a mode

change and various security issues. A management meeting was held

April 1, 1986, to discuss SALP Report 50-382/85-30. A management

meeting was held on September 19, 1986, to discuss general plant

status. An enforcement conference was held November 18, 1986, to

discuss security matters relating to access control.

F.

Confirmation of Action Letters

None.

G.

Review of Licensee Event Reports and 10 CFR Part 21 Reports

Submitted by the Licensee

1.

Licensee Event Reports (LERs)

During this assessment period, a review was conducted for LERs

submitted during the period January 1,1986, through January 31,

1987. This review included LERs 382/86-01 through 382/87-04.

The technical content of LERs was greatly improved during this

assessment period. Table III contains a tabulation of LERs by

performance category.

.

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-27-

4

An additional evaluation of the content and quality of a

representative sample of the LERs submitted between January 1,

1986, and January 1,1987, was performed by the NRC Office of

Analysis and Evaluation of Operational Data (AE00). This

-

analysis was provided to LP&L under a cover letter dated

,

March 5, 1987. This, the second evaluation of the licensee

'

using AE0D's methodology, resulted in an overall score of 8.8

r

out of a possible 10 points which was a large improvement over a

previous average score of 7.3.

The current industry average is

,

8.2.

>

.

One weakness involving the requirements to uniquely identify

failed components was identified. Two strong points involved

i

the discussions concerning safety assessments and the failure

mode mechanism /effect of failed components.

'

2.

Part 21 Reports

None,

,

,

H.

Licensing Activities

[l

1.

NRR/ Licensee Meetings

2/18-19/86

Meeting to discuss basemat confirmatory analyses

/

,

3/26/86

Meeting to discuss results of basemat

/

'

confirmatory analyses

5/13/86

SPDS Design Review

~

~

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5/13/86

Reload Scoping Meeting

5/14/86

Basemat

6/3/86

Scheduling and Resource Management for Reload

.

,'

4

8/28/86

Review of updated basemat crack mapping effort

2.

NRR Site Visits

4/1/86

SALP Management Meeting

-

,

7/31/86

Inspection of previously unmapped basemat cracks

10/15/86

EP Exercise

1/14-15/87

Project Director Site Visit

3.

Commission Briefings

None

.

4.

Scheduler Extensions Granted

None

~

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,

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5.

Reliefs Granted

-

EDG inspection per manufacturer's recommendations delayed until

first refueling)and scheduled at 24-month intervals thereafter

(vice 18 months

1J

6.

Exemptions Granted

Appendix J exemption for postponement of LLRT until first

refueling outage

g

7.

License Amendments Issued

^

11

o

.,i

)

8.

Emergency Technical Specifications Issued

,

None

9.

Orders Issued

'

,

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,

<

None

10.

NRR/ Licensee Management Conferences

2/21/86

Additional basemat confirmatory analyses

refinements

3/27/86

Basemat confirmatory analyses

'

7/2/86

Basemat surveillance program and crack

,

mapping / reload

<

,

.

Analyses and supporting Technical Specification

changes

9/9/86

Reload - related submittals and analyses

10/21/86

Discussion of licensee's recent reorganization

'

and reload - related activities

,

' 12/9/86

Discussion of refueling outage progress-to-date

and schedule for startup testing and return

to power

~

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t

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t

1

4

5

,

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__

.

TABLE I

ENFORCEMENT ACTIVITY

  • No. of Violations in Each

Severity Level

4

Functional Area

III

IV

V

Deviation

A.

Plant Operations

1

2

2

-

.

B.

Radiological Controls

-

-

-

-

C.

Maintenance

-

3

-

-

D.

Surveillance

1

-

-

-

E.

Fire Protections

-

1

-

-

F.

Emergency Preparedness

-

1

1

-

G.

Security and Safeguards

1

12

1

-

H.

Outages

-

2

-

-

i

I,

Quality Programs and

6

1

-

-

Administrative Controls

Affecting Quality

J.

Licensing Activities

-

-

-

-

,

K.

Training and Qualification

-

-

-

-

Effectiveness

.

J

_

_

-

-

-

_

_

.

.

TABLE II

ENFORCEMENT ACTIVITY

TABULATION OF VIOLATIONS AND DEVIATIONS

BY

PERFORitANCE CATEGORY

A.

Plant Operations

Violations

Failure to meet the limiting condit'an for operation for a

.

containment spray pump.

(Severity Level III, 50-382/86-02)

Failure to use an adequate RWP and failure to use an approved

.

procedure.

(Severity Level IV, 50-382/86-02)

Failure to meet 10 CFR Part 50.72 and 50.73 reporting requirements.

.

(Severity Level IV, 50-382/86-15)

Deviations

Failure to fully implenent the actions specified in response to IE

.

Bulletin 86-01.

(50-382/86-13)

Failure to update an operating procedure within the time period

.

specified in LER-382/86-15.

(50-382/86-33)

B.

Radiological Controls

Violations

None

Deviations

None

C.

Maintenance

Violations

Failure to properly document essential chiller retest.

(Severity

,

Level IV, 50-382/86-02)

Failure to recall pastdue measuring and test equipment.

(Severity

.

Level IV, 50-382/86-15)

Failure to properly control temporary removal and replacement of

.

current limiting fuses.

(Severity Level IV, 50-382/86-28)

1

_

,

-

_ - - _ _ _ _ _ _ _ _ _ _ _

.

.

.

-2-

Deviations

None

D.

Surveillance

Violations

Failure to perform valve lineup (Severity Level IV, 50-382/86-29) quired

on fire protection valves as re

.

by Technical Specifications.

Deviations

-

None

E.

Fire Protection

Violations

Failure to p operly control flammable liquids.

(Severity Level IV,

.

50-362/86-16

Deviations

None

F.

Emergency Preparedness

Violations

Failure to provide adequate emergency response training.

(Severity

.

Level IV, 50-382/86-04)

Failure to follow procedures for updating documents.

(Severity

.

Level V, 50-382/86-27)

Deviations

None

G.

Security

Violations

Failure to demonstrate positive access control personnel.

(Severity

.

Level IV, 50-382/86-01)

Failure to maintain positive access control through posting of a

.

security officer.

(Severity Level IV, 50-382/86-01)

.

._

. ~ ~

._

. _ . .

_

..

.

.

__ ._

.

.

.

1

-3-

Failure to change locks, keys, and/or. combinations as required.-

.

(Severity Level IV, 50-382/86-01)

Failure to properly control access control-packages. - (Severity

.

Level IV, 50-382/86-01)

-

.

(Severity

50-382/86-01) pond to a vital area alarm.

Failure to properly res

.

Level IV,

Failure to positively control all points of personnel access into a

.

vital area.

(Severity Level IV, 50-382/86-01)

Failure to positively control allipoints of personnel access into a

'

.

vital- area ~.

(Severity Level IV, 50-382/86-01)

Failure to conduct an adequate audit ~of'ths security program.

.

(Severity Level'IV, 50-382/86-10) .

.

Failure to provide positive access control to' vital areas.

(Severity

.

.

Level III, 50-382/86-14 and 50-382/86-23)

!

Failure to report a major loss of physical security effectiveness.

.

(Severity Level IV, 50-382/86-14)

Failure to record tests as required.

(Severity Level V, 50-382/86-14)

.

f

Failure to follow procedures detailing duties and responsibilities of

.

security personnel.

(Severity Level IV, 50-382/86-16)

Failure to perform surveillance of the se'curity diesel generator at

.

,

the requested interval.

(Severity Level IV, 50-382/86-26)

!

i

j

Failure to follow procedures for escorting of visitors.

(Severity

.

Level IV, 50-382/86-29)

i

~

Deviations-

None-

H.

Outages

f

Violations

Failure to follow new fuel receipt procedures.

(Severity Level IV,

.

50-382/86-29)

Failure to follow radiation work permit procedures.

(Severity

1

.

Level IV, 50-382/86-33)

.

, . . - - .

,

, - . - ,

,

. . - . >

, , - ,

,,N',,..

r

,.w-

,

,

.

.

4

-4-

Deviations

None

I.

Quality Programs and Administrative Controls Affecting Quality

Violations

Failure to take prompt co.Tective action.

(Severity Level IV, 50-382/86-13)

.

Failure to update drawings following a station modification.

.

(Severity Level IV, 50-382/86-13)

Failure to adequately inspect installation of safety-related

.

components.

(Severity Level IV, 50-382/86-16)

Failure to follow procedures for station modification installation.

.

(Severity Level IV, 50-382/86-31)

Failure to control the use of nonconforming components.

(Severity

.

Level IV, 50-382/86-31)

Failure to follow procedures for evaluation of suppliers.

(Severity

.

Level IV, 50-382/87-01)

Failure to specify plant management succession as required by

.

Techaical Specifications.

(Severity Level V, 50-382/87-01)

Deviations

None

J.

Licensing Activities

Violations

None

Deviations

.

None

K.

Training and Qualifications Effectiveness

Violations

None

Deviations

None

__

_

_ _ _ _ _ _ _ _ _

_ - _ _ _ _ _ _

.

.

.

TABLE III

TABULATION OF LICENSEE EVENT REPORTS

BY

PERFORMANCE CATEGORY

A.

Plant Operations

Thirteen LERs involved activities in the ' functional area of plant

operations.

Reactor trip on dropped control element assembly.

(382/86-01)

.

Reactor trip due to dropped control element assembly Number

.

88 and failure of blowdown valves to close.

(382/86-02)

Reed switch failure results in reactor trip on low departure from

.

nucleate boiling ratio.

(382/86-09)

Simultaneously using two methods of draining reactor coolant system

.

results in lost of rhutdown cooling.

(382/86-15)

Insufficient procedural cequirements resulted in the boron concentration

.

for the safety injection tanks to fall below the Technical Specification

limit.

(382/86-16)

Reactor trip due to a. turbine trip caused by Hi-Hi level in moisture

.

separator reheater shell Drain Tank-2A.

(382/86-19)

Automatic actuations of engineered safety features portion of the

,

.

control room ventilation system including electrical spikes, spurious

alarms, and equipment failures.

(382/86-03,382/86-20,382/86-22,

and 382/86-29)

Reactor trip due to dropped control element assembly.

(382/86-23)

.

Inadvertent discharge of boric acid condensate tank due to procedure

.

noncompliance.

(382/86-24)

i

Reactor trip during startup due to prolonged low power operation.

.

(382/86-25)

B.

Radiological Controls

One LER involved activities in the functional area of radiological

controls.

Technician wore contaminated clothing offsite.

(382/87-03)

.

i

,

.

.

-

_

--

.

.

.

--

.

.

.

.

-2-

.

I

C.

Maintenance-

-

Three LERs involved activities in the functional area of maintenance.

Personnel error resulted in improper ~ tag-out causing the , low pressure

.

safety injection pump being inoperable due to the discharge valve

being closed.

(382/86-04)

Improper connection of contro1' element assembly cable resulted in

.

reactor trip.

(382/86-13)

"

Inadvertently opening of safety injection tank isolation valves due

.

to inadequate work instructions.

(382/86-14)

Inadvertent fuel handling ventilation system actuation due to personnel

.

error.

(382/86-26)

Containment isolation valve inoperable due to improper reassembly.

.

(382/87-01)

Small size snubber test failures due to improper installation.

.

,

l

(382/87-02)

D.

Surveillance

Five LERs involved activities in the functional area of surveillance.

Surveillance procedure resulted in suspect hot leg temperature

.

monitoring operability.

(382/86-05)

,

Mode change without performing surveillance on the boric acid makeup

.

tank.

(382/86-06)'

Operator error during surveillance testing resulted in inadvertent

.

activation of emergency feedwater system.

(382/86-08)

Improper filing of. scheduling card results in failure to perform

.

required secondary activity sample.

(382/86-10)

,

Failure to sample the proper gas decay tank. -(382/86-17)

.

Fire protection valve lineup not checked due:to inadequate procedure.

.

(382/86-27)

E.

Fire Protection

4

Five LERs involved activities in the functional area of Fire Protection-

Missed fire watch tour.

(382/86-07)

.

Missing internal penetration fire seals. ;(382/86-11)

.

Deficient fire door surveillance.

(382/86-12)

.

.

i

..

- - - . -

, - . - ,

-.

.y---

,

,,, ,

,,

,

-,

-

, - -

.

t

.

-3-

Fire watch tour not performed.

(382/86-21)

.

Fire barrier requirement not met.

(382/87-04)

.

F.

Emergency Preparedness

No LERs were issued in this functional area.

G.

Security and Safeguards

No LERs were issued in this functional area.

H.

0: stages

No LERs were issued in this functional area.

I.

Quality Programs and Administrative Controls Affecting Quality

The two LERs listed below involved activities in this functional area.

Hydrogen recombiner panel not securely mounted due to missing

.

structural weld.

(382/86-18)

Loose steam generator tube plugs due to inadequate installation.

.

(382/86-28)

J.

Licensing Activities

No LERs were issued in this functional area.

K.

Training and Qualifications Effectiveness

No LERs were issued in this functional area.