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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211N0161999-09-0202 September 1999 Safety Evaluation Supporting GL 95-07 to License NPF-42 ML20210T0071999-08-0909 August 1999 Safety Evaluation Supporting Amend 126 to License NPF-42 ML20209G2881999-07-0808 July 1999 Safety Evaluation Supporting Amend 125 to License NPF-42 ML20195D5261999-06-0202 June 1999 Safety Evaluation Approving Proposed ISI Program Alternative for Limited Reactor Vessel Shell Weld Exams & Relief Request from Requirements of ASME Code,Section XI ML20206D4571999-04-27027 April 1999 Safety Evaluation Supporting Amend 124 to License NPF-42 ML20205G1891999-03-31031 March 1999 Safety Evaluation Supporting Amend 123 to License NPF-42 ML20205B7781999-03-23023 March 1999 Safety Evaluation Supporting Amend 121 to License NPF-42 ML20205B7121999-03-23023 March 1999 Safety Evaluation Supporting Amend 122 to License NPF-42 ML20205B8251999-03-22022 March 1999 Safety Evaluation Supporting Amend 120 to License NPF-42 ML20195H9801998-11-17017 November 1998 Safety Evaluation Supporting Proposed Changes to WCGS Radiological Emergency Response Plan ML20236U8091998-07-21021 July 1998 Safety Evaluation Supporting Amend 119 to License NPF-42 ML20236S2151998-07-18018 July 1998 Safety Evaluation Supporting Amend 118 to License NPF-42 ML20248D3921998-05-28028 May 1998 Safety Evaluation Supporting Amend 117 to License NPF-42 ML20217K8051998-04-27027 April 1998 Safety Evaluation Supporting Amend 116 to License NPF-42 ML20216J7791998-04-15015 April 1998 SER Approving Requests for Relief I1R-46 Through I1R-49 & I2R-21 Submitted by Licensee on 970523.Relief for Exam Category B-A,Item B1.12,RPV Shell Welds Deferred Until Licensee Satisfies Regulations for Augmented Rv Exam ML20216C2641998-04-0606 April 1998 SER Accepting Addl Info Re GL 92-08, Thermo- Lag 330-1 Fire Barriers, for Plant ML20217H3491998-03-31031 March 1998 SER Accepting Operational Quality Assurance Program Description Change for Wolf Creek Generating Station ML20217J9971998-03-30030 March 1998 Safety Evaluation Supporting Amend 115 to License NPF-42 ML20217H7241998-03-30030 March 1998 SER Accepting Proposed Change to Operational Quality Assurance Program for Plant ML20202B9791997-11-26026 November 1997 Safety Evaluation Accepting Relief Requests 2VR-7 VR-8 from ASME Boiler & Pressure Vessel Code,Section XI Requirements for Inservice Testing Program ML20198Q2821997-10-24024 October 1997 Safety Evaluation Granting Relief for Second 10-yr Interval ISI Program Plan & Associated Requests for Plant ML20212F5501997-10-20020 October 1997 Safety Evaluation Supporting Amend 113 to License NPF-42 ML20217J7071997-10-0909 October 1997 Safety Evaluation Accepting Second 10-yr ISI Interval Relief Request I2R-22 ML20217G7101997-10-0707 October 1997 Safety Evaluation Supporting Amend 112 to License NPF-42 ML20217D9231997-09-29029 September 1997 Safety Evaluation Supporting Amend 111 to License NPF-42 ML20149F7911997-07-11011 July 1997 Safety Evaluation Supporting Amend 107 to License NPF-42 ML20141D0501997-06-23023 June 1997 Safety Evaluation Supporting Requests for Relief to Use ASME Code Case N-508-1 for Plant ML20147C1561997-01-31031 January 1997 Safety Evaluation Accepting Licensee Structural Integrity & Operability ML20117M7981996-09-0404 September 1996 Safety Evaluation Supporting Amend 102 to License NPF-42 ML20116M0131996-08-0909 August 1996 Safety Evaluation Supporting Amend 101 to License NPF-42 ML20100R5521996-03-0101 March 1996 Safety Evaluation Supporting Amend 97 to License NPF-42 ML20095E7081995-12-12012 December 1995 Safety Evaluation Supporting Amend 93 to License NPF-42 ML20087C3451995-08-0303 August 1995 Safety Evaluation Supporting Amend 88 to License NPF-42 ML20083Q6421995-05-17017 May 1995 Safety Evaluation Supporting Amend 86 to License NPF-42 ML20082F5221995-04-0303 April 1995 Safety Evaluation Supporting Amend 85 to License NPF-42 ML20077Q2801995-01-0909 January 1995 Safety Evaluation Supporting Amend 83 to License NPF-42 ML20077K4331994-12-29029 December 1994 Safety Evaluation Supporting Amend 81 to License NPF-42 ML20072G0961994-08-16016 August 1994 Safety Evaluation Supporting Amend 77 to License NPF-42 ML20072F4191994-08-12012 August 1994 Safety Evaluation Supporting Amend 76 to License NPF-42 ML20072C6651994-08-11011 August 1994 Safety Evaluation Supporting Amend 75 to License NPF-42 ML20062J5351993-10-29029 October 1993 Safety Evaluation Supporting Amend 68 to License NPF-42 ML20056G1781993-08-16016 August 1993 Safety Evaluation Supporting Amend 66 to License NPF-42 ML20056E3121993-08-0404 August 1993 Safety Evaluation Supporting Amend 65 to License NPF-42 ML20045G1181993-07-0707 July 1993 Safety Evaluation Supporting Amend 64 to License NPF-42 ML20035C8471993-04-0606 April 1993 Safety Evaluation Supporting Amend 62 to License NPF-42 ML20035C6211993-03-30030 March 1993 Safety Evaluation Supporting Amend 61 to License NPF-42 ML20044C1071993-03-12012 March 1993 Safety Evaluation Accepting Relief Request VR-24 Re Adoption of Asme/Asni OMA-1988,part 10 ML20034G4351993-02-26026 February 1993 Safety Evaluation Supporting Amend 58 to License NPF-42 ML20105C9661992-09-10010 September 1992 Safety Evaluation Supporting Amend 56 to License NPF-42 ML20091F3861991-11-19019 November 1991 Safety Evaluation Supporting Amend 53 to License NPF-42 1999-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000482/LER-1999-014, :on 991024,determined That Plant Entered Mode 4 Following Seventh RFO Without Satisfying TS Sr.Caused by Failure to Identify TS Requirements 3.5.2 & 3.5.3 with Respect to Plant Conditions.Procedures Revised1999-10-15015 October 1999
- on 991024,determined That Plant Entered Mode 4 Following Seventh RFO Without Satisfying TS Sr.Caused by Failure to Identify TS Requirements 3.5.2 & 3.5.3 with Respect to Plant Conditions.Procedures Revised
05000482/LER-1999-002, :on 990312,testing of Phase a (Cisa) Ctnt Isolation Valves Was Performed in Wrong Mode.Caused by Sp Not Being Properly Developed.Revised Applicable Procedures1999-10-15015 October 1999
- on 990312,testing of Phase a (Cisa) Ctnt Isolation Valves Was Performed in Wrong Mode.Caused by Sp Not Being Properly Developed.Revised Applicable Procedures
ML20217G1521999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Wolf Creek Generating Station.With 05000482/LER-1999-011, :on 990820,determined That TS Surveillance 4.5.2.h.1(b) Had Not Been Met for CCP Line Flow Rate.Caused by Inadequate Procedure.Licensee Will Revise Procedure STS BG-004 & Will Review Similar Sys Configurations1999-09-17017 September 1999
- on 990820,determined That TS Surveillance 4.5.2.h.1(b) Had Not Been Met for CCP Line Flow Rate.Caused by Inadequate Procedure.Licensee Will Revise Procedure STS BG-004 & Will Review Similar Sys Configurations
05000482/LER-1999-010, :on 990817,failure to Perform TS Surveillance 4.3.3.6 Was Noted.Caused by Inadequate Procedure Revision. Corrected Performance of Sp STS ML-001 & Revised Procedures STS ML-001 & STS CR-0011999-09-16016 September 1999
- on 990817,failure to Perform TS Surveillance 4.3.3.6 Was Noted.Caused by Inadequate Procedure Revision. Corrected Performance of Sp STS ML-001 & Revised Procedures STS ML-001 & STS CR-001
05000482/LER-1999-006, :on 990524,identified That Certian Processes of PASS & Hydrogen Analyzer Sys,Ts 3.6.1.1 Were Not Entered. Caused by Procedural Deficiencies.Procedures & Training Programs Revised1999-09-15015 September 1999
- on 990524,identified That Certian Processes of PASS & Hydrogen Analyzer Sys,Ts 3.6.1.1 Were Not Entered. Caused by Procedural Deficiencies.Procedures & Training Programs Revised
05000482/LER-1999-009, :on 990811,discovered That Inadequate Fire Separation Could Result in Loss of Charging Water Capability.Caused by Several Unvalidated Engineering Judgements Re Safe Shutdown Equipment.Revised Procedures1999-09-10010 September 1999
- on 990811,discovered That Inadequate Fire Separation Could Result in Loss of Charging Water Capability.Caused by Several Unvalidated Engineering Judgements Re Safe Shutdown Equipment.Revised Procedures
05000482/LER-1999-008, :on 990805,ESFA Due to Closure of D SG FW Regulating Valve Occurred.Caused by Failure of W 7300 Process Control Ncb Group 1 Controller Card.Replaced W 7300 Process Control Ncb Group 1 Controller Card1999-09-0303 September 1999
- on 990805,ESFA Due to Closure of D SG FW Regulating Valve Occurred.Caused by Failure of W 7300 Process Control Ncb Group 1 Controller Card.Replaced W 7300 Process Control Ncb Group 1 Controller Card
ML20211N0161999-09-0202 September 1999 Safety Evaluation Supporting GL 95-07 to License NPF-42 ML20212A0251999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Wolf Creek Generating Station.With ML20217P6451999-08-30030 August 1999 Requests Commission Approval to Publish Encl Pr,Rg & SRP & to Issue Encl Ltr to Parties of Wolf Creek Transfer Proceeding Re Disposition of Existing Antitrust License Conditions in Event OL Transfer Approved ML20210T0071999-08-0909 August 1999 Safety Evaluation Supporting Amend 126 to License NPF-42 ML20210R5741999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Wolf Creek Generating Station ML20210J1561999-07-29029 July 1999 Rev 0 to Wolf Creek Generating Station,Unit 1 Pressure & Temp Limts Rept ML20209G2881999-07-0808 July 1999 Safety Evaluation Supporting Amend 125 to License NPF-42 ML20209H0821999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20210R5921999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Wolf Creek Generating Station 05000482/LER-1999-006, :on 990524,procedures Allowed Loss of Containment Integrity Without Entering TS 3.6.1.1.Caused by Failure to Translate Containment Hydrogen Control Sys & Pass Sys Design Bases Into Plant Procedures.Revised Procedures1999-06-23023 June 1999
- on 990524,procedures Allowed Loss of Containment Integrity Without Entering TS 3.6.1.1.Caused by Failure to Translate Containment Hydrogen Control Sys & Pass Sys Design Bases Into Plant Procedures.Revised Procedures
ML20195D5261999-06-0202 June 1999 Safety Evaluation Approving Proposed ISI Program Alternative for Limited Reactor Vessel Shell Weld Exams & Relief Request from Requirements of ASME Code,Section XI ML20210R5871999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1021999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20196L3401999-04-30030 April 1999 Rev 1 to WCGS Cycle 11 Colr ML20206P8261999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Wcgs.With ML20210R5841999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Wolf Creek Generating Station ML20195K1071999-04-30030 April 1999 Revised MOR for Apr 1999 for Wolf Creek Generating Station ML20206D4571999-04-27027 April 1999 Safety Evaluation Supporting Amend 124 to License NPF-42 05000482/LER-1999-002, :on 990312,noted That Testing of Phase a (Cisa) CTMT Isolation Valves Were Performed in Wrong Mode. Caused by Improperly Developed Sps.Revised Applicable Procedures1999-04-10010 April 1999
- on 990312,noted That Testing of Phase a (Cisa) CTMT Isolation Valves Were Performed in Wrong Mode. Caused by Improperly Developed Sps.Revised Applicable Procedures
ML20205G1891999-03-31031 March 1999 Safety Evaluation Supporting Amend 123 to License NPF-42 ML20205Q0761999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Wolf Creek Generating Station.With ML20205B7121999-03-23023 March 1999 Safety Evaluation Supporting Amend 122 to License NPF-42 ML20205B7781999-03-23023 March 1999 Safety Evaluation Supporting Amend 121 to License NPF-42 ML20205B8251999-03-22022 March 1999 Safety Evaluation Supporting Amend 120 to License NPF-42 ML20207K5991999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Wolf Creek Generating Station.With ML20207K9761998-12-31031 December 1998 Annual SER 14,for Period 980101-1231, for WCGS ML20195B9901998-12-31031 December 1998 Western Resources Annual Rept for 1998 ML20195C0011998-12-31031 December 1998 Ks City Power & Light Co 1998 Annual Rept & Financial Statements as of 981231 & 1997 for Ks Electric Power Cooperative,Inc ML20199E6531998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Wolf Creek Generating Station.With ML20198D7321998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Wolf Creek Generating Station.With ML20195H9801998-11-17017 November 1998 Safety Evaluation Supporting Proposed Changes to WCGS Radiological Emergency Response Plan ML20195E7591998-11-10010 November 1998 WCNOC Proposed PASS Function Reduction 05000482/LER-1998-004, :on 981008,identified That Vol Control Tank Isolation Valve Does Not Have Redundant Fusing.Caused by Inadequate Administrative Controls.Programs & Processes Described in Listed Procedures Have Been Implemented1998-11-0606 November 1998
- on 981008,identified That Vol Control Tank Isolation Valve Does Not Have Redundant Fusing.Caused by Inadequate Administrative Controls.Programs & Processes Described in Listed Procedures Have Been Implemented
ML20195D1791998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Wolf Creek Generating Station.With ML20154L4591998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Wolf Creek Generating Station.With ML20153G2851998-09-30030 September 1998 Rev 1 to WCAP-15080, Evaluation of Pressurized Thermal Shock for Wolf Creek ML20153G2771998-09-30030 September 1998 Rev 1 to WCAP-15079, Wolf Creek Heatup & Cooldown Limit Curves for Normal Operation ML20153G2691998-09-30030 September 1998 Rev 1 to WCAP-15078, Analysis of Capsule V from Wolf Creek Nuclear Operating Corp Wolf Creek Reactor Vessel Radiation Surveillance Program ML20153G7301998-09-23023 September 1998 Special Rept 98-003:on 980814,station Entered TS 3.3.3.6, Action Statment a Due to Inoperability of RVLIS B Train. Cause Has Not Yet Been Identified.Work Order 98-202813-000 Has Been Generated ML20151W1491998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Wcgs.With ML20237B7381998-08-14014 August 1998 Special Rept 98-001:on 980615,oxygen Analyzer on Wgs Was Declared Inoperable.Wgs Oxygen Analyzer OARC-1119A Was Indicating 0 Ppm on 980814 & Fluctuated Between 200 & 900 Ppm on 980615.Completed Work Order & Declared Wgs Operable ML20237B0841998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Wolf Creek Generating Station 1999-09-30
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UNITED STATE 8
.j NUCLEAR REGULATORY COMMISSION s...../
WASHINGTON, D.C. enana annt SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REAOTOR REGULATION RELATED TO AMENDMENT NO.125 TO FACILITY OPERATING LICENSE NO. NPF-42 WOLF CREEK NUCLEAR OPERATING CORPORATION WOLF CREEK GENERATING STATION DOCKET NO. 50-482 1.0 INTRODUCTlQN
_ By lettar dated January 12,1999, as supplemented by letters dated May 11 and June 30,1999,
. Wolf Creek Nuclear Operating Corporation (the licensee) requested changes to the Technical Specifications (TSs), Appendix A to Facility Operating License No. NPF-42, for the Wolf Creek i
Generating Station (WCGS). The proposed changes would revise TS 3/4.7.5, Ultimate Heat i
Sink, by adding a new action statement to be used in the event that plant inlet water
- temperature exceeds 90*F. Specifically, the new action statement would allow, until September 30,1999, continued operation of the plant with plant inlet water temperature between 90 and 94*F for up to 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> before requiring shutdown of the plant. The licensee will pursue a pcmanent change to the inlet water temperature limit through the Westinghouse Owners Group as a proposed change to the Standard Technical Specifications.
The licensee's proposed amendment is the same proposal that the licensee submitted on July 17,1998, and the staff approved in Amendment 118 that was issued on July 18,1998.
The amendment was issued under emergency conditions, in accordance with 10 CFR
' 50.91(a)(5), because the cooling lue for WCGS exceeded 89*F and it was projected that the
- water temperature would exceed the TS limit of 90*F and the plant would have to unnecessarily shut down because of the then harsh meteorological conditions.
palen&nent 118 was effective until September 30,1998. In the letter of January 12,1999, the licens, s proposed a permanent change to TS 3/4.7.5; however, the staff concluded that the proposed change was ger.oric in nature and requested that the licensee propose a limited
. duration amendment similar to that approved in Amendment 118. The licensee's modified proposals are in the letters of May 11 and June 30,1999, both of which are of limited duration l
and would be effective only until September 30,1999.
The May 11 and June 30,1999, supplemental letters provided additional clarifying information,
~ did not expand the scope of the application as originally noticed and did not change the staff's or!ginal proposed no significant hazards consideration determination published in the Federal i
RePter on February 24,1999 (64 FR 9203), except that in the June 30,1999, letter the licensee proposed a maximum plant inlet water temperature of 95*F where the letters of January 12 and May 11,1999, proposed only 94*F.
(90719011599070s W
p ADOCK 05000482 PDR
i A
& The licensee's proposal that the statt is considering at this time is the plant inlet temperature limit of 94 F from the letters dated January 12 and May 11,1999, and the action statements but not the temperature limit from the letter dated June 30,1999. Thus, as limited, the letter of June 30,1999, does not expand the scope of the application as originally noticed and does not change the staff's original proposed no significant hazards consideration determination published in the Federal Register on February 24,1999 (64 FR 9203).
The current temperature of the cooling lake for WCGS is 85 F and rising. It is possible that the water temperature may exceed the TS limit of 90 F during the summer.
2.0 LICENSEE'S PROPOSAL The proposed new action statement to TS 3/4.7.5 being considered by the staff is the following:
NOTE: Until September 30,1999, the following actions supersede the above action (of
)
TS 3/4.7.5):
a.
With the pant inlet water temperature >90 F but <94 F:
- 1. Within one hour verify two trains of residual heat removal, two trains of component cooling water, and two trains of essential service water are
- operable,
- 2. Verify at least once per hour that the plant inlet temperature is <94 F, and
- 3. Within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> restore the plant inlet water temperature to 90'F or less.
- 4. With any of the above requirements not satisfied, be in at least hot standby
. within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />, i
b.
With the ultimate heat sink (UHS) inoperable for any reason other than the j
temperature, be in at least hot standby wi'hin the 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown i
within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
The new action statement only applies to the case of the plant inlet water temperature is above the TS limit of 90*F, requires more frequent checking of the temperature above 90 F and plant cooling systems, only allows operation above 90 F for the limited time period of 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, and does not change the time period in the current action statement to shut down.
3.0 E. VALUATION The ultimate heat sink (UHS) for WCGS is the normally submerged Seismic Category I cooling pond. The UHS is formed by providing a volume of cooling water behind a Seismic Category I dam built in one finger of the WCGS cooling lake. The two principal functions of the UHS are the dissipation of residua: heat after reactor shutdown, and dissipation of residJa! heat after an accident. The basic performance requirements for the UHS are that a 30-day supply of water be available, and that the design-basis temperatures of safety-related equipment not be i
R s-exceeded. The UHS design assures that the design temperature of safety-related equipment is not exceeded. The design temperature of water supplied to the plant is 95'F.
The UHS is the sink for heat removed from the reactor core following all accidents and anticipated operational occurrences in which the unit is cooled down and placed on residual heat removal (RHR) operation. Its maximum post-accident heat load occurs after a design
- basis loss-of-coolant-accident (LOCA) when the unit switches from injection to recirculation and the containment cooling system and RHR are required to remove the core decay heat.
Section 9.2.5 of the Updated Safety Analysis Report (USAR) provides the details of the assumptions used in the heat transfer analysis for the worst-case LOCA, which include worst expected meteorological conditions, conservative uncertainties when calculating decay heat,
)
and worst-case single failure. In addition, for the analysis, it was assumed that all of the water i
in the UHS was at 90*F at the start of the event.
l The analysis predicted 95'F as the highest plant inlet water temperature occurring during the maximum temperature period following the loss of the main dam with the average water temperature generally being below 94'F.
The licensee evaluated the effect of the proposed change on normal plant operation and normal plant 6,hutdown with the main dam intact, and safe shutdown or post-accident operation without the main dam.
Normal Plant Operation with the Main Dam Intact: Short term operation with an inlet water temperature of up to 95'F is not expected to negatively affect plant operation, with the possible exception of turbine backpressure. A slight load reduction may be necessary to maintain acceptable turbine backpressure. Existing plant guidance will be employed if any unexpected transients are experienced.
Shutdown with the Main Dam Intact: Increasing the inlet water temperature from 90'F to 95'F may cause the calculated single train time required to cool the unit below 200*F to exceed the cooldown time needed to comply with some TS. To compensate for this concern, the requested action statement requires verification of operability of two RHR trains when the inlet water temperature is greater than 90*F. This will ensure the cooling capacity is available to meet the shutdown time requirements.
LOCA with the Main Dam ininst: The effect of full power plant operation on plant inlet water temperature during worst case predicted summer environmental conditions is approximately 0.5'F. The peak heat rejection rate by the plant post-LOOA would be approximately 5 percent of the continuous heat rejection rate of the plant during normal operation. Thereforecthe effect of post-LOCA heat loads on plant inlet water temperature would be less than 0.1 *F. The current UHS analysis assumes that there has been a main dam failure and uses worst case environmental conditions. The results indicate that with an initial UHS temperature of 90P, plant intake water temperature will not exceed 95*F. The UHS analysis results also indicate i
that the environmental conditions have a much greater effect on peak plant intake water temperature than does the heat rejected from the plant. The current UHS analysis is recognized as bounding the LOCA condition without a main dam failure because the volume of the UHS is significantly smaller than the volume of the WCGS cooling lake, approximately 1
a i '
i i
percent. The probabilliy of environmental conditions significantly worse than those causing entry into the limiting condition for operation is low. The probability of these conditions occurring simultaneously with a LOCA is even lower.
Safe Shutdown or Post-Accident Operation without the Main Dam: The TS limit of 90*F is not
- being changed; however, the license amendment provides an allowance for operation above that limit for a 12-hour period. The Wolf Creek accident analyses assume a plant inlet water temperature of 95'F. Based on a review of recent WCGS cooling lake data,12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> may be necessary to restore the lake below 90*F through diurnal effects. Safe shutdown capability and post-accident operation without the main dam is ensured when the plant is operated within TS limits. The probability of main dam failure is low, comparable to the frequency of a large break l
LOCA initiating event. The probability of main dam failure during the 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> when the inlet
{
water temperature is above 90*F in conjunction with an accident is even lower. A seismic event is a possible initiating event for causing failure of the main dam. The frequency of the seismic initiator on an annual basis is nearly equal to that of a large break LOCA. It is also noted that WCGS has a dam monitoring program in place to ensure continued integrity of the main dam.
Therefore, it is concluded that this proposed change is of low risk significance.
Based on the above review and the license amendment No.118 dated July 18,1998, the staff concludes that with the dem intact, adequate heat removal will be available during normal plant operation, shutdown, and LOCA conditions to maintain equipment temperatures at or below their maximum design temperature of 95'F. Further, the staff concludes that the probability of a LOCA concurrent with a dam fahure is very low and, therefore, acceptable.
Based on the above, the staff finds the proposed change to the WCGS TS to add a new action statement to support continued plant operation in the event that plant inlet water temperature exceeds 90*F and remains less than 95'F acceptable. Therefore, limiting the plant inlet water temperature limit to 94'F is also acceptable. The licensee's proposal to raise the plant inlet water temperature at 95'F will be addressed in a later evaluation,
4.0 STATE CONSULTATION
in accordance with the Commission's regulations, the Kansas State official was notified of the proposed issuance of the amendment on July 8,1999. The State official had no objections to the amendment.
5.0 ENVIRONMENTAL OONSIDERATlQN The amendment changes a requirement with respect to installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20. The NRC staff has determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The 4
Commission has previously issued proposed findings that the amendment involves no significant hazards consideration, and there base been no public comment on such findings (64 FR 920?). Accordingly, the amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9). Pursuant to 10 CFR 51.22(b) no environmental i
E e
Irr)act statement or environmental assessment need be prepared in connection with the issuance of the amendment.
6.0 CONCLUSION
The Commission has concluded, based on the considerations discussed above, that: (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, (2) such activities will be conducted in compliance with the Commission's regulations, and (3) the issuance of the amondment will not be inimical to the common defense and security or to the health and safety of the public.
PrincipalContributor: K. Thomas Date:
July 8, 1999 l
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