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MONTHYEARML20237G2591987-08-0707 August 1987 Proposed Tech Specs,Removing All Safety Features Actuation Sys Response Times & Containment Isolation Time Requirements from Valves on Secondary Side of Steam Generators Project stage: Other ML20237F8171987-08-0707 August 1987 Application for Amend to License NPF-3,removing All Safety Features Actuation Sys Response Times & Containment Isolation Time Requirements in Tech Specs 3/4.3.2 & 3/4.6.3 Project stage: Request ML20237F8041987-08-0707 August 1987 Forwards Application for Amend to License NPF-3,removing Safety Features Actuation Sys Response Times & Containment Isolation Time Requirements from Valves on Secondary Side of Steam Generators.Fee Paid Project stage: Request ML20237A6881987-12-0808 December 1987 Informs of Changes Necessary to Support Fifth Refueling Outage in Feb 1988.Key Amend Requests Placed Into 1 of 3 Listed Categories.Nrc Should Allocate Necessary Resources to Provide Timely Support for Review & Issuance of Amends Project stage: Other ML20148J7291988-03-21021 March 1988 Responds to NRC 880303 Request for Addl Info Re 870807 Application to Amend Tech Specs 3/4.3.2 & 3/4.6.3.Amend Re Proposed Removing Closure Time Requirements for Ten Valves Connected to Secondary Side of Steam Generators Project stage: Request ML20148J7151988-03-24024 March 1988 Forwards Request for Addl Info Re Proposed Tech Spec Change to Delete Safety Features Actuation Signal to Certain Valves Project stage: RAI ML20154A8061988-05-0202 May 1988 Provides Supplemental Info Re Application for Amend Re Removing Closure Time Requirements for Valves Connected to Secondary Side of Steam Generators Listed in Tech Spec Tables 3.3-5 & 3.6-2 Project stage: Supplement ML20207E3931988-08-0202 August 1988 Safety Evaluation Supporting Amend 114 to License NPF-3 Project stage: Approval ML20207E3861988-08-0202 August 1988 Amend 114 to License NPF-3,changing Tech Specs to Delete Safety Features Actuation Sys Signals to Certain Valves on Secondary Side of Steam Generators & Delete Closure Time Requirements for Certain Valves Project stage: Other 1988-03-21
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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 ML20249A7661998-06-11011 June 1998 Safety Evaluation Supporting Amend 222 to License NPF-3 ML20249A7551998-06-11011 June 1998 Safety Evaluation Supporting Amend 223 to License NPF-3 ML20216B9401998-04-15015 April 1998 Safety Evaluation Supporting Amend 221 to License NPF-3 ML20216B8381998-04-14014 April 1998 Safety Evaluation Supporting Amend 220 to License NPF-3 ML20202C6131998-02-0303 February 1998 Safety Evaluation Supporting Amend 219 to License NPF-3 ML20199J9511998-01-30030 January 1998 SER Related to Exemption from Section Iii.O of App R,To 10CFR50,for Davis-Besse Nuclear Power Station,Unit 1 ML20198R4771998-01-13013 January 1998 SER Approving Second 10-year Interval Inservice Inspection Program Plan Requests for Relief for Davis-Besse Nuclear Power Station,Unit 1 ML20203C1401997-12-0202 December 1997 Safety Evaluation Supporting Amend 217 to License NPF-3 ML20203B2141997-12-0202 December 1997 Safety Evaluation Supporting Amend 218 to License NPF-3 ML20203C2701997-12-0202 December 1997 Safety Evaluation Supporting Amend 216 to License NPF-3 ML20138L0491997-02-11011 February 1997 Safety Evaluation Supporting Amend 214 to License NPF-3 ML20128L3001996-10-0202 October 1996 SER Supporting Dbnp IPE Process of Identifying Most Likely Severe Accidents & Severe Accident Vulnerabilities ML20058M9591993-09-28028 September 1993 SE Accepting Licensee Response to GL 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants.' ML20057A3791993-08-20020 August 1993 SE Concluding That Second 10-yr Interval Inservice Insp Program Plan for Plant Has Unacceptable Exam Sample as Discussed in Encl Inel TER ML20056G4301993-08-18018 August 1993 Safety Evaluation Re Inservice Testing Program Requests for Relief.Licensee Made Changes to Subj Program to Include Exercising & fail-safe Testing of Auxiliary Feedwater Valves AF-6451 & AF-6452,in Response to TER Anomaly 8 ML20126A3051992-12-0808 December 1992 Safety Evaluation Supporting Amend 176 to License NPF-3 ML20056B2721990-08-20020 August 1990 Safety Evaluation Granting Relief from ASME Code Repair Requirements for ASME Code 3 Piping ML20248H6371989-10-0303 October 1989 Safety Evaluation Supporting Amend 139 to License NPF-3 ML20248D8271989-09-29029 September 1989 Safety Evaluation Accepting Util 890228 & 0630 Submittals Presenting Proposed Designs to Comply w/10CFR50.62 ATWS Rule Requirements ML20248E2771989-09-20020 September 1989 Safety Evaluation Supporting Amend 138 to License NPF-3 ML20248B3801989-09-20020 September 1989 Safety Evaluation Supporting Amend 137 to License NPF-3 ML20247E6901989-09-0505 September 1989 Safety Evaluation of Audit of Facility Design for Resolution of IE Bulletin 79-27 Re Loss of non-Class IE Instrumentation & Control Power Sys Bus During Operation.Preventive Maint & Testing Program Should Be Developed for Bus Power Sources ML20245K1871989-08-15015 August 1989 Safety Evaluation Supporting Amend 136 to License NPF-3 ML20245F5791989-08-0404 August 1989 Safety Evaluation Supporting Amend 134 to License NPF-3 ML20245H9531989-08-0404 August 1989 Safety Evaluation Supporting Amend 135 to License NPF-3 ML20247J8731989-05-18018 May 1989 Safety Evaluation Supporting Amend 133 to License NPF-3 ML20245G0371989-04-25025 April 1989 Safety Evaluation Supporting Amend 131 to License NPF-3 ML20245F0631989-04-25025 April 1989 Safety Evaluation Supporting Amend 132 to License NPF-3 ML20244D4031989-04-13013 April 1989 Safety Evaluation Supporting Amend 130 to License NPF-3 ML20196D9601988-12-0808 December 1988 Safety Evaluation Re Util Response Concerning Auxiliary Feedwater Sys Reliability Study.Util Should Ensure That Sys Mods Do Not Result in Net Reduction in Sys Reliability ML20207K7911988-10-0404 October 1988 Safety Evaluation Supporting Operation in Cycle 6 W/O Removing Flaws in Cracked HPI Nozzle ML20207K1071988-09-19019 September 1988 Safety Evaluation Supporting Amend 120 to License NPF-3 ML20207H9271988-08-24024 August 1988 Safety Evaluation Supporting Amend 117 to License NPF-3 ML20207H3891988-08-19019 August 1988 Safety Evaluation Supporting Amend 116 to License NPF-3 ML20207E3931988-08-0202 August 1988 Safety Evaluation Supporting Amend 114 to License NPF-3 ML20207D5171988-08-0202 August 1988 Safety Evaluation Supporting Amend 115 to License NPF-3 ML20150C4621988-03-0909 March 1988 Safety Evaluation Supporting Amend 109 to License NPF-3 1999-08-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
[Table view] |
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UNITED STATES NUCLEAR REGULATORY COMMISSION g
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W ASHING TON, D. C. 20655
%.....l SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDHENT NO. 114 TO FACILITY OPERATING LICENSE NO. NPF-3 TOLEDO EDISON COMPANY AND THE CLEVELAND ELECTRIC ILLUMINATING COMPANY DAVIS-BESSE NUCl. EAR POWER STATION, UNIT NO. 1 DOCKET NO. 50-346
1.0 INTRODUCTION
By letters dated August 7, 1987 and March 21 and May 2, 1988, Toledo Edison requested several changes to the plant Technical Specifications (TS) for the delete the Safety Features Actuation System (SFAS) posed changes would (1)
Davis-Besse Nuclear Power Station, Unit 1.
The pro signals from certain valves listed in Table 3.3-5, Safety Features System Response Times, on the secondary side of the steam generators; and (2) delete the containment isolation closure time requirements from Table 3.6-2, Containment Isolation Yalves. The valves involved are the main steam isolation valves (MSIV's, MS 100 and 101), main steam warm-up valves (MS 100-1 and 101-1), main steam warm-up drain valves (MS 375 and 394), atraospheric vent valves (AVV's, ICS 11A and B), main feedwater stop valves (W 601 and 612), and steam generator blowdown valves (MS 603 and 604).
The licensees asserted that the purpose of the proposed changes was to eliminate unnecessary redundancy in containment isolation features, to improve reliability and availability of the main feedwater (MFW) system by reducing inadvertent SFAS actuation, and to minimize challenges to the auxiliary feedwater system.
2.0 EVALUATION 2.1 Proposed change to revise TS Section 3/4.3.2 Table 3.3-5 to delete the reference to the MSIV, MFW stop valves, and main steam warmup valves receiving a high-high containment pressure SFAS automatic signal.
The licensees indicated that the above valves currently receive Steam and Feedwater Rupture Control System (SFRCS) signals which provide sufficient redundancy tn automatically isolate them as necessary in the event of a design basis accident. The high-high containment pressure SFAS signal, which is actuated at 38.4 psia, can be caused only by a large break (greater than 0.5 square f t.) loss of coolant accident (LOCA).
For a large break LOCA, the RCS will rapidly depressurize to a value below the saturation pressure of the water in the secondary side of the steam generator (SG). This depressurization effectively seals the SG as a leakage path from the reactor coolant system (RCS); therefore, radioactive releases are not sensitive to the containment h{%3Oh $
6 P
2 isolation closure time of the valves on the SG secondary side. As the SG secondary side pressure falls to approximately 600 psia, a SFRCS steam line low-pressure trip will occur.
The SFRCS trip causes SG isolation valves associated with the feedwater and main steam system to automatically close on both SG's.
The SFRC system can also detect a main steam line break (MSLB) by sensing a steam line low pressure condition in the faulted SG's steam line. The system senses a feedwater line rupture by detecting a steam line low pressure on the faulted SG or a high reverse differential pressure between the unaffected SG and its feedwater line.
For the accidents discussed above, the valves affected by this change will be closed automatically due to the SFRCS trip, and the closure times do not significantly impact radiological consequences.
Further, these valves can also be closed remote manually from the control room. Due to the duplication of automatic isolation function between SFRCS and SFAS for these valves, the staff finds this proposed change acceptable.
2.2 Proposed change to revise TS 3/4.3.2, Table 3.3-5 to delete reference to MS warmup drain and AVV's receiving a high containment pressuie or low reactor coolant system pressure SFAS automatic signal.
The licensees indicated that the above valves are closed during norwal plant operation and the SFAS signals serve to provide a backup to procedural requirements for maintaining the valves in a closed position. During a steam generator tube rupture (SGTR) event, when the condenser is not available, the AVV's will be used to control the cooldown and to minimize main steam safety valve lifts. The SFAS signal due to low reactor coolant system pressure is counter-productive for the above accident mitigation operation when opening of the AVV's is desired.
For a small break LOCA, it is desirable to make these valves available in conjunction with the auxiliary feedwater system for removing decay heat from the SG secondary side.
For a MSLB and feedwater rupture, the AVY's are automatically isolated by an SFRCS signal, which provides a redundant, automatic function to isolate these valves as described in Section 2.1.
For a large break LOCA, the pressure gradients between the primary and secondary system prevent leakage into the secondary system until isolation is initiated by SFRCS low steam-line pressure. When comparing the safety significance of having a backup to a closed containment isolation valve in the secondary system against the enhanced availability of decay heat removal, the staff finds the latter to be more important and, therefore, finds the proposed change to be acceptable.
2.3 Proposed change to revise TS 3/4.3.2 Table 3.3-5 to delete the reference to the AVV's, MS warmup drain valves MSIV's MFW stop valves, and MS line warmup valves receiving a manual SFAS.
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3-T5e licentces indicated that the capability to operate manually the acove valves is available independent of SFAS, and these valves are listed in TS Section 3/4.6.3, Table 3.6-2, Containment Isolation Valves. The oper6bility of these valves including the manual function, is required by TS 3.6.3.1.
Surveillance of the manual operation capability is required by either TS 4.0.5 Surveillance Requirements for inservice inspection of ASME Class 1, 2 and 3 components, or TS Sections 4.3.2.2.1 through 4.3.2.2.3 which include SFRCS operability requirements.
Because of the above duplication in the TS manual operation function, the staff finds the proposed change acceptable.
2.4 Proposed change to revise TS Section 3/4.3.6 Table 3.6-2 to delete isolation time requirements for MS!V, main steam wannup valves, MFW stop valves, AVV, main steam warmup drain valves, and steam generator blowdown valves.
The licensees indicated that the response times for the MSlY, and MFW Rupture Control System (y specified in TS Table 3.3-13. Steam and Feedwater stop valves are currentl SFRCS)ResponseTimes.
Further, the stroke time performance will be monitored as a part of the in-service inspection and testing program, as required by TS 4.0.5, Surveillance Requirements for inservics *aspection of ASME Class 1, 2 and 3 components.
As discussed previously in Sections 2.1 and 2.2, the valve closure times for these containment isolation valves are not critical from the standpoint of containment isolation and limiting radiological releases. Therefore, the valve closure time requirements from the SFRCS and in-service inspection and testing program are adequate, and the staff finds the proposed change acceptable.
4.0 ENVIRONMENTAL CONSIDERATION
Pursuant to 10 CFR 51.?1. 51.32, and 51.35, an environmental assessment and finding of no significant impact has been prepared and published in the Federal Register on June 16, 1988 (53 FR 22588). Accordingly, based upon the environmental asses; ment, the Consnission has determined that the issuance of this amendment will not have a significant effect on the quality of the human environment.
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5.0 CONCLUSION
I The staff has concluded, based on the considerations discussed above, that:
will not be endangered by operation in the proposed manner, and (2) public (1) there is reasonable assurance that the health and safety of the l
such l
activities will be conducted in compliance with the Cosmission's regulations, i
and the issuance of this amendment will not be inimical to the comon defense l
and security or to the health and safety of the public.
Principal Contributor: Chang-Yang Li Dated: August 2, 1988 l
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