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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211N0161999-09-0202 September 1999 Safety Evaluation Supporting GL 95-07 to License NPF-42 ML20210T0071999-08-0909 August 1999 Safety Evaluation Supporting Amend 126 to License NPF-42 ML20209G2881999-07-0808 July 1999 Safety Evaluation Supporting Amend 125 to License NPF-42 ML20195D5261999-06-0202 June 1999 Safety Evaluation Approving Proposed ISI Program Alternative for Limited Reactor Vessel Shell Weld Exams & Relief Request from Requirements of ASME Code,Section XI ML20206D4571999-04-27027 April 1999 Safety Evaluation Supporting Amend 124 to License NPF-42 ML20205G1891999-03-31031 March 1999 Safety Evaluation Supporting Amend 123 to License NPF-42 ML20205B7781999-03-23023 March 1999 Safety Evaluation Supporting Amend 121 to License NPF-42 ML20205B7121999-03-23023 March 1999 Safety Evaluation Supporting Amend 122 to License NPF-42 ML20205B8251999-03-22022 March 1999 Safety Evaluation Supporting Amend 120 to License NPF-42 ML20195H9801998-11-17017 November 1998 Safety Evaluation Supporting Proposed Changes to WCGS Radiological Emergency Response Plan ML20236U8091998-07-21021 July 1998 Safety Evaluation Supporting Amend 119 to License NPF-42 ML20236S2151998-07-18018 July 1998 Safety Evaluation Supporting Amend 118 to License NPF-42 ML20248D3921998-05-28028 May 1998 Safety Evaluation Supporting Amend 117 to License NPF-42 ML20217K8051998-04-27027 April 1998 Safety Evaluation Supporting Amend 116 to License NPF-42 ML20216J7791998-04-15015 April 1998 SER Approving Requests for Relief I1R-46 Through I1R-49 & I2R-21 Submitted by Licensee on 970523.Relief for Exam Category B-A,Item B1.12,RPV Shell Welds Deferred Until Licensee Satisfies Regulations for Augmented Rv Exam ML20216C2641998-04-0606 April 1998 SER Accepting Addl Info Re GL 92-08, Thermo- Lag 330-1 Fire Barriers, for Plant ML20217H3491998-03-31031 March 1998 SER Accepting Operational Quality Assurance Program Description Change for Wolf Creek Generating Station ML20217J9971998-03-30030 March 1998 Safety Evaluation Supporting Amend 115 to License NPF-42 ML20217H7241998-03-30030 March 1998 SER Accepting Proposed Change to Operational Quality Assurance Program for Plant ML20202B9791997-11-26026 November 1997 Safety Evaluation Accepting Relief Requests 2VR-7 VR-8 from ASME Boiler & Pressure Vessel Code,Section XI Requirements for Inservice Testing Program ML20198Q2821997-10-24024 October 1997 Safety Evaluation Granting Relief for Second 10-yr Interval ISI Program Plan & Associated Requests for Plant ML20212F5501997-10-20020 October 1997 Safety Evaluation Supporting Amend 113 to License NPF-42 ML20217J7071997-10-0909 October 1997 Safety Evaluation Accepting Second 10-yr ISI Interval Relief Request I2R-22 ML20217G7101997-10-0707 October 1997 Safety Evaluation Supporting Amend 112 to License NPF-42 ML20217D9231997-09-29029 September 1997 Safety Evaluation Supporting Amend 111 to License NPF-42 ML20149F7911997-07-11011 July 1997 Safety Evaluation Supporting Amend 107 to License NPF-42 ML20141D0501997-06-23023 June 1997 Safety Evaluation Supporting Requests for Relief to Use ASME Code Case N-508-1 for Plant ML20147C1561997-01-31031 January 1997 Safety Evaluation Accepting Licensee Structural Integrity & Operability ML20117M7981996-09-0404 September 1996 Safety Evaluation Supporting Amend 102 to License NPF-42 ML20116M0131996-08-0909 August 1996 Safety Evaluation Supporting Amend 101 to License NPF-42 ML20100R5521996-03-0101 March 1996 Safety Evaluation Supporting Amend 97 to License NPF-42 ML20095E7081995-12-12012 December 1995 Safety Evaluation Supporting Amend 93 to License NPF-42 ML20087C3451995-08-0303 August 1995 Safety Evaluation Supporting Amend 88 to License NPF-42 ML20083Q6421995-05-17017 May 1995 Safety Evaluation Supporting Amend 86 to License NPF-42 ML20082F5221995-04-0303 April 1995 Safety Evaluation Supporting Amend 85 to License NPF-42 ML20077Q2801995-01-0909 January 1995 Safety Evaluation Supporting Amend 83 to License NPF-42 ML20077K4331994-12-29029 December 1994 Safety Evaluation Supporting Amend 81 to License NPF-42 ML20072G0961994-08-16016 August 1994 Safety Evaluation Supporting Amend 77 to License NPF-42 ML20072F4191994-08-12012 August 1994 Safety Evaluation Supporting Amend 76 to License NPF-42 ML20072C6651994-08-11011 August 1994 Safety Evaluation Supporting Amend 75 to License NPF-42 ML20062J5351993-10-29029 October 1993 Safety Evaluation Supporting Amend 68 to License NPF-42 ML20056G1781993-08-16016 August 1993 Safety Evaluation Supporting Amend 66 to License NPF-42 ML20056E3121993-08-0404 August 1993 Safety Evaluation Supporting Amend 65 to License NPF-42 ML20045G1181993-07-0707 July 1993 Safety Evaluation Supporting Amend 64 to License NPF-42 ML20035C6211993-03-30030 March 1993 Safety Evaluation Supporting Amend 61 to License NPF-42 ML20044C1071993-03-12012 March 1993 Safety Evaluation Accepting Relief Request VR-24 Re Adoption of Asme/Asni OMA-1988,part 10 ML20034G4351993-02-26026 February 1993 Safety Evaluation Supporting Amend 58 to License NPF-42 ML20105C9661992-09-10010 September 1992 Safety Evaluation Supporting Amend 56 to License NPF-42 ML20091F3861991-11-19019 November 1991 Safety Evaluation Supporting Amend 53 to License NPF-42 ML20086D8161991-11-0707 November 1991 Safety Evaluation Supporting Amend 52 to License NPF-42 1999-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000482/LER-1999-014, :on 991024,determined That Plant Entered Mode 4 Following Seventh RFO Without Satisfying TS Sr.Caused by Failure to Identify TS Requirements 3.5.2 & 3.5.3 with Respect to Plant Conditions.Procedures Revised1999-10-15015 October 1999
- on 991024,determined That Plant Entered Mode 4 Following Seventh RFO Without Satisfying TS Sr.Caused by Failure to Identify TS Requirements 3.5.2 & 3.5.3 with Respect to Plant Conditions.Procedures Revised
05000482/LER-1999-002, :on 990312,testing of Phase a (Cisa) Ctnt Isolation Valves Was Performed in Wrong Mode.Caused by Sp Not Being Properly Developed.Revised Applicable Procedures1999-10-15015 October 1999
- on 990312,testing of Phase a (Cisa) Ctnt Isolation Valves Was Performed in Wrong Mode.Caused by Sp Not Being Properly Developed.Revised Applicable Procedures
ML20217G1521999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Wolf Creek Generating Station.With 05000482/LER-1999-011, :on 990820,determined That TS Surveillance 4.5.2.h.1(b) Had Not Been Met for CCP Line Flow Rate.Caused by Inadequate Procedure.Licensee Will Revise Procedure STS BG-004 & Will Review Similar Sys Configurations1999-09-17017 September 1999
- on 990820,determined That TS Surveillance 4.5.2.h.1(b) Had Not Been Met for CCP Line Flow Rate.Caused by Inadequate Procedure.Licensee Will Revise Procedure STS BG-004 & Will Review Similar Sys Configurations
05000482/LER-1999-010, :on 990817,failure to Perform TS Surveillance 4.3.3.6 Was Noted.Caused by Inadequate Procedure Revision. Corrected Performance of Sp STS ML-001 & Revised Procedures STS ML-001 & STS CR-0011999-09-16016 September 1999
- on 990817,failure to Perform TS Surveillance 4.3.3.6 Was Noted.Caused by Inadequate Procedure Revision. Corrected Performance of Sp STS ML-001 & Revised Procedures STS ML-001 & STS CR-001
05000482/LER-1999-006, :on 990524,identified That Certian Processes of PASS & Hydrogen Analyzer Sys,Ts 3.6.1.1 Were Not Entered. Caused by Procedural Deficiencies.Procedures & Training Programs Revised1999-09-15015 September 1999
- on 990524,identified That Certian Processes of PASS & Hydrogen Analyzer Sys,Ts 3.6.1.1 Were Not Entered. Caused by Procedural Deficiencies.Procedures & Training Programs Revised
05000482/LER-1999-009, :on 990811,discovered That Inadequate Fire Separation Could Result in Loss of Charging Water Capability.Caused by Several Unvalidated Engineering Judgements Re Safe Shutdown Equipment.Revised Procedures1999-09-10010 September 1999
- on 990811,discovered That Inadequate Fire Separation Could Result in Loss of Charging Water Capability.Caused by Several Unvalidated Engineering Judgements Re Safe Shutdown Equipment.Revised Procedures
05000482/LER-1999-008, :on 990805,ESFA Due to Closure of D SG FW Regulating Valve Occurred.Caused by Failure of W 7300 Process Control Ncb Group 1 Controller Card.Replaced W 7300 Process Control Ncb Group 1 Controller Card1999-09-0303 September 1999
- on 990805,ESFA Due to Closure of D SG FW Regulating Valve Occurred.Caused by Failure of W 7300 Process Control Ncb Group 1 Controller Card.Replaced W 7300 Process Control Ncb Group 1 Controller Card
ML20211N0161999-09-0202 September 1999 Safety Evaluation Supporting GL 95-07 to License NPF-42 ML20212A0251999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Wolf Creek Generating Station.With ML20217P6451999-08-30030 August 1999 Requests Commission Approval to Publish Encl Pr,Rg & SRP & to Issue Encl Ltr to Parties of Wolf Creek Transfer Proceeding Re Disposition of Existing Antitrust License Conditions in Event OL Transfer Approved ML20210T0071999-08-0909 August 1999 Safety Evaluation Supporting Amend 126 to License NPF-42 ML20210R5741999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Wolf Creek Generating Station ML20210J1561999-07-29029 July 1999 Rev 0 to Wolf Creek Generating Station,Unit 1 Pressure & Temp Limts Rept ML20209G2881999-07-0808 July 1999 Safety Evaluation Supporting Amend 125 to License NPF-42 ML20209H0821999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Wolf Creek Generating Station ML20210R5921999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Wolf Creek Generating Station 05000482/LER-1999-006, :on 990524,procedures Allowed Loss of Containment Integrity Without Entering TS 3.6.1.1.Caused by Failure to Translate Containment Hydrogen Control Sys & Pass Sys Design Bases Into Plant Procedures.Revised Procedures1999-06-23023 June 1999
- on 990524,procedures Allowed Loss of Containment Integrity Without Entering TS 3.6.1.1.Caused by Failure to Translate Containment Hydrogen Control Sys & Pass Sys Design Bases Into Plant Procedures.Revised Procedures
ML20195D5261999-06-0202 June 1999 Safety Evaluation Approving Proposed ISI Program Alternative for Limited Reactor Vessel Shell Weld Exams & Relief Request from Requirements of ASME Code,Section XI ML20210R5871999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20195K1021999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Wolf Creek Generating Station ML20196L3401999-04-30030 April 1999 Rev 1 to WCGS Cycle 11 Colr ML20206P8261999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Wcgs.With ML20210R5841999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Wolf Creek Generating Station ML20195K1071999-04-30030 April 1999 Revised MOR for Apr 1999 for Wolf Creek Generating Station ML20206D4571999-04-27027 April 1999 Safety Evaluation Supporting Amend 124 to License NPF-42 05000482/LER-1999-002, :on 990312,noted That Testing of Phase a (Cisa) CTMT Isolation Valves Were Performed in Wrong Mode. Caused by Improperly Developed Sps.Revised Applicable Procedures1999-04-10010 April 1999
- on 990312,noted That Testing of Phase a (Cisa) CTMT Isolation Valves Were Performed in Wrong Mode. Caused by Improperly Developed Sps.Revised Applicable Procedures
ML20205G1891999-03-31031 March 1999 Safety Evaluation Supporting Amend 123 to License NPF-42 ML20205Q0761999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Wolf Creek Generating Station.With ML20205B7121999-03-23023 March 1999 Safety Evaluation Supporting Amend 122 to License NPF-42 ML20205B7781999-03-23023 March 1999 Safety Evaluation Supporting Amend 121 to License NPF-42 ML20205B8251999-03-22022 March 1999 Safety Evaluation Supporting Amend 120 to License NPF-42 ML20207K5991999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Wolf Creek Generating Station.With ML20207K9761998-12-31031 December 1998 Annual SER 14,for Period 980101-1231, for WCGS ML20195B9901998-12-31031 December 1998 Western Resources Annual Rept for 1998 ML20195C0011998-12-31031 December 1998 Ks City Power & Light Co 1998 Annual Rept & Financial Statements as of 981231 & 1997 for Ks Electric Power Cooperative,Inc ML20199E6531998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Wolf Creek Generating Station.With ML20198D7321998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Wolf Creek Generating Station.With ML20195H9801998-11-17017 November 1998 Safety Evaluation Supporting Proposed Changes to WCGS Radiological Emergency Response Plan ML20195E7591998-11-10010 November 1998 WCNOC Proposed PASS Function Reduction 05000482/LER-1998-004, :on 981008,identified That Vol Control Tank Isolation Valve Does Not Have Redundant Fusing.Caused by Inadequate Administrative Controls.Programs & Processes Described in Listed Procedures Have Been Implemented1998-11-0606 November 1998
- on 981008,identified That Vol Control Tank Isolation Valve Does Not Have Redundant Fusing.Caused by Inadequate Administrative Controls.Programs & Processes Described in Listed Procedures Have Been Implemented
ML20195D1791998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Wolf Creek Generating Station.With ML20154L4591998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Wolf Creek Generating Station.With ML20153G2851998-09-30030 September 1998 Rev 1 to WCAP-15080, Evaluation of Pressurized Thermal Shock for Wolf Creek ML20153G2771998-09-30030 September 1998 Rev 1 to WCAP-15079, Wolf Creek Heatup & Cooldown Limit Curves for Normal Operation ML20153G2691998-09-30030 September 1998 Rev 1 to WCAP-15078, Analysis of Capsule V from Wolf Creek Nuclear Operating Corp Wolf Creek Reactor Vessel Radiation Surveillance Program ML20153G7301998-09-23023 September 1998 Special Rept 98-003:on 980814,station Entered TS 3.3.3.6, Action Statment a Due to Inoperability of RVLIS B Train. Cause Has Not Yet Been Identified.Work Order 98-202813-000 Has Been Generated ML20151W1491998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Wcgs.With ML20237B7381998-08-14014 August 1998 Special Rept 98-001:on 980615,oxygen Analyzer on Wgs Was Declared Inoperable.Wgs Oxygen Analyzer OARC-1119A Was Indicating 0 Ppm on 980814 & Fluctuated Between 200 & 900 Ppm on 980615.Completed Work Order & Declared Wgs Operable ML20237B0841998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Wolf Creek Generating Station 1999-09-30
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UNITED STATES p
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NUCLEAR REGULATORY COMMISSION t
WASHINGTON, D.C. 30ees 4cM 59.....
SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO. 124 TO FACILITY OPERATING LICENSE NO. NPF-42 WOLF CREEK NUCLEAR OPERATING CORPORATION WOLF CREEK GENERATING STAT.lQN DOCKET NO. 50-482
1.0 INTRODUCTION
By letter dated October 23,1998, Wolf Creek Nuclear Operating Corporation (WCNOC, the licensee) requested changes to the Technical Specifications (TS) (Appendix A to Facility Operating License No. NPF-42) for the Wolf Creek Generating Station (WCGS). The proposed changes would revise TS 3/4.5.1, " Emergency Core Cooling Systems - Accumulators," and the applicable Bases. Specifically, the allowed outage time (AOT) or completion time for ACTION b (to restore an inoperable accumulator, if inoperable for reason other than the boron concentration outside of the requirements), would be changed to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> instead of the current time of one hour. This proposal is based on the methodology described in Topical Report WCAP-15049, " Risk-informed Evaluation of an Extension to Accumulator Completion Times," dated August 1998.
The staff has reviewed WCAP-15049 and concluded that the deterministic and probabilistic safety analysis (PSA) results and insights of WCAP-15049 supported the proposed accumulator AOT extension for all Westinghouse plants. Specifically, the staff concluded that because (1) there is no change to the LCO and consequently no cnange to the Chapter 15 Safety Analysis, and (2) this is an extension of an existing condition, the deterministic aspect of this change is acceptable in addition, the staff found that Westinghouse performed a comprehensive risk analysis to support the proposed AOT extension, which indicated that the impact on risk would be small, as defined in risk-informed Regulatory Guides (RG) 1.174, "An Approach for Using Procabilistic Risk Assessment in Risk-Informed Decisions on Plant-Specific j
Changes to the Licensing Basis," dated July 1998, and RG 1.177, "An Approach for Plant-l Specific, Risk-Informed Decision Making: Technical Specifications," dated August 1998. The j
staff's approval of WCAP-15049 is contained in a letter dated February 19,1999, to the l
Westinghouse Owners Group.
2.0 EVALUATION 2.1 Deterministic Evaluation The purpose of the emergency core cooling system (ECCS) accumulators is to supply water to the reactor vessel during the blowdown phase of a loss-of-coolant accident (LOCA). The j
accumulators are large volume tanks, filled with borated water and pressurized with nitrogen.
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,O' The cover-pressure is less than that of the reactor coolant system (RCS) so that following an accident, when the RCS pressure decreases below tank pressure, the accumulators inject the borated water into the RCS cold legs.
Currently, the TS allows for one of the four accumulators to be inoperable for one hour (for reasons other than boron concentration not within limits) during MODES 1,2, and in MODE 3 with pressurizer pressure greater than 1000 psig. With one accumulator inoperable, the remaining three accumulators will remain available to mitigate the consequences of a LOCA event. The licensee is requesting to increase the AOT for one accumulator from one hour to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Since the duration of an allowed TS AOT is not an input into the safety analysis (i.e., the
)
safety analysis assumes the accumulators are operable), the extension of the AOT to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> has no impact on the safety analysis. Deterministically, there is no difference between a one hour and a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> AOT. Based on the above, the current safety analysis remains valid, and therefore, the change is acceptable.
The difference in the current TS versus the proposed extension is the added risk due to the extension of the AOT.which is reviewed in the following section of this evaluation.
2.2 Risk Evaluation The staff review of WCAP-15049 concluded that the risk analysis performed in support of the change for "all Westinghouse plants" was comprehensive and reasonable, and that the proposed change would result in a small risk increase, as defined in risk-informed RGs 1.174 and 1.177. The risk impact includes core damage frequency and large early release frequency, and it meets the intent of the guidance in the RGs.
The licensee provided an evaluation that demonstrated the applicability of the topical report to WCGS by way of examining key comparable parameters and assumptions used in both the WCGS probabilistic safety analysis (PSA) model and the WCAP evaluation. The staff finds that the WCAP evaluation envelops, or is comparable with, the WCGS case.
Based on the above, the staff concludes that the risk insights and findings support the
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deterministic evaluation of the accumulator AOT extension. Therefore, the changes are acceptable.
In addition, the staff reviewed the proposed change to TS Bases 3/4.5.1, " Emergency Core Cooling Systems - Bases - Accumulators," and found it to be consistent with the proposed TS I
change.
3.0 STATE CONSULTATION
in accordance with the Commission's regulations, the Kansas State official was notified of the proposed issuance of the amendment. The State official had no comments.
.' 4.0. ENVIRONMENTAL CONSIDERATION This amendment changes a requirement with respect to installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20. The staff has determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluent that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that the amendment involves no significant hazards consideration, and there has been no public comment on such finding (63 FR 64127). Accordingly, the amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9). Pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendmeht.
5.0 CONCLUSION
The staff has concluded, based on the considerations discussed above, that: (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner; (2) such activities will be conducted in compliance with the Commission's regulations; and (3) the issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public.
Principal Contributors:
S. Brewer I.Jung K. Thomas Date: April 27,1999 S
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